ML20086H090

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Telecopy AO 75-67:on 751021,torus Makeup Supply Isolation Check Valve 276Y Found Leaking in Excess of 2,000 Cc/Minute. Cause Under Investigation.Corrective Actions to Be Determined After Investigation
ML20086H090
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 10/21/1975
From: Ullrich W
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20086H089 List:
References
AO-75-67, NUDOCS 8401130423
Download: ML20086H090 (1)


Text

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. s..,...:.- 4, n,.. n --.~ -- ~ - - -- ~m,a, --~n' . e.. PHILADELPHIA ELECTRIC COMPANY v, Peach Motton Atomic Power Station Delta. Pennsylvania l II31 October 21, 1975 Mr. James P. O'Reilly, Director Office of Inspection and Enforcement' _s t U States Nuclear Regulatory Commission g d4/Y7M 631 Park Avenue King of Prussia, PennsWivania 19k06

Subject:

Aboormal Occurrence PL-Hour Notification Confirming'R. S. Fleischmann 's phone conversation with Mr. Walt Baunack, .. Region 1. United States Nuclear Regulatcry Conmission on October 21, 1975 ~

Reference:

Lice 5se Number DPR-56 P=ahn4eal Speci.ficmAdon

Reference:

Table 3.7.k i. Report No.: 50-278-75-67 Report Date: October 21, 1975 Occurrence Date ,0ctober 21, 1975 {' Facility: Peach Bottom Atomic Power Station R.D.

1. Delta, Pennsylvania 1731L l

I5entification of Occurrence: ,'l Excessive leakage thru the 1" - 276Y check valve in the nitrogen inerting system dryvell purge supply to penetration U-205B. Conditions Prior to Occurrence: Reactor power 555. i Description of Occurrence: DurinE local leak rate testing of the torus make-up supply isolation e check valve, it was found to leak in excess of 2000 cc/ min. .k. Designation of Apparent cause of Occu,rrence: , J. Under investigation. I, i Analysis of Occurrence: s The safety implications cf this occurrence are minimal beenuse

manual isolation valve was closed when the leakage was detected.

i ^ Corrective Action: I s-To be determined after investigation. The nanual isolation valve was vcrified to be leak ti6ht in the closed condition. This valve ~ - will be naintained in the closed condition until repairs are 1, } - conpleted. i Failure Data: Abnornal Occurrence Report Numbers 50-277-75-33, 50-277-75-25 and i 50-2TT-75-1T. Very truly yours, M W. T. Ullrich, Superintendent Peach Botton Atomic Power Station N (Jus) e401%ho DR pDR -{. 6 l 5 i e p _. - -}}