ML20151E037

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SALP Rept 50-416/88-09 for Facility for Nov 1986 - Apr 1988. Continued Superior Performance Noted in Areas of Radiological Controls,Security & Outages & Significant Improvement in Plant Operations & Fire Protection
ML20151E037
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 07/08/1988
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20151E027 List:
References
50-416-88-09, 50-416-88-9, NUDOCS 8807250340
Download: ML20151E037 (41)


See also: IR 05000416/1988009

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ENCLOSURE

SALP REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION

REPORT NUMBERS

50-416/88-09

System Energy Resources, Inc.

Grand Gulf

November 1, 1986 through April 30, 1988

8807250340 88070s

PDR ADOCK 05000416

O PDC

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-I. INTRODUCTION

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The : Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC <taff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance based upon this

information. The SALP-is supplemental to normal regulatory processes used

to ensure compliance with NRC rules and regulations. The SALP is intended

to be sufficiently diagnostic to provide a rational basis for allocating

NRC resources and. to provide meaningful guidance to the licensee's

management to_ promote the quality and safety of plant construction and

operation.

An NRC SALP Board, composed of the staff members listed below, met on

June 13, 1988, to review the collection of performance observations and

data to assess the licensee performance in accordance with the guidance in

NRC Manual Chapter 0516, "Systematic Assessment of Licensee Performance."

A summary of the guidance and evaluation criteria is provided in Section

II of this report.

This report is the SALP Board's assessment of the licensee's safety -

performance for the Grand Gulf facility for the period November 1,1986

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through April 30, 1988.

SALP Board for the Grand Gulf facility:

L. A. Reyes, Director, Division of Reactor Projects (Chairman)

A. F. Gibson, Director, Division of Reactor Safety, RII

J. P. Stohr, Directer, Division of Radiation Safety and Safeguards, RII

0. M. Verrelli, Chief, Projects Branch 2, ORP, RII

E. G. Adensam, Director, Project Directorate II-1, NRR

R. C. Butcher, Senior Resident Inspector, Grand Gulf, ORP, RII

L._L. Kintner, Senior Project Manager, Project Directorate 11-1, NRR

Attendees at SALP Board Meeting:

K. D. Landis, Chief, Technical Support Staff (TSS), DRp, RII

H. C. Dance, Chief, Project Section 2B, DRP, RII

L. P. Modenos, Project Engineer, Project Section 28, DRP, RIl

J. L. Mathis, Resident Inspector Grand Gulf, ORP, RII

II. CRITERIA

Licensee performance is assessed in certain functional areas depending

upon whether the facility has been in the construction, preoperational, or

operating phase. Each functional area normally represents an area which

is significant to nuclear safety and the environment and which is a normal

programmatic area. Some functional areas may not be assessed because of

little or no licensee activities or lack of meaningful observations.

Special areas may be added to highlight significant observations.

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'One or more of the following evaluation criteria were used to assess each

functional area; however, ~ the SALP Board is not limited to these criteria

and others may have been used where appropriate.

A. Mar,agement involvement in assuring quality

B. . Approach to the resolution of technical issues from a safety

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C. Responsiveness to NRC initiatives

10. Enforcement history

E.. Operational and construction events (including response to, analysis

of, and corrective actions for)

F. Staffing (including management).

G. . Training.and qualification effectiveness

Based upon the SALP Board assessment, each functional area evaluated is

classified into one of the three performance categories. The definitions

of these performance categories are:

Category 1: Reduced NRC attention .may be appropriate. Licensee

management attention and involvement are aggressive and oriented

toward nuclear safety; licensee resources are ample and effectively

used so that a high level of performance with respect to operational

. safety or construction is being achieved.

Category 2: NRC attention should be maintained at normal levels.

Licensee management attention and involvement are evident and are

concerned with nuclear safety; licensee resources are adequate and

are reasonably effective so that satisfactory performance with

respect to operational safety or construction is being achieved.

Category 3: Both NRC and licensee attention should be increased.

Licensee management attention and involvement is acceptable and

considers nuclear safety, but weaknesses are evident. Licensee

resources appear to be strained or not effectively used so that

minimally satisfactory performance with respect to operational safety

or construction is being achieved.

The functional rea being evaluated may have some attributes that would

place the evaluation in Category 1, and others that would place it in

either Category 2 or 3. The final rating for each functional area is a

composite of the attributes tempered with the judgement of NRC management

as to the significance of individual items.

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The SALP Board may also include an appraisa' of the performan'ce trend of a

functional area. This performance trend will only be used when both a

n definite trend of performance within the evaluation period is discernable .

and the Board believes that continuation of the trend may result in a

change of performance level. The trend, if used, is defined as:

Improving: Licensee performance was determined to be improving near the

close of the assessment period. -

Declining: Licensee performance was determined to be declining near the

'close of the assessment period.

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III. SUMMARY OF RESULTS

A. Overall Facility Performance

The responsibility to maintain and operate the Grand Gulf Nuclear

Station-was turned over to System Energy Resources, Inc. (SERI) from

Mississippi Power and Light (MP&L) on December 20, 1986 following NRC

review and approval. Middle South Utilities, Inc., announced the

formation of SERI on July 28, 1986, in order to bring about a

concentration of leadership, management, financial, engineering and

other technical talent to place strong management attention in

operating a nuclear facility.

On May 9, 1988, SERI announced plans to assume management and

operating responsibility for the Middle South Utilities (MSU) nuclear

operations. SERI is a wholly-owned subsidiary of MSU. Under the

plan, SERI will assume operating responsibility for MSU's four

nuclear units: Arkansas Nuclear One, Units 1 and 2; Waterford 3 and

Grand Gulf Unit 1. All necessary regulatory approvals and corporate

arrangements are expected to be completed by December 31, 1988.

Overall performance has shown a measurable improvement. Continued

superior performance was noted in the functional areas of Radio-

logical Controls, Security and Outages. Significant improvement was

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evident in the areas of Plant Operations, and Fire Protection result-

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ing in a SALP rating change from Category 2 to Category 1. Emergency

Preparedness and Maintenance areas were rated Category 2 with an

improving trend and the licensee is encouraged to maintain their

level of effort in these areas. One new area rated was Engineering

Support which was rated Category 2. There were no areas rated as

Category 3. During this evaluation period there were approximately

the same number of inspections as the previous SALP period including

three special inspections: Probabilistic Risk Assessment, Environ-

mental Qualification and Emergency Operating Procedures. There were

22 noncompliances identified versus 38 noncomoliances for the previous

SALP period. There were no escalated enforcement issues.

A concern noted through several functional areas is related to the

quality and adherence to procedures. Specifically, failure to follow

procedures and failure to establish acceptance criteria and tolerance

in the surveillance area,

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The licensee has initiated several organizational changes to

distribute workload, censolidate and strengthen functions to effect

improved performance. Organizational changes included new positions

for the manager of emergency preparedness, a site controller and an

administrative assistant reporting to the general manager. The

licensee has attempted to upgrade the operational knowledge of all

key personnel. Key Managers / Superintendents currently maintain or

previously held Senior Reactor Operator licenses.

SERI's college degree program was started in September 1985 and

brings the college faculty to the job site. The first person to

graduate from this program, a supervisor in the Training Department,

received a Bachelor of Science degree in Nuclear Engineering

Technology.

As a result of an Institute of Nuclear Power Operations (INPO) audit

of September 1987, the licensee received a rating of exemplary overall

performance. Industry standards of excellence were met in many areas

and no significant weakness were noted. Full INP0 accreditation was

achieved.

Unit 2 construction activities are essentially stopped. Therefore,

Unit 2 was not evaluated for this assessment period.

B. The performance categories for the current and previous SALP period

in each functional area are as follows;

May 1, 1985 - November 1, 1986 -

Functional Area October 31, 1986 April 30, 1988

Plant Operations 2 1

Radiological Controls 1 1

Maintenance 2 2 Improving

Surveillance 2 2

Fire Protection 2 1

Emergency Preparedness 2 2 Improving

Security 1 1

Outages (includes refueling) 1 1

Quality Programs and 2 2

Administrative Controls

Affecting Quality

Licensing Activities 2 2

Training 2 2

Engineering N/A 2

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IV. Performance Analysis

A. Plant Operations

1. Analysi s .

During this assessment period, inspections were performed by the

resident and regional inspection staffs.

Overall facility operation has shown definite improvement. The plant

scram rate was 0.5 per 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> critical at power (i.e., >15%)

versus approximately 2 scrams per 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> critical for the previous

SALP period. The overall Nuclear Industry average is slightly less

than 1.0 scr m per 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> critical for this period. Marked

improvements have been identified in the reduction of scrams at

power. All five scrams from power were the result of equipment

problems, but the root cause for some of the scrams indicates they

could pessibly have been prevented. For example, a scram on August 6,

1987, resulted from moisture condensation in a switchyard control

cabinet creating a short in a lockout relay resulting in the

inadvertent opening of two switchyard breakers. A reactor scram on

March 15, 1988, resulted from a loose screw in a terminal box that

had deenergized the Division 1 solenoids on 29 scram pilot valves,

causing 29 control rods to insert (scram) when a surveillance was run

on Division 2 and causing a reactor scram on reactor vessel low water

level. Four scram signals received while in shutdown indicates that

improvements are needed in management controls during shutdown

operations. Of the four scrams while non-critical, two were due to

personnel error ard one was due to procedural error. The fourth

scram was due to equipment failure. A scram reduction program

initiated in early 1985 has been effective. Ten scram reduction

program items, six of which were hardvare changes, were completed

this SALP period. The plant set a boiling water reactor world record

of a 171 day run for the second fuel cycle.

The licensee has initiated a review board consisting of the

Manager-Plant Maintenance, Manager-Plant Operations and Manager-Plant

Support to meet and review each incident involving a personnel error

and provide a written report of their findings and recommendations to

the General Manager, Some plant management personnel recently

completed a one week INPO training course entitled Human Performance

Evaluation Systems Training. Since human performance problems are a

major contributor to significant events, programs that reduce the

occurrerce of human performance problems contribute significantly to

increased safety. This program has been termed the Near Miss program

because that is the essence of the program, to identify near miss

situations that could affect plant operability or safety. The

employee is provided p'otection from reprisal for incidents in order

to encourage reporting of near miss situations.

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To improve the actual operational experience level of other

organizations, several licensed operators have been temporarily or

permanently assigned to other areas. Some cross utilization of

licensed operators was as follows: In July 1985, a Senior Reactor

Operator transferred to the Training department and returned to

Operations in July 1987. In December 1987, a Reactor Operator

transferred from Operations to the Training Department. In

February 1988, a Senior Reactor Operator and a Reactor Operator

transferred from Operations to the Training Department. In July

1987, a Senior Reactor Operator transferred to the Outage Scheduling

Department to help prepare for the second Refueling Outage that

started November 1987. He transferred back to Operations in January

1988. In March 1987, a Reactor Operator transferred to Quality

Programs and returned to Operations in Fabruary 1988. In January

1988, another Reactor Operator transferred to Quality Programs. The

rotation of these individuals enhanced the operational experience

level of the various support groups.

The licensee is responsive to NRC conorns that have been ider.tified

to them. An example of this is an issue regarding operations

personnel potentially having restricted access to some areas of the

plant during emergency events. A comment to this effect was made

during the special operational safety inspection on Probabilistic

Risk Assessment. In November 1987, a standing order was issued

requiring four operators plus the fire brigade leader to carry

security series keys that a? low passage in case of key card fa' lures.

Previously, only the fire brigade leader had carried a security

series key.

The licensee is committed to improving operations. During the second

refueling outage a control room redesign was incorporated. The Shift

Supervisor's office is now accessible thru a glass window arrangement

such that people processing work authorizations now enter thru a door

i outside the control room. This limits control room congestie and

l noise. The Shift Superintendent's desk and the control room

l operator's desk were both elevated to enhance control room

l visibility. The simulator has also been updated to reflect the

! actual control room configuration. A set of management standards was

developed to be used in the day-to-day execution of operations

duties. These management standards define such things as control

room command ano organization, communications, thif t turnover, and

conduct of rounds. Another initiative just getting started is the

movement of the Shift Technical Advisors from the Technical Support

section to the Operations section. The intent is to send those Shift

Technical Advisors that volunteer through the Senior Recctor Operator

program. This will increase the number of available Seniar Reactor

Operators who hold a college degree. Additionally, the Operations

Suerintendent has four licensed Senior Reactor Operators as

assistants in addition to those on shift. NRC observat'ons confirmed

that the plant has had an ef fective claanliness and nousekeeping

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program with periodic scheduled cleanup days where all personnel are

. involved. Control room decorum has improved over the previous SALP

period. The conduct of shift personnel in the Control Room is

professional. The licensee has an active program to reduce the

number-_of illuminated annunciators during operation. The number of

lit annunciators has been drastically reduced since initial startup.

The licensee's goal is to achieve a black boar'd.during power operations

The NRC also observed a high morale of plant personnel which reflects

positive management involvement in daily activities. Management has

also strived to provide operators with essential tools for the conduct

of routine operations, such as up to date ari legible drawings and

procedures. The plant operating procedures are clearly written

'and thorough. There has been no turnover of licensed personnel.

During this evaluation period 39 LERs were submitted by the licensee.

The LERs were evaluated by the NRC staff to determine the event

cause. The number of LERs caused by personnel errors was 24 for this

SALP period as opposed . to 59 during the previous 'SALP period.

Although there was a reduction in the number of LERs, personnel error

still stood out as the number one root cause of LERs and should

receive. increased management attention.

The LERs adequately described all the major aspects of the event,

including all component or system failures that contributed to the

event and the significant corrective actions taken or planned to

prevent recurrence. The reports were thorough, detailed, and

generally well written and easy to understand. The quality and

preciseness of the information in the LERs was high. The narrative

sections typically included specific details of the event such as

valve identification numbers, model numbers, number of operable

redundant systems, the date of completion of repairs, etc., to

provide a good understanding of the event. The root cause of the

event was clearly identified in most cases. Previous similar

occurrences were properiy referenced in the LF.Rs as applicable except

for two LERs which required resubmittal. lhe licensee updated

' several LERs in the assessment period. The updated LERs provided new

'information, denoted by a vertical line in the right hand margin, se

that the new information could be easily determined by the reader.

We note that Grand Gulf updated LERs when the corrective actions

listed in the original LERs were completed.

There were two violations identified in the Ooerations area The

decreased number of violaticos indicate a significant improvement

over the previous SALP period in which ten violations were

identified, This improvement reflects 'a increased operational

experience of the operations personnel and a dedicated effort by

operations personnel and management to improve performance. The two

violations do not indicate a programmatic deficiency but are in the

area of failure to follow procedures which needs more attention.

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a. . Severity Level IV Violation for failure to follow procedures to

properly store -nitrogen bottles within containment.

(416/88-01-01)'

tn Severity Level V Violation for failure to follow procedures and

" implement coldfweather oreparations.

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(416/87-29-02)

2. Conclusion

Category: 1

3. Recommendations

A high level cf performance was achieved in this area. The NRC

staff resources applied to the routine inspection program should.

be' reduced.

B. Radiological Controls

1. Analysis

During this hssessment pericd, inspections were performed by the

resident and regional inspection staffs. Eight routine radiation

protection, radwaste and chemistry inspectio7s were performed durino

the _ assessment period including one confirmatory measurements v'

inspection. One special inspection was performed in response to

hydrogen burn in the charcoal beds of the offgas adsorber system.

The licenset's health physics staffing levels were appropriate and

compared well to other utilities having a facility of similar size.

The licensee has budgeted 70 health physics positions , 68 of which

were filled as of April 30, 1988. During the assessment period, the

licensee added three new supervisory positions for dosimetry

processing, dosimetry administration, and instrumentation. The

licensee added an additional health physics crew to the rotating

shift schedule to allow a dedicated week for training purposes in the

b rotation. The plant Health Physicist / Technical Assistant osition

also-became a permanent staff position during the assessment period.

An adequate number of ANSI qualified licensee and contract health

physics technicians were available to support routine and outage

operations. The licensee did not rely on contract personnel to

support routine operations or supplement technical capabilities.

While the licensee was able to obtain all of the contract personnel

needed, the licensee has recognized the shortage of health physics

contract support help available in the industry. The licensee is

participating in a Middle South Utility System Task Force

investigating ways to meet health physics manpower needs for the

future.

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The knowledge and experience 1.evel ' of the site health physics

personnel were good. The health physics personnel have an effective

training program. The licensee received Institute of Nuclear Power

Operation-(INPO) accreditation of their Health Physics and Chemistry

Training programs in June 1987.

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The radiological effluent and radwaste staffing levels were adequate

with a quality training program that is presented by knowledgeable

and well- qualified instructors. The chemistry personnel have strong

'and capable managers and supervisors with a stable and espable staff

of technicians.

The performance of the health physics personnel in support of routine

. operations and outages was good. No substantive issues were

identified in this area. Only one radiation protection related

violation (for failure to follow procedures) was identified during

the assessment period and that violation was identified by the

licensee.

Management support and involvement in matters related to radiation

protection 'and radwaste control was very good as evidenced by

approval of the newly created and filled health physics positions.

Management support for ALARA and radioactive protection programs

included the procurement of equipment such as a cavity dall

decontamination device, remote closed circutt TV's, and computer

programs developed to track calibration ad inventory of portable

radiation survey instruments. The pie is radiation protection

manager received the support of other plant managers in implementing

the radiation protection program.

Resolutions of technical issues by the healtL physics personnel was

good as evidenced by their actions associated with defective

thermolumin'escent dosimeters (TLDs). The health physics personnel

. identified a problem with vaporization of the TLD material,

discontinued use of their own system and obtained contract TLD

service while investigating the problem. They identified the source

of the problem and modified the readout temperature parameters as

recommended by the TLD vendor. The licer.see returned their TLD

system ' to service after verification that the problem had been

corrected. The lice.1see also provided periodic updates to NRC staff

on the progress of its corrective actions.

Responses to NRC initiatives were conducted in an effective and

acceptable manner as evidenced by the licensee's willingness to

improve plant fuel handling procedures for radiological safety

considerations and improve the bases for dosimetry programs through

additional energy spectrum measurements and dose algorithm documenta-

tion. The licensee revised refueling procedures to address ALARA

considerations and communication requirements for haalth physics and

operations personnel. The procedures require operations personnel to

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notify health physics personnel prior to movement of the first' fuel

bundle from the reactor -core and to restrict -the movement of fuel

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bundles over the downcomer -region except to directly enter or exit

the-cattle chute.

The . licensee's ' radiation . work permit and respiratory protection

programs were found :to be satisfactory. The number of Personnel

~ Contamination Reports declined during the assessment period. The

licensee ended.1986 with 246 personnel contamination reports, 168 cf

which included skin contamination. In 1987, the personnel

contamination reports decreased to 156 of which 96 included skin

contamination for decreases of 63% and 57% respectively. As of

April 30, 1988, the licensee had documented 31 cases of personnel

contamination which included 14 cases of u skin contamination. The

licensee has developed procedures addressing hot particles, however,

hot particles were not an exposure problem during the assessment

period. The number of personnel having a positive indication of

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internal contamination decreased during the assessment period. In

1986, the licensee documented 15 measurements of persons having more

e that 1 % maximum permissible organ burden (MP0B) and less than 5%

MP0B and only 1 person within that range in 1987, and 1 person

through April 30, 1988. The licensee did not have any whole body

measurements in excess of 5% MP0B in 1986, 1987, or through April 30,

1988. The licensee attributes the reductions of positive

measurements to improved training programs and improved worker

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experience.

At the end of 1986, the licensee had 31,166 square feet (f t 2 ) of

contaminated area which represented 6.3% of the radiologically

controlled area of the plant. The licensee had reduced t..e

contaminated area down to 19,125 f ' or 3.1% of the . radiologically

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-controlled areas by April 30, 1988. Management attention in

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investigating contamination sources and increased ef ficiency of the

assigned decontamination crew ere factors which have helptd the

licensee reduce the contamination area.

The 1986 and 1987 cumulative radiation exposures were 436 and

399 person-rem, respectively. This compares favorably to the

national average exposures of 622 person-rem per unit in 1986, and

521 person-rem per unit in 1987, at other BWR facilities. The

licensee als: met their ALARA goals of 600 person-rem in 1986, and

425 person-rem in 1987. Through the end of April 1988, the licensee

had accumulated 64 person-rem and had established a person-rem goal

of 160 person-rem in 1988 when no refueling outages are planned. The

licensee attributes the success in meeting its 1987 goal to better

planning and involvement between the plant groups. The licensee

added two ALARA Specialists to its personnel during the assessment

period and utilized the experience gained form the first refueling

outage in planning and determining person-rem per task. The ple.rt

personnel improved their efficiency at certain tasks as h unstrated

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by an' Intermediate Range Monitor (IRM) replacement job that was

c performed in the first refueling outage-- in 29 hours3.356481e-4 days <br />0.00806 hours <br />4.794974e-5 weeks <br />1.10345e-5 months <br /> with

0.46 person-rem and repeated in the second refueling outage at

slightly elevated dose rate fields in -only 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> with

0.11 person-rem. Improvements.in radiation dose exposures were noted

in auxiliary. and feedwater control valve work, tne installation of

temporary shielding and routine fuel movement activities.

During 1986, the licensee disposed of 17,564 cubic feet (ft ) of

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solid waste containing 1360 curies. The volume of solid waste

decreased in 1987 to 13,833 ft3 while the activity increased to

1663 curies. As of April 30, 1988, the licensee had shipped 8895 ft3

of solid waste containing 196 curies. The licensee experienced some

leakage in one fuel bundle in 1987, which caused the activity of the

radioactive waste to increase. The deteriorated fuel was removed

during the second refueling outage. The licensee has a waste volume

reduction plan which includes surveys, sorting, and segregation cf

waste into clean or contaminated waste for release to burn. The

licensee placed emphasis on reducing radioactive waste volume by

limiting the material entering the radiological controlled area.

Liquid and gaseous radioactive effluents were within the Technical

Specification l i mi t:, and in compliance with 40 CFR 190 limits for

radiation dose and radioactivity concentration in effluents. In

general the total amounts of radioactive effluents has increased over

the past three years; however, the liquid and gaseous releases were

less . than the average annual releases reported by four Region II

plants of similar size and type for 1986. There were no unplanned

liquid or gaseous releases above limits required to be reported to

the NRC during the evaluation period. Annual effluent release and

dose summaries for 1985-1987 can be found in Section V.K.

A confirmatory measurement inspection conducted during February 1987,

indicated agreement for all measured isotopes. A simulated liquid

waste sample which contained H-3, Sr-89, Sr-90, and Fe-55 was

provided during May 1987. The licensee successfully analyzed the

liquid spike itnd all results compared favorably (ir agreement) with

the NRC values using the NRC established comparison criteria.

A special inspection was conducted during March 1988 in response to a

hydrogen burn in the off gas system. The inspection determined that

the system integrity did not appear to have been compromised and that

no radiological effluent limits were exceeded during the event. The

cause was attributed to system design defh ancies combined with

temperature monitoring equipment malfunctioning. The licensee

responded promptly and correctly in identifying the problem and

taking corrective actions.

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The- plant made significant improvement in its chemistry control

program in the last year. These advances were attributed to strong

cnd . knowledgeable managers and supervisors who were hired

approximately- two years ago. The plant had been plagued by

microbiological induced corrosion problems throughout its service

water systems and was the first plant in Region II to chemically

clean a safety related system. An inadequate 10 CFR 50.59 safety

evaluation prior to this chemical cleaning resulted in violation b.

below.

Two violations were identified in the Radiological Controls area.

a. Severity Level IV violation fo'r failure to install standby

service water basin chemical addition system as shown on

temporary a1teration. (416/87-10-09)

b. Severity Level IV violation for an inadequate safety evaluation

for chemical cleaning of s tar.dby service water piping.

(416/87-39-01)

2. Conclusion

Category: 1

3. Recommendations

A high level of performance was achieved in this area. The NRC

staff resources applied to the routine inspection program should

be reduced.

C. Maintenance

1. Analysis

During this assessment period, inspections were conducted by the

resident and regional inspection staff. Significant maintenance

activities were performed during the two major refueling outages

during this SALP -period. Inspections were performed on the

-Maintenance program, its implementation and of equipment availability

and accessibility by a PRA-based inspection team.

Licensee management has been responsive to NRC concerns. For

example, inspectors identified the use of excessive amounts of what

appeared to be silicone grease on airlock door seals to enhance

inflatable seal performance and noted that the airlock door seal

testing was not being conducted in the as-found condition. Based on

the inspectors comments, licensee management initiated procedural

changes to test the inflatable seals in the as-found condition and

the use of excessive lubricant on the seals was minimized such that

there is no visible evidence of lubricant.

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The licensee's approach to the resolution of technical issues was

good and management's involvement was evident. Fur ev. ample, during

the second refueling outage the licensee fcund indications of cracks

in the exhaust manifold inlet housing for the turbo-charger on the

Division 1 diesel generator. In two followup telecons the licensee

informed the NRC of their findings and planneJ actions. A final

report was thorough and responsive to the NRC on this issue.

At times maintenance activities were not always well controlled. For

example a valve in the control rod drive hydraulic system was found

with the bonnet removed and with no protection from foreign material

intrusion. A previous event at Grand Gulf documented in IE Informa-

tion Notice 86-89 oi an uncontrolled control rod withdrawal event

where the licensee had concluded that particulate accumulation on a

solenoid operated directional control valve caused an incomplete

closure of that valve allowing drive water pressure to leak past the

valve and force the uncontrolled control rod withdrawal.

The licensee has initiated a Maintenance Improvement Program. In

1986 and 1987 there were multiple assessments by Middle South

Utilities, INPO and other industry groups. Various improvement

initiatives were recommended. One major initiative incorporated to

date includes a new Planning and Scheduling department with a

Planning & Scheduling Superintendent having a Planning Group, a

Scheduling Group and a Maintenance Engineering Group reporting to

him. These tasks were formerly spread out among the Electrical,

Mechanical, and Instrumentation and Control Superintandents.

Another initiative the licensee has taken was to purchase equipment

to perform Motor Operated Valves (MOV) testing in order to determine

the desired torque switch setting for safety related MOVs. The

result of the testing in response to IE Bulletin 85-03 was completed

in January 1988.

The objectives of the maintenance programs inspections were to

determine whether the GGNS maintenance program is being implemented

in accordance with Regulatory requirements, and to determine the

ability of the licensee to conduct an effective maintenance program

on important plant equipment. There were no adverse findings

identified.

The PRA-Based team inspection in October 1987 examined equipment

availability and accessibility. Management involvement and ' nowledge

of maintenance activities was indicated by clear, concise ;rocedures

l provided for maintaining safety-related and balance of plant

components. The licensee's procedures were generally wr 11 prepa ed

especially with regard to technical content and humin factors l

considerations. Minor discrepancies were noted in a fsw procedures

(e.g. , partly illegible figures). Good records were available to

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determine equipment- status. An - automated + racking system for

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maintenance is being developed. The procedures for design control

were judged to be above average. The program calls for updating

control . room drawings within 14 days and other drawings within 90

days.after a plant modification has been completed. This program has

made. significant improvements and appears to be working very well.

Numerous _ questions were raised regarding electrical 6esign and

maintenance practice. These questions were promptly responded to and

generally were accepted as welcomed ideas-to improve plant safety and

maintenance.

Two violations were identified. This reflects a significant

improvement over the previous SALP in which seven violations were

Identified.

.a. Severity Level IV Violation for failure to follow procedures for

procurement of components. (416/88-07-03)

b. _ Severity Level V Violation for failure to document the deficient

reassembly of a relief valve. (416/87-10-04)

2. Conclusion

Category: 2 Improving

3. Recommendations

The NRC staff resources applied to the routine inspection

program should be maintained.

D. Surveillance

1. Analysis

During this assessment period, inspections were performed by the

resident and regional inspection staffs. Inspections performed were

associated with the PRA-based team inspection, core power testing,

routine surveillance observation, safety valve testing, and event

followup.

Meetings were held with SERI management during April and June 1987

to discuss NRC concerns in the surveillance area. The licensee has

,

been responsive to NRC concerns and has tcken actions that reduced

the number of missed surveillances. During tne previous SALP period

12 LERs were in the area of missed surveillances out in the current

SALP period only one LER was in the area of missed surveillances.

The total number of LERs in the surveillance area for this SALP

period was 16 as opposed to 26 during the previous SALP period.

Although this shows improvement, there is still need for management

attention.

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Surveillance procedures were not always clear in defining acceptance

criteria. In' many cases the technician in the. field 'was lef t with -

the decision . of what tolerances were acceptable during certain

calibration _ or functional tests. For example, it was noted that

iduring a calibration . step, the procedurc required an LPRM gain

control adjustment to achieve 8.000 DC volts on the digital volt

meter and no tolerance was specified. Licensee personnel involved in -

the_ calibration accepted from 7.990 to 8.010 DC volts which was not

allowed by the procedure. A diesel generator functional test

required that the fuel oil transfer pump should automatically start

when the day tank -level reaches 26 inches and should automatically

stop when the day tank level reaches 39 inches but no tolerance was

specified. The fuel oil transfer pump started and stopped within

approximately one inch of the noted values and was accepted.

An example of an inadequate event followup is the March 2, 1988 trip

of _ the Division 2 Diesel Generator during a surveillance and the

Special Report that was suomitted. Ther_e were several erroneous

statements in the Special Report that were corrected during a telecon

on March 31, 1988, between NRC Region II and licensee management

regarding this event. A second similar diesel trip had occurred on

March 30, 1988, and the Special Report was revised to correct the

reason for the diesel trips and other erroneous statements. The

licensee has subsequently experienced similar diesel generator trips

that may be related to the events discussed in the Special Report.

The licensee and the diesel manufacturer are presently investigating

the. trips.

Surveillance programs for electrical switchyard equipment, emergency

diesel generators and standby service water system were inspected

during the PRA-Based- inspection conducted in October 1987.

Procedures were examined, some tests were witnessed and past test

records were reviewed. Generally, the procedures were well written,

clear and concise. Records are complete and well maintained and the

procedures appear to be followed.

One deviation _was identified which involved failure to complete a

functional surveillance test on protective relay systems. The FSAR

committed to a functional test of the relays and control equipment on

a two year or less frequency. This test was last done in June 1983,

almost 4-1/2 years late. The licensee researched this finding and

took prompt corrective action. The problem was attributed to

interface problems involving two separate organizations. All other

safety-related and balance of plant surveillance activities inspected

were found satisfactory.

Safety relief va!ve (SRV) set point testing and safety relief valve

logic system function testing was also inspected. Several safety relief

valves experienced set point drift that exceeded Technical

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GGNS guidelines requiring further disassembly and inspection. The

greatest deviation was 6.1%. There was no evidence of the cause of

drift. Other valves required setpoint readjustment. NRC has issued

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several Information Notices concerning SRV failure to lift. Review

of _ licensee procedures indicate . technically sound and thorough

responses to these information notices.

Reactor core stability testing was conducted in a well organized

manner. Personnel present performing the test were knowledgeable

about the testing to be performed, Management took an active part in

insuring the testing would be performed as scheduled and that the

< plant would.not be maneuvered into operational regions not called out

in the' test or into operational regions where core thermal limits

would be approached. The test was being performed voluntarily to

take data in regions of operation estimated to be approaching

instability. .The test verified actual stability was higher than

estimated.

The licensee's improved program for core power distribution

monitoring, and analysis and control of thermal limits reflects a

considerable investment in equipment and human resources. The major

equipment investment is in two . computers, 'each redundant to the

other, in order to perform rapid online analysis not possible in the

originally -installed system, which now functions primarily as a data

link to the new computers. In addition, the licensee has installed

computer terminals at the residences of three specially and

intensively trained engineers, one of whom is always on call. This

effort has provided operations around-the-clock, on demand

assistance. This assistance includes prediction of control rod -

movement effects on thermal limits, fuel preconditioning, and fuel

utilization; all derived from the capability to perform full-core,

three-dimensional calculations in a matter of minutes.

Five violations and one deviation were identified. Although the

violations are diverse and do not indicate a programmatic deficiency,

they do reflect a lack of attention to detail.

a. Severity Level IV violation for failure to provide and implement

an adequate procedure for the surveillance testing of the

Standby Liquid Control System. (416/87-14-03)

b. Severity Level IV violation for failure tu document and evaluate

test discrepancies during Standby Liquid Control System Testing.

(416/87-26-03)

c. Severity Level IV violation for failure to document nitrogen

hookup to offgas system charcoal beds and the inadvertent

actuation of an ECCS. (416/88-03-01)

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d. Severity Level V violabon for failure 4 determine normal

indicated delta pre.-sure and set LPCS and LPCI header delta

. pressure instrumentation as required by T! 4.5.1.c.2(b).

(416/87-40-01)

e. Severity Level V violation for failure to follow procedures for

the'IRM. Range 6 to Range 7 correlation ter . (416/86-39-07)-

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f.. . Deviation' for failure to perform functional check on 500 KV

relay system as committed in the FShR. (416/87-27-01)

1

2 .- Conclusion-

Category: 2

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. 3. Recommendations

The-Board noted that' inadequate procedures resulted in increased

ESF: actuations. Additionally, acceptance criteria was

inadequate .in that it did not clearly specify tolerance bands.

'The NRC - staf f resources ~ applied to the routine inspection

program should be maintained.

E. . Fire Protection

1. Analysis

During this assessment period, inspections were conducted by the

. gional and' resident inspection staff to review the licensee's

implementation of the fire protection program and followup on

previously ' identified enforcement matters.

The . licensee has issued revisions to procedures for the

administrative control of fire hazards within the plant, surveillance

and maintenance of the fire protection systems and equipment, and

organization and training of the plant fire brigade. These

procedures were reviewed during the staff inspections and found to

meet NRC requirements and guidelines.

The staff inspections also reviewed the licensee's implementation of

the fire preventive administrative controls. General Nusekeeping

arid control of combustible and flammable materials in safety-related

plant areas were found to be very good. The fire protection

extinguishing systems, fire detection systems and fire barrier

assemblies protecting plant systems required for safe shutdown were

found to be functional. In addition, the surveillance inspections,

tests and maintenance instructions for the plant fire protection

systems were found to be very good and they met the criteria of tne

plant technical specifications.

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The~ annual fire protection / prevention audit and 24 month QA fire

protection program audit by offsite organizations' and the triennial

audit by an outside fire protection l organization required by .the

technical specifications were. reviewed. These audits were conducted

within the specified frequency. .The licensee had implemented the

corrective actions on discrepancies identified by these audits.

, Management involvement and cont'rol in assuring quality in the fire

=

protection program is evident due to' the well developed, issued and

. implemented fire protection administrative procedures. The

. licensee's approach to resolution of technical fire protection issues-

indicates an understanding of issues, and is sound and timely. The

responsiveness to NRC initiatives are timely and thorough. Fire

protection related violations are rare. When violations do occur,

effective corrective action is promptly taken. Fire protection

related events and discrepancies identified by the licensee are

properly analyzed and promptly reported and effective corrective

actions are taken.

The organization and staffing of the plant fire brigade is adequate

to meet NRC guidelines. Fire protection personnel are identified and

authorities' and responsibilities are clearly defined. Personnel

. appear well qualified for their assigned duties.

Management attention to the fire protection area is evident from the

large reduction in the number cf outstanding limiting conditions for

= operation in-this area during this SALP period.

No violations were identified in this area.

2. Conclusion

Category: 1

3. Recommendations

A high ' level of performance was achieved in this area. The NRC

staff resources applied to the routine inspection program should

be reduced.

F. Emergency Preparedness

1. Analysis

During the assessment period, inspections were performed by resident

and regional inspection staffs. These included observation of the

annual emergency prep'a redness exercises in December 1986 and November

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The ~ two emergency exercises during this assessment period reflected

the increased management attention being directed to improving the -

emergency preparedness program. . Weaknesses noted in the report of

the previous assessment period were corrected. There were no

exercise weaknesses observed during the exercises and only five minor

observations that warranted attention / improvement by . the licensee.

The exercise observations indicated that the primary responsibilities

for emergency response by site personnel. and supporting corporate

staff had been.specifically established and could be implemented in a

timely and effective manner. The emergency organization used its

emergency classification and action level scheme to promptly and

properly classify the emergency situations. The required

notifications were made promptly and protective action

recommendations were made correctly in accordance with procedures.

The emergency personnel demonstrated effective teamwork in accessing

and mitigating the postulated accident scenarios.

The routine inspections disclosed that the licensee had an adequate.

' emergency preparedness program for emergency detection and

classification, protective action decision-making, shift staffing and

augmentation, notifications and communications, changes to the

emergency preparedness program, and licensee audits. The knowledge

and performance of duties were found adequate with the exception of a

violation for failure to provide training for two emergency response

personnel in accordance with the emergency plan procedure. It was

also'noted that training records needed te be maintained better.

In order to place greater emphasis on Emergency Preparedness, the

licensee created the position of Manager of Emergency Preparedness

who answers directly to the Vice President, Nuclear Operations.

The licensee has been responsive to NRC concerns. For example, in the

inspection report citing Violation b. below, the inspectors also

-noted concerns regarding the licensee's overall alert notification

system. In response, the licensee developed an extensive long term

and short term corrective action program involving procedural,

- training and equipment changes. Within thirty days, the existing

Claiborne County transmitter and antenna were replaced to increase

system reliability. The licensee is procuring a computerized siren

activation and monitoring system which will provide the local

government agencies the capability to monitor the status of each

siren from the control station. The new system will eliminate the

need for manual data retrieval as presently required. The licensee

now expects to have the new system installed by July 1988.

i As part of the transition from MP&L to SERI, the licensee presented

l an Emergency Preparedness Transition Plan to the NRC. The transition

has been accomplished smoothly and in a professional manner with no

impact on emergency preparedness capability. To ensure the NRC was

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kept aware of the SERI change over status, the licensee held

L quarterly update meetings.

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Two violations' were identified.

a. Severity Level IV violation for failure to provide training for

emergency response personnel in accordance with emergency plan

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procedure-(416/87-16-01).

.b . ' Severity Level IV violation for failure to notify -the NRC of

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alert notification failure. (416/87-18-05)

'2. Conclusion

Category: 2' Improving

3. Recommendations

The Board noted that management attention and initiative is high

with day to day involvement resulting in significant effort

towards correcting previous -issues. The NRC staff resources

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applied to the routine inspection program should be maintained.

G. Security

1. Analysis

During this assessment period, inspections were performed by the

resident and regional inspection staffs. There is clearly

demonstrated a continued strong management support of the security

. program at both corporate and . site levels. The site security force

continues to implement and enforce regulatory requirements in an

effective and aggressive manner. The contract security force

productivity is assured - by application of credible supervisory

expertise and professional managerial oversight by . proprietary

managers as evidenced by . the effectiveness of the security force

noted during inspections.

The licensee continued to demonstrate awareness of changes and new

requirements prescribed by . regulatory directives and initiated

necessary changes to -plans and procedures in a timely manner.

Changes to physical security, safeguards contingency and security

-training and qualification plans are detailed and clearly define

commitments and implementing requirements. The manner and timeliness

in which the licensee implemented the provision of 10 CFR 73.57 with

regard to submissions of fingerprint cards for all personnel

requiring protected area access to safeguards information was

noteworthy. The licensee has also been responsive to NRC concerns.

For example, in response to NRC comments regarding the lack of

clarity of ~ the image on x-ray equipment, the licensee replaced the

existing x-ray machines with improved model X-ray machines with

greater resolution.

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~As previously reported, the licensee.has not finalized their decision

.on upgrading the interim protected area barrier between the-

operational Unit ~1 and Unit 2. Their decision' has been delayed

.pending the final resolution of Unit 2. However, in the interim the

' licensee: has enhanced the security of the interim barrier beyond

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-commitments of the Physical Security - Plan by installing intrusion

detection equipment on the roof of the control and turbine buildings-  !

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and increasing the frequency of security patrols.

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The ~ licensee continues to log and report as appropriate, physical

security events in accordance with 10 CFR 73.71 accurately and in a

timely manner except as noted below. During the first quarter of

FY-88 the licensee conservatively reported under the revised criteria

of 10 CFR 73.71, a total of 312 physical security events. Unit 1 was

undergoing a refueling _ outage during this period, and _ many of the

events were intrusion alarms attributed to outage personnel failing

l- to adhere to access control procedures. During the second quarter of

FY-88 the event rate was reduced by 65% to a total of 109 events

which.is partly attributed to additional guidance provided by the NRC

l

on.reportability under 10 CFR 73.71.

! A special inspection during this assessment period confirmed the

i occurrence of two licensee identified violations relating to a delay

'

in response to an intrusion alarm from a vital area door and

exceeding the one hour reportability requirement. The licensee's

corrective- actions were in accordance with criteria for categoriza-

tion as licensee identified violations and no violations were cited.

No violations were identified in the security area.

2. Conclusion

Category: 1

3. Board Recommendations

A high level of performance was achieved in this area. The NRC

staff resources applied to the routine inspection program should

be reduced.

H. Outages

1. Analysis

i

During this assessment period, inspections were performed by the

[

resident and regional inspection staffs. Two major refueling outages

occurred during this SALP period.

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The . first refueling outage started on September 5, 1986, and was

- scheduled to end on November 22, 1986. Reactor restart was initiated

on November 30,1986 but while attempting to roll the turbine for the

-turbine overspeed trip . test, damage to the turbine / generator rotor

and number 10 bearing was discovered. A wrench socket had

inadvertently been left in the bearing during outage work. -The plant

resumed corenercial operation on ' January 9,- 1987. The major tasks of

the first re 'ueling outage were the rework of the cooling tower for

inc eased efficiency, the replacement of 264 fuel bundles in the

reactor core, the modification of the A standby service water system

for increased capacity, the disassembly and inspection of the

Division 2 diesel generator and the license conditions requiring

modifications. The plant General Manager held meetings on January 8

& 9, 1987-to discuss GGNS performance during 1986 with all employees

and to. discuss lessons learned from the first refueling outage.

The second refueling outage began on November 7, 1987, with a

scheduled .startup date of January 5,1988. The plant went back on

line January 6, 1988. Major work items during the second refueling

outage consisted of disassembly / inspection of one low pressure

turbine with rotor disc UT inspection, replacement of 288 fuel

bundles, reactor vessel internals inservice inspection, disassembly

and inspection of the Division I diesel generator, chemical cleaning

of the standby service water basin and flow balance, chemical

cleaning of the circulating water system, installation of an on-line

condenser tube - cleaning system, control room redesign work and

standby liquid control system redesign work.

The refueling floor activities were conducted in a controlled manner.

The actual fuel handling was accomplished by GE personnel with a SERI

Senio. Reactor Operator in charge of the refuel floor. A Senior

Reactor Operator remained on the refueling bridge during actual core

alterations conducted from the refueling bridge. One event occurred

where a polar crane operator attempted to move a reactor vessel head

stud tensioner over the corner of the upper containment pool fue.1

storage racks. Only new fuel was stored in this area but Technical

Specifications prohibit loads over 1140 pounds being moved over this

area. The Senior Reactor Operator on the refuel floor stopped the

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crane but not before it reached the corner of the fuel storage racks.

The licensee required GE to formalize their control over refueling

floor activities and added a SERI manager on the refuel floor to

oversee GE's performance until adequate performance was demonstrated.

Management was heavily involved in the planning and scheduling of the

refueling outages. Management attention was evident due to the

assignment of key personnel to major work areas. An experienced

Senior Reactor 09erator was assigned to the Outage Scheduling group

in July 1987 to help prepare for the November 1987 outage and the

Technical Assistant to the Manager, Plant 7perations, who holds a

Senior Reactor Operator license, was assigned as the Outage Director.

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One event that displayed management involvement concerned a stuck

fuel bundle. On November 19, 1987, during a core fuel shuffle a

peripheral fuel bundle could not - be removed within the technical

specification limit of-1200 pounds on the refueling platform bridge

main hoist. The licensee with GE's assistance evaluated the problem

and with discretionary enforcement relief from the NRC, managed to

remove the stuck fuel bundle without any damage. The~ licensee has

incorporated procedural improvements to prevent the recurrence of

this event.

Plant management was actively involved in plant activities on a daily

basis and was involved ir ensuring that operational decisions were

made at the appropriate level. Plant management has been very

responsive to NRC concerns and their actions have reflected a careful

conservative approach to safety and operational issues. Management's i

conservative approach has been emphasized during outage briefings by {

asking everyone to contribute to meeting the work schedule but not at

the expense of safety or quality. Licensee Management took special

- precautions to minimize potential problems during the outage. For

example, to minimize the potential for draining the reactor vessel,

controls were established to require both the Refueling Floor

Coordinator and the Shift Superintendent to approve manipulation of

any valve which could drain the vessel while the vessel head was

detensioned. A status board was aoded in the control room indicating

the operable ECCS system, the shutdown cooling mode being utilized

and the status of all systems which could cause inadvertent vessel

draining. The duration that two RHR shutdown cooling loops were

inoperable was minimized. Some contingencies added for evacuation

and closure of containment were a temporary containment hatch which

could be set in place in less than five minutes to minimize air flow

between containment and the auxiliary building and the containment

air locks were maintained in a condition where a' least one door

could be manually closed.

Inservice Inspection (ISI) activities were examined in three

inspections conducted during the assessment period. The activities

were found to be closely and effectively monitored and controlled by

licensee manacement. The procedures, work and records were judged

sound and conservative in addressing technical issues and in

implementing responses to NRC initiatives. ISI related issues, such

as those described in NRC Generic Letter 84-11, were found to be

, promptly and satisfactorily resolved. Procedures and records were

complete, technically adequate and well-maintained. Licensee control

of contractors performing ISI was exemplary.

Two violations were identified. During the first refueling outage

one violation was issued with six examples of failure to follow

procedures or failure to have adequate procedures. Additionally,

there were other events that occurred that did not result in a

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violation bu't indicated inadequate control of work activities in the

. plant. The residents discussed their concerns with plant management

and work activities were reviewed by the licensee and better work

controls were established. For example, the Shift Superintendents

duty -station was moved into the. control room and additional reviews

of work' packages was initiated. The rate of incident occurrences

decreased during the latter portion of the first refueling outage.

' During thel second refueling outage, one violation was issued with

four examples of failure to follow procedures ~ or failure to have

adequate procedures. Although the number of events were less than

during the first refueling outage, there still appeared to be an

excessive number and indicates a need for further work control

improvements. Primarily, the events resulted in -the inadvertent

actuation of engineered safety features (ESF) and the reactor

protection system indicating a loss of control of plant status. The

licensee recognizes that violation b. is a repeat of the violation a.

and that additional management controls are still required.

Corrective actions were initiated during the latter part of the

second refueling outage to prevent recurrence of the noted events.

Also, the licensee is conducting a post outage cr'tique to identify

any further programmatic control changes that may be required. Plant

procedure improvement regarding major power outages is scheduled to

be available by the start of the third refueling outage.

a. Severity Level IV Violation with six examples. Four examples of

inadequate procedures resulting in ESF actuations and faulty

equipment installation, one personnel error resulting in an ESF

actuation and one failure to follow procedure resulting in

possible equipment damage. (416/86-37-01)

b. Severity Level IV Violation with four examples. Three examples

of inadequate procedures resulting in an ESF actuation, a

reactor protection system actuation and capping a post accident

pressure sensing line and one example of failure to follow

procedure resulting in an ESF actuation. (416/87-35-01)

2. "onclusion

Category: 1

3. Recommendations

A high level of performance was achieved in this area. The NRC

staff resources applied to the routine inspection program should

be reduced.

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I. Quality Programs and Administrative Controls Affecting Quality

1. Analysis

, During- the assessment period, inspections were performed by the

resident and regional inspection staff.

For the purposes of this assessment, this area is an evaluation of

the ability of the licensee to identify and correct their own

problems. 'It encompasses all plant activities, all plant personnel,

as well as those corporate functions and personnel that provide

services to the plant. The plant and corporate QA staff have

responsibility. for verifying quality. The rating in this area

specifically denotes results for various groups in achieving quality

as-well as the QA staff in verifying that quality.

A QA effectiveness review was performed in March 1988, to assess the

effectiveness of licensee actions to correct weaknesses identified in

selected functional areas during the. September 1986 QA effectiveness

review. Both of these reviews utilized licensee imposed performance

indicators as a basis for assessment.

During the March review, several previously identified weaknesses had

improved. The ' licensee had reduced the number of reactor trips

resulting from- operator errors and/or procedural -inadequacies.

Improvements were made in configuration control, design control and

in the reduction in the number of change notices to design

modifications.

Effective July 1987 the Director, Quality Assurance became the

Director, Quality Programs; the Manager, Nuclear Site QA became the

Maaager, Quality Services; the Manager. Audits QA became the Manager,

Quality Systems; and the position of Manager, Programs QA was

deleted.

To have an effective corrective action program all significant

personnel errors, equipment failures, etc. must be documented for

review and analysis so appropriate corrective actions can be taken to

preclude repetition. Sometimes the licensee was hesitant to document

such events. The residents identified the licensee's failure to

initiate nonconformance reports on discrepancies nott d during Standby

Liquid Control (SLC) system operability testing and SLC system relief

valve functional testing. Violation b. in the Surveillance section

of this report discusses the licensee's failure to document these

discrepancies.

The licensee's program has failed to identify some significant

deficiencies. An example is the event discussed in the Engineering

Section concerning the resident inspector's identification of a

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missing bolt sin a- control rod drive Hydraulic Control- Unit (4CU)

mounting _ structure. .In addition to _ the inadequate Engineering

evaluation, it is significant to note that the work in question had

'been performed by Reactor Controls _ Incorporated (RCI). The licensee

had previously submitted several Potentially Reportable Deficiencies

(PRDs) during the construction phase regarding deficiencies _with work

performed by RCI. The failure to identify the .significant-construction

deficiency even after-the noted concerns indicates a failure in the

-licensee's Quality programs.

One initiative' by the licensee to enhance the audit process was to

H combine the efforts of Quality Programs (QPs) and Radiological and

Environmental Services (R&ES). The licensee observed that QP audits

and R&ES appraisals of similar scope would be performed at approxi-

mately the same time frame placing an unnecessary burden on plant

.

_ personnel. To perform more ef fective audits, the QP audit teams now

utilize the R&ES technical personnel as' technical specialists when

possible for audit functions.

'

The -licensee has shown the ability to correct problems, once

identified, as evidenced by initiating a scram reduction program and

the near miss program, improving f ;el handling procedures, improving

the numbers of missed surveillances and personnel errors leading to

LERs, improving the alert notification system, and . improving the

design . review program. Many of these improved programs were the

result of problems identified by the NRC inspection program.

The licensee was not effective in identifying problems as evidenced-

by poor ; tolerance acceptance criteria in some calibration _ and

. functional tests, functional testing of relays and control equipment

'on a two year frequency, repeat examples of failure .to follow

procedures or inadequate procedure dur.ing refueling activities,

documenting personnel errors and equipment failures so that adequate

corrective action could be taken, problems with HPCS, LPCS, LPCI

header delta pressure, and multiple examples of inaccurate P& ids.

-

No violations were identified.

2. Conclusion

'

Category: 2

3. Recommendations

The NRC staff resources applied to the routine inspection

program should be maintained.

__ . _ - _ _ _ _ _ _ _ _ - - __

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J. Licensing Activities

1. ' Analysis

The licensee's management has been consistently involved in the

planning and assignment of priorities - for licensing activities.

During this rating period, the last half of the first refueling

outage (RF01) was completed (January 6, 1987) and the second refuel-

ing outage (RF02) was completed. Five months prior to RF02, which

began November 6, 1987, the Vice President - Nuclear Operations, Vice

President - Nuclear Engineering and Support, Director -

Nuclear

Licensing and ati propriate licensee managers and supervisors met with

the NRC Director of Project Directorate II-2, NRC Senior Resident

Inspector, and the NRC Project Manager to brief the staff on RF02

activities and schedule milestones and associated licensing activi-

ties needed to support the outage. An outage goal of eight weeks was

set and the actual outage was eight weeks and two days, which demon-

strates good planning and . implementation of the outage modification

and surveillance activities. Decision' making regarding licensing

activities was adequate and had adequate management involvement in

the decisions reached. Reviews were generally timely, thorough and

technically sound. Most of the submittals of licensing actions

needed to support the outage schedule were timely. For example,

requests to defer TDI diesel generator Division II baseline

inspection recommended by the TDI Diesel Generator Owners Group

(submitted June 30, 1987) and installation of neutron monitors to

meet Regulatory Guide 1.97 recommendations (submitted July 1,1987)

were reviewed and approved in October 1987 without the need for

supplemental information. Another request for relief from a commit-

ment to install containment 4 solation valves was submitted early and

amply supported to allow approval in September 1987, before the

outage started. Similarly, requests for changes to Technical

Specifications regarding snubber surveillance and core alterations

were submitted in a timely manner with adequate technical bases. The

fuel reload was an Exxon fuel reload and used the same analysis '

methods as those approved for reload No. 1 and, therefore, the

October 9,1987 submittal could be approved in a timely manner on

December 15, 1987.

The approach to resolution of technical issues from a safety stand-

point generally demonstrates an understanding of the issues. Out of

33 licansing actions during this SALP period, 50% of the submittals

were timely, demonstrated a clear understanding of issues and were

technically sound and thorough. Another 40% of the submittals were

generally sound and thorough and usually demonstrated a good under-

standing of the issues. However, in 10% of the licensing actions,

the submittals were lacking an understanding of the issues and

thoroughness and resolutions were delayed. Three following examples

illustrate delays due to inadequate submittals.

\

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.On July 6, 1987, the licensee requested exceptions to Technical

-

Specification 3.0.4 to allow operational mode changes during the

outage without having ECC systems and the RHR system nperational.

The application did-not have adequate technical bases to support its

conclusion that an unspecified alternate decay heat removal means

could be used throughout the outage instead of the specified residual

heat removal system. The licensee was advised soon af ter submittal

that the submittal was inadequate, but it was not until October 8

that a meeting was held in which technical agreement was reached.

The revised application was submitted October 23 and additional

information . was provided November 19. The amendment was issued

December 4, for a TS change needed December 9 when both RHR trains

were scheduled to be removed from service.

A second example of inadequate bases for initial submittal and

delayed resolution of a technical issue is the request to change

Technical _ Specifications for modifications to the standby liquid

. control system to meet 10 CFR 50.62 requirements. The initial

submittal August 13 was technically inadequate because of inadequate

margin between operating pressure and system design pressure and the

proposed change of ASME Code Class 1 piping inside the drywell to

ASME Code Class 2 piping. On August 21 and -September 1, the staff

requested additional information regarding these matters, but it was

not until October 23 that the licensee responded partially and

November 25 when satisfactory piping design modifications were

pioposed. The amendment was needed for startup prior to the

expiration of_ the 30 day comment period and so an exigent Technical

Specification change was issued.

The third example of delayed resolution of a technical issue is the

request to change the Technical Specifications regarding the reactor

water cleanup (RWCU) system. On July 29, 1987, the licensee

discovered that two containment iso * 1 tion valves or, the RWCU pur

suction line used in series shared ne same divisional power supply.

.The licensee's design review of the RWCU also disclosed that piping

components out to the outboard drywell isolation valve were ASME Code

Class 2 and not ASME Code Class 1 as required by 10 CFR 50.55a for

components of the reactor coolant pressure boundary. These errors

and potential corrective measures were discussed with the staff on

September 15. A proposal to exchange power supplied to the two

isolation valves was submitted October 28, 1987, but no proposal was

made regarding the Code classification. The staff returned the

application on November 10 and a revised submittal was made

November 25 simultaneously with a request for exemption from the

requirements of 10 CFR 50.55a regarding ASME Code requirements for

the reactor coolant pressure boundary. The staff granted the

exemption on the basis that an ASME Code Class 1 stress analysis and

ASME Code Class 1 inservice inspections would be performed on the

applicable section of the RWCU piping. However, the late date of an

acceptable resolution resulted in the expiration of the 30 day

. - _ ..

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29

4

comment period. and amendment issuance on January 4, 1988,'one day

after plant startup began on January 3, 1988. The licensee is

addressing the problem of late resolution of issues needed for

restart from outages and will work with the staff to establish firm

milestones for early resoiation. For example, resolution of neutron

monitors.to meet Regulatory Guide 1.97 is being actively pursued, as

discussed below. Overall, in the resolution of technical issues,

viable and' generally sound and thorough approaches are used and con-

servatism is generally exhibited.

The licensee is generally responsive to NRC initiatives. In many

licensing actions, telephone calls discussir.g the technical issues

resulted in appropriate revisions to the submittals. Most of the

license conditions resulting from the operating license review were '

i

completed by the end of second refueling outage. The few

longstanding regulatory issues, such as containment purge criteria

and hydrogen control final analyses per. 10 CFR 50.44, are not

attributable to the licensee. The licensee has satisfactorily

responded to tne NUREG-0737 issues regarding TMI Action Items and

NUREG-0737, Supplement I regarding emergency response facilities. At

the end of the SALP rating period, only one of these items remains

. unresolved. This i '.e m , a neutron flux monitor to meet the

requirements of Regulatory Guide 1.97, is currently scheduled to be

installed at RF03 and resolutior. of this issue is actively being

pursued by the licensee.

The licensee has also teen responsive -to NRC concerns regarding

procedures for determiaing operability of equipment which is found to

be nonconforming. For example, Material Nonconformance Report (MNCR)

0166-87 was written on May 6,1987, documenting that the electrical

wiring used in the contair, ment and drywell hydrogen analyzer panels

had been replaced with wiring that had not had environmental

qualification testing performed as required by 10 CFR 50.49. A

telecon was held with members of the NRC on May 7, 1987. During this

conversation, the NRC raised the question of permissible time between

the identification of a safety system deficiency and system ,

operability determination. The licensee had expressed the opinion

that, per their procedures, they were allowed seven days for

evaluation. Knowing the wiring in the hydrogen analyzers was

unqualified made the hydrogen analyzers technically inoperable and,

therefore, TS limits for operation with Table 3.3.7.5-1 would have

limited operation to 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. Generic Letter 86-15, which addresses

the issue of the lack of environmental qualification states that the

licensee shall make a prompt determination of operability and shall

have a written justification for continued operation. The use of the

licensee's procedural guidance of seven days for evaluation was

misleading. Based on NRC comments, the licensee revised their MNCR

procedure to delete the seven day evaluation reference and now

requires the Duty Manager be involved immediately in evaluations

regarding equipment operability. Ihis is significant when it is

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realized that in the fou'rth quarter of 1987, 75 MNCRs were designated

as requiring further engineering evaluation and, therefore, seven

days were considered available.

The licensee requested discretionary enforcement when it was not

really required due to an inadequate Technical Support Instruction.

On May 13,=1987, the licensee contacted' NRR and NRC Region II for

possible discretionary enforcement. While the NRC was considering

. the request for discretionary enforcement, the licensee found a

letter to the NRC dated June 1984 that nad revised the definition of

trip systems such that the licensee could bypass level trips associ-

ated with a faulty water level reference leg and still meet TS action

statements. .The licensee. had failed to update their Technical

Support Instruction to reflect this change. This is an example of

poor quality assurance on a TS supporting document.

The licensee's staffing for licensing activities was changed when the

Director of Nuclear Licensing and Safety stayed with Mississippi

Power & Light Company after licensing activities were assumed by

System Energy Resources, Inc. The Manager of Nuclear Licensing moved

up to become Director and one of his staf f became the Manager of

Nuclear Licensing. Both of these persons. have long experience in

GGNS nuc:2ar licensing. The day-to-day contacts, coordinating

personnel for telephone calls and meetings have remained good. Some

of the-licensing personnel are onsite and have operational experience

for coordinating and communicating licensing matters to operations

personnel and to the NRC resident inspectors. Positions are

identified and authorities and responsibilities are well defined.

Coordination between licensing personnel onsite with those in the

corporate . of fice is usually good. Staffing has been ample during

this rating period.

The' licensee's submittals of no significant hazards considerations

for licensing amendments vary widely in acceptability. Some are

excellent; for example, the June 3,1987 submittal on core altera-

tions and the July 1,1987 submittal on the relief from the require-

ment for flow measurement in the standby liquid control system.

Deficiencies include a lack of a clear description of the effect of

the change on accident probabilities and consequences. Additional

training in the area of accident analyses should be considered for

the evaluators of license amendment applications.

No violations were identified.

2. Conclusion

Category: 2

3. Recommendations

None

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31

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K. Training

- 1. Analysis

During the assessment . period, inspections were performed by the

(7 resident and regional staffs. Special team inspections involving

! ..

training;were conducted by the: Probabilistic Risk Assessment and

Emergency Operating Procedures inspections.

Licensing examinations were given to 8 Reactor Operator (RO) and 2-

'

,

Senior Reactor Operator (SRO)- candidates in May 1987. Examination

results yielded .a pass rate of 88% (7 of 8) for R0 candidates and a

50% pass rate'for SRD candidates. Examinations were administered in

-April 1988 to three SR0 candidates as well as one RO candidate and

one SR0 candidate who had failed the previous examinations. Three of

-the four SR0s and the R0 passed. The overall pass rate, of 80% is

above the industry average.

Several -weaknesses identified during the May 1987 operating

examinations related to operators improperly paralleling the diesel

generators to the electrical busses.

An evaluation of the ~ requalification program was conducted by

Region II in December 1986. The overall program was rated as

marginally satisfactory. On May 27, 1987, representatives of System

Energy Resources Inc. (SERI) met with NRC Region II personnel to

discuss' improvements to be made in the requalification program as a

result of an internal.. examination. The NRC staff acknowledged the

changes made to the requalification program and ' agreed that those

changes would enhance the program. A similar meeting was. held on

March 2, 1988, in 'which SERI representa'.ives outlined further

improvements which had been incorporated ir;to 'their requalification

program since the meeting with Region-II on-May 27, 1987.

In order to. place a higher level of direct management attention on

training activities at the plant site, beginning in April 1987, the

Training Superintendent started reporting directly to the -Site

Director. The Training Superintendent previously reported to the

Manager, Plant Support.

, Management attention in the area of operator training was eviJett.

There was a special inspection conducted by t;ie NRC in the area of

Emergency Operating Procedures (EOPs). Although there were problems

identified in the E0P program area, operator performance was very

good during the simulator scenarios which were conducted to evaluate

the E0Ps. Also, a special PRA-Based inspection team noted that the

operators performance during the simulator assessments was above

average. The comments reflected the licensees high standard for

,

operator training.

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The licensee instituted a training program to instruct its personnel

4

- in the preparation of 10 CFR 50.59 safety evaluations, based on the

NUMARC draft guidelines which are currently being reviewed by the NRC

staff. Although some retraining may be necessary when agreement on

appropriate guidelines is reached between NRC and NUMARC, many of the

procedural aspects of the training will remain valid and should

improve the' safety evaluations. Evaluators of design and procedure

changes are tested and qualified by supervisors who have experience

in performing these evaluations. The training and qualification

program contributes to an adequate understanding of work and fair

adherence to procedure.

One of the areas inspected during the PRA-Based inspection in October

1987 was operator awareness and training on PRA findings. This was

done by interviewing a number of operators and through use of the

simulator. Two severe accident scenarios were selected for

demonstration on the plant simulator, using an operations crew to

mitigate and recover from the event.

It was found that the operators had not been specifically trained for

the station blackout scenario selected. Their performance, on the

simulator was good, but not as good as for the ATWS event, which was

the second event selected. The training program has not yet embodied

,

blackout recovery, or actions to take to limit the event.

The operators appeared to be well trained on the emergency procedures

as they currently exist. Management involvement and commitment to

training was indicated by the planned modification to the simulator

to match the control room. Modification to the control room was

indicated through a human engineering study and these same changes

were installed at the simulator. The quality of the training program

was indicated by the excellent actions during the simulation of an

ATWS. Operators followed procedures and demonstrated their previous

training on this event.

The licensee attributes the decrease in personnel contaminations to

the improved general employee training progrcms which began to place

stronger emphasis s n practical factor training in late 1986. The

training personnel nrovided the radiation workers with comprehensive

one-on-one practical factor training in mockup of a

contaminated / radiation area. Successful completion of the practical

factor segment of the training was required for course completion.

The training and drills for the fire brigade members met the

frequency specified by the procedures and the NRC guidelines.

No violations were identified in this area.

2. Conclusion

Category: 2

. _.

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' 3. Recommendations

The NRC istaff resources applied to the routine inspection

program should be maintained.

L. Engineering

1. Analysis

-During this evaluation period, inspections were performed by the

resident and regional staffs. A' special team inspection was

performed in the area of environmental qualifications (EQ) of

electrical equipment.

Effective July 1987, the Nuclear Plant Engineering Department was

'

reorganized to minimize the number of positions reporting directly to

the Director of Nuclear Plant Engineering. Only the Manager, Nuclear

Design, Manager, Engineering Support and Manager, Operational

Analysis now report directly to the Director of Nuclear Plant

Engineering.

The licensee has been responsive to NRC concerns. Due to tne

numerous design basis documentation / analysis deficiencies that have

been identified and NRC concerns, the licensee initiated a comprehen-

sive design review program. The licensee's design review initiatives

were discussed in an enforcement conference on February 4, 1987.

Although there appears to be a high number of design / documentation

deficiencies, the licensee is commended for initiating the design

review verification program that identified some of the more subtle

deficiencies.

Some engineering evaluations were not conducted to the depth required

to identify tne root cause and implement adequate corrective actions.

The resident inspectors identified a missing bolt in a control rod

drive Hydraulic Control Unit (HCU) mounting structure. Upon

investigation, the licensee then identified numerous additional

installation deficiencies. The first response from Nuclear Plant

Engineering indicated that the as found condition was satisfactory,

but a close review of the analysis by NRC inspectors indicated that

the analysis only covered the configuration after some corrective

actions had been taken. Another example of an inadequate investiga-

tion is the header del ta pressure instrumentation for the high

pressure core spray (HPCS) system, the low pressure core spray (LPCS)

and the low pressure coolant injection (LPCI) systems. See violation

d. in the Surveillance area. In January 1988 during startup from the

second refueling outage the LPCS/LPCI A line break annunciator

alarmed indicating unsatisfactory header delta pressure. Investiga-

tion revealed that the setpoint for the LPCS/LPCI A header delta

pressure had been based upon original design calculations rather than

normal indicated delta pressure as required by Technical

Specifications. Although this same type of problem had previously

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occurred on the HPCS header delta pressure and a GE Service

-

-Information Letter and an IE Circular had been ' issued in 1979

addressing this type of problem, the normal indicated header delta

pressure as required by TS had not been determined.

Inadequate drawings -sometimes' contributed to events at GGNS. 'For

example, -there was an event where the concentration of Molybdate in

the SSW basin was decreasing with no apparent cause. The licensee

'found that'a vent line,that acts as a vacuum bre.=ker on the SSW basin

overflow pipe had been inadvertently buried and therefore blocked

causing a siphoning. of water to the storm drain system. The appli-

cable Piping and Ins;rumentation Diagram (P&ID) did not show the vent

line. Even more disturbing is the fact that the vent line was buried .,

and not shown on the P&ID even after a comprehensive de.,ign review

had been conducted on the SSW system due to the many previously

identified design and documentation discrepancies. Another event

where an inaccurate P&ID was a contributor concerns the instrument

air system. P&ID M1067 showed a P53-F496 valve in the Unit 2

instrument air line from the Unit 2 instrument air compressor / dryer

system. The Unit 2 instrument air compressor / dryer system is utilized

as a bhckup to the Unit 1 instrument air compressor / dryer system. An

operator was sent to red tag the Unit 2 P53-F496 valve and mistakenly

red tagged the Unit 1 P53-F496 valve resulting in the loss of

instrument air and almost a scram. The label for valve P53-F496 did

not identify the valve as a Unit 1 valve and the Unit 2 P53-F496

valve shown on the drawing did not exist in the plant. Previous SALP

reports have noted the discrepancies and poor legibility o 5e

P& ids. Although the licensee has initiated an extensive d. . ng

improvement program and significant improvement has been noted, the

events noted above indicate the significance and the need for further

improvement.

During review of IE Bulletin 85-03, "Motor Operated Common Mode

Failures During Plant Transients Dua to Improper Switch Setting," it

was evident that corporate management was involved in site

activities. While completing the bulletin program, the licensee has

encountered relatively few problems. A lot of effort was put forth

to establish a good program from the start which demonstrate a clear

understanding of the issues. All required bulletin responses were

equally timely.

The EQ inspection revealed that the files were generally well

organized, detailed and complete. The EQ program was considered to

be good except in the areas of procurement, train 1ng of material

specialists and dedication process for commercial grade replacement

parts. The weakness in the procurement area resulted in Violation

a. below.

The licensee's actions with regard to NRC initiatives, especially

during the EQ inspection, were timely, correct and thorough. The

resolution of technical issues from a safety standpoint were

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generally sound; however, there were examples identified ifur'ing the

inspection and documented in the report as violatiens and unresolved

items,that indicated a better job could have been done in establish-

ing more complete EQ documentation and better EQ procurement and

maintenance practices. ,

The first four violations were in

~

Six' violations were identified.

the ~ EQ - area ' which did not indicate .a progra;nmatic breakdown.

Management demonstrated an active participation in EQ issues and

placed EQ issues on a high priority.

a. . Severity Level -IV violation for commercial gradc components

installed in EQ equipment (416/87-32-01).

b. Severity Level IV violation of limitorque MOV T-Drains and

grease reliefs (416/87-32-02). <

c. Severity Level IV violation for installation of Raychem heat

shrink tubing in unqualified ccnfigurations (416/97-32-03).

d. Severity Level IV violation on qualifications pacPage for

lubricants (416/87-32-04).

e. Severity Level IV Violation for failure to perform a w.-iaen

safety evaluation. (416/88-07-02)

f. S1 verity Level IV violation for failure to install control rod

drive hydraulic units per design drawings (416/87-10-10).

2. Conclusion

Catenory: 2

3. Recommendations

The NRC staff resources applied +o the routine inspection

program should be maintained.

V. SUPPORTING DATA AND SUMMARIES

A. Licensee Activities

During this assessment period, the licensee completed refueling

outage No. 1, fuel cycle No. 2, refueling outage No. 2 and four

months of fuel cycle No. 3.

This performance assessment is based on the evaluation of the

licensee's performance in supoort of licensing actions for Unit 1.

(Licensing activities for Un' 2 were minimal). The Un't i licensing

._ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __ __ _ _ _ , _ _

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actions included the licensee requests for license amendments,

responses to generic letters and various submittals of information

for multiplant and NUREG-0737 actions.

'

There were 20 plant specific licensing actions completed during this

SAlp period. Of these, three concerned resolution of outstanding

issues in license. conditions, two concerned deletion of requirements

based on operating experience, two involved training program reviews,

one was relief from a prelicensing-commitment, three were results of

performance or surveillance tests, two related to design analysis of

modifications, three were revisions to the ODCM or PCP, one was

administrative, and three were responses 'to generic letters. The

more significant submittals were design of equipment for ATWS

. mitigation per.10 CFR 50.62 and conformance to Regulatory Guide 1.97

per-NUREG-0737, Supplement 1.

During this SALP period, there were 17 meetings with the licensee.

Six meetings were held to discuss the scope and schedule for

licensing. actions. Five meetings were held to have technical

discussions of specific licensing actions, including containment

purging, reactor core thermal and hydraulic limits, exceptions to

Section 3.0.4 of=the. Technical Specifications, relief from inservice

inspection. requirements for the reactor pressure . vessel and

modifications to the reactor water cleanup system and the standby

liquid control. system. Four trips to the plant were made to observe

core thermal hydraulic tests, to tour the facility, and to be briefed

on operations by plant operations personnel. In two trips to the

plant, the Project Manager participated in inspection activities.

B. Inspection Activities

During the assessment period, routine inspections were performed

by the resident and regional inspection staffs. Special team

inspections were corducted in the areas environmental qualification

, of electrical equipment, probabilistic risk assessment and emergency

"

operating procedures. Two emergency preparedness exercises were

evaluated.

C. Licensing Activities

Schedule Extensions Granted

Two schedule extensions were granted during this SALP period;

completion of the TDI Division II inspection recommended by the TDI

Diesel Generator Owners Group was deferred from the second refueling

to the five year inspection, and the installation of neutron monitors

to meet the requirements of Regulatory Guide 1.97 was deferred from

the second refueling to the third refueling.

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-Relief from the~ requiv ements of Section XI of- the ASME Boiler and

Pressure Vessel Code far inservice inspection of the reactor coolant

Mystem was granted for fivs areas.

'

Exemptions to the rules were granted for (1) use of MSA GMR-1

canisters in high radiation areas, in lieu of oxygen . supplied

breathing masks, and (2) use of ASME Code Class 2 piping in lieu of

ASME Code Class 1 piping in the reactor water cleanup system.

Twenty license amendments were issued. Major amendments included;

addition of TOI diesel generator maintenance and surveillance-

requirements, ' transfer of control of licensed activities from-

Mississippi-_ Power & Light Company to System Energy Resources, Inc. ,

and Technical Specification changes to implement decreased cold fast

starts of diesel generators, exceptions to Section 3.0.4 of Technical

Specifications-(TS) for the second refueling outage and ATWS-related

equipment modifications.

One emergency TS was granted to prevent delay in restart from the

refueling outage. The TS for ATWS related equipment was issued with

less than the 30-day comment period required for a normal amendment,

because the licensee was able to improve its outage schedule by

several days.

~D. Investigations Review

None

E. Enforcement History

'1. Civil Penalties

No escalated enforcement actions were issued during this period.

2. Orders

None-

F. Licensse Conferences

December 15, 1986 Meeting at GGNS by Region II management to

assess the plant status, major problems and

corrective actions and plant tour.

February 4, 1987 Enforcement conference at Region II to

review NRC concerns regarding the Standoy

Service Water system problems. No violation

was issued.

V September 15, 1987 Management meeting at Region II to discuss

two recently identified design deficiencies.

The design deficiencies were in the RWCU

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system where two -redundant isolation valves

shared a . common. power source and where

control building ventilation duct sections

were .not designed to . withstand a design -

basis tornado loads.

December 2, 1987 Management meeting at .GGNS to' brief NRR's

' Director, . Project Directorate II-1, and the

assistant Director for Region II Reactors on

SERI's Operations and status.

February 2, 1988 Management meeting at GGNS to brief the NRC

Region II Regional Administrator and the

Deputy Director, Division of Reactor Safety

on.SERI's operations and status.

March 4, 1988.

.

Management meeting at GGNS to brief the NRC

Region II Dire; tor, Division of Reactor

Projects, and the cognizant Branch Chief on

SERI's operation and status.

G. Discretionary Enforcement

November 23, 1987 Permitted the refueling platform main hoist

cable load to reach 2000 pounds and an

auxiliary hoist to reach 1000 pcunds - to

remove a misaligned stu;k fuel bundle,

' Technical Specification 3.9.6.1 limited

..

loads on the refueling platform main hoist

to 1250 pounds.

-H. Licensee Event Reports (LERs)

The distribution of the events analyzed by cause by the licensee were

as follows:

l

Cause

l' Component Failure 8

i Design 4

'

Construction, Fabrication, or Installation 2

4

Personnel

- Operating Activity 5

- Maintenance Activity 5

- Test / Calibration 4

- Other 6

Quality Contro; 4

Out of Calibration U

Other _1

TOTAL 39

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I. Ins- tion Activity and Enforcement

,

FUNCT10NAL NO. OF DEVIATIONS AND VIOLATIONS IN EACH'

SEVERITY LEVEL

AREA- Dev V IV III- II' I

Plant Operations 1 1

Radiological Controls 2

Maintenance. 1 1

'

Surveillance 1 2 3-

Fire Protection

Emergency Preparedness 2 .

Security _

Outages 2

Licensing

Quality Programs and.

Administrative ~ Controls

Affecting Quality

Training

Engineering 6

TOTAL 1 4 17

J. Reictor Trips

June 29, 1987 The unit was operating at 100*4 core themal power

(LER 87-009) when a main turbine trip resulted in a reactor

scram. Ar Agastat relay f ailure resulted in the

closure of the steam jet air ejector main steam  ;

isolation valve resulting in the loss of the

steam jet air ejector and loss of main condenser

vacuum giving-the turbine. trip,

August 6. 1987 The unit was operating at 100*4 core thermal

(LER 87-012) power when a turbine control valve fast closure

resulted in a reactor. scram. Moisture

condensation in a switchyard ~ terminal' cabinet ,

caused operation of a lockout relay opening two

switchyard breakers giving a main generator load

rejectiore.

January 10, 1988 The unit was operating at 95"; reactor thermal .

4

(LER 88-002) power when a main turbine trip resulted in a  !

reactor scram. The B main ' transformer failed

giving a phase differential load reject and

turbine control valve fast closure.

t

- . . , _ . . _ . _ . _ . __ _ ~ . _ _ _ . _ _ . _ - _ _ _ - - - -

_- _ _ -

'

*'- *

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s

40

January 20, 1988 The unit was operating at 96% reactor thermal-

(LER 88-006) power when a low reactor. water level gave a

reactor scram. The A circulating water IP

condenser manway leaked spraying water onto the

low hotwell level switches causing a 'short and

false low condenser hotwell level signal and trip

of the condensate pumps.

March 15, 1988 The unit was operating at 100% reactor thermal

power when 29 rods inserted during a Rx sessell

water level surveillance. The surveillance

inserted a half scram and 29. control rods had

lost power to the opposite division scram

solenoid (A Div) due to a loose screw in a

terminal cabinet.

EFFLVENT SUMMARY FOR GRAND GULF

Activity Released (curies) 1985 1986 1982

1. Gaseous Effluents

Fission and Activation Gases 1.51 +28 1.34E+2 2.08E+2 ,

Iodines and Particulates 7.53E-4 4.85E-4 4.28E-3

- ,

2. Liquid Effluents *- 4

'

Fission and-Activation 2.13E-1 3.03E-1 3.66E-1

Products

Tritium 5.17E0 1.47E+1 1.83E+1

Offsite Oose Estimate (mrem)

Maxim;m Whole Body: Liquid 7.02E-2 6.21E-2 1.00E0

Gas 3.11E-i 1.78E0 3.40E-1

Maximum Organ: Liquid 3.92E-1 5.67E-1 1.41E0

Gas 9.03E-2 6.83E-2 ' 36E-1

.

i

2 - 1.51E+2 is equivalent to 1.51 X 10+ I

.

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