SBK-L-06036, January 2006 Monthly Operating Report for Seabrook Station
| ML060530417 | |
| Person / Time | |
|---|---|
| Site: | Seabrook |
| Issue date: | 02/08/2006 |
| From: | St.Pierre G Florida Power & Light Energy Seabrook |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| SBK-L-06036 | |
| Download: ML060530417 (2) | |
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FPL Energy Seabrook Station FPL Energy Seabrook Station P.O. Box 300 Seabrook, NH 03874 (603) 773-7000 February 8, 2006 Docket No. 50-443 SBK-L-06036 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555-0001 Seabrook Station January 2006 Monthly Operating Report Enclosed please find Monthly Operating Report 06-01. This report addresses the operating and shutdown experience relating to Seabrook Station Unit 1 for the month of January, 2006 and is submitted in accordance with the requirements of Seabrook Station Technical Specification 6.8.1.5.
Should you require further information regarding this matter, please contact Mr. Paul V. Gurney, Reactor Engineering Supervisor, at (603) 773-7776.
Very truly yours, FPL Energy Seabrook, LLC Gene F. St. Prre Site Vice President cc:
S. J. Collins, NRC Region I Adminisirator G.E. Miller, NRC Project Manager, Project Directorate I-2 G.T. Dentel, NRC Senior Resident Inspector an FPL Group company
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OPERATING DATA REPORT DOCKET NO.
UNIT NAIME DATE COMPLETED BY TELEPHONE REPORTING PERIOD 50-443 Seabrook I February 06, 2006 Peter Nardone (603) 773-7074 January 2006
- 1. Design Electrical Rating
- 2.
Maximum Dependable Capacity (MWe-Net) 1,222.00 1,221.00
- 3.
Number of Hours the Reactorwas Critical
- 4.
Number of Hours Generator On-line
- 5.
Reserve Shutdown Hours
- 6.
Net Ellectrical Energy Generated (MWHrs)
This Month Yr-to-Date Cumulative 744.00 744.00 120,371.68 744.00 744.00 117,371.16 0.00 0.00 0.00 907,402.97 907,402.97 132,993,906.23 UNIT SHUTDOWNS Type Method of Date F: Forced Duration Rea 1
Shutting Cause & Corrective Action S: Scheduled (Hours)
Down 2 Comments
SUMMARY
- The unit operated at 100% power for the entire month. This yielded an availability factor of 100% and a capacity factor of 99.89% based on the MDC value of 12.21.0 Net MWe.
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Reason:
A Equipment Failure (Explain)
B Maintenance or Test C
Refueling D
Regulatory Restriction E
Operator Training & License Examination F
Administration G
Operational -Error (Explain)
H Other (Explain)
Method:
I Manual 2
Manual Trip/Scram 3
Automatic Trip/Scram 4
Continuation 5
Other (Explain)
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