IR 05000275/2007005: Difference between revisions

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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors: (1) walked down portions of the below listed risk important system and reviewed plant procedures and documents to verify that critical portions of the selected
The inspectors:
: (1) walked down portions of the below listed risk important system and reviewed plant procedures and documents to verify that critical portions of the selected


system were correctly aligned; and, (2) compared deficiencies identified during the walk
system were correctly aligned; and,
: (2) compared deficiencies identified during the walk


down to the FSAR Update and corrective action program (CAP) to ensure problems
down to the FSAR Update and corrective action program (CAP) to ensure problems
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condition of active and passive fire protection features and their operational lineup and
condition of active and passive fire protection features and their operational lineup and


readiness. The inspectors: (1) verified that transient combustibles and hot work
readiness. The inspectors:
: (1) verified that transient combustibles and hot work


activities were controlled in accordance with plant procedures; (2) observed the
activities were controlled in accordance with plant procedures;
: (2) observed the


condition of fire detection devices to verify that they remained functional; (3) observed
condition of fire detection devices to verify that they remained functional;
: (3) observed


fire suppression systems to verify that they remained functional and that access to  
fire suppression systems to verify that they remained functional and that access to  
-6-manual actuators was unobstructed; (4) verified that fire extinguishers and hose stations were provided at their designated locations and that they were in a satisfactory
-6-manual actuators was unobstructed;
: (4) verified that fire extinguishers and hose stations were provided at their designated locations and that they were in a satisfactory


condition; (5) verified that passive fire protection features (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems)
condition;
: (5) verified that passive fire protection features (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems)


were in a satisfactory material condition; (6) verified that adequate compensatory
were in a satisfactory material condition;
: (6) verified that adequate compensatory


measures were established for degraded or inoperable fire protection features and that
measures were established for degraded or inoperable fire protection features and that
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the compensatory measures were commensurate with the significance of the deficiency;
the compensatory measures were commensurate with the significance of the deficiency;


and, (7) reviewed the FSAR Update to determine if PG&E identified and corrected fire
and,
: (7) reviewed the FSAR Update to determine if PG&E identified and corrected fire


protection problems.*November 19, 2007: Unit 1, Fire Area 14-E, Component cooling water heat exchanger room*November 19, 2007: Unit 2, Fire Area 19-E, Component cooling water heat exchanger room*November 19, 2007: Unit 1, Fire Area 7-A, Cable spreading room
protection problems.*November 19, 2007: Unit 1, Fire Area 14-E, Component cooling water heat exchanger room*November 19, 2007: Unit 2, Fire Area 19-E, Component cooling water heat exchanger room*November 19, 2007: Unit 1, Fire Area 7-A, Cable spreading room
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The inspectors reviewed PG&E's programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for
The inspectors reviewed PG&E's programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for


Component Cooling Water Heat Exchangers 1-1 and 1-2. The inspectors verified that:  
Component Cooling Water Heat Exchangers 1-1 and 1-2. The inspectors verified that:
: (1) performance tests were satisfactorily conducted for heat exchangers/heat sinks and


(1) performance tests were satisfactorily conducted for heat exchangers/heat sinks and
reviewed for problems or errors;
 
: (2) PG&E utilized the periodic maintenance method
reviewed for problems or errors; (2) PG&E utilized the periodic maintenance method


outlined in EPRI NP-7552, "Heat Exchanger Performance Monitoring Guidelines;"
outlined in EPRI NP-7552, "Heat Exchanger Performance Monitoring Guidelines;"
(3) PG&E properly utilized biofouling controls; (4) PG&E's heat exchanger inspections
: (3) PG&E properly utilized biofouling controls;
: (4) PG&E's heat exchanger inspections


adequately assessed the state of cleanliness of their tubes, and, (5) the heat
adequately assessed the state of cleanliness of their tubes, and,
: (5) the heat


exchangers were correctly categorized under the Maintenance Rule.
exchangers were correctly categorized under the Maintenance Rule.
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November 2007, and also a verification of reasonable model performance based on the
November 2007, and also a verification of reasonable model performance based on the


current design of the plant. These tests were: (1) design basis loss of coolant accident
current design of the plant. These tests were:
: (1) design basis loss of coolant accident


with subsequent loss of off-site power transient test eight; (2) maximum size unisolable
with subsequent loss of off-site power transient test eight;
: (2) maximum size unisolable


main steam line rupture transient test nine; (3) slow primary system depressurization to
main steam line rupture transient test nine;
: (3) slow primary system depressurization to


saturation condition with pressurizer relief or safety valve stuck open (inhibit activation of
saturation condition with pressurizer relief or safety valve stuck open (inhibit activation of


high pressure emergency core cooling system) transient test ten; (4) scenario-based test
high pressure emergency core cooling system) transient test ten;
: (4) scenario-based test


package for mid-loop operations; and, (5) discrepancy work closeout package for
package for mid-loop operations; and,
: (5) discrepancy work closeout package for


radiation monitor failures discovered during a loss of coolant accident scenario test.
radiation monitor failures discovered during a loss of coolant accident scenario test.
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with NUREG-1021, Revision 9, Supplement 1, "Operator Licensing Examination
with NUREG-1021, Revision 9, Supplement 1, "Operator Licensing Examination


Standards for Power Reactors."1R12Maintenance Effectiveness (71111.12) Routine Maintenance Effectiveness Inspection The inspectors reviewed the listed maintenance activities to: (1) verify the appropriate handling of structure, system, and component (SSC) performance or condition problems; (2) verify the appropriate handling of degraded SSC functional performance; (3) evaluate
Standards for Power Reactors."1R12Maintenance Effectiveness (71111.12) Routine Maintenance Effectiveness Inspection The inspectors reviewed the listed maintenance activities to:
: (1) verify the appropriate handling of structure, system, and component (SSC) performance or condition problems;
: (2) verify the appropriate handling of degraded SSC functional performance;
: (3) evaluate


the role of work practices and common cause problems; and, (4) evaluate the handling
the role of work practices and common cause problems; and,
: (4) evaluate the handling


of SSC issues reviewed under the requirements of the Maintenance Rule, 10 CFR
of SSC issues reviewed under the requirements of the Maintenance Rule, 10 CFR
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the listed assessment activities to verify: (1) performance of risk assessments when required by 10 CFR 50.65(a)(4) and PG&E procedures prior to
The inspectors reviewed the listed assessment activities to verify:
: (1) performance of risk assessments when required by 10 CFR 50.65(a)(4) and PG&E procedures prior to


changes in plant configuration for maintenance activities and plant operations; (2) the
changes in plant configuration for maintenance activities and plant operations;
: (2) the


accuracy, adequacy, and completeness of the information considered in the risk
accuracy, adequacy, and completeness of the information considered in the risk


assessment; (3) that PG&E recognizes, and/or enters as applicable, the appropriate risk
assessment;
: (3) that PG&E recognizes, and/or enters as applicable, the appropriate risk


category according to the risk assessment results and PG&E procedures; and (4) PG&E  
category according to the risk assessment results and PG&E procedures; and
: (4) PG&E  
-10-identified and corrected problems related to maintenance risk assessments.*October 9, 2007: Unit 1, Auxiliary Saltwater Pump 1-1 maintenance
-10-identified and corrected problems related to maintenance risk assessments.*October 9, 2007: Unit 1, Auxiliary Saltwater Pump 1-1 maintenance
*October 17, 2007: Unit 1, Reactor coolant pump under voltage and under frequency relay calibration*November 6, 2007: Unit 2, Emergency Diesel Generator 2-1 maintenance outage
*October 17, 2007: Unit 1, Reactor coolant pump under voltage and under frequency relay calibration*November 6, 2007: Unit 2, Emergency Diesel Generator 2-1 maintenance outage
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors: (1) verified that PG&E performed actions to minimize the probability of initiating events and maintained the functional capability of mitigating systems and
The inspectors:
: (1) verified that PG&E performed actions to minimize the probability of initiating events and maintained the functional capability of mitigating systems and


barrier integrity systems; (2) verified that emergent work related activities such as
barrier integrity systems;
: (2) verified that emergent work related activities such as


troubleshooting, work planning/scheduling, establishing plant conditions, aligning
troubleshooting, work planning/scheduling, establishing plant conditions, aligning
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equipment, tagging, temporary modifications, and equipment restoration did not place
equipment, tagging, temporary modifications, and equipment restoration did not place


the plant in an unacceptable configuration; and, (3) reviewed the FSAR Update to
the plant in an unacceptable configuration; and,
: (3) reviewed the FSAR Update to


determine if PG&E identified and corrected risk assessment and emergent work control
determine if PG&E identified and corrected risk assessment and emergent work control
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors: (1) reviewed plant status documents such as operator shift logs, emergent work documentation, deferred modifications, and standing orders to determine
The inspectors:
: (1) reviewed plant status documents such as operator shift logs, emergent work documentation, deferred modifications, and standing orders to determine


if an operability evaluation was warranted for degraded components; (2) referred to the
if an operability evaluation was warranted for degraded components;
: (2) referred to the


FSAR Update and design bases documents to review the technical adequacy of the
FSAR Update and design bases documents to review the technical adequacy of the


operability evaluations; (3) evaluated compensatory measures associated with
operability evaluations;
: (3) evaluated compensatory measures associated with


operability evaluations; (4) determined degraded component impact on any TS; (5) used
operability evaluations;
: (4) determined degraded component impact on any TS;
: (5) used


the Significance Determination Process to evaluate the risk significance of degraded or
the Significance Determination Process to evaluate the risk significance of degraded or


inoperable equipment; and, (6) verified that PG&E has identified and implemented
inoperable equipment; and,
: (6) verified that PG&E has identified and implemented


appropriate corrective actions associated with degraded components.*October 9, 2007: Unit 1, Emergency Diesel Generator 1-3 oil leak
appropriate corrective actions associated with degraded components.*October 9, 2007: Unit 1, Emergency Diesel Generator 1-3 oil leak
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The inspectors selected the listed postmaintenance test activities of risk significant
The inspectors selected the listed postmaintenance test activities of risk significant


systems or components. For each item, the inspectors: (1) reviewed the applicable
systems or components. For each item, the inspectors:
: (1) reviewed the applicable


licensing basis and/or design basis documents to determine the safety functions;
licensing basis and/or design basis documents to determine the safety functions;
: (2) evaluated the safety functions that may have been affected by the maintenance


(2) evaluated the safety functions that may have been affected by the maintenance
activity; and,
 
: (3) reviewed the test procedure to ensure it adequately tested the safety
activity; and, (3) reviewed the test procedure to ensure it adequately tested the safety


function that may have been affected. The inspectors either witnessed or reviewed the
function that may have been affected. The inspectors either witnessed or reviewed the
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or reviewed the test data to verify that the following significant surveillance test attributes
or reviewed the test data to verify that the following significant surveillance test attributes


were adequate: (1) preconditioning; (2) evaluation of testing impact on the plant;
were adequate:
: (1) preconditioning;
: (2) evaluation of testing impact on the plant;
: (3) acceptance criteria;
: (4) test equipment;
: (5) procedures;
: (6) jumpers;
: (7) test data;
: (8) testing frequency and method demonstrated TS operability;
: (9) test equipment


(3) acceptance criteria; (4) test equipment; (5) procedures; (6) jumpers; (7) test data;
removal;
: (10) restoration of plant systems;
: (11) fulfillment of American Society of


(8) testing frequency and method demonstrated TS operability; (9) test equipment
Mechanical Engineers Code requirements;
: (12) updating of performance indicator data;
: (13) engineering evaluations, root causes, and bases for returning tested SSCs not


removal; (10) restoration of plant systems; (11) fulfillment of American Society of
meeting the test acceptance criteria were correct;
 
: (14) reference setting data; and,
Mechanical Engineers Code requirements; (12) updating of performance indicator data;
: (15) annunciators and alarm setpoints. The inspectors also verified that PG&E identified
 
(13) engineering evaluations, root causes, and bases for returning tested SSCs not
 
meeting the test acceptance criteria were correct; (14) reference setting data; and, (15) annunciators and alarm setpoints. The inspectors also verified that PG&E identified


and implemented any needed corrective actions associated with the surveillance testing.*October 9, 2007: Unit 1, Check valve inspections, inservice test  
and implemented any needed corrective actions associated with the surveillance testing.*October 9, 2007: Unit 1, Check valve inspections, inservice test  
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the FSAR Update, plant drawings, procedure requirements, and TSs to ensure that listed temporary modi fications were properly implemented. The inspectors: (1) verified that the modifications did not have an effect on system
The inspectors reviewed the FSAR Update, plant drawings, procedure requirements, and TSs to ensure that listed temporary modi fications were properly implemented. The inspectors:
: (1) verified that the modifications did not have an effect on system


operability/availability; (2) verified that the installation was consistent with modification
operability/availability;
: (2) verified that the installation was consistent with modification


documents; (3) ensured that the postinstallation test results were satisfactory and that
documents;
: (3) ensured that the postinstallation test results were satisfactory and that


the impact of the temporary modifications on permanently installed SSCs were
the impact of the temporary modifications on permanently installed SSCs were


supported by the test; (4) verified that the modifications were identified on control room
supported by the test;
: (4) verified that the modifications were identified on control room


drawings and that appropriate identification tags were placed on the affected drawings;
drawings and that appropriate identification tags were placed on the affected drawings;


and (5) verified that appropriate safety evaluations were completed. The inspectors
and
: (5) verified that appropriate safety evaluations were completed. The inspectors


verified that PG&E identified and implemented any needed corrective actions associated
verified that PG&E identified and implemented any needed corrective actions associated
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====a. Inspection Scope====
====a. Inspection Scope====
For the listed drill contributing to Drill/Exercise Performance and Emergency Response Organization Performance Indicators, the inspectors: (1) observed the training evolution
For the listed drill contributing to Drill/Exercise Performance and Emergency Response Organization Performance Indicators, the inspectors:
: (1) observed the training evolution


to identify any weaknesses and deficiencies in the emergency response organization;
to identify any weaknesses and deficiencies in the emergency response organization;
: (2) compared the identified weaknesses and deficiencies against PG&E identified


(2) compared the identified weaknesses and deficiencies against PG&E identified
findings to determine whether PG&E is properly identifying failures; and
 
: (3) determined
findings to determine whether PG&E is properly identifying failures; and (3) determined


whether PG&E performance is in accordance with the guidance of the NEI 99-02, "Voluntary Submission of Performance Indicator Data," acceptance criteria.*July 25, 2007, Units 1 and 2, full emergency drill
whether PG&E performance is in accordance with the guidance of the NEI 99-02, "Voluntary Submission of Performance Indicator Data," acceptance criteria.*July 25, 2007, Units 1 and 2, full emergency drill
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inspectors attended the condition adverse to quality screening meeting. The inspectors:
inspectors attended the condition adverse to quality screening meeting. The inspectors:
 
: (1) verified that equipment, human performance, and program issues were being
(1) verified that equipment, human performance, and program issues were being


identified by PG&E at an appropriate threshold and that the issues were entered into the
identified by PG&E at an appropriate threshold and that the issues were entered into the


corrective action program; (2) verified that corrective actions were commensurate with
corrective action program;
: (2) verified that corrective actions were commensurate with


the significance of the issue; and, (3) identified conditions that might warrant additional
the significance of the issue; and,
: (3) identified conditions that might warrant additional


follow-up through other baseline inspection procedures.
follow-up through other baseline inspection procedures.
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In addition to the daily screening, the inspectors conducted an in-depth review of the listed issues. The inspectors considered the following during the review of PG&E's
In addition to the daily screening, the inspectors conducted an in-depth review of the listed issues. The inspectors considered the following during the review of PG&E's


actions: (1) complete and accurate identification of the problem in a timely manner;
actions:
 
: (1) complete and accurate identification of the problem in a timely manner;
(2) evaluation and disposition of operability/reportability issues; (3) consideration of
: (2) evaluation and disposition of operability/reportability issues;
: (3) consideration of


extent of condition, generic implications, common cause, and previous occurrences;
extent of condition, generic implications, common cause, and previous occurrences;
: (4) classification and prioritization of the resolution of the problem;
: (5) identification of


(4) classification and prioritization of the resolution of the problem; (5) identification of
root and contributing causes of the problem;
 
: (6) identification of corrective actions; and,
root and contributing causes of the problem; (6) identification of corrective actions; and, (7) completion of corrective actions in a timely manner.*A0710652, November 21, 2007, Discrepancies associated with ultrasonic flow monitor nozzle fouling factor input into secondary system heat balance
: (7) completion of corrective actions in a timely manner.*A0710652, November 21, 2007, Discrepancies associated with ultrasonic flow monitor nozzle fouling factor input into secondary system heat balance


calculations*A0712404, November 20, 2007, Evaluate if licensee bases impact evaluation screen for less than adequate reactor water storage tank level required a license
calculations*A0712404, November 20, 2007, Evaluate if licensee bases impact evaluation screen for less than adequate reactor water storage tank level required a license
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operation. On this basis, the item impacts the Mitigating System Cornerstone and
operation. On this basis, the item impacts the Mitigating System Cornerstone and


screens to GREEN using IMC 0609, Phase 1 SDP Evaluation, Appendix A, because (a) the finding is not a design or qualification deficiency, (b) there is no loss of safety
screens to GREEN using IMC 0609, Phase 1 SDP Evaluation, Appendix A, because
: (a) the finding is not a design or qualification deficiency,
: (b) there is no loss of safety


function for a mitigating system and, (c) there are no seismic, fire, flooding or severe
function for a mitigating system and,
: (c) there are no seismic, fire, flooding or severe


weather initiating implications associated with the finding. This finding has a
weather initiating implications associated with the finding. This finding has a

Revision as of 18:30, 20 September 2018

IR 05000275-07-005, 05000323-07-05 & 07200026-07-001 on 10/01/2007 - 12/31/2007 for Diablo Canyon, Units 1 and 2, Surveillance Testing, Identification and Resolution of Problems
ML080360630
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 02/05/2008
From: Vincent Gaddy
NRC/RGN-IV/DRP/RPB-B
To: Keenan J S
Pacific Gas & Electric Co
References
FOIA/PA-2011-0221 IR-07-001
Download: ML080360630 (42)


Text

February 5, 2008

John Senior Vice President - Generation

and Chief Nuclear Officer

Pacific Gas and Electric Company

P.O. Box 770000

Mail Code B32

San Francisco, CA 94177-0001

SUBJECT: DIABLO CANYON POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000275/2007005; 05000323/2007005 AND 07200026/2007001

Dear Mr. Keenan:

On December 31, 2007, the U.S. Nuclear Regulatory Commission completed an inspection at your Diablo Canyon Power Plant, Units 1 and 2, facility. The enclosed integrated report

documents the inspection findings that were discussed on January 9, 2008, with John Conway

and members of your staff.

This inspection examined activities conducted under your licenses as they relate to safety and compliance with the Commission's rules and regulations, and with the conditions of your

license. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

There was one NRC-identified finding of very low safety significance (Green) and one Severity Level IV violation identified in this report. These findings involved violations of NRC

requirements. However, because of their very low risk significance and because they are

entered into your corrective action program, the NRC is treating these two findings as noncited

violations (NCVs) consistent with Section VI.A of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive, Suite

400, Arlington, Texas 76011-4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Diablo

Canyon Power Plant.

Pacific Gas and Electric Company-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/Vince G. Gaddy, Chief Project Branch B

Division of Reactor Projects Dockets: 50-275 50-323 72-026 Licenses: DPR-80

DPR-82 SNM-2511

Enclosure:

NRC Inspection Report 05000275/2007005, 05000323/2007005, and 07200026/2007001

w/attachment:

Supplemental Information cc w/enclosure:

Sierra Club San Lucia Chapter

ATTN: Andrew Christie

P.O. Box 15755

San Luis Obispo, CA 93406 Nancy Culver San Luis Obispo

Mothers for Peace

P.O. Box 164

Pismo Beach, CA 93448 Chairman San Luis Obispo County Board of

Supervisors

County Government Building

1055 Monterey Street, Suite D430

San Luis Obispo, CA 93408 Pacific Gas and Electric Company-3-

Truman Burns\Robert Kinosian California Public Utilities Commission

505 Van Ness Ave., Rm. 4102

San Francisco, CA 94102-3298 Diablo Canyon Independent Safety Committee Robert R. Wellington, Esq.

Legal Counsel

857 Cass Street, Suite D

Monterey, CA 93940 Director, Radiological Health Branch State Department of Health Services

P.O. Box 997414 (MS 7610)

Sacramento, CA 95899-7414 Jennifer Post, Esq.

Pacific Gas and Electric Company

P.O. Box 7442

San Francisco, CA 94120 City Editor The Tribune

3825 South Higuera Street

P.O. Box 112

San Luis Obispo, CA 93406-0112 James D. Boyd, Commissioner California Energy Commission

1516 Ninth Street (MS 34)

Sacramento, CA 95814 James R. Becker, Vice President Diablo Canyon Operations and

Station Director, Pacific Gas and

Electric Company

Diablo Canyon Power Plant

P.O. Box 56

Avila Beach, CA 93424 Jennifer Tang Field Representative

United States Senator Barbara Boxer

1700 Montgomery Street, Suite 240

San Francisco, CA 94111 John T. Conway Pacific Gas and Electric Company-4-

Site Vice President Diablo Canyon Power Plant

P.O. Box 56

Avila Beach, CA 93424 Chief, Radiological Emergency Preparedness Section National Preparedness Directorate

Technological Hazards Division

Department of Homeland Security

1111 Broadway, Suite 1200

Oakland, CA 94607-4052 Pacific Gas and Electric Company-5-

Electronic distribution by RIV:

Regional Administrator (EEC)DRP Director (DDC)DRS Director (RJC1)DRS Deputy Director (ACC)Senior Resident Inspector (MSP)Branch Chief, DRP/B (VGG)Senior Project Engineer, DRP/E (RWD)Team Leader, DRP/TSS (CJP)RITS Coordinator (MSH3)DRS STA (DAP)V. Dricks, PAO (VLD)A. Powell, OCA Region IV Coordinator (AXP10)D. Pelton, OEDO RIV Coordinator (DLP)ROPreports DC Site Secretary (AWC1)D. Spitzberg. FCDB/B (DBS)

SUNSI Review Completed: __VGG__ADAMS: Yes G No Initials: _VGG

_ Publicly Available G Non-Publicly Available G Sensitive Non-SensitiveR:\REACTORS\_DC\2007\DC2007-05-MSP-VGG.wpdADAMS ML080360630RIV:RI:DRP/BSRI:DRP/BC:DRS/EB1C:DRP/PSC:DRS/OB MABrownMSPeckRLBywaterMPShannonRELantz

/RA VGG for//RA VGG for//RA//RA//RA/01/ 31/0801/31/0801/17/0801/22/0801/17/08C:DRS/EB2DNMSDNMSC:DRP/BLJSmithRLKellarBSpitzbergVGGaddy

/RA NFO for//RA DBS for//RA//RA/01/31/0801/29/0801/29/0802/5/08OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax Enclosure-1-U.S. NUCLEAR REGULATORY COMMISSION REGION IVDockets:50-275, 50-323,72-026 Licenses:DPR-80, DPR-82, SNM-2511 Report:05000275/2007005 05000323/2007005

07200026/2007001Licensee:Pacific Gas and Electric Company Facility:Diablo Canyon Power Plant, Units 1 and 2 Location:7 1/2 miles NW of Avila Beach Avila Beach, CaliforniaDates:October 1 through December 31, 2007 Inspectors:M. Peck, Senior Resident Inspector M. Brown, Resident Inspector

K. Clayton, Senior Operations Engineer

D. Stearns, Health Physicist, Plant Support Branch

R. Kellar, Health PhysicistApproved By:V. G. Gaddy, Chief, Projects Branch B Division of Reactor Projects Enclosure-2-

SUMMARY OF FINDINGS

IR 05000275/2007-005, 05000323/2007-005; 10/1/07 - 12/31/07; Diablo Canyon Power Plant

Unit 1; Surveillance Testing, Identification and Resolution of Problems.

This report covered a 13-week period of inspection by resident inspectors and announced inspections on operator licensing and radiation protection. One NRC-identified, Green, noncited violation and one NRC-identified Severity Level IV noncited violation were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using

Inspection Manual Chapter 0609 "Significance Determination Process." Findings for which the

Significance Determination Process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process,"

Revision 3, dated July 2000.A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a noncited violation of 10 CFR 50, Appendix B, "Corrective Action," after Pacific Gas and Electric failed to identify a degraded emergency diesel generator. On October 15, 2007, the inspectors identified a buildup of black soot on the Emergency Diesel Generator 1-1 exhaust manifold.

Licensee personnel subsequently identified that one of the four fasteners connecting the exhaust manifold to the turbo charger was missing. The licensee declared the diesel generator inoperable based on the potential reduction of electrical power output due to exhaust gas bypassing the turbo charger and the adverse affect of the missing fastener on seismic qualification. Plant operators determined that overall plant risk was significantly degraded (Orange) due to the combination of the unavailable diesel generator and other plant equipment removed from service at the time. The licensee had prior opportunity to identify the degraded diesel generator during operator rounds between September 23 and October 15, 2007.

This finding is greater than minor because, if left uncorrected, continued failure to perform adequate operator rounds would become a more significant safety concern. This finding affected the mitigating systems cornerstone because the issue involved an emergency diesel generator. Using the Inspection Manual

Chapter 0609, "Significance Determination Process," Phase 1 worksheet, this finding was determined to have very low safety significance because it did not result in a loss of operability of a single train, for greater than Technical

Specification allowed outage time, did not result in the loss of safety function, and was not potentially risk significant from a seismic, flooding or severe weather perspective. This finding has a crosscutting aspect in the area of problem identification and resolution associated with the corrective action program component because plant operators did not maintain a low threshold for identifying issues P.1(a). This issue was entered into the licensee's corrective action program as Action Request A0710082 (Section 4OA2.1).

Enclosure-4-*SL IV. The inspectors identified a noncited Severity Level IV violation of 10 CFR 50.59 after Pacific Gas and Electric failed to perform an adequate safety evaluation of Unit 1 containment sump modifications. As a result, the licensee failed to obtain prior NRC approval for a change to the technical specifications incorporated in the license. On March 6, 2007, the licensee identified that the current refueling water storage tank minimum technical specification level was not adequate to ensure that the new containment sump would perform the required safety function. On April 20, 2007, Pacific Gas and Electric completed a 10 CFR 50.59, "Licensing Basis Impact Evaluation Screen of the Containment

Sump Modification." The licensee concluded that the modification did not involve a change to the plant technical specifications and that the required refueling water storage tank level was unaffected by the modification. On May 25, 2007,

Pacific Gas and Electric placed Unit 1 into Mode 4 without an approved technical specification change.

The inspectors concluded that the finding was more than minor because the modification required prior NRC approval. Because the issue affected the NRC's ability to perform its regulatory function, this finding was evaluated using the traditional enforcement process. The issue was classified as Severity Level IV because the violation of 10 CFR 50.59 involved conditions evaluated as having very low safety significance by the Significance Determination Process. The finding was determined to be of very low safety significance because the safety function was maintained since Pacific Gas and Electric had administratively maintained the refueling water storage tank at an adequate level during plant operation. On this basis, the item impacts the mitigating systems cornerstone and screens to Green, using the Inspection Manual Chapter 0609, "Significance

Determination Process," Phase 1 evaluation, Appendix A, because (a) the finding is not a design or qualification deficiency, (b) there is no loss of safety function for the mitigating system; and, (c) there are no seismic, fire, flooding or severe weather initiating implications associated with the finding. This finding has a crosscutting aspect in the area of problem identification and resolution associated with the corrective action program component because the licensee did not appropriately prioritize and evaluate the problem of an inadequate refueling water storage tank level after the problem was entered into the corrective action program, P.1(c). This issue was entered into the licensee's corrective action program as Action Request A07145625 (Section 4OA2.2).

REPORT DETAILS

Summary of Plant Status

At the beginning of the inspection period, Pacific Gas and Electric Company (PG&E) was operating both units at Diablo Canyon at full power. On December 3, 2007, PG&E reduced both

units to 24 percent power to mitigate high storm seas. The licensee returned Unit 1 to full

power on December 5 and Unit 2 to full power on December 8, 2007. PG&E operated both

units at full power for the remainder of the inspection period.1.REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R04Equipment Alignments (71111.04)

Partial System Walkdowns

a. Inspection Scope

The inspectors:

(1) walked down portions of the below listed risk important system and reviewed plant procedures and documents to verify that critical portions of the selected

system were correctly aligned; and,

(2) compared deficiencies identified during the walk

down to the FSAR Update and corrective action program (CAP) to ensure problems

were being identified and corrected. *October 15, 2007, Unit 1, Emergency Diesel Generator 1-1

The inspectors reviewed Procedure STP M-9A, "Diesel Generator Routine Surveillance,"

and Drawings 106721, "Diesel Engine Generator" for the inspection.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

Quarterly Inspection

a. Inspection Scope

The inspectors walked down the below listed plant areas to assess the material

condition of active and passive fire protection features and their operational lineup and

readiness. The inspectors:

(1) verified that transient combustibles and hot work

activities were controlled in accordance with plant procedures;

(2) observed the

condition of fire detection devices to verify that they remained functional;

(3) observed

fire suppression systems to verify that they remained functional and that access to

-6-manual actuators was unobstructed;

(4) verified that fire extinguishers and hose stations were provided at their designated locations and that they were in a satisfactory

condition;

(5) verified that passive fire protection features (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems)

were in a satisfactory material condition;

(6) verified that adequate compensatory

measures were established for degraded or inoperable fire protection features and that

the compensatory measures were commensurate with the significance of the deficiency;

and,

(7) reviewed the FSAR Update to determine if PG&E identified and corrected fire

protection problems.*November 19, 2007: Unit 1, Fire Area 14-E, Component cooling water heat exchanger room*November 19, 2007: Unit 2, Fire Area 19-E, Component cooling water heat exchanger room*November 19, 2007: Unit 1, Fire Area 7-A, Cable spreading room

  • November 19, 2007: Unit 2, Fire Area 7-B, Cable spreading room
  • November 23, 2007: Unit 1, Fire Area 3-Q-2, Motor driven auxiliary feedwater pump*November 23, 2007: Unit 2, Fire Area 3-T-2, Motor driven auxiliary feedwater pump*December 14, 2007: Unit 2, Fire Area 1-A, Containment annular area
  • December 14, 2007: Unit 2, Fire Area 1-C, Containment operating deck

Documents reviewed by the inspectors included:

  • Diablo Canyon Power Plant Units 1 and 2 FSAR Update, Appendix 9.5A, "Fire Hazards Analysis," Revision 17*Diablo Canyon Power Plant Fire Protection Pre-Plan, May 14, 2003

The inspectors completed eight samples.

b. Findings

No findings of significance were identified.

-7-1R07Heat Sink Performance (71111.07)

a. Inspection Scope

The inspectors reviewed PG&E's programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for

Component Cooling Water Heat Exchangers 1-1 and 1-2. The inspectors verified that:

(1) performance tests were satisfactorily conducted for heat exchangers/heat sinks and

reviewed for problems or errors;

(2) PG&E utilized the periodic maintenance method

outlined in EPRI NP-7552, "Heat Exchanger Performance Monitoring Guidelines;"

(3) PG&E properly utilized biofouling controls;
(4) PG&E's heat exchanger inspections

adequately assessed the state of cleanliness of their tubes, and,

(5) the heat

exchangers were correctly categorized under the Maintenance Rule.

The inspectors reviewed Diablo Canyon Power Plant Component Cooling Water 1-1 and 1-2 Heat Exchanger Test, Pre-1R14, May 2007, and Procedure PEP M-234, "Component Cooling Water Heat Exchanger Performance Test," Revision 9, for the

inspection.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

.1 Quarterly Inspection

a. Inspection Scope

On October 30, 2007, the inspectors observed a seismic event with anticipated transient without scram evaluation on the plant simulator. The inspectors observed the evaluation

to identify any deficiencies and discrepancies in the training to assess operator

performance and the evaluator's critique.

Documents reviewed by the inspectors in cluded Lesson FRS1-A, "Seismic Event with ATWS," Revision 15.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

-8-

.2 Biennial Inspection

a. Inspection Scope

The inspectors reviewed the licensee's simulator activities using Inspection Procedure 71111.11, "Licensed Operator Requalification Program," and 10 CFR 55.46, "Simulation Facilities," as acceptance criteria. The purpose of this review was to

determine if the simulator was capable of supporting initial examinations, supporting

requalification training required for all licensed operators on shift, and supporting

reactivity and control manipulations for initial license applications. The inspectors reviewed the simulator annual performance test book for 2007, in which most of the annual tests were conducted between September and November 2007, using ANS/ANSI 3.5-998, "Nuclear Power Plant Simulators for Use in Operator Training

and Examination," as committed to by PG&E in the Simulator Testing Procedure "Configuration Management Plan for the Operator Training Simulator," CF2.DC1, Revision 4. Because the licensee informed the inspectors that the simulator would be

used for reactivity manipulation credits on the next initial examination scheduled for June 2008, several core performance test documents were reviewed in order to assess

the adequacy of the simulator in supporting reactivity and control manipulations as

documented on NRC Form 398, "Personal Qualification Statement." While the simulator

use for reactivity and control manipulation is permitted by 10 CFR 55.46, the simulator

must meet the appropriate standards of fidelity, as required by 10 CFR 55.46(c)(2). The

inspectors reviewed the criteria in 10 CFR 55.46(c)(2) against the core performance test

document samples and the Cycle 15 test data from the plant. The simulator was using

the Cycle 15 core load for the current training cycle and no issues were found. Three transient tests, one scenario-based test package, and a work package closeout test were run on the simulator in order to verify that the data collected from the previous

tests was an accurate representation of the test data run during the testing in

November 2007, and also a verification of reasonable model performance based on the

current design of the plant. These tests were:

(1) design basis loss of coolant accident

with subsequent loss of off-site power transient test eight;

(2) maximum size unisolable

main steam line rupture transient test nine;

(3) slow primary system depressurization to

saturation condition with pressurizer relief or safety valve stuck open (inhibit activation of

high pressure emergency core cooling system) transient test ten;

(4) scenario-based test

package for mid-loop operations; and,

(5) discrepancy work closeout package for

radiation monitor failures discovered during a loss of coolant accident scenario test.

As part of this review, the inspectors interviewed one instructor, one evaluator, two reactor operators, two senior reactor operators, one simulator engineer, and the

simulator support supervisor. The interviews were performed to collect feedback

regarding the fidelity of the simulator, the simulator discrepancy reporting system

effectiveness, and training on differences between the simulator and the plant. The

inspectors reviewed several program documents that describe the overall simulator

program. One item specifically related to this review was how management groups, such as the simulator review board, coordinate discrepancy priorities and subsequent

repair decisions. These items were reviewed in order to satisfy the requirements of

10 CFR 55.46(d) for continued assurance of simulator fidelity through problem

-9-identification and resolution, proper reporting, root cause evaluations, and a planned schedule for implementing timely corrective actions with proper content.

Documents reviewed by the inspectors are listed in the attachment.

b. Findings

The inspectors confirmed that the licensee's simulator was adequate for reactivity manipulation credits on the next initial licensi ng examination provided that they continue to maintain the simulator core model on the most recent core load as the plant for which

licenses are being sought and the core testing program and results are maintained for

the examiners to review on the respective examination validation week in accordance

with NUREG-1021, Revision 9, Supplement 1, "Operator Licensing Examination

Standards for Power Reactors."1R12Maintenance Effectiveness (71111.12) Routine Maintenance Effectiveness Inspection The inspectors reviewed the listed maintenance activities to:

(1) verify the appropriate handling of structure, system, and component (SSC) performance or condition problems;
(2) verify the appropriate handling of degraded SSC functional performance;
(3) evaluate

the role of work practices and common cause problems; and,

(4) evaluate the handling

of SSC issues reviewed under the requirements of the Maintenance Rule, 10 CFR

Part 50, Appendix B, and the Technical Specifications:*October 26, 2007: Unit 1 and Unit 2, Plant process computer failures *December 5, 2007: Unit 2, Containment Air Particulate Monitor RM-11 failures Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Risk Assessments and Management of Risk

a. Inspection Scope

The inspectors reviewed the listed assessment activities to verify:

(1) performance of risk assessments when required by 10 CFR 50.65(a)(4) and PG&E procedures prior to

changes in plant configuration for maintenance activities and plant operations;

(2) the

accuracy, adequacy, and completeness of the information considered in the risk

assessment;

(3) that PG&E recognizes, and/or enters as applicable, the appropriate risk

category according to the risk assessment results and PG&E procedures; and

(4) PG&E

-10-identified and corrected problems related to maintenance risk assessments.*October 9, 2007: Unit 1, Auxiliary Saltwater Pump 1-1 maintenance

  • November 20, 2007: Unit 1, Component Cooling Water Heat Exchanger 1-2 and Auxiliary Saltwater Pump 1-2*December 14, 2007: Unit 2, Steam generator replacement project controls and plans to minimize adverse impact on the Unit 1 and common systems Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed five samples.

b. Findings

No findings of significance were identified.

.2 Emergent Work

a. Inspection Scope

The inspectors:

(1) verified that PG&E performed actions to minimize the probability of initiating events and maintained the functional capability of mitigating systems and

barrier integrity systems;

(2) verified that emergent work related activities such as

troubleshooting, work planning/scheduling, establishing plant conditions, aligning

equipment, tagging, temporary modifications, and equipment restoration did not place

the plant in an unacceptable configuration; and,

(3) reviewed the FSAR Update to

determine if PG&E identified and corrected risk assessment and emergent work control

problems.*October 17, 2007; Unit 1 Emergency Diesel Generator 1-1, unplanned outage to repair exhaust manifold Documents reviewed by the inspectors included Procedure AD7.DC6, "On-line Maintenance Risk Management," Revision 9.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

-11-

a. Inspection Scope

The inspectors:

(1) reviewed plant status documents such as operator shift logs, emergent work documentation, deferred modifications, and standing orders to determine

if an operability evaluation was warranted for degraded components;

(2) referred to the

FSAR Update and design bases documents to review the technical adequacy of the

operability evaluations;

(3) evaluated compensatory measures associated with

operability evaluations;

(4) determined degraded component impact on any TS;
(5) used

the Significance Determination Process to evaluate the risk significance of degraded or

inoperable equipment; and,

(6) verified that PG&E has identified and implemented

appropriate corrective actions associated with degraded components.*October 9, 2007: Unit 1, Emergency Diesel Generator 1-3 oil leak

  • October 31, 2007: Unit 2, Battery charger soldering deficiencies
  • December 3, 2007: Unit 2, Auxilia ry building ventilation system damper maintenance*December 4, 2007: Unit 1, Turbine Driven AFW Pump Steam Supply Valve FCV-95 incorrect valve stem lubrication*December 31, 2007: Unit 2, Seismic degradation of control room panels

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed six samples.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors selected the listed postmaintenance test activities of risk significant

systems or components. For each item, the inspectors:

(1) reviewed the applicable

licensing basis and/or design basis documents to determine the safety functions;

(2) evaluated the safety functions that may have been affected by the maintenance

activity; and,

(3) reviewed the test procedure to ensure it adequately tested the safety

function that may have been affected. The inspectors either witnessed or reviewed the

test data to verify that acceptance criteria were met, plant impacts were evaluated, test

equipment was calibrated, procedures were followed, jumpers were properly controlled, the test data results were complete and accurate, the test equipment was removed, the

system was properly realigned, and deficiencies during testing were documented. The

inspectors also reviewed the FSAR Update to determine if PG&E identified and

-12-corrected problems related to postmaintenance testing:*October 10, 2007: Unit 1 Auxiliary Saltwater Pump 1-1 preventive maintenance

  • October 15 and 16, 2007: Unit 1 Diesel Generator 1-1 preventive maintenance
  • November 1, 2007: Unit 2, Safety Injection Pump Motor 2-1 preventive maintenance*November 2, 2007: Unit 2 Safety Injection Pump 2-1 preventive maintenance
  • December 9, 2007: Unit 2, Turbine Driven Auxiliary Feedwater Pump 2-1 preventive maintenance*December 10, 2007: Unit 1 Fuel Handling Building Ventilation System Exhaust Fan E-6 preventive maintenance Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed eight samples.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the FSAR Update, procedure requirements, and TS to ensure that the below listed surveillance activities demonstrated that the SSCs tested were

capable of performing their intended safety functions. The inspectors either witnessed

or reviewed the test data to verify that the following significant surveillance test attributes

were adequate:

(1) preconditioning;
(2) evaluation of testing impact on the plant;
(3) acceptance criteria;
(4) test equipment;
(5) procedures;
(6) jumpers;
(7) test data;
(8) testing frequency and method demonstrated TS operability;
(9) test equipment

removal;

(10) restoration of plant systems;
(11) fulfillment of American Society of

Mechanical Engineers Code requirements;

(12) updating of performance indicator data;
(13) engineering evaluations, root causes, and bases for returning tested SSCs not

meeting the test acceptance criteria were correct;

(14) reference setting data; and,
(15) annunciators and alarm setpoints. The inspectors also verified that PG&E identified

and implemented any needed corrective actions associated with the surveillance testing.*October 9, 2007: Unit 1, Check valve inspections, inservice test

-13-*October 23, 2007: Unit 1, Containment Air Particulate Radiation Detector RM-11*November 1, 2007: Unit 2, Emergency Dies el Generator 2-3 room carbon dioxide fire system test*November 21, 2007: Unit 2, Emergency core cooling venting

  • December 9, 2007: Unit 2, Inservice te st of turbine driven Auxiliary Feedwater Steam Stop Valve FCV-95*December 9, 2007: Unit 2, Inservice test of steam supply to turbine driven Auxiliary Feedwater Turbine FCV-37 and FCV-38*December 9, 2007: Unit 2, Inservice test of Auxiliary FeedwaterPump Discharge Valves LCV-106, 107, 108, and 109 *December 23, 2007: Unit 1, Reactor coolant system water inventory balance

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one RCS leak detection, three routine, and four inservice testsamples.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed the FSAR Update, plant drawings, procedure requirements, and TSs to ensure that listed temporary modi fications were properly implemented. The inspectors:

(1) verified that the modifications did not have an effect on system

operability/availability;

(2) verified that the installation was consistent with modification

documents;

(3) ensured that the postinstallation test results were satisfactory and that

the impact of the temporary modifications on permanently installed SSCs were

supported by the test;

(4) verified that the modifications were identified on control room

drawings and that appropriate identification tags were placed on the affected drawings;

and

(5) verified that appropriate safety evaluations were completed. The inspectors

verified that PG&E identified and implemented any needed corrective actions associated

with temporary modifications. *October 29, 2007: Unauthorized temporary modification installing 480 volt power in the Unit 1 component cooling water heat exchanger room*November 15, 2007: Unit 1, 12kV Bus E potential transformer temporary connection

-14-*December 13, 2007: Unit 2, Steam generator replacement project engineering design, modification, and analysis associated with steam generator lifting and

rigging Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed three samples.

b. Findings

No findings of significance were identified.

Cornerstone:

Emergency Preparedness1EP6Emergency Preparedness Evaluation (71114.06)

a. Inspection Scope

For the listed drill contributing to Drill/Exercise Performance and Emergency Response Organization Performance Indicators, the inspectors:

(1) observed the training evolution

to identify any weaknesses and deficiencies in the emergency response organization;

(2) compared the identified weaknesses and deficiencies against PG&E identified

findings to determine whether PG&E is properly identifying failures; and

(3) determined

whether PG&E performance is in accordance with the guidance of the NEI 99-02, "Voluntary Submission of Performance Indicator Data," acceptance criteria.*July 25, 2007, Units 1 and 2, full emergency drill

Documents reviewed by the inspectors included the Diablo Canyon Power Plant Emergency Plan, Revision 4.

The inspectors completed one sample.2.RADIATION SAFETY

Cornerstone:

Occupational Radiation Safety2OS1Access Control To Radiologically Significant Areas (71121.01)

a. Inspection Scope

The inspectors assessed the licensee's performance in implementing physical and administrative controls for airborne radioactivity areas, radiation areas, high radiation

areas, and worker adherence to these controls. The inspectors used the requirements

in 10 CFR Part 20, the TSs, and the licensee's procedures required by the TSs as

criteria for determining compliance. During the inspection, the inspectors interviewed

the radiation protection manager, radiation protection supervisors, and radiation workers.

-15-The inspectors performed independent radiation dose rate measurements and reviewed the following:*Performance indicator events and associated documentation packages reported by PG&E in the occupational radiation safety cornerstone*Controls (surveys, posting, and barricades) of three radiation, high radiation, or airborne radioactivity areas

  • Barrier integrity and performance of engineering controls in airborne radioactivity areas*Adequacy of the licensee's internal dose assessment for any actual internal exposure greater than 50 millirem committed effective dose equivalent *Self-assessments, audits, licensee event reports, and special reports related to the access control program since the last inspection*Corrective action documents related to access controls
  • Radiation work permit briefings and worker instructions
  • Posting and locking of entrances to all accessible high dose rate - high radiation areas and very high radiation areas*Radiation worker and radiation protection technician performance with respect to radiation protection work requirements Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed 13 samples.

b. Findings

No findings of significance were identified.2OS2As Low As is Reasonably Achievable (ALARA) Planning and Controls (71121.02)

a. Inspection Scope

The inspectors assessed PG&E's performance with respect to maintaining individual and collective radiation exposures as low as is reasonably achievable (ALARA). The

inspectors used the requirements in 10 CFR Part 20 and the licensee's procedures

required by TSs as criteria for determining compliance. The inspectors interviewed

PG&E personnel and reviewed:*Current 3-year rolling average collective exposure

  • Site-specific trends in collective exposures, plant historical data, and source-term measurements*Site-specific ALARA procedures

-16-*Five work activities of highest exposure significance completed during the last outage *ALARA work activity evaluations, exposure estimates, and exposure mitigation requirements*Intended versus actual work activity doses and the reasons for any inconsistencies *Person-hour estimates provided by maintenance planning and other groups to the radiation protection group with the actual work activity time requirements *Post-job (work activity) reviews

  • Method for adjusting exposure estimates, or replanning work, when unexpected changes in scope or emergent work were encountered*Exposures of individuals from selected work groups*Radiation worker and radiation protection technician performance during work activities in radiation areas, airborne radioactivity areas, or high radiation areas *Self-assessments, audits, and special reports related to the ALARA program since the last inspection*Resolution through the corrective action process of problems identified through post-job reviews and post-outage ALARA report critiques*Corrective action documents related to the ALARA program and followup activities, such as initial problem identification, characterization, and tracking Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed 14 samples.

b. Findings

No findings of significance were identified.4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Cornerstone:

Barrier Integrity

a. Inspection Scope

The inspectors sampled PG&E submittals for the two performance indicators listed below for the period from September 2006 to September 2007, for Units 1 and 2. The

definitions and guidance of NEI 99-02, "Regulatory Assessment Indicator Guideline,"

Revision 4, were used to verify PG&E's basis for reporting each data element in order to

verify the accuracy of PI data reported during the assessment period.

-17-*RCS Specific Activity*RCS Leakage The inspectors completed two samples.

b. Findings

No findings of significance were identified.

.2 Cornerstone:

Occupational Radiation Safety

a. Inspection Scope

The inspectors reviewed licensee documents from April 1 through September 30, 2007, in regards to occupational exposure control effectiveness. The review included

corrective action documentation that identified occurrences in locked high radiation

areas (as defined in the licensee's technical specifications), very high radiation areas (as

defined in 10 CFR 20.1003), and unplanned personnel exposures (as defined in Nuclear

Energy Institute (NEI) 99-02, "Regulatory Assessment Indicator Guideline," Revision 5).

Additional records reviewed included ALARA records and whole body counts of selected

individual exposures. The inspectors interviewed PG&E personnel that were

accountable for collecting and evaluating the performance indicator data. In addition, the inspectors toured plant areas to verify that high radiation, locked high radiation, and

very high radiation areas were properly controlled. Performance indicator definitions and

guidance contained in NEI 99-02, Revision 5, were used to verify the basis in reporting

for each data element.

Document reviewed by the inspectors included the Action Request A 0696907.The inspectors completed one inspection sample.

b. Findings

No findings of significance were identified.

.3 Cornerstone:

Public Radiation Safety The inspectors reviewed licensee documents from April 1 through September 30, 2007, in regards to radiological effluent technical specification/offsite dose calculation manual

radiological effluent occurrences. The review included corrective action documentation

that identified occurrences for liquid or gaseous effluent releases that exceeded

performance indicator thresholds and those reported to the NRC. The inspectors

interviewed PG&E personnel that were accountable for collecting and evaluating the

performance indicator data. Performance indicator definitions and guidance contained

in NEI 99-02, Revision 5, were used to verify the basis in reporting for each data

element.The inspectors completed one sample in this cornerstone.

b. Findings

No findings of significance were identified.

-18-4OA2Identification and Resolution of Problems (71152)

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a daily screening of items entered into the corrective action program. This assessment was accomplished by reviewing action requests and event

trend reports, and attending daily operational meetings. On November 5, 2007, the

inspectors attended the condition adverse to quality screening meeting. The inspectors:

(1) verified that equipment, human performance, and program issues were being

identified by PG&E at an appropriate threshold and that the issues were entered into the

corrective action program;

(2) verified that corrective actions were commensurate with

the significance of the issue; and,

(3) identified conditions that might warrant additional

follow-up through other baseline inspection procedures.

b. Findings

Introduction.

The inspectors identified a Green noncited violation of 10 CFR 50, Appendix B, "Corrective Action," after PG&E failed to identify a degraded emergency

diesel generator.

Description.

On October 15, 2007, the inspectors identified black soot on the Emergency Diesel Generator 1-1 exhaust manifold. Licensee personnel subsequently

identified that one of four fasteners connecting the exhaust manifold to the turbo charger

was missing. The licensee declared the diesel generator inoperable based on the

potential reduction of electrical power output due to exhaust gas bypassing the turbo

charger and the adverse affect of the missing fastener on seismic qualification. Plant

operators determined that overall plant ri sk elevated to significantly degraded (Orange)due the combination of the unavailable diesel generator and other plant equipment

removed from service at the time. The licensee repaired and returned the diesel

generator to service on October 19, 2007. Plant engineering personnel subsequently

concluded that the loss of the fastener would not have prevented the diesel generator

from performing the required safety function. The soot buildup was present since the

last previous operation of the diesel generator on September 23, 2007. The licensee

had prior opportunity to identify the degraded diesel generator. Plant operators

performed at least one inspection of the diesel generator each shift in accordance with

Procedure OP1.DC3, "Operator Routine Plant Equipment Inspections," Revision 8.

Operations Policy A-22, "Expectations for Nuclear Operator Watchstanders,"

November 16, 2004, required operators to maintain an awareness of equipment

condition and to report problems in a timely manner.

Analysis.

Failure of PG&E operations personnel to identify the degraded diesel generator during operator rounds was a performance deficiency. This finding is greater

than minor because, if left uncorrected, continued failure to perform adequate operator

rounds would become a more significant safety concern. This finding involved an

emergency diesel generator and affected the mitigating systems cornerstone. Using the

Manual Chapter 0609, "Significance Determination Process," Phase 1 worksheet, this

finding was determined to have very low safety significance because it did not result in a

loss of operability of a single train, for greater than Technical Specification allowed

outage time, did not result in the loss of safety function, and was not potentially risk

significant from a seismic, flooding or severe weather perspective. This finding has a

-19-crosscutting aspect in the area of problem identification and resolution associated with the corrective action program component because plant operators did not maintain a low

threshold for identifying issues, P.1(a).

Enforcement.

Title 10 of the Code of Federal Regulations, Part 50, Appendix B,Criterion XVI, "Corrective Action," requires that measures be taken to assure that

conditions adverse to quality are promptly identified and corrected. Contrary to the

above, the licensee failed to identify a condition adverse to quality. Specifically, between

September 23 and October 15, 2007, plant operators did not identify the degraded

Emergency Diesel Generator 1-1 exhaust. Because this finding is of very low safety

significance and was entered into the corrective action program as Action Request

A0710082, this violation is being treated as a noncited violation in accordance with

Section VI.A.1 of the Enforcement Policy: NCV 05000275/2007005-01, "Plant Operators

Failed to Identify a Degraded Emergency Diesel Generator."

.2 Selected Issue Follow-Up Inspection

a. Inspection Scope

In addition to the daily screening, the inspectors conducted an in-depth review of the listed issues. The inspectors considered the following during the review of PG&E's

actions:

(1) complete and accurate identification of the problem in a timely manner;
(2) evaluation and disposition of operability/reportability issues;
(3) consideration of

extent of condition, generic implications, common cause, and previous occurrences;

(4) classification and prioritization of the resolution of the problem;
(5) identification of

root and contributing causes of the problem;

(6) identification of corrective actions; and,
(7) completion of corrective actions in a timely manner.*A0710652, November 21, 2007, Discrepancies associated with ultrasonic flow monitor nozzle fouling factor input into secondary system heat balance

calculations*A0712404, November 20, 2007, Evaluate if licensee bases impact evaluation screen for less than adequate reactor water storage tank level required a license

amendment Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed two in-depth review samples.

b. Findings

Introduction.

The inspectors identified a noncited Severity Level IV violation of 10 CFR 50.59 after PG&E failed to perform an adequate safety evaluation of Unit 1

containment sump modifications. As a result, the licensee failed to obtained prior NRC

approval for a change to the technical specifications incorporated in the license.

Description.

PG&E modified the Unit 1 containment sump during the Spring 2007 refueling outage. Technical Specification 3.5.4, "Refueling Water Storage Tank,"

required 81.5 percent indicated level (400,000 gallons). This technical specification

ensured enough water was provided during accident mitigation to ensure the residual

heat removal pump net positive suction head during the transition from cold leg injection

-20-mode to cold leg recirculation mode emergency core cooling. After the containment sump modification, 93.6 percent level in the refueling water storage tank (RWST) was

required to ensure residual heat removal pump net positive suction head. On

March 6, 2007, the licensee identified that the current RWST minimum technical

specification level was not adequate to ensure the new containment sump would

perform the required safety function. This was entered into the corrective action

program as Action Request A0690337. On April 20, 2007, PG&E completed a

10 CFR 50.59 Licensing Basis Impact Evaluation Screen of the containment sump

modification. The licensee concluded that the modification did not involve a change to

the technical specifications and that the RWST Technical Specification was unaffected

by the modification. On May 25, 2007, PG&E placed Unit 1 into Mode 4 without an

approved technical specification change. On October 2, 2007, the licensee submitted a

License Amendment Request to raise the RWST technical specification minimum level to meet the new sump design requirements. Plant operators had administratively

maintained the Unit 1 RWST at the higher level since entry into Mode 4.

Analysis.

The failure of PG&E to perform an adequate safety evaluation of the containment sump modification, to identify that prior NRC approval was required, is a

performance deficiency. The inspectors concluded that the finding was more than minor

because the modification required NRC prior review and approval. Because the issue

affected the NRC's ability to perform its regulatory function, this finding was evaluated

using the traditional enforcement process. The issue was classified as Severity Level IV

because the violation of 10 CFR 50.59 involved conditions evaluated as having very low

safety significance by the SDP. The finding was determined to be of very low safety

significance because the safety function was maintained since PG&E had

administratively maintained the RWST at least 93.6 percent indicated level during plant

operation. On this basis, the item impacts the Mitigating System Cornerstone and

screens to GREEN using IMC 0609, Phase 1 SDP Evaluation, Appendix A, because

(a) the finding is not a design or qualification deficiency,
(b) there is no loss of safety

function for a mitigating system and,

(c) there are no seismic, fire, flooding or severe

weather initiating implications associated with the finding. This finding has a

crosscutting aspect in the area of problem identification and resolution associated with

the corrective action program component because the licensee did not appropriately

prioritize and evaluate the problem of an inadequate refueling water storage tank level

after the problem was entered into the corrective action program, P.1(c).

Enforcement.

Title 10 of the Code of Federal Regulations, Part 50.59(c)(1) requires, in part, that a licensee may make changes in the facility as described in the final safety

analysis report without obtaining a license amendment only if a change to the technical

specifications incorporated in the license is not required. Title 10 CFR 50.36 requires, in

part, that a technical specification limiting condition for operation of a nuclear reactor

must be established for a structure, system, or component that is part of the primary

success path and which functions or actuates to mitigate a design basis accident or

transient that either assumes the failure of or presents a challenge to the integrity of a

fission product barrier. Contrary to the above, on May 25, 2007, PG&E made changes

to the facility as described in the final safety analysis report without obtaining a license

amendment when a change to the technical specifications incorporated in the license

was required. Specifically, PG&E changed the containment sump design such that

additional minimum Technical Specification level was required to ensure the design

basis accident primary success path. Because this finding is of very low safety

significance and was entered into the corrective action program as Action

Request A0715625, this violation is being treated as a noncited violation in accordance

-21-with Section VI.A.1 of the Enforcement Policy: NCV 05000275/2007005-02, "Inadequate 50.59 Evaluation for Unit 1 Containment Sump Modification."

.3 Semiannual Trend Review

a. Inspection Scope

The inspectors completed a semiannual trend review of repetitive or closely related issues that were documented in action requests, maintenance rule reports, system

health reports, problem lists, and performance indicators to identify trends that might

indicate the existence of more safety significant issues. The inspectors' review

consisted of the six-month period from July to December 2007. When warranted, some

of the samples expanded beyond those dates to fully assess the issue. Corrective

actions associated with a sample of the issues identified in PG&E's trend report were

reviewed for adequacy.

b. Findings

Continued Adverse Trend in Plant Equipment Material Condition The inspectors concluded that the adverse trend in plant material condition, discussed in Diablo Canyon Power Plant Integrated Inspection Report 05000275/2007003 and

05000323/2007003, continued through the inspection period. Current examples of poor

material condition identified by the inspectors included:*A0710082, Diesel Generator 1-1 Exhaust Leak

  • A0710921, Control room air conditioner condenser missing nine fasteners
  • A0706792, Control Room Air Conditioner CR-38 corrosion
  • A0710807, Component Cooling Water Heat Exchanger Saltwater Inlet Valve FCV-603 corrosion*A0710817, Oil seeping from Component Cooling Water Valve 1-21
  • A0719815 and A0710809, Component cooling water corroded conduits
  • A0710801, Corrosion on Component Cooling Water Valve FCV-602
  • A0710987, Component Cooling Water gasket for ASW to S/Gs

PG&E capture this adverse trend in the corrective action program as Action Request A0711113.

NRC Identified Adverse Trend in Managing Maintenance Risk The inspectors identified that the maintenance risk management thresholds established by the licensee were considerably below thre sholds established in the industry guidance provided in NUMARC 93-01, "Nuclear Energy Institute, Industry Guideline for Monitoring

the Effectiveness of Maintenance at Nuclear Power Plants," Revision 3. Because of low

threshold, PG&E typically entered elevated "Yellow Risk" (Integral Core Damage

-22-Probability 1x10

-6 to 1x10-5 ) an average of 12 times per week. The licensee also entered elevated "Orange Risk" (Integral Core Damage Probability greater than 1x10

-5 )several times during the inspection. The inspectors concluded that routine and repetitive

declaration of elevated plant maintenance risk resulted in plant of personal desensitized

to the subsequent risk management actions.

Examples included:*A0711074, Failure to control access to redundant equipment following removal of a Unit 2 component cooling water pump during declared "Yellow Risk."*A0711107, October 31, 2007, Removal of protective area around Unit 2 main feed water pumps while Diesel Generator 2-3 was planned to be removed from

service for fire protection testing, during declared "Yellow Risk." *A07164454, November 6, 2007, Unit 1 Shift Foreman was unaware of risk management actions following removal of a control room ventilation system

during declared "Yellow Risk."*A0711876, Unit 2 did not document entry into "Orange risk."

The inspectors concluded that each example was minor because actual industry risk threshold values for the required risk management actions were not exceeded. The

licensee entered this adverse trend into the corrective action program as Action

Request A0711061.

Documents reviewed by the inspectors are listed in the attachment.

The inspectors completed one sample in this inspection.

.4 Operator Workaround Review

The inspectors conducted a review to verify that the licensee is identifying operator workaround problems at an appropriate threshold, entered these issues into the

corrective action program and that the licensee has proposed or implemented

appropriate corrective actions. The inspectors reviewed the November 9, 2007, Operator

Workaround and Control Room Deficiency Report.

The inspectors completed one workaround sample.

.5 Occupational Radiation Safety

a. Inspection Scope

The inspectors evaluated the effectiveness of PG&E's problem identification and resolution process with respect to the following inspection areas:*Access Control to Radiologically Significant Areas (Section 2OS1)*ALARA Planning and Controls (Section 2OS2)

b. Findings

No findings of significance were identified.

-23-4OA3Event Followup (71153)

.1 (Closed) Licensee Event Report 05000275/2007001-00, Emergency Diesel Generator

Auto-start on Loss of Offsite 230kV Startup Power On May 12, 2007, offsite startup power was lost to both units at Diablo Canyon after a Morro Bay-Diablo Canyon 230 kV line transmission failed. The Unit 1 reactor was

defueled at the time and powered by the startup bus. Diesel Generators 1-1 and 1-2

automatically started and powered vital buses per plant design. This event was

previously discussed in Diablo Canyon Power Plant Integrated Inspection Report

323/2007003. No violation of NRC requirements was identified in this LER. This LER is

closed.

.2 (Closed) Licensee Event Report 05000275/2007002-00, Manual Reactor Trips During

Mode 3 Rod Testing Due to Crud Related Rod On May 27, 2007, Control Rod N-13 slipped from 42 steps to 24 steps while operators

were performing Surveillance Test Procedure STP R-1C, "Digital Rod Position Indicator

Functional Test," Revision 16, while Unit 1 was in Mode 3. Plant operators manually

tripped the reactor. The licensee concluded that the rod slippage was due to the crud

buildup on the control rod drive shaft. The vendor recommended that operators exercise

Control Bank 'C' out and back in five times in order to remove the crud from the drive

shaft. During the sequence of five rod exercises, Control Rod N-13 slipped three more

times, with each sequential slip occurring at higher steps out of the core. Operators

exercised Control Bank 'C' five more times without any additional control rod slippage.

PG&E staff subsequently concluded that the crud on the Control Rod N-13 drive shaft

had been removed to the reactor coolant syst em. This event was previously discussed in Diablo Canyon Power Plant Integrated Inspection Report 05000323/2007003. No

violation of NRC requirements was identified in this LER. This LER is closed.

.3 (Closed) Licensee Event Report 05000275/2007003-00, Emergency Diesel Generator

Actuation Due to a Transient Undervoltage Condition On May 28, 2007, an unplanned automatic start of Diesel Generator 1-2 occurred due to degraded bus voltage after Circulating Water Pump 1-2 was started. Plant operators

had transferred all plant electrical loads from the auxiliary power supply to startup power

in preparation of paralleling the main generator to the electric grid. Once all plant

electrical loads were connected to the startup power, operators started Circulating Water

Pump 1-2. Due to the large in-rush current required to start the pump, voltage degraded

on all plant electrical buses, including the vital 4 kV buses. The voltage on the vital 4 kV

buses degraded to the point that the second-level undervoltage relays actuated and

began the time delay sequence. The voltage on Vital 4 kV Buses F and H recovered

prior to the end of the time sequence. However, the voltage on Vital Bus G did not

sufficiently recover resulting in a trip of the startup power supply breaker and an

automatic start of the diesel generator. Plant engineering personnel determined that the

large circulating water pump motor in-rush current along with low startup power supply

margin resulted in the degraded voltage on the vital buses. The inspectors reviewed the

event sequence, equipment performance, operator actions, and plant electrical design

as they relate to this event. No violation of NRC requirements was identified in the LER.

This LER is closed.

-24-4OA5Other.1 Onsite Fabrication of Components and Construction of an Independent Spent Fuel Storage Installation (ISFSI) (60853)

a. Inspection Scope

The inspectors witnessed the final portion of the vertical cask transporter (VCT)functional testing performed at Diablo Canyon and completed reviews of documentation

from tests that had been conducted at the fabricator facility. The VCT is classified as

Important to Safety (ITS) and used to transport the loaded multi-purpose canister (MPC)

inside the HI-TRAC transfer cask from the fuel building to the ISFSI. The VCT is

seismically qualified and has redundant drop protection features in accordance with the

applicable guidelines of NUREG-0612, "Control of Heavy Loads at Nuclear Power

Plants." The VCT will also serve as the cask transfer facility (CTF) to lower the MPC into

the HI-STORM concrete overpack.

The NRC performed an inspection of the VCT fabrication at Lift Systems, Inc., located at Moline, Illinois, in January 22-26, 2007 (ML070400122). The factory acceptance testing

called for a 100 percent functional test, 125 percent static load test, 150 percent MPC

downloader test, 125 percent test of the seismic restraint lugs and an inclined functional

test. Overall, the fabrication activities were found to be in compliance with

10 CFR Part 72 regulations and the NRC approved Holtec QA program. The MPC

downloader test and nondestructive examinations of the critical welds were performed

after the NRC inspection. The inclined functional test was scheduled to be performed

after the VCT was delivered to Diablo Canyon.

Holtec provided a copy of the completed factory acceptance testing Holtec Project Procedure (HPP) 1073-6, Revision 2, which documented the successful 150 percent

load test of the MPC downloader. The MPC downloader is used to transfer the loaded

MPC from the HI-TRAC transfer cask into the HI-STORM overpack. The MPC

downloader test documentation stated that a test load of 67.5 tons (+10 tons/-0 tons)

had been used to perform the load test and the test load had been held for at least

10 minutes. A list of the VCT critical welds which were examined by nondestructive

examination following the load tests was provided by Holtec. The welds were classified

as critical per Section 3.4 of Holtec Standard Procedure HSP 187, "Interface Procedure

for Manufacturing of ITS B Transporters at Lift Systems," Revision 3, as a weld on an

essential component whose failure would directly lead to an uncontrolled lowering of the

lifted load or failure of other critical design function. The classification was stated to

conform to the evaluation criteria contained in NUREG-0612, Section 5.1, and the

definition of a critical load per ANSI N14.6, Section 3.4. The inspectors reviewed the

visual and magnetic particle test reports for selected welds that were classified as

critical. No discrepancies were found during the review. The VCT cask restraint system

design and fabrication were documented to meet the requirements of the ASME NF

Code. NUREG-0612 does not address horizontal loads such as those associated with

the cask restraint system. The spent fuel storage and transportation staff determined

that meeting the design and fabrication requirements of the ASME NF Code would be

sufficient to ensure that the cask restraint system operated safely.

The VCT was shipped to Diablo Canyon to perform the inclined functional test. The inclined functional test utilized the HI-TRAC transfer cask with an MPC that included

sufficient weight (82,500 pounds) to simulate a fully loaded MPC. The inclined functional

-25-test consisted of transporting the HI-TRAC and MPC from the entrance of the radiological controlled area (RCA) down the 8.5 percent grade and up the nominal

6 percent grade to the CTF. The distance of the transport path was approximately

1.2 miles in length.

The transport path or roadway from the fuel building to the ISFSI was designed and constructed to meet AASHTO H-20 loadings. The licensee had recently discovered that

the loadings imposed by the VCT tracks exceeded the H-20 design loadings. Minor

modification package AT-MM A0710693 was originated to evaluate the impact upon

embedded structures located beneath the roadway from the actual loads that were

exerted by the VCT along the route affected by the inclined function test. The minor

modification package verified that there were no safety related components located

underneath the portion of the roadway used for the inclined functional test. However, several portions of the roadway were required to be reinforced and minimum stand-off

distances were specified from the VCT to several of the boxes/vaults located along the

transport route. The licensee noted that the use of the roadway for movement of spent

fuel (including the area inside the RCA) will be addressed by a separate design change

package.The inclined functional load test was conducted after 1800 on Monday, December 10, 2007. The HI-TRAC with the simulated weight MPC was lifted by the VCT and secured

by the cask restraint system. The VCT was taken inside the protected area of the plant

up to the RCA fence. The VCT then traversed down the 8.5 percent grade and across

the relatively flat area of the plant site. Prior to beginning the trip up the nominal

6 percent grade, the 50 gallon fuel tank was refilled and the VCT then negotiated the

nominal 6 percent incline to the CTF.

A minor delay was experienced when hydraulic fluid was discovered leaking from an "O" ring fitting. The VCT inclined functional load

test was completed satisfactorily without any safety significant findings.

Diablo Canyon Technical Specification 4.3.1.c required that the cask transporter be designed, fabricated, inspected, maintained, operated, and tested in accordance with

the applicable guidelines of NUREG 0612. The staff reviewed the cask transporter

documentation to determine if the cask transporter met the applicable guidelines of

NUREG 0612. During this review, two questions were raised by the staff that required

additional clarification from the licensee.

The first question was associated with how the licensee had determined the testing requirements for the transporter load/lift links, which were part of the VCT lifting

mechanism. The load/lift links had been designed to meet the increased design stress

factors of 6 for yield and 10 for ultimate strength as required by ANSI N14.6. The load

testing of the load/lift links had been performed at 125 percent of the VCT rated load as

required by ASME B30.2, "Overhead and Gantry Cranes." The licensee stated that this

methodology was based on the previously appr oved use of similar lifting devices that were required to meet multiple criteria of NUREG 0612. The staff determined that the

licensee testing of the VCT load/lift links met the applicable portions of NUREG 0612.

The second question raised by the staff was how the requirements of NUREG 0612, Section 5.1.1(6) which specified that the crane (transporter) be inspected, tested, and

maintained in accordance with Chapter 2-2 of ASME B30.2 was to be achieved. The

vendor had provided a maintenance manual for the transporter. However, the

maintenance manual did not specify any frequent or periodic inspections for the VCT

which would parallel the inspection requirements that were contained in Chapter 2-2 of

-26-ASME B30.2. The licensee committed to providing additional instructions in the maintenance manual that would meet the inspection and maintenance recommendations

contained in NUREG 0612, Section 5.1.1(6) and instructions for meeting the

specifications contained in ANSI N14.6 for the MPC downloader. The revised VCT

maintenance manual will be reviewed during a future inspection.

b. Findings

No findings of significance were identified.4OA6Meetings, Including Exit

Exit Meeting Summary

On November 8, 2007, the inspectors presented the occupational radiation safety inspection results to Mr. John Conway, Site Vice President, and other members of his

staff who acknowledged the findings.

On December 11, 2007, the inspectors presented the independent spent fuel storage installation inspection results to Mr. John Conway, Site Vice President, and other

members of his staff.

On December 12, 2007, the inspectors discussed the inspection results of the simulator fidelity portion of the licensed operator biennial requalification inspection with

Mr. Jim Welsch, Operations Manager, and other members of his staff.

On January 9, 2008, the resident inspection results were presented to Mr. John Conway, Site Vice President and other members of PG&E management. PG&E acknowledged

the findings presented.

In each case, the inspectors asked PG&E whether any materials examined during the inspection should be considered proprietary. Proprietary information was reviewed by

the inspectors and left with PG&E at the end of the inspection.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

PG&E personnel

J. Becker, Vice President - Diablo Canyon Operations and Station Director
S. Hamilton, Supervisor, Regulatory Services
R. Hite, Manager, Radiation Protection
D. Jacobs, Vice President - Nuclear Services
S. Ketelsen, Manager, Regulatory Services
K. Langdon, Director, Operations Services
R. Lovell, Senior Nuclear Engineer
M. Meko, Director, Site Services
K. Peters, Director, Engineering Services
J. Purkis, Director, Maintenance Services
P. Roller, Director, Performance Improvement
M. Somerville, Manager, Radiation Protection
D. Taggart, Manager, Quality Verification
R. Waltos, Manager, Emergency Preparedness

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000275/2007005-01NCV

Plant Operators Failed to Identify a Degraded Emergency

Diesel Generator (Section 4OA2.1)05000275/2007005-02NCV

Inadequate 50.59 Evaluation for Unit 1 Containment Sump

Modification (Section 4OA2.2)

Closed

05000275/LER-2007-001-00LEREmergency Diesel Generator Auto-start on Loss of Offsite
230kV Startup Power (Section 4OA3.1)
05000275/LER-2007-002-00LERManual Reactor Trips During Mode 3 Rod Testing Due to
Crud Related Rod Slippage (Section 4OA3.2)
05000275/LER-2007-003-00LEREmergency Diesel Generator Actuation Due To A Transient
Undervoltage Condition (Section 4OA3.3)

LIST OF DOCUMENTS REVIEWED

Section 1R11:

Licensed Operator Requalification (71111.11)
Biennial Inspection

Procedures

Number Title RevisionCF2.DC1Configuration Management Plan for the Operator Training Simulator 4SQA 99-2Operator Training Simulator Software Quality Assurance Plan 0STP R7-ADetermination of Moderator Temperature Coefficient at
HZP,
BOL 15STP R31Rod Worth Measurements Using Rod Swap Method12

Other Documents

Simulator Scenario for Mid-Loop Operations, R075S1, Rev. 0
Open Simulator discrepancy report (all)
Closed Simulator discrepancy report from November 2005 thru November, 2007
Annual Operability Test packages*Steady state power test (83% and 25%)*Transients Reviewed (All 11)
  • Core test package for cycle 15
Simulator versus Plant differences list
Work package closeout and post-test for simulator SCR # 04-062, where high radiation alarms during a Loss of Coolant Accident scenario failed to work

Section 1R12:

Maintenance Effectiveness (71111.12)
Action RequestsA0595654A0684348A0692558A0702988A0671226A0697363A0709074A0709405A0712454A0712518

Procedures

Number Title RevisionSTP I-100AContainment Air Particulate/Gas Radiation Monitor RM-
11/RM-12 Functional Test

Other Documents

Title
Date/Revision System Report Details, System 43A "Plant Process Computer"7/1 - 9/30/2007System Report Details, System 39A/B "Rad. Monitoring System"10/1 - 12/31/2007

Section 1R13:

Maintenance Risk Assessments and Emergent Work Control (71111.13)
Action RequestsA0711265A0711289A0711270

Procedures

Number Title RevisionAD7.DC6On-Line Maintenance Risk Management10OP J-6B:IXDiesel Generator Extended On-Line Maintenance1
AD8.ID1Outage Planning and Management9
TP 22.0Risk Management Task Plan0
OP
AP-9Loss of Instrument Air23
OP AP
SD-4Loss of Component Cooling Water16

Section 1R15:

Operability Evaluations (71111.15)
Action RequestsA0691325A0697545A0709245A0710347A0710345A0710346A0690663A0710353A0712157A0454787A0711781A0664398
A0712272A0712386A0715324

Procedures

Number Title RevisionMP I-2.17-1Guidelines for Printed Circuit Board Repair and Inspection

3OM4 .ID3Assessment of Industry Operating Experience12STP

M-21-ENG.1Diesel Engine Generator Procedure (Every Refueling Outage)8 Other Documents Title
Date/RevisionWork Order,
C0216111 "DEG 2-1 Repair (Lube Oil Filter Housing Leak)"11/17/2007

Section 1R19:

Postmaintenance Testing (71111.19)
Action RequestsA0712336A0712337A0701654A0711712

Procedures

Number Title RevisionSTP M-9ADiesel Engine Generator Routine Surveillance Test74STP M-9XDiesel generator Operability Verification20
STP M-9D1Diesel Generator Full Load Rejection Test12
MP E-57.10CGeneric 4kV Motor Preventive Maintenance0
STP P-RHR-11Routine Surveillance Test of RHR Pump 1-120
STP P-SIP-21Routine Surveillance test of Safety Injection Pump 2-120
STP P-AFW-21Routine Surveillance Test of Turbine Driven AFW Pump20
MP M-17.9Auxiliary Salt Water Pump Maintenance20
STP M-5Surveillance Test of the Fuel Handling Building Ventilation System

Other Documents

Title
Date/RevisionWork Order, R0285110, "RHR PP 1-1 Discharge Miniflow Control"11/30/2007Work Order, R0285591, "4KV RHR PP 1-1"11/29/2007
Work Order, R0299925, "RHR Pump 1"11/21/2007
Work Order, R0306079, "Residual Heat Removal Pump 1-1"11/21/2007
Design Criteria
Memorandum S-10, "Residual Heat Removal System"15
Work Order, R0295991, "E-6 Motor: Clean, Inspect, and Test"12/6/2007

Section 1R22:

Surveillance Testing (71111.22)
Action RequestsA0710155A0711107A0691531

Procedures

Number Title RevisionSTP I-100AContainment Air Particulate/Gas Radiation Monitor RM-
11/RM-12 Functional Test
14STP M-39A3Routine Surveillance Test of Diesel Generator 1-3 (2-3)
Room Carbon Dioxide Fire System Operation
2STP M-89Unit 2, ECCS System Venting37STP R-10CReactor Coolant System Water Inventory Balance34
STP V-3P5Exercising Valves
LCV-106, 107, 108, and 109 Auxiliary Feedwater pump Discharge
20STP V-18MCheck Valve Inspections - High Maintenance Valves10
STP-V-3R5Exercising Steam Supply to AFW Pump Turbine Stop Valve 19STP-V-3R6Exercising Steam Supply to AFW Pump Turbine Isolation Valves 10

Drawings

Number Title Revision663227-55Air Flow Diagram -
RE 11/RE 124102931-11Instrument Schematic - Radiation Instruments57

Section 1R23: Temporary Plant Modifications (71111.23)

Action Requests

AR0711967 Procedures Number Title RevisionCF4.ID7Temporalty Modifications 19TP
TD-070312kV Bus "E" Potential Transformer Repair at Power0
TS3.ID2Licensing Basis Impact Evaluation22

Drawings

Number Title Revision437612-1Unit 1 Electrical Schematic Diagram Bus Potential &
Synchronizing 12kV System

Other Documents

Title Date/Revision Design Change Package
C-050743, "SGRP - Rigging and Handling Inside Containment" Design Change Package
C-050745, "SGRP - Rigging and Handling Outside Containment" Calculation # 52.15.141, "SGRP Load Path Evaluation - Impact on Elev.
140' Auxiliary Building Area GE and K Response Spectra due to
Movement of New/Old Steam Generators (Enova calc. 0104-031-C01)
2A Calculation # 52.15.142, "SGRP Load Path Evaluation - Seismic Stability Analysis of the Steam Generator/Transporter at Elev. 140' Auxiliary
Building Area GE and K (Enova calc. 0104-032-C01)
1A
Calculation # 52.15.143, "SGRP Load Path Evaluation - Evaluation of Floor at Elev. 140' Auxiliary Building Area GE and K due to Movement of
New/Old Steam Generators (Enova calc. 0104-032-C03)
R0309046 02 Diesel generator 2-3 installation of recorder to monitor
DEG start, December 21, 2007

Section 2OS1:

Access Controls to Radiologically Significant Areas (71121.01)
Action RequestsA0695011A0695199A0695353A0695683A0695740A0695961A0696887A0696907A0697100A0697727A0698424A0700022
A0700672A0703336A0703338A0703339
Audits and Self-Assessments Diablo Canyon Power Plant Quality Performance Assessment Report, 1

st Period 2007

Diablo Canyon Power Plant Quality Performance Assessment Report, 2

nd

Period 2007
2007 Radiation Protection Program Audit dated August 9, 2007

Procedures

Number Title RevisionRP1Radiation Protection4ARCP D-240Radiological Posting17
RCP D-370Evaluation of Internal Deposition of Radioactive Material7
RCP D-500Routine and Job Coverage Surveys23

Section 2OS2:

ALARA Planning and Controls (71121.02)
Action RequestsA0695351A0695591A0695595A0695730A0695936A0695974A0696277A0696286A0696352A0696741A0697472A0697722
A0698373A0698378A0698387A0698396A0698548A0698582
A0699099A0701401A0703330A0703352
Radiation Work PermitsSWP 10021R14 Scaffolding in ContainmentSWP 10331R14 RHR Recirc & Containment Sump
SWP 10441R14 Eddy Current Inspection & Tube Work
AttachmentSWP 10741R14 Fire Stops and Insulation ReplacementSWP 10771R14 Insulation Double Banding

Procedures

Number Title RevisionRP1 D-200Writing Radiation Work Permits37RCP D-205Performing ALARA Reviews15
RCP D-211Control of Work in Radiologically Significant Areas3
RCP D-220Control of Access to High, Locked High, and Very High Radiation Areas
2RCP D-222Radiation Protection Lock and Key Control5

Section 4OA2:

Identification and Resolution of Problems (71152)
Action RequestsA0695011A0695199A0695353A0695683A0695740A0695961A0487341A0487674A0616447A0619113A0638538A0650060
A0711967A0777733A0710082A0677367A0675465A0710868
A0710817A0715625A0657428A0686900A0706229A0708847
A0710652 Audits and Self-Assessments Diablo Canyon Power Plant Quality Performance Assessment Report, 1

st Period 2007

Diablo Canyon Power Plant Quality Performance Assessment Report, 2

nd

Period 2007
2007 Radiation Protection Program Audit dated August 9, 2007

Procedures

Number Title RevisionTS3.ID2Licensing Basis Impact Evaluations8PEP M-98AComparison of Final Feedwater Flow Nozzles to "AMAG" Ultrasonic Flow Instrumentation

Miscellaneous

Title Date/Revision
CENPD-397-P, "Improved Flow Measurement Accuracy Using Crossflow Ultrasonic Flow Measurement Technology"
01-P A-DP1-PS-0001, "Feedwater Flow Measurement Using the Crossflow Ultrasonic Flowmeter at PG&E Diablo Canyon Unit 1" 000 Semiannual Trend Review Assessment Reports Diablo Canyon Power Plant, Quality Performance Assessment Report, 4

th Period 2006

Diablo Canyon Power Plant, Quality Performance Assessment Report, 1

st Period 2007

Diablo Canyon Power Plant, Quality Performance Assessment Report, 2

nd Period 2007

Diablo Canyon Power Plant, Plant Perfor mance Improvement Report, September 2007
Diablo Canyon Power Plant, Plant Perf ormance Improvement Report, August 2007
Quality Verification Department Bi-Weekly Observation Report, December 27, 2007

Miscellaneous

PCPP Observation Card (ID# 21788) Operation Decision Meeting following failed reactor coolant pump breaker undervoltage relay, November 2, 2007

Section 4OA5: Other

Miscellaneous

Holtec Project Procedure
HPP-1073-6, "VCT Factory Test Procedure," Revision 2
Holtec Project Procedure
HPP-1073-6, "VCT Factory Test Procedure," Revision 3
Everett Shipyard SS MPC Dummy Training Weight Equipment No. 505 Certified Weight
Holtec Standard Procedure
HSP-187, "Interface Procedure For Manufacturing of ITS B
Transporters at Lift Systems," Revision 3
Diablo Canyon Transporter Manual, Revision 0

LIST OF ACRONYMS

ADAMSagency document and management systemAFWauxiliary feedwater

ALARAas low as is reasonably achievable

ARaction request

AASHTOAmerican Association of State Highway and Transportation Officials

CFRCode of Federal Regulations

DEGdiesel engine generator

FSARFinal Safety Analysis Report

HPPHoltec project procedure

HSPHoltec standard procedure

ISFSIindependent spent fuel storage installation

ITSImportant to Safety

LERlicensee event report

MPCmulti-purpose canister

NDEnondestructive examination

NRCNuclear Regulatory Commission

PARSPublicly Available Records System

PDTPacific daylight time

PG&EPacific Gas and Electric Company

RWSTrefueling water storage tank

SSCstructure, system and component

SLURSsecond-level undervoltage relays

TSTechnical Specifications

VCT vertical cask transporter