SBK-L-06147, June 2006 Operating Report for Seabrook Station

From kanterella
Jump to navigation Jump to search
June 2006 Operating Report for Seabrook Station
ML062000039
Person / Time
Site: Seabrook NextEra Energy icon.png
Issue date: 07/12/2006
From: St.Pierre G
Florida Power & Light Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
SBK-L-06147
Download: ML062000039 (2)


Text

FPL Energy Seabrook Station RO. Box 300 FPL Energy Seabrook, NH 03874 Seabrook Station (603) 773-7000 July 12, 2006 Docket No. 50-443 SBK-L-06147 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555-0001 Seabrook Station June 2006 Monthly Operating Report Enclosed please find Monthly Operating Report 06-06. This report addresses the operating and shutdown experience relating to Seabrook Station Unit 1 for the month of June, 2006 and is submitted in accordance with the requirements of Seabrook Station Technical Specification 6.8.1.5.

Should you require further information regarding this matter, please contact Mr. Paul V. Gurney, Reactor Engineering Supervisor, at (603) 773-7776.

Very truly yours, FPL Energy Seabrook, LLC Gene F. St. Pierre Site Vice President cc: S. J. Collins, NRC Region I Administrator G. E. Miller, NRC Project Manager, Project Directorate 1-2 G. T. Dentel, NRC Senior Resident Inspector an FPL Group company

OPERATING DATA REPORT DOCKET NO. 5p0-443 UNIT NAME eabrook 1 DATE Jruly 10, 2006 COMPLETED BY F=eter Nardone TELEPHONE 603) 773-7074 REPORTING PERIOD: June 2006

1. Design Electrical Rating 1,22~2.0
2. Maximum Dependable Capacity (MWe-Net) 1,2100 This Month Yr-to-Date Cumulative
3. Number of Hours the Reactor was Critical 720.00 4,343.00 123,970.68
4. Number of Hours Generator On-line 720.00 4,343.00 120,970.16
5. Reserve Shutdown Hours 0.00 0.00 0.00
6. Net Electrical Energy Generated (MWHrs) 879,274.97 5,300,256.80 137,386,760.06 UNIT SHUTDOWNS Type Method of No. Date F: Forced Duration Reason Shutting Cause & Corrective Action S: Scheduled (Hours) Down 2 Comments

SUMMARY

The unit operated at 100% power for the entire month. This yielded an availability factor of 100% and a capacity factor of 100.02% based on the MDC value of 1221.0 Net MWe.

1 2 Reason: Method:

A Equipment Failure (Explain) I Manual B Maintenance or Test 2 Manual Trip/Scram C Refueling 3 Autcmatic Trip/Scram D Regulatory Restriction 4 Cont!*uat!on E Operator Training & License Examination 5 Other (Explain)

F Administration G Operational Error (Explain)

H Other (Explain)

Page 1 of 1