|
---|
Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs ML20217F4341998-03-19019 March 1998 SER Related to Proposed Restructuring New York State Electric & Gas Corp,Nine Mile Point Nuclear Station,Unit 2 ML20198H9941997-12-29029 December 1997 SE Supporting Approval of Application Re Long Island Power Authority Aquisition of Long Island Lighting Co,Subject to Discussed Condition ML20197C4771997-01-0303 January 1997 Safety Evaluation Supporting Nine Mile Point Unit 1 Reactor & Turbine Building Blowout Panels ML20197C4541997-01-0202 January 1997 Safety Evaluation Supporting Resolution of Nine Mile Point Reactor/Turbine Building Pressure Relief Panel Outside Design Basis Issue ML20056H4751993-08-27027 August 1993 Safety Evaluation Accepting Licensee Proposal for Continued Insp & Repair of Flaw in Weld Joining HPCS Nozzle Safe to safe-end Extension ML20205R1311988-10-31031 October 1988 Safety Evaluation Supporting Amend 101 to License DPR-63 ML20153F3851987-05-0404 May 1987 SER Accepting Util 870301 & 0407 Requests for Rev to Tech Specs,Modifying MSIV Actuation Control Sys,Per IEEE Std 279 & GDC 21 ML20153F3671987-04-30030 April 1987 Safety Evaluation Accepting Util 870311 Proposed Changes to Tech Spec Tables 2.2.1-1,3.6.1.2-1 & 3.6.3-1 Re MSIV-closure Setpoint ML20238C7121987-04-0808 April 1987 Safety Evaluation Concluding That Facility May Resume Operation W/O Leakage Control Sys But w/post-accident Leakage Mgt ML20153F3511987-02-0707 February 1987 Safety Evaluation Accepting Util Latest Design Mods to MSIV Actuation Control Sys,Per IEEE 279 & GDC 21 ML20238C6501987-02-0505 February 1987 Safety Evaluation Accepting MSIVs for Facility Operation Up to First Refueling,Contingent on Successful Completion of Preoperational Tests & Prototype Testing Program.Briefing for Commissioner Asselstine Re MSIVs & SALP Input Also Encl ML20238C5801987-02-0202 February 1987 Safety Evaluation Concluding That Facility May Resume Startup Testing & Operation for First Operating Cycle W/ Installed Refurbished Msivs.Necessity of Addl Leak Testing to Be Determined After Review of Prototype Test Results ML20238C1331986-10-27027 October 1986 Safety Evaluation Accepting Refurbished MSIVs for Plant Use Up to First Refueling,Contingent on Prototype Test Performance.Conditions Stated ML20238C1161986-10-22022 October 1986 Safety Evaluation Supporting Schedular Exemption from GDC 54 & 55 Re MSIV Operability to Permit Fuel Load.Salp Input Also Encl ML20153F6291986-08-27027 August 1986 Safety Evaluation Concurring W/Applicant 860703 Exemption Request Re Testing of 16 Relief Valves,Per 10CFR50,App J ML20197C0511978-10-27027 October 1978 Safety Evaluation Rept Supporting Amend 1 to CPPR-112 ML20244E2701974-11-15015 November 1974 Suppl 1 to AEC SER Re Licensee Conversion from Provisional OL to full-term OL for Util 1999-06-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20217K4631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Nine Mile Point, Unit 1.With ML20216J9251999-09-30030 September 1999 Suppl to Special Rept:On 990621,11 Containment Hydrogen Monitoring Sys Chart Recorder Was Indicating Below Normal Operating Range.Caused by Excessive Wear on Valve Body & Discs of Bypass Pump.Sample Pump Replaced ML20212F7301999-09-21021 September 1999 Special Rept:On 990907,CR Operators Declared 12 Containment Hydrogen Monitoring Sys Inoperable for Planned Maint.Cause of Low Flow Condition Was Determined to Be Foreign Matl. Replaced Sample Pump Valve Discs ML20212B9081999-09-14014 September 1999 Special Rept:On 990901, 12 Containment Hydrogen Monitoring Sys Was Declared Inoperable for Planned Maint.Caused by Planned Maint Being Performed as Corrective Action.Check Valves with O Rings Were Replaced ML20212C4601999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Nine Mile Point Nuclear Station,Unit 1.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20210U4591999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Nine Mile Point, Unit 1.With ML20209D0291999-07-0202 July 1999 Special Rept:On 990621,operator Identified That Number 11 Hydrogen Monitoring Sys (Hms) Chart Recorder Was Indicating Below Normal Operating Range.Cause Indeterminate.Licensee Will Complete Troubleshooting of Subject Hms by 990709 ML20210B9081999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Nine Mile Point Unit 1.With ML20209F8811999-06-0808 June 1999 Rev 1 to NMP Unit 1 COLR for Cycle 14 ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20196E2111999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Nmp,Unit 1.With ML20207B0241999-05-18018 May 1999 Safety Evaluation of Topical Rept TR-107285, BWR Vessel & Intervals Project,Bwr Top Guide Insp & Flaw Evaluation Guidelines (BWRVIP-26), Dtd December 1996.Rept Acceptable ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20196L2301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Nmp,Unit 1.With ML20205L0541999-04-0101 April 1999 Nonproprietary Replacement Pages to HI-91738,consisting of Section 5.0, Thermal-Hydraulic Analysis ML20205S5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for NMP Unit 1.With ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207G2671999-03-0101 March 1999 Special Rept:On 990315,Nine Mile Point,Unit 1 Declared Number 12 Containment Hydrogen Monitoring Sys Inoperable. Caused by Degraded Encapsulated Reed Switch within Flow Switch FS-201.2-1495.Technicians Replaced Flow Switch ML20204C9971999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Nine Mile Point,Unit 1.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML17059C5501999-01-31031 January 1999 Rev 0 to MPR-1966(NP), NMP Unit 1 Core Shroud Vertical Weld Repair Design Rept. ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199K9331998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20210R8441998-12-31031 December 1998 1998 Annual Rept for Energy East ML20206P2391998-12-31031 December 1998 Special Rept:On 981222,operators Removed non-TS Channel 12 Drywell Pressure Recorder & Associated TS Pressure Indicator from Svc.Caused by Intermittent Measuring Cable Connection in non-TS Recorder Circuitry.Replaced Cable ML20206P2421998-12-30030 December 1998 Special Rept:On 981219,number 12 Hydrogen Monitoring Sys (Hms) Was Declared Inoperable When Operators Closed Valve 201.2-601.Caused by Indeterminate Failure of Valve 201.2-71. Supplemental Rept Will Be Submitted After Valve Is Repaired ML20198M3571998-12-23023 December 1998 Special Rept:On 981210,operators Declared Number 11 Inoperable,Due to Failure of CR Chart Recorder.Caused by Inverter Board in Power Supply Circuitry of Recorder Due to Component Aging.Maint Personnel Replaced Failed Inverter ML20198D9361998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Nine Mile Point,Unit 1.With ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20195J4141998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs ML20154P1821998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20153B2001998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Nmpns,Unit 1.With ML20237C6351998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20236T5911998-07-20020 July 1998 LER 98-S01-00:on 980618,security Force Member Left Nine Mile Point,Unit 2 Vehicle Gate Unattended Without Ensuring,Gate Alarm Had Been Reactivated.Caused by Inadequate Work Practice.Vehicle Gate Alarm Was Activated ML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML20236Q1701998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML20151P1751998-06-16016 June 1998 Rev 0 to SIR-98-067, Evaluation of NMP Unit 2 Feedwater Nozzle-to-Safe End Weld Butter Indication (Weld 2RPV-KB20, N4D) ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML20249B4971998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20198B4991998-05-15015 May 1998 Non-proprietary Replacement Pages for Attachment F to Which Proposed to Change TS 5.5, Storage of Unirradiated & Sf ML20247R1141998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20217B0621998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1681998-03-19019 March 1998 Revised Niagara Mohawk Powerchoice Settlement Document for NMPC PSC Case Numbers 94-E-0098 & 94-E-0099, Vols 1 & 2 ML20217F4341998-03-19019 March 1998 SER Related to Proposed Restructuring New York State Electric & Gas Corp,Nine Mile Point Nuclear Station,Unit 2 ML17059B9051998-02-28028 February 1998 NMP Unit 1 Boat Samples Analyses Part Iii:Tension Tests, RDD:98:55863-004-000:01 1999-09-30
[Table view] |
Text
~
j.'. .
A ,
m0
(
'l 1
l t'
t 1 ,
y SUPPLEMENT NO. 1 TO THE SAFETY EVALUATION REPORT BY THE DIRECTORATE OF LICENSING U. S. ATOMIC ENERGY COMMISSION
. IN THE MATTER OF I
NIAGARA MOHAWK POWER CORPORATION CONVERSION FROM PROVISIONAL OPERATING LICENSE TO FULL-TERM OPERATING LICENSE
} .4
(
NINE MILE POINT UNIT 1 i
l DOCKET NO. 50-220 NOVEMBER'15,'1974
(
f t
/
l .
y
'I 8904240387 890413 PDR FOIA WETTERH89-101 PDR ,
..r _ - _ . _ _ _ _ , _ _ _ . _ . .
,(
TABLE OF CONTENTS e
1.0 INTRODUCTION
2.0 REPORT OF ADVISORY C0!C41TTEE ON REACTOR SAFECUARDS (ACRS)
!' 2.,1 Main Steam Line Isolation Valve Leakage T 2.2 Reactor Pressure Vessel In-Service Inspection 2.3 Possible Additional Backfit Improvements t
3.0 QUALITY ASSURANCE PROGRAM
, 440 CONCLUSIONS I
f L.
d' .,
l APPENDICES *-
l (
62PENDIX A Report of ACRS f
S k
1 .
l I
e 9-
.,A-
~
+ , q.
) 4
, , . -)*
'S' N p + p , ,, .,
w , . , x
. 4 9 ....e- -
+: .
N . s ' ~
- g. h ., , ,_
I'
~ x_
- n. -
~ .
, g- ,
, ,, .p - h '$ -- - 4 ' - ; * - e* *6 eleW- , y=***'
r s' ,
4 , .
~- .. . . .,
~ % - e.
t w e .
- .. .-r - - 8 ( ". ' ,
, 9 -
g xt a -
4 $ ,
t
-,r- a,,
e -
e s,
w .
.s _. _
- .> v. .
+ .. . % -
r,
& .. ,k ^
'd ;
[ g a
. 4 '
. e * , ,% ; 'a s 9 ' --
,, . 4
-s.
,< .1
. . . . . u ,i -
~ - .-
. r . s MI ,. g; -
- , i
- g. y.
9 .
, . s , -
_ :q Q , ,..,. , , , _ * ,
. p -
j.
, ^ . .,
rc . . .
e s ,,
,Y , . e . W
g -
'. . s.. .
W A
? .
- e. ;. . *
- g. ' - '= k . .
=> . , , , ..
- . . s o
, g4 s
.h . ,
,M I '
y , ',. ;
p.
+ -
7
. . 4.z g-
, s
-S .
s g i . .
X '
s -
p .a
- + '
y
+
k' 4_ -
z>
-p. .
V . .' . . - - ,. .
, g -
s m
_e ,
~: - -
-; ,~ .
& &= * ' '
s e e A i * .
8,'
{ e .
.i-e p *,a. 4 .
.P *
, H -
4 . .,
I \ ,
i- #rt .. 4. .
Q s *. v- *
, ? . a .
4 1 4
.- ' 4 . '.
..e __
- e - . .. W 1
4
. . ),
g i ,
\.
~
u.,
g *
- ' .s e ,,
'.' V #
? *s 3.
' 'b y , . . = y T
- e. .p .,
) t.h. . u . -A 3
f g *4* .
S' .. , - , 3 p # y 1 b m- -
,s.
r a g
.' e. 4 4'*
4,'-
j .
w s -; $ ,
, ,g ; ,
) - - . . *s 9 -
4.,
s:, g
<o
+ -
p ( P e
- I' #
g y
, . , 3 . ,
f .
S', 5
?
3 *
. . + ~ . . . . . . . . . , .
. .. ... ., .; . , , rp
, .g , + .
- .,..s 1 4 .:,. . ' . ., ..
g 4
= . ..
- a. <9
.o W ' * -
't> , - * - i k I . -
'r s 7, D .
- - ) e- - -
y .'y :6 i e +
p 4 1 i e ' i *
,.4 i
...) * - s 8 + "
W + 4 4. 4- ar-.--a -
4
.,,s
, , , . . , , . ' , , . ' '".,'.,;'.. . s .: . .?
' . ' . ' , . ,3., Y.%
r 4 a
$ , -,- .'t- -
f- ..
g -*
. ,- , ,..M g . ..- -
- ,+ -
+
3 #
. . . .. w
. c
.t . .. . . . .
.. y .
r g ,, - ' _ ' $g '
- n . > - - - .,
'- 4; ,. N N *
.. j A - * - - -
P
,$'e
+- * = ,J l'ga 4 ,
I t
4 'j(:s. , ' . . .. l l
'l.. " ;- <
y . . ' ' % ,- . ,.
, v.
4".? g.
1: *q "'
,* *y . }
,, 'g .
- 4e *e.,468='s ,'i. ' ' ' ' ' . , . . . . . . . . . .. . .,,... . ,.
A .
, e 4 g #.
s a .
' ', . * . .t;g. g 5
g g s r
+
- r- 4
.v g ,k p
's b .
.,, W > , y . ' .
- .l (
1.0 INTRODUCTION
The AEC Regulatory staff's Safety Evaluation Report (SER), in the matter of the Niagara Mohawk Power Corporation (herein l
{
referred to as hHPC or the licensee) application for conversion s
. }* '
of Provisional Operating License No. DPR-17 to a full-term
{
operating license for Mine Mile Point Unit 1 (KMP-1) was issued I
on July 3, 1974. Copics of this report were made available to the Advisory Committee on Reactor Safeguards (ACRS or Committee) to assist it in its review of this application. The Comittee I completed its review of the licensee's application in September 1974 and reported its fir. dings to the Commission by letter dated September 10, 1974.
- t
(
. 2.0 REPORT OF THE ADVISORY COMMITTEE ON REACTOR SAFEGUARDS A copy of the ACRS report to.the Commission is included as 1
Appendix A. We have considered the comments and recommendations I made by the ACRS in this report and the actions which we have
')
j taken or will take relative to these comments and recommendations
, are described in the following paragraphs. The Committee identified three matters for further surveillance: these matters consist of maintaining leak tightnesa of main steam line isolation valves; possible improvements in accessibility for in-service inspection of the reactor pressure vessel to assure continued vessel integrity; and consideration to the possible advisability of additional backfitting where significant and practical safety improvements can be made. The Committee concluded t' hat there
(
t I
m _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ . _ _ . _ _ . . _ _ _ _ _ _ . _ _ ___ _ _ _ . _ _ _ _ . _ _ _ _ . _ _ . _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ ._ . _ _ _ _ _ _ . _ _ .._o
7 ___ - __- _ _ _ _ - --__ - __-_ _____ _
e
, . (
exists reasonable assurance that' the Nine Mile Point Nuclear Station Unit 1 can continue to be operated at power levels up to 1850 MWt without undue risk to the health and safety of the public. Moreover, the Ccmmittee concurred in conversion of the c
i present provisional operating license to a full-term operating license.
I 2.1 Main Steam Line Isolation Valve Leakage The Cor.mittee 16dicated its awareness of the difficulty that has
, been experienced at hMP-1 in maintaining the required leak tightness of the main steam line isolation valves (MSLIV) and stated that the Regulatory sta'ff should continue to follow this matter closely.
The licensee stated its belief that leakage through these valves will be maintained at acceptable rates below the Technical 5h Specification limits as a result of changes in maintenance J
'k procedures involving the valve seats and plugs, initiated during the 1974 refueling shutdown. The next Icakage rate test of the' I
g MSL1Vs will be performed during the 1975 refueling shutdown.
i
. The Regulatory staff will follow his matter to confirm that the problem is corrected.
r 2.2 Reactor Pressure Vessel In-Service Inspection The Committee expressed its belief that additional means for l
assuring continued vessel integrity, including possible improvement g in accessibility for inspection,should continue to be actively studied and implemented to the degree practical. The licensee has stated its interest to continue to seek possible improvements in the matter of vessel accessibility and to implement sucli m_ _ _ _ _ . . ._ _ _ _ _ . __ _ _.
Li .
-~3 -
.(
f-improvements to the degree practical. Our on-going review of the operating f acility will monitor progress in this area.
.2.3 Possible Additional Backfit Improvements l
l The Committee recommended that the Regulatory staff and the licensee
[
' give further consideration to additional backfitting where significant 3
}
and practical safety improvements can be made. The licensee has indicated that it has a continuing program of review to determine the conf ormance of NMP-1 with new Regulatory Guides as these are l: The Regulatory staff will continue its on-going review of issued.
NMP-1, including consideration of backfitting where significant and practical safety improvements can be made, i
3.0 QUALITY ASSURANCE (QA) PROGRM4
{
Lt i As stated in our SER, we have reviewed the licensee's QA Program l, '
1 and concluded that it is acceptable. The licensee's QA Program j , was described in four different submittals. This information was Lj' superseded by the licensee's submittal of August 28, 1974, entitled,
! " Tenth Supplement to the Final Safety Analysis Report" which consolidates and unifica the earlier submittals. We have reviewed
' and determined that the Tenth Supplement to the FSAR is the same as the QA Program which we had previously reviewed and found acceptable.
4.0 CONCLUSION
S Our conclusions as stated in the Safety Evaluation Report remain I unchanged.
g ,g=
.