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 Issue dateTitleTopic
ML20086G2708 January 1976AO 75-79:on 751229,local Leak Test Identified through- Leakage of B Loop RHR Torus Spray Valve MO-3-10-38B & Torus Cooling Return Valve MO-3-10-34B.Cause Under Investigation
ML20086G2725 January 1976AO 75-78:on 751226,drywell Radiation Monitor Inoperative. Caused by Flow Blockage in on Stream Sample Line.Sample Point Changed to Reestablish Sample Flow to Drywell Radiation Monitor
ML20086G27430 December 1975AO 75-76:on 751220-21,local Leak Rate Test Identified through-leakage on Loop a & B RHR Outboard Injection Valves MO-3-10-154A & B.Cause Not Determined.Inboard Isolation Valves Verified as Leaktight & Closed
ML20086H0415 December 1975AO 75-72:on 751126,core Spray 3A Full Flow Test Valve MO-3-14-26A Failed to Close.Caused by Broken Wire on Closing Torque Switch in Valve Operator.Broken Wire Repaired & Proper Valve Operator Verified
ML20086F8435 December 1975AO 75-77:on 751126,LS-4223 Failed to Operate RHR Head Spray Line High Point Vent SV-4223 on Low Accumulator Level.Caused by Blown Fuse in Solenoid Valve Circuit.Grounded Wire Repaired & Vent Valve Returned to Svc
ML20086F8491 December 1975Telecopy AO 75-77:on 751126,LS-4223 Failed to Operate SV-4223 on Low Accumulator Level.Caused by Blown Fuse in Solenoid Valve Circuit.Operator Manually Vented Accumulator to Ensure Head Spray Line Maintained Filled
ML20086F87126 November 1975AO 75-75:on 751117,reservoirs of Two Hydraulic Snubbers Found Empty.Caused by Leaking O-rings & Gaskets.Defective gaskets,seals,O-rings & Fittings Will Be Replaced & Snubbers Will Be Checked
ML20086F85526 November 1975AO 75-76:on 751117,rigid Pipe Support Found Broken on RHR Shutdown Cooling Suction Line.Caused by Component Failure. Pipe Support Replaced.Investigation Continuing
ML20086F88026 November 1975AO 75-74:on 751116,setpoint of RCIC Steam Supply Line Area High Temp Switch TE-TS 4939A Found Less Conservative than Specified by Tech Specs.Caused by Slight Setpoint Drift. Switch Recalibr,Tested & Returned to Svc
ML20086H04626 November 1975Telecopy AO 75-72:on 751126,core Spray Full Flow Test Valve MO-3-14-26A Failed to Close.Caused by Broken Wire on Closing Torque Switch in Valve Operator.Broken Wire Repaired & Proper Valve Operation Verified
ML20086F89621 November 1975AO 75-73:on 751113,leak Observed on RHR Sys Relief Valve RV-35B.Caused by Throttling of MO-2-10-154B Valve Resulting in Crack.Weld Repairs Will Be Made to Relief Valve in Accordance W/Approved Procedures
ML20086F86118 November 1975Telecopy AO 75-76:on 751117,rigid Pipe Support Found Broken on RHR Shutdown Cooling Suction Line.Cause Under Investigation.Corrective Action to Be Determined After Investigation
ML20086F87418 November 1975Telecopy AO 75-75:on 751117,two Outside Drywell Snubbers Found to Have Empty Reservoirs.Cause Under Investigation. Corrective Action to Be Determined After Investigation
ML20086F89017 November 1975Telecopy AO 75-74:on 751116,setpoint of RCIC Steam Supply Line High Temp Switch TE-TS 4939A Found Less Conservative than Allowed by Tech Specs.Caused by Slight Setpoint Drift. Switch Recalibr & Returned to Svc
ML20086F90617 November 1975AO 75-71:on 751107,cracked Weld on 1-inch Line to Relief Valve RV-35B Observed.Caused by Throttling MO-2-10-154B Resulting in Cracked Weld.Repairs Completed in Accordance W/Approved Procedure
ML20086F91814 November 1975AO 75-70:on 751104,reservoirs of Five Hydraulic Snubbers Found Empty.Caused by Leaking O-rings & Gaskets.Defective Gaskets & O-rings Will Be Replaced
ML20086F90214 November 1975Telecopy AO 75-73:on 751113,leak on Body of RV-35B RHR Sys Relief Valve Observed.Caused by Throttling of MO-2-10-154B Valve Resulting in Crack.Rhr Loop B Shut Down in Preparation for Repair of Relief Valve
ML20086F91110 November 1975Telecopy AO 75-71:on 751107,cracked Weld on Line to RV-35B Observed.Caused by Throttling Down on MO-2-10-154B Resulting in Weld Crack.Repairs Completed.Pipe Vibration Readings Taken to Determine If Mods Required
ML20086H0527 November 1975AO 75-71:on 751030,drywell Oxygen Analyzer Sample Sys Outer Isolation Valve SV-3978B Failed.Caused by Dirt on Seat & in Body of Valve.Valve Internals & Seat Cleaned.Valve Disc, Piston Rings & Bonnet O-ring Replaced
ML20086F9235 November 1975Telecopy AO 75-70:on 751104,reservoirs of Five Hydraulic Snubbers Found Empty.Cause Under Investigation.Corrective Action to Be Determined After Investigation
ML20086H0623 November 1975AO 75-70:on 751024,drywell Purge Supply Isolation Valve A0-3520 Operated W/O Manual Initiation.Caused by Incorrect Implementation of Mod.Piping Corrected & Will Be Monitored
ML20086H07531 October 1975AO 75-68:on 751021,torus Makeup Supply Isolation Valve AO-3523 Found to Leak in Excess of 2,000 Cc/Minute.Caused by Closing Spring Not Providing Sufficient Force to Fully Close Valve.Closing Spring Adjusted
ML20086H05631 October 1975Telecopy AO 75-71:on 751030,isolation Valve SV 3978B Failed. Cause Under Investigation.Corrective Action to Be Determined
ML20086F92931 October 1975AO 75-69:on 751021,nitrogen Found to Leak Out of Test Connection on Inboard Flange of AO-2519.Caused by Use of Wrong Connection for Testing Double O-ring Seal.Connection Capped & Leak Checked Successfully
ML20086H08531 October 1975AO 75-67:on 751021,torus Makeup Supply Isolation Check Valve 276Y Found Leaking in Excess of 2,000 Cc/Minute.Caused by Valve Piston Being Hung Up During Operation.Check Valve Repaired & Local Rate Test Repeated
ML20086F93831 October 1975AO 75-68:on 751021,O-ring Gasket Leak Discovered on Torus Purge Supply Valve AO-2521B.Caused by Use of Improper Connection for Testing Double O-ring Seal.Connection Capped & Leak Checked Successfully
ML20086F95230 October 1975AO 75-66:on 751020,APRM B Flow Bias Signal Failed Upscale. Caused by Internal Ground in Channel Flow Transmitter D Combined W/Installed Instrument Loop Ground,Lowering Total Loop Resistance.Defective Components Replaced
ML20086F96624 October 1975AO 75-65:on 751015,setpoints on Reactor High Pressure Scram Switches Found Less Conservative than Specified by Tech Specs.Caused by Instrument Setpoint Shift.Channel D Switch Recalibr,Tested & Returned to Svc
ML20086H07424 October 1975Telecopy AO 75-69:on 751023,O-ring Gasket Leak Found on Drywell Purge Supply Valve AO-3505.Cause Under Investigation.Corrective Action to Be Determined After Investigation
ML20086H06824 October 1975Telecopy AO 75-70:on 751024,drywell Purge Supply Isolation Valve AO-3520 Operated W/O Manual Initiation.Caused by Incorrect Implementation of Mod.Valve Failed Closed & Will Be Repaired
ML20086F93321 October 1975Telecopy AO 75-69:on 751021,O-ring Gasket Leak Discovered on Drywell & Torus Inerting Nitrogen Supply Valve AO-2519.Cause Under Investigation.Corrective Action to Be Determined After Investigation
ML20086F94921 October 1975Telecopy AO 75-67:on 751021,diesel Generator Breaker E-4 Inoperable.Caused by Inoperative Charging Motor Failing Due to Brush Wear.Breaker Replaced
ML20086H09021 October 1975Telecopy AO 75-67:on 751021,torus Makeup Supply Isolation Check Valve 276Y Found Leaking in Excess of 2,000 Cc/Minute. Cause Under Investigation.Corrective Actions to Be Determined After Investigation
ML20086H08121 October 1975Telecopy AO 75-68:on 751021,torus Makeup Sys Isolation Valve AO-3523 Found to Leak in Excess of 2,000 Cc/Minute.Cause Under Investigation.Corrective Action to Be Determined After Investigation
ML20086F95821 October 1975Telecopy AO 75-66:on 751020,logic Aprm/Rbm B Flow Bias Signal from FT-2-2-110D Failed Upscale.Caused by Failure of Second Ground on Recirculation Drive Flow Transmitter Signal Loop.Flow Signal Corrected
ML20086F94421 October 1975Telecopy AO 75-68:on 751021,leak Found on O-ring Gasket on Torus Purge Supply Valve AO 2521A.Cause Under Investigation. Corrective Action to Be Determined After Investigation
ML20086H09616 October 1975AO 75-66:on 751006,RCIC Inboard Steam Supply Isolation Valve MO-3-13-15 Failed to Close.Cause Not Identified.Valve Stroked Successfully.Failure Not Repeatable
ML20086F97016 October 1975Telecopy AO 75-65:on 751015,setpoint on Reactor High Pressure Scram Switches Found to Be Less Conservative than Specified by Tech Specs.Caused by Instrument Setpoint Shift. Channel D Switch Recalibr,Tested & Returned to Svc
ML20086H10610 October 1975AO 75-65:on 751002,drywell Radiation Monitor Inoperable. Caused by Rust Blockage of Pressure Control Valve.Valve Cleaned,Reassembled & Returned to Svc
ML20086F98110 October 1975AO 75-64:on 751002,upper Isolation Valve to LS-2-3-231C Found Closed.Caused by Technician Error.Technicians Involved Interviewed & Seriousness of Error StressedScram Discharge Volume
ML20086H1179 October 1975AO 75-64:on 750929,main Steam Line High Flow Switch DPIS-3-2-116A Found to Trip at Value Slightly Higher than Tech Spec.Caused by Setpoint Shift.Device Checked for Setpoint Repeatability & Recalibr
ML20086H1017 October 1975Telecopy AO 75-66:on 751006,RCIC Inboard Steam Supply Isolation Valve MO-3-13-15 Failed to Close.Cause Under Investigation.Corrective Action to Be Determined After Investigation
ML20086F9743 October 1975Telecopy AO 75-65:on 751015,alarm Received Indicating Sampling Sys Exhaust Pump Suction Low.Cause Under Investigation.Corrective Action to Be Determined After Investigation
ML20086H1113 October 1975Telecopy AO 75-65:on 751002,drywell Radiation Monitor Inoperable.Cause Under Investigation.Corrective Action to Be Determined After Investigation
ML20086F9863 October 1975Telecopy AO 75-64:on 751002,upper Isolation Valve to LS-2-3-231C Found Closed.Caused by Technician Error. Technicians Involved Interviewed & Seriousness of Error StressedScram Discharge Volume
ML20086F98930 September 1975Telecopy AO 75-63:on 750929,outer Isolation Valves 86C & 86D Closed in 1.7 & 2.3 S,Respectively.Caused by Insufficient Hydraulic Fluid in Valve Actuator.Hydraulic Fluid Added & Adjustments Made to Closing Speed
ML20086G42230 September 1975AOs 50-277-75-62 & 50-278-75-61:on 750920,main Stack Flow Transmitters Failed.Caused by Lightning Strike.Damaged Components Replaced.Util Begun Study to Provide Permanent Resolution of Problem
ML20086H12029 September 1975Telecopy AO 75-64:on 750929,main Steam Line High Flow Switch DPIS-3-2-116A Found at Value Slightly Higher than Specified by Tech Spec.Caused by Setpoint Shift.Device Checked for Setpoint Repeatability & Recalibr
ML20086H13022 September 1975Telecopy AO 75-62:in 750921,RHR Head Spray Stay Fill Vent LS-5223 Found Inoperable.Caused by Binding in Switch Float Assembly.Stay Fill Tank Refilled & Switch Will Be Repaired
ML20086G42622 September 1975Telecopy AOs 50-277-75-62 & 50-278-75-61:on 750920,main Stack Flow Transmitters Failed.Caused by Lightning Strike. Damaged Components Replaced