ML20140E380

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Rev 0 to Damage Assessment Rept for Break in Extraction Steam Line
ML20140E380
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 05/03/1997
From: Core M, Phelps R
OMAHA PUBLIC POWER DISTRICT
To:
Shared Package
ML20140E365 List:
References
NUDOCS 9706120033
Download: ML20140E380 (73)


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CT Attachment 3

. Damage Assessment Report for the Break in the Extraction Steam Line Revision 0, May 3,1997 l

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i DAMAGE ASSESSMENT REPORT -

l FOR THE BREAKIN THE

! EXTRACTION STEAM LINE i 1 1

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I l l RCVIS10n U, May 3,1997 .

R. L. Phelps, P.E.

Manager - Station Engineenng M. R. Core, P.E.

Manager - System Engineering

l l- Damane Assessment Renon for the Break in the Extraction Steam Line l 1. Methodolorv -

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Failure analysis of the pipe break will be performed by FPI, International, with the metallurgical analysis performed by Altran Laboratories. The results of this failure analysis will be used to help identify other high risk pipe locations that need to be inspected before restart and will also be used as input to the RCA and to the overall j erosion / corrosion program assessment. This effort is discussed in a separate report.

l Assessment of Erosion / Corrosion program will be perfonned by the assessment team l headed by J. L. Skiles. This activity will help ensure plant piping systems are being l maintained consistent with safe and reliable operation. This effon is also discussed in a -

separate repon.

All other damage assessments will be led by System Engineering teams. Walkdowns will ensure necessary repairs and testing are identified and supponing analyses per-formed where reqmred. MWRs will be prepared and work scheduled for completion.

This effon is the subject of this report.

l - 2. Srant The scope of the Damage Assessment is defined as follows:  ;

A. Experienced individuals (i.e., System Engineer, Design Engineer, and/or Maintenance l

Planner or Craft) will be assigned to teams to investigate systems and report damage in

" Damage Assessment Reports." Central to this investigation is a walkdown of equipment in the break affected zone.

B. Every plant system that could be potentially affected by the break will be considered.

C. The break affected zone will be the primary area for walkdowns.

D. System interactions outside the break affected zone will be considered (e.g., electrical bus gmunds, instrument air, etc.).

E. The following parameters will, at a minimum, be considered by the Damage i

Assessment Teams:

The effects of the physical movement of equipment and supponing mechanisms caused by the steam release.

, The effects of steam impingement on equipment. I The effects of wetting of equipment due to steam condensation.

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. The long term effects of the event on equipment.

. The effects of the insulation and dust distributed throughout the break affected zone by the event:

l To assist the damage assessment teams in planning 'and executing the walkdowns, a matrix entitled " Anomaly Resolution Guideline" has been ymiced. System Engineers

, will utilize the functional requirements from this matrix in scoping and performing the

! walkdowns for each system to ensure critical break effects are. considered. This guide-line is attached to this report.

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l l F. Teams will be assigned equipment for walkdowns based on the System Engineers l L

assigned systems.

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( G. The break affected zone is defined as the Turbine Building. The area in the blowdown l zone is considered the primary area for walkdowns. The basis for this is discussed in i the following section. l H. The System Engmeer representative on each walkdown team will ensare appropriate Maintenance Work Documents are prepared.

I. It is intended that the initial damage assessment be completed as soon as possible to i

, allow the scheduling and planning process as much time as possible to prepare work l packages for execution. However, it is also intended that the damage assessment be l dynamic to ensure all issues are identified to assure safe operation and high reliability l of the station following restart. Therefore, follow-up walkdowns and analyses may be required. .

l J. It is intended that the Syr, tem Engineer representstive provide input to assure the proper l prioritization of work activities within the resources allocated.

K. Above all, it is imperative that the System / Design Engineer ensure that his/her l walkdowns will assure the continued safe and reliable operation of Fort Calhoun .

l Station. The very nature of this damage assessment will rely heavily on the experience

! of the Engineering and Maintenance / Planning staff.

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3. Basis for the Dammoe Accacement Scone .

A. Definition of the break affected zone. .

After a pieliminary walkdown and discussions with personnel that were on site during l the event, the Turbine Building was the only area selected es needing damage assessment. The reasoning in selecting only the Turbine Building and components l located in the Turbine Building for damage assessment includes the following:

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l. 1. There was no evidence of any steam intmsion into any of the following buildings:

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  • Service Building

- Maintenance Shop

  • Auxiliary Building This was confirmed by interviews with personnel on site during the event and the lack of any fire detection alarms for these buildings, with the exception of two fire detector alarms in Corridor 53 and two detector alarms in the Water Plant, before, during, or after the event. All four fue detector alarms would be expected after reviewing their locations and the steam plume. All of the buildings in question, Service Building, Maintenance Shop, Auxiliary Building, and Turbine Building have separate, non-communicating HVAC systems, with the exception of a grille between the Water Plant and the east wall of the Turbine Building and a fire barrier between the cable spread room and the west wall of the Turbine Building.

Additionally, all the buildings are in different fire areas, which means that there l

are fire barriers between the buildings. The fire barriers are not designed as steam I barriers; however, as evidenced by the lack of fire detection alarms, they are l effective as a low pressure steam barrier. ..

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2. There was no evidence of dust or insulation particle migration from the Turbme  :

Building into the Service Building. There was some very light dusting in the Service Building of what apM to be ceiling tile dust that is judged to have '

been deposited on desk and table tops from the turbine trip. This is not an uncommon phenomenon following a turbine trip from full power.

3. There was no evidence of dust or insulation particles in the Maintenance Shop after the event with the exception of a small area in the south east comer of the shop. There was a light dusting of dust or very fine insulation particles that could have been dislodged during the turbine trip.
4. There was no evidence of dust or insulation particles in the Auxiliary Building.

I S. A qualitative evaluation of the blowdown from the high energy line bicak reveals that the blowdown lasted for less than 20 seconds. 'Ibe zone from the blowdown extended from the pipe outward to iapact on the motor control center (MCC 4CS) 3

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! and then the Maintenance Building wall with a diameter about 20-30 feet. In this .

! zone, the temperature of the two phase b:owdown could range from operating temperature of about 400*F to some lower temperature above 212*F. Outside .

I thisjet impingement zone, the steam would rapidly cool and depressurize, so that the areas in the Turbine Building around thejet impingement zone would likely be at or below 212* F with virtually no pressurization until the blowdown terminated, at which time any steam would rapidly cool and condense.

Consequently, the observations above regarding no visible effects in the Service, Maintenance or Auxiliary buildings are valid, and it is reasonable to conclude that the break affected zone should be limited to the Turbine. Building and, in 1 particular, the areas near the break. Other areas in the Turbine Building are most i likely subject to the effects of a wet environment and should also be walked down with this in mind.

l B. The following are the Fort Calhoun Station Systems and the basis for their inclusion in the recovery. effort or why the system was not specifically included in the recovery effort: ,

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e Architectural (AE) - The Turbine Building is covered in the scope of the l l i

inspection. Before power operation of the station, Procedure SE-PM-SE-1003,

" Turbine Building Structure Inspection," will be performed. Any anomalies l noted will either be repaired or evaluated for start-up.

  • Auxiliary Feed Water (AFW) - The portion of the AFW system located in the Turbine Building (FW-54 and associated support equipment) is included in the scope of the recovery effort. A walkdown was performed by Merl Core (Manager - S.E.) and no problems were noted. FW-54 functioned satisfwtorily for several days after the event with no problems noted. ..

e Auxiliary Steam (AS)- The AS system was walked down by Carmen Ovici l

(S.E.). No damage to the system piping was noted; however, a maintenance work document was generated to inspect and clean the affected auxiliary steam heater.

l e Auxiliary Monitoring Systems (including Seismic Monitoring, Loose Parts l Monitor, Intemal Vibration Monitoring, Toxic Gas, Contamment Hydrogen, Meteorological Monitoring, 800 Mz Radios, Station Grounding, and Catix>dic Protection Systems) are not included in the scope of the recovery effort since they are not located in the Turbine Building.

e Auxiliary Monitoring Systems (including Plant Communication Systems and Plant Alarms) are not included in the scope of the recovery since they are included in the PRC Start up list.

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  • Chemical Feed (CF) - The Turbine Building portion of the CF system is included -

in the scope of the recovery effort. A walkdown was performed by Mark Nay (S.E.) and no problems were noted. The majority of the CF equipment is located' in a, Kelly enclosure on the opposite end of the Turbine Building.

  • Chemical and Volume Control (CH) - The CH system is not included in the scope of the recovery effort since none of the components of this system are located in the Turbine Building.

l e Circulating Water (CW)- The CW system is included in the scope of the recovery

! effort. The Turbine Building portion of the CW system was walked down by l Carmen Ovici(S.E.). No abnormalities were noted.

! e Compressed Air (CA) - The CA system is not included in the scope of the recovery effort since the source of air for the CA system is in Room 19 of the l Auxiliary Building. As discussed above, it is not reasonable to believe that a steam environment existed in any portion of the Auxiliary Building; therefore, there is no reason to believe that moisture entered the CA system. Note: The Turbine Building portion of the CA system was visually inspected, during tours, for physical damage.

l e Component Cooling Water (CCW) - The CCW system is not included in the j scope of the recovery effort since none of the components of this system are l located in the Turbine Building.

e Control Element Drive Mechanisms (CEDM) - The CEDM system (including l position indication system, clutch power supply, and rod drop test panel) is not l included in the scope of the recovery effort since none of the components of this -

system are located in the Turbine Building.

o Demineralized Water (DW) - The DW system is included in the scope of the

! recovery effort. The Turbine Building portion of the system was walked down by l Carmen Ovici (S.E.). No abnormalities were noted.

l e Electrical (EE) - The EE system components located in the Turbine Building are l included in the scope of the recovery effort.

The Turbine Room Motor Control Centers (MCC) were walked down by Steve Miller (S.E.) and Meri Core (Manager - S.E.). The damage assessment report generated from that walk-down is attached.

I Cable Systems were walked down by John Tucker (S.E.) and Jim Foley (S.E.).

The damage assessment report generated from that walk-down is attached.

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The damage assessment to the MCCs and to cabling in the break affected zone -

entails review and analysis for the extent of the inspections prior to walkdown and l

MWR preparation. Detailed inspection plans were yweized for this assessment '

and are attached.

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  • Emergency Diesel Generator (DG) - The DG system is not included in the scope of the recovery effort since none of the components of this system are located in the Turbine Building.

l e Engineered Safeguards Features (ESF) - The ESF system is not included in the i

! scope of the recovery effort since none of the components of this system are i located in the Turbine Building.

  • Feedwater (FW) - The FW system (including the condensate system), located in the Turbine Building is included in the scope of the recovery effort and was walked down by Craig Fritts (S.E.) and Ben Bickels (S.F.M.). The damage  !

j assessment report generated from that walk-down is attached. '

l e Fire Protection (FP) - The FP system, located in the Turbine Building is included in the scope of the recovery effort and was walked down by Chris Sterba (S.E.)

and Mark Stanley (Planner). The damage assessment report generated from that walkdown is attached. Note: The Turbino Building Fire Protection System is also included on the PRC Startup List as item #6.

  • Fuel / Lube Oil (FO, LO) - The FO system is not included in the scope of the recovery effort, with the exception of that portion of the system that supplies the diesel driven AFW pump, since the rest of the system is not located in the Turbine

, Building. The portion of the FO system that feeds FW-54 was walked down by -

1 Merl Core (Manager - S.E.) with no abnormalities noted. FW-54 functioned satisfactorily for several days after the event with no problems noted. The LO system is included in the scope of the recovery effort and was walked down by Kevin Naser (S.E.) and Jerry Mixan (Planner). The damage assessment report generated from that walk-down is attached.

e Fuel Handling and Spent Fuel Pool (FH & SFP) - The FH and SFP systems are not included in the recovery effort since none of these systems are located in the Turbine Building.

l e Gas Piping (HG/CO2 )- The HG/CO 2system is included in the scope of the recovery effort and was walked down by Mark Nay (S.E.). No problems were noted. The gas systems are closed systems and are not open to the Turbine Building atmosphere. The systems also functioned for several hours after the

! event with no problems noted.

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e Heating, Ventilating, and Air Conditioning (HVAC) - The HVAC system is -

included in the scope of the recovery effon; however, since the design of the l' Turbine Building HVAC is such that there are only supply fans and roof fr.ns, and no " internal" air-handling systems, the scope will be limited to the long term

effects on the roof fans froin an economic stand point only. This ponion of the
inspection effon will not be performed until after re-start and all clean-up efforts are complete.

I e Instrument Air (IA) - The IA system is not included in the scope of the recovery effort since the source of air for the IA system is in Room 19 of the Auxiliary i Budding. As discussed above, it is not reasonable to believe that a steam environment existed in any portion of the Auxiliary Building; therefore, there is no reason to believe that moisture entered the IA system. Note: The Turbine

Building portion of the IA system (including instrument lines and actuators) was j visually inspected, dunng tours, for physical damage. j i

e Main Steam (MS) - The Turbine Building portion of the MS system is included in j

!' the scope of the recovery effort and was walked down by Craig Fritts (S.E.) and i l Ben Bickels (S.F.M.). The damage assessment report generated from that walk-i down is attached.

e Plant Computer System (PC) - The PC system (including ERF computer, QSPDS l

i and SMM) is not included in the scope of the recovery effort since the computer systems are not located in the Turbine Building.

j e Plant Security System (PS) - The PS system is not included in the scope of the recovery effort since the system is electronically monitored and was checked by i

the guard force for operability. Additionally, because of the closed loop -

monitoring system incorporated into the system, any anomaly would be detected by the SAS or CAS monitoring officer.
  • Potable Water (PW) - The PW system was included in the scope of the recovery effort and was walked down by Carmen Ovici (S.E.). No damage was noted.

e Radiation Monitoring (RM) - The Turbine Building portion of the RM system (RM-057 and RM-064) is included in the scope of the recovery effort. A walkdown was performed by Don Flegle (S.E.) with no problems noted.

e Raw Water (RW) - The RW discharge header and the raw water backup discharge header, located under the mezzanine level of the Turbine Building, on the north side, are included in the scope of the recovery effort. Both headers were inspected for damage by Tom Dailey, (S.E.). Both headers appeared to be in good condition with no damage being noted either to the pipe or associated pipe supports .

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4 e Reactor Coolant (RC) - The RC system (including the reactor, steam generators, -

and associated equipment) is not included in the scope of the recovery effort since none of the components of this system are located in the Turbine Building. -

e Reactor Protection System (RPS) - The RPS system (including NI, DSS, and Neutron Flux Monitor) is not included in the scope of the recovery effort with the exception of turbine stop valve limit switches which supply a turbine trip signal to the RPS and are located in the Turbine Building. A walkdown was performed by

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' John Tucker (S.E.) and Maintenance Work Order 971409 was written to inspect the switches.

Safety Injection (SI) - The SI system is not included in the scope of the recovery .

effort since none of the components of this system are located in the Turbine Building.

  • Sampling (SL) - Portions of the SL system are included in the scope of the recovery effort and were walked down by Chris Sterba (S.E.). The secondary sampling panel is located in the Turbine Building, but did not sustain any damage due to the steam leak. The system has been in operation since the event and no problems have been reported.

e Main Turbine (ST) - The ST system (including EHC, control valves, stop valves, and turbine axillaries) is included in the scope of the recovery effort and was walked down by Kevin Naser (S.E.) and Jerry Mixan (Planner). The damage assessment report generated from that walk-down is attached. The Generator, Alterrex, and Stator Cooling Systems were walked down by Rich Ronning (S.E.),

Tom Kazor (Electrician), and Cal Huey (General Electric Technical Representative). The damage assessment report generated from that walkdown is -

attached.

e Waste Disposal (WD) - The WD system (Radwaste Systems) is not included in the scope of the recovery effort since none of the components of this s'ystem are located in the Turbine Building.

e Turbine Plant Cooling Water (TPCW) - The TPCW system was included in the scope of the recovery effort and was walked down by Carmen Ovici (S.E.). No  ;

damage was noted. i b

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l 4. Summary of Dammoe Aa, ament and Recovery Actintigg .

To date, with the exception of the extraction steam piping, and motor control centers located in the bretk affected zone, there have been no major anomalies noted in the Turbine Building. There have been severaljunction boxes noted that had slight amounts of moisture inside that was easily cleaned up by blowing them down with compressed air. Additionally, there have been no cables tested that were unsatisfactory. There has been no structural damage to the Turbine Building itself, and no indications of steam or dust particle entry into any other building in the power block except for the Turbine Building.

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During the event, and the subsequent plant cool-down, all equipment performed as expected, even during the time of elevated humidity, even that equipment in the break affected zone.

Much of the equipment operated for several days following the event and equipment has l been retumed to operation following walk-downs and in preparation for re-start of the i station. All equipment in this category has operated satisfactorily. As a precautionary measure, to assure reliability of the station following start-up, several preventative l maintenance measures were undertaken. These measures include, but are not limited to, the following:

e Replacement of turbine servo valves e Calibration checks of selected instruments in the Turbine Building e Checks of the Gai-Tronics system and associated emergency alarms j s Checks of the Station Blackout emergency lighting as well as station battery emergency lighting e Preventative maintenance of MCC breakers that could have been affected e Detailed cleaning and inspections of all MCCs at the north end of the Turbine Building e General clean-up of the entire Turbine Building e Numerous building tours by management, system engineers, operations staff, and craft -

persons of all systems located in the Turbine Building, or systems that could have been affected by the break affected zone Note: These activities are either in-progress and will be complete prior to return to power or are complete at this time.

In summary, detailed walk-downs and inspections have been underway in the entire Turbine Building and especially intensive in the break affected zone since April 22,1997. Other than " expected" damage to the motor control center, MCC-4CS, the damage to the extraction steam lines, and damage caused by high energy steam impingement, there have i been no other components discovered, to date, that have failed due to the event.

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. 5. Further recovery actions crior to return to oower oneration include the following:

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  • Completion of the attached recovery effort matrix for those items that need to be i completed and/or evaluated prior to retum to power e Engineering management interviews with system engineers and, where appropriate, l craft persons to assure management that systems are ready for return to power operation l

e Continued walk-downs of selected equipment, primarily in the steam affected zone, i

after plant heat-up to assure management that there are no lingering effects from the event

6. Onnoino recoverv actions to ac=ne lonn term relinhility of the =tation j The Manager - System Engineering will keep the master copy of this Damage Assessment report until it no longer provides any valuable information, at which time it will be l

transmitted to the file by means of a letter from Manager - System Engineering to Manager -

l Station Engineering. The Manager - System Engineering will attach to this repon any l additional information that is received, such as, closure or summary reports from system engineers.

The following items will be scheduled after return to power operation to assure the long l term reliability of the station:

e . Scheduling future walk-downs and inspections of selected equipment to assure that there are no long term effects from the event, such as rust, degradation, etc. -

o Close monitoring of any Condition Reports for trending equipment failures that could l l possibly be connected with this event

. i e Monitoring of the above by the Fon Calhoun Station Reliability Committee  !

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.i it ANOMALY RESOLETION t

GEIDELINE e

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Anomalv Resolation List I. MschanicalIssues

1. Pipe break failure analysis and rer, air FPI Int.

J. Skiles

a. Perform failure analysis ofbreak
b. Review checkworks meth'.xiology for generic issues. J. Skiles
c. Inspect similar pipe locations for thinning.
d. Replace or repair pipe as needed. D. Rollins
e. Inspect and repair pipe supports in break affected zone. T. Daily
2. Jet Impingement or Envir.onmental Effects and repair as needed
a. Steam System Functions
1. Inspect adjacent pipe and supports and repair as needed J. Bottom .

T. Daily C. Fritts l

2. Inspect break asca for structural damage and repair as needed J. Simodynes D. Rock l b. Inspect for security system damage D. Sloderbeck 1
1. Locks R. Garfoot
c. Inspect secondary sample panel C. Sterba
d. Inspect all sightglasses in break area C. Sterba May 2,1997 Rev. 6 I

TASK ' RESPONSIBLE -

3. HVAC Functions C. Ovici B. Phillips
1. Inspect HVAC Systems for damage
2. Inspect Switchgear Panel AI-187
3. Inspect TB Office HVAC
4. Turbine-Generator Functions *
a. Inspect turbine plant cooling system. C. Ovici
b. Inspect and repair EHC completely K. Naser J. Mixan
1. Structuraldamage
2. Tubing connections
3. Sample fluid & replace or filter as needed.
4. Water / Steam effects (EHC-1) .

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5. Replace desicant in EHC-7
c. Inspect and repair control /stop valves operating mechanisms K. Naser J. Mixan  !
1. Tubing
2. CV-1-0
3. CV-3-0 j
4. PT-CV-1 i
5. PT-CV-3 t

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May 2,1997 Rev. 6 2

" TASK.: J PESPONSIBLs

d. Verify recovery procedure for bowed shaR K. Naser
e. Ensure turning gear is operable K. Naser
f. Lube Oil System K. Naser-
a. Sample oil & filter as needed
b. Inspect bowser & clean ifneeded .
5. Plant Support Systems
a. Repairlighting
b. Inspect Eme:gency Lighting D. Flegle
c. Inspect Gai-Trordes C. Sterba
6. Restore Fire Protection Systems S. Chomos/

C. Sterba

a. Inspect and repair sprinkler pipe and heads.
b. Inspect / repair / test detectors C. Sterba
7. Other Plant Systems M. Nay C. Fritts
a. Inspect Main Steam System M. Bose
b. Inspect Feedwater System
c. Inspect Condensate System i
d. Inspect Instrument Air System

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May 2,1997 Rev. 6 3

. TASK': ..

iRESPONSIBLE.

11. Electrical Issues S. Miller
  • M. Core
1. MCC 4C3 and 4C5 Inspections / Repairs M. Elzway j a. Inspect and scope damage i
b. Determine repair or replace I
c. Inspect all 480V breakers
1. Repair or recalibrate and test .
d. Inspect au 125V indication / con'.rol
l. Verify fuses operability
e. Develop plan to re-energize MCCs and operability check loads.
f. Meggar MCC 480V cabling affected by break.
2. Inspect Generator ,
a. Inspect Stator Cooling System R. Ronning
b. Indication (local) and transmitters for environmental (steam) effects K. Naser
c. Inspect conduitfjunction boxes for condensation .
e. Inspect bearing cooling system i
f. Inspect all 125V instruments / controls l g. Verify alllube oil systems operable
a. Lube oil pump motors
b. Pressure switches & local indications
h. Inspect Alterex
3. Inspect Electrical Connections in break affected area R. Garfoot J. Foley j
a. Inspect conduitfjunction boxes for steam / condensation effects A. Nosier
b. Inspect / repair conduit and mounting i
c. Megger high voltage cables (480V)
d. Inspect MOVs in affected area
e. Repair damage cable trays
1. Restorefirebarrier r
f. Inspect basement instruments (eg transmitters) within potential affected areas  !

May 2,1997 Rev. 6 4 t

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a DAMAGE ASSESSMEXT i

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, - 1 DAMAGE ASSESSMENT REPORT 4/28/97 0630 ,

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Personnel: S. Miller M. Core Functional Area: MCC's Observatiens: Observed MCC-4C5 to be distorted. Appears that ,

sections A, B, and C are the three affected i

cubicle columns. The MCC appears to be about 4 I inches out of plumb, from the top to the bottom.

The back panels were opened and deformed by the steam impingement. MCC-4C5 was the only MCC in ,

i direct line of sight from the area of the steam l l pipe rupture. MCC-4C3 appears to have no '

! structural damage. Other MCC's in this area are  !

! just dirty. MCC-3C4C-2 was not affected. No cable j l damage was observed.

l Actions: Generated MWO 971276 to clean and inspect MCC-4C5 I Generated MWO 971278 to clean and inspect MCC-4C3 Generated MWR 9701424 to clean and inspect MCC-4B2 Generated MWO 971289 to meggar the cables '

associated with the loads on MCC-4C5 Generated MWO 971291 to inspect the cable trays i and conduit associated with MCC-4C5 ,

1 I Generated MWO 971396 to inspect the auxiliary relays in compartments of MCC-4C5 l

1 i Generated CR 199700466 on damage to MCC-4C5 and to evaluate recovery options GE Representative scheduled to arrive on Tuesday 4/29/97 to inspect MCC-4C5 l

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DAMME ASSESSMENT REPORT 4/28/97 0630 .

. Personnel: J. Tucker J. Foley FunctionalAhea: Cable Assessment Observations: Inspected cables and cable trays in the damaged area around Control Valve No. 1, Stop Valve No. 1, and MCC-4C5. There are two cables hanging from open conduits. These cables are believed to be for plant lighting.

Cable Tray south of Control valves: This tray appears to primarily carry the cables for the-Control valves. The 12 inch tray consists of 2

, tiers. The east and of this tray was extensively l damaged, particularly the lower tray section. The l l last few feet of the lower tray were empty, i hawever the damage did affect the connecting conduits and cables for the 2 eastern most control Valves. The unistrut cable tray support has been j significantly damaged.

Cable Tray below Stop Valves: This tray appears to carry cables for the Stop Valves. This tray is also 2 tiers. No tray damage was noted. The cables leaving this tray in sealtight to the east most Stop Valve may have been subjected to the steam blast and stressed. .

Cable Tray' north of HCC-4C5: one of the unistrut support hangers unnediately east of T6 for this cable tray is twisted. This support has an emergency horn and light mounted to it. The light support bracket appears stressed. Several tray covers west of T6 are displaced and it looks like a tray section divider is sticking out of the third tier from the top. Two pieces of lumber (2X4) can be observed in the fourth tier from the bottom. These could have been present prior to the steam line rupture.

Conduit to MOV RCV-978 has been bent.

Debris was observed above the riser into cable ,

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DAMMIE ASSESSMENT REPORT 4/28/97 0630 -

tray west of T6 above VA-161F. .

? There is an open conduit that appears to be empty on the north wall above VA-161G.

Actions: MNR 9701508 written for east section of lower cable tray south of Control Valves that needs to be repaired. Also includes the unistrut support.

MWR 9701510 written to inspect cable trays east and west of T6 and clean out debris. Tray covers and fastners need replacement. Emergency horn and light needs to be repaired.

Mwo 971509 written for repair of RCV-978 conduit.

l The two open conduits with exposed wires need to be confirmed to be for plant lighting. No work document generated for this yet, i

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DAMAGE ASSE55MDt? REPORT 4/28/97 0630 .

. Personnel: C. Fritts B. Bickels Functional Area: Main Steam /Feedwater/ Condensate Observations: Walked down the subject systems on night of Thursday, 4/24/97, to assess damage from the extraction steam pipe rupture. The scope of the (

inspection included 2nd and 4th stage extraction  ;

steam pipes from the turbine to the feedwater heaters; FW-14A/B, FN-15A/B, FN-16A/B feedwater heaters; Feedwater and Condensate pipes in the -

North end of the Turbine Building; Main Steam pipes from the Stop and Control Valves to the turbine, and associated drain lines; traps, vent valves, drain valves and instrumentation  ;

associated with the above.

With the exception of the equipment in the immediate vicinity of the rupture, the systems were in very good condition. Any damage identified was photographed and documented.

Actions: The following MNRs were generated for damage that had not been previously identified:

Igg DESCRIPTION 9701406 SV-2 Upper drain line bent ,

9701407 SV-1 Lower drain line bent coming our of the " Tee" from SV-2 drain line 9701408 Insulation severely damaged on MS-171, -

172, -301 and -302 9701409 FN-316 Insulation damaged 9701411 Auxiliary Steam Unit Heaters will need

cleaning / replacement l 9701412 Main Steam Lines coming out of the Control Valves - They have original insulation on them - it is sagging and should be replaced 9701413 Hanger in TB Baskment fram SV 2 drain line bent t

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DAMME ASSESSMENT REPORT 4/28/97 0630 -  !

l Personnel: C. Sterba M. Stanley Functional Area: Fire Protection / Fire Detection Observations: Found 7 sprinkler heads open in North East corner of the Turbine Building Basament and Heater Deck.

No sprinkler heads were found open on the mezzanine level. Several mezzanine level heads were found with damaged head cages and heat shields. Inspected Turbine Lube 011 reservoir sprinkler system and found Thermostatic Release actuated by rate of rise with the fixed temperature portion of the system still intact.

Found sprinkler piping support broken for mezzanine level above lube oil reservoir.

Inspected Turbine Generator Preaction System and did not find any open heads. Supervisory air still present on system.

Fire detectors in steam release area appeared dirty.

Actions: Generated MWO 971332 to inspect and replace damaged or actuated sprinkler heads.

Submitted OSCAR for Fire Detection Procedure EM-CP-06-FDZ-TB. This procedure inspects, cleans and tests detectors in the Turbine Building. .

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DAMAGE ASSESSMDIT REPORT 4/28/97 0630 .

. Personnel: K. Naser J. Mixan l Functional Area: Turbine /EHC/ Control & Stop Valves ,

Observations: 1. The steam chest needs to reinsulated in the area of CV-1 and CV-3

2. The solenoid and servo valves on CV-1, CV-3, SV-1, and SV-2 need to be replaced.
3. The wires to the servos and' solenoids on CV-1 ,

l and CV-3 need to be closely inspected. This will be done during the replacement NWO's.

4. The LVDT's on CV-1-0, CV-3-0, SV-2-0, and SV-1-0 need to be replaced.
5. Two of three conduits are pulled out of the Junction Box on CV-1.
6. The EHC tubing to CV-1 is damaced and needs '

to be replaced.

7. All of the junction boxes on the CV's and SV's need to be opened and inspected. j
8. The actuators for CV-1 and CV-3 were in the '

steam plume and need to be disassembled and inspected for heat damage to o-rings, etc. J

9. The push-button's for;MOV-51, MOV-S2, MOV-B 1 were directly in front of the break and should be disassembled and inspected.
10. The conduits to RCV-978 are damaged.
11. EHC-7 desiccant needs to be changed.
12. EHC accumulator charge should be checked. ,
13. EHC fluid needs to be sampled, but general condition of EHC skid is good.
14. HG-4 liquid detector has oil in it.
15. PI-5071 (lube oil header pressure gauge) is stuck at 17 psig.
16. The lube oil in the bowser looks milky, probably has a lot of insulation dust in it.

The particle count was high in the sample

(~40,000).

Actions: 1. Generated MWR 9701427 to reinsulate steam chest in area of CV-1 and CV-3 l

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DAMAGE ASSESSMDIT REPORT 4/28/97 0630 ,

Functional Area: Turbine /EHC/ Control & Stop Valves (cont.) ,

' Actions: '

, 2. Generated the following MNRs for servos and solenoid valves:

CV-1-20A MNR 9701431 CV-1-20B MNR 9701432 CV-3-20A MNR 9701433 CV-3-20B MNR 9701434 SV-1-20A MNR 9701435 SV-1-20B MNR 9701436 SV-2-20A MNR 9701437 SV-2-20B MNR 9701438 PT-CV-1 MNR 9701337 PT-CV-3 MNR 9701368

5. Generated MNR 9701338 on conduits pulled from JB
6. Generated MNR 9701337 for bent hydraulic lines.
8. MNR 9701368 for CV-1 and MNR 9701369 for CV-3 already generated
9. Generated the following MNRs:

MOV-51 MNR 9701428 l MOV-51 MNR 9701429 MOV-B MNR 9701430

10. MNR 9701336 already written for bent conduits
11. MNR 9701375 written for desiccant replacement in EHC-7
12. Generated the following MNR's for LVDT replacement: '

I CV-1-0 MNR 9701446 '

CV-3-0 MNR 9701447 SV-2-0 MNR 9701448 SV-1-0 MNR 9701449 l 13. Generated the following MNR's for stroking

turbine valves:

! Control Valves MNR 9701465

Stop Valves MNR 9701469 l 14. Generated MNR 9701452 to inspect CV & SV l junction boxes.

l 15. Generated MNR 9701471 to sample and test EHC fluid.

16. Generated MNR 9701451 to repair PI-5071
17. Generated MNR 9701450 to check / change bowser filer bags.
18. MMO 971393 already exists for filtering the lube oil with a temporary filter skid.

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. l DAMAGE ASSESSMENT REPORT 4/28/97 0630 .

Personnel: R. Ronning T. Kazor C. Huey (GE) l Functional A'rea: Generator /Alterrex/ Stator Cooling observations:

There is no visible damage to the main generator or the Alterrex housing on the turbine deck. The only;need is to clean the exterior of the generator and the Alterrex housing. The voltage regulator panels suffered no damage. The stator cooling pump skid and associated piping and equipment is also undamaged.

The piping and equipment associated with the hydrogen system is also undamaged. The stator cooling panel AI-134 is undamaged with the only anomaly being that flow meter (FIA-1288) which measures stator cooling flow is flashing. I&C was contacted and it is believed that this flashing could be a problem in the loop.

No other generator problems were observed.

Actions.:

MWR 9701468 has been written tWe investigate the problem with .

l FIA-1288.

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DAMAGE ASSESSMENT REPORT 4/28/97 0630 -

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. Personnel: T. Dailey S. Bottum l Functional Area: Equipment Supports Observations: Pipe supports and equipment supports in the general area of the pipe rupture were inspected for evidence of damage and to assess the need for repairs. Only three damage supports were noted on the inspection; all three being on the 4th stage extraction steam line that ruptured.

The first damaged support is MSH-61 which is a spring can hanger immediate).y upstream of the pipe rupture. The upper rigid 'aanger rod is bent due to the pipe movement afte. the failure. The second damaged support l'> the rod hanger just downstream of the pipe ;:upture. The damage to the rod hanger is minor r.d almost appears to have existed prior to tFs event. The third damaged pipe support is a rigid horizontal restraint weld to column TC-7X. The damage to the support is considered moderate and must be repaired.

The only other abnormality noted was on the steam dump header that leads into the condenser. The insulation on the pipe appears to have evidence of a thru wall leak or a flange leak. The insulation I was discolored but not wet at the time of the .

inspection. This deficiency is not related to the pipe rupture.

l Actions: Generated MWR 9701345 for pipe support MSH-61.

l Generated MWR 9701346 for bent hanger rod.

Generated MWR 9701347 for damage horizontal pipe i restraint.

l l Generated MWR 9701344 for steam dump header leak.

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m RECOVERY PLANS FOR MCC-4C5

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CABLE SYSTEMS l l

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MCC-4C5 .

RECOVERY PLAN Damage Assessment

  • Back panels were opened and deformed by the steam jet impingement.
  • Debris was blown into the back of the MCC. Cables inside the MCC and MCC interior panels are coated with debris. Full extent of debris intrusion is unknown, but assumed to be limited to the back side of the MCC.
  • Field report was that the MCC is leaning forward (away from the steam leak source), indicating possible structural damage to the MCC.
  • The MCC is still energized, providing power to selected loads. One phase of the 3-phase 480-volt feed is grounded (i.e., 0 volts to ground on one leg). Ground has been cleared.

Required Repairs

1. General cleanup of MCC interior and cables, then additional damage assessment to determine best course of action.
  • Inspect each cable in the exposed portion of the MCC for insulation damage.
  • Isolata and megger each load on the MCC to ensure none of the loads are grounded.
  • Inspect each MCC cubicle (MCC-4C5) for damage and debris.
2. Determine and eliminate source of ground on power feed. (Complete)
3. Replace / repair any damaged cables. -

Recovery Options

1. Salvage MCC for return to service
  • Reform or replace back panels on MCC. Replacement panels can either be procured or taken from spare sections of MCC-3C4C-2.

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  • Replace MCC cabling as necessary.
  • Stabilize MCC structure (may require input from DEN-Mechanical).

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2. If damage is too severe, replace MCC-4C5 (see Options 2a and 2b below) .

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a. Procure new MCC (DEN-Electrical assistance required to evaluate.

replacement MCC) l An' entire MCC would be procured under this option. Depending on the compatibility of the new MCC with the existing cubicles, existing cubicles may be transferred from MCC-4C5 to the new MCC.

If it is determined that the new MCC will not bs compatible with the existing cubicles, then new cubicles will also need to be purchased.

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  • De-energize, disconnect and remove old MCC-4C5 i Install new MCC in location of old MCC-4C5
  • Connect cabling to new MCC cubicle assemblies
  • Test each load to ensure proper operation
b. Use available sections of MCC-3C4C-2 at MCC-4C5 Much of MCC-3C4C-2 has been abandoned (due to water plant abandonment) and several entire sections are available for use.

Feasibility of this option would need to be explored when MCC-

3C4C-2 is available for inspection.

i e De-energize, disconnect and remove old MCC-4C5 1

  • De-energize, disconnect and remove available sections of MCC-3C4C-2 j
  • Restore power to remaining portions of MCC-3C4C-2 -

Install removed sections of MCC-3C4C-2 at MCC-4C5 location, I transferring cubicles from old MCO-4C5 to the MCC-3C4C-2 )

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  • Connect cabling to new MCC sections j
  • Test each load to ensure proper operation 4 .

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RECOMMENDATIONS FOR CABLE INSPECTIONS 1.) Perform a 100% inspections of all cables (36 total) in cable tray T5.

These are all instrumentation and control cables for the control valves and stop valves. Kevin Naser is determining the tests and procedures l

' that will exercise the valves and insure the associated instrumentation / control signals are functioning properly. Attachment I lists the cables in tray T5.

2.) Perform a complete visual inspection and 33% megger inspection of the 480VAC power cables in cable tray T6 which is located north of MCC-4C5.

l There are a total of 56 cables in sections P4, P4A, and P3 of tray T6.

l Emphasis will be placed on meggering the pump and ' fan motor loads versus i the valve motors. If problems are found, the scope of cables to be meggered will be adjusted accordingly. The selected cables to be meggered are as follows:

1 CABLE # SOURCE: DESTINATION: l B512 MCC-4B2-006 MOV-B-C7-M B685 MCC-4B2-D01 FP-5-H l l 8536 MCC-482-C01 ST-4B-M B542 PKC-4C3-D06 VD-78-M B564 MCC-4C3-A02 EE-2G-1B l B668 MCC-4C3-E05 CF-7B-M B570 MCC4C3-D06 VD-58-M B521 MCC-4C3-C01 ST-6B-M 872 MCC-3C4C-2-G01 MPP-2 -

A504 MCC-3A4-006 MOV-A-C7-M l A520 MCC-3A4-D01 ST-6A-M l A529 MCC-3A4-C03 VD-1A-M l

A522 MCC-3B2-C04 CF-4-M A523 MCC-382-E05 CF-5-M l A541 MCC-3B2-006 VD-7A-M A563 PKC-382-A02 EE-2G-1A 4569 MCC-382-D05 VD-5A-M A10183 MCC-382-802 VA-766-M l

3.) Instrumentation and control cable in cable tray T6 will be visually inspected for signs of damage and cracking. No megger tests are i

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proposed for these low voltage cables unless damage is visually ~

observed.

4.) Electrical junction boxes in the area of the steam line rupture and -

immediately below will be inspected for signs of excessive moisture and to dry out the boxes as necessary. All boxes north of the condenser on the 1011' level shown on drawing Il436-E-283 will be inspected. Push button stations in this area will also be checked. Chuck Schaffer is

! identifying these boxes and push button stations.

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ATTACl#fENT I: CABLE TRAY T5 CABLES m

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4 CABLE ORIGINA- DESTIN- LOOP /EQUIPNENT ,

# TION ATION 4

2445A JB-31T SV-1 VLV CL LIM SW SVCS-1 INTLK W/ 86/SVGI-2445B JB-31T. - SV-2 VLV CL LIM SW SVCS-2 INTLK W/ 86/SVG1 2445C JB-31T SV-3 VLY CL LIM SW SVCS-3 INTLK W/ 86/SVG1 l 2445D JB-3}T SV-4 VLV CL LIM SW SVCS-4 INTLK W/ 86/SVG1 8963 CV-1-33D AI-50 CV-1 LIMIT SWITCH

8978 JB-TB7 AI-50 PS-101 i

j 8991 SV-1-0 AI-50 OPEN LIM SW (SV05-1) TEST SW (SVTS-1) TRIP 8995 SV-1-0 Al-50 VALVE POSITION TRANSDUCER (PT-SV1) 8996 SV-1-0 AI-50 VALVE POSITION TRANSDUCER (PT-SV1) 8997 SV-2-0 Al-50 OPEN LIM SW (SV05-2) TEST SW (SVTS-2) 8999 SV-2-0 Al-50 VALVE SERVO VALVE (20-SV2) ,

9000 SV-2-0 AI-50 VALVE SERVO VALVE (20-SV2)& POSN XDCR (PT-SV2) l 9003 SV-2-0 AI-50 VALVE POSITION TRANSDUCER (PT-SV2) l 9005 SV-3-0 AI-50 OPEN LIM SW (SY05-3) TEST SW (SVTS-3) TRIP l 9009 SV-3-0 AI-50 VALVE POSITION TRANSDUCER (PT-SV3) 9010 SV-3-0 AI-50 VALVE POSITION TRANSDUCER (PT-SV3) 9011 SV-4-0 AI-50 OPEN LIM SW (SV05-4) TEST SW (SVTS-4) TRIP l

9015 SV-4-0 AI-30 VALVE POSITION TRANSDUCER (PT-SV4) ,

j 9016 SV-4-0 AI-50 VALVE POSITION TRANSDUCER (PT-SV4) l 9017 CV-1-0 Al-50 CLOSE LIM SW (CVCS-1) TEST SW (CVTS-1) l 9019 CV-1 AI-50 VALVE SERVO VALVE (20-CV1) 9020 CV-1-0 AI-50 VLVSERVO(20TCVI) POSN XDCR (PT-CV1) 9023 CV-1-0 AI-50 VALVE POSITION TRANSDUCER (PT-CY1) 9025 CV-3-0 AI-50 CLOSED LIM SW (CVCS-3) TEST SW (CVTS-3) 9027 CV-3-0 AI-50 VALVE SERVO VALVE (20-CV3) 9028 CV-3-0 AI-50 VALVE SERVO VALVE (20-CV3)& POSN XDCR (PT-CV3) 9031 CV-3-0 AI-50 VALVE POSITION TRANSDUCER (PT-CV3) 9033 CV-4-0 AI-50 CLOSED LIM SW (CVCS-4) TEST SW (CVTS-4)

9034 CV-4-0 Al-50 CLOSED LIM SW (CVCS-4) TEST SW (CVTS-'4) -

9035 CV-4-0 Al-50 VALVESERVOVALVE(20-CV4}

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9036 CV-4-0 AI-50 VALVE SERVO VALVE (20-CV4)& POSN XDCR (PT-CV4)

, 9039 CV-4-O' AI-50 VALVE POSITION TRANSDUCER (PT-CV4) 9041 CV-2-0 AI-50 .

CLOSED LIM SW (CVCS-2) TEST SW (CVTS-2) 9043 CV-2-0 AI-50 VALVE SERVO VALVE (20-CV2)

9044 CV-2-0 AI-50 VALVE SERVO VALVE (20-CV2)& POSN XDCR (PT-CV2) 9047 CV-2-0 AI-50 VALVE POSITION TRANSDUCER (PT-CV2)

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l MWR 9701367 - ATTACMENT 1 TERMIKal BOXES AND PUSH BUTTON STATIONS .

MOISTURE INTRUSION INSPECTION

'990' LEVEL:

TERMINALh0XES:

TAG # DESCRIPTION LOCATION j JB-116T JB FOR VA-161A, VA-161B 14rTC-Or9 0995 l

JB-54T JB FOR FCV-1151B, FW-318, PS-Il51B/E 1rTC1-Or9 0990 JB-55T JB FOR FCV-IISIC, FW-317, PS-1151C/F 4rTC-Or9 0990 JB-142T JB FOR PC-1148C, PC-1150C, PC-1149C, PC-1149 8rTB-135'9 0994 JB-153T JB FOR PUMP FW-5A OWTB-10r7 0996 JB-41T JB FOR 100A DISC SW 2E'TD-0S'8X 0990 JD-140T J8 FOR PC-1148A, PC-1150A, PC-1149A, PC-1149 2E'TE-14S'9 0993 JB-53T JB FOR FCV-1151A, FW-319, PS-1151A/D 18rTD-26r8 0990 JB-141T JB FOR PC-11488, PC-11508, PC-Il49B, PC-1149 6E'TD-135'9 0993 PUSH BUTTON STATIONS:

PUSH BUTTON SWITCH TYPE DESCRIPTION OM/48 SGFEEDPUMPLOC5LPANELB OM/15 JB-116T (CA8LE 8398)

OM/15 JB-116T (CABLE B390)

OM/48 SG FEED PUMP LOCAL PANEL C OM/1 7 (CABLES D5532, B5524, A5516)

OM/11 EHC-3A-PB OM/3 EHC-9-PB OM/l EHC-3A-PB AND EHC-3B-PB OM/38 JB-41T OR WR-598A-DS i

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I~ MWR 9701367 - ATTACHMENT 1 I -

TERMINAL BOXES AND PUSH BUTTON STATIONS i MOISTURE INTRUSION INSPECTION b

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'1011' LEVEL:

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i TERMINAL BOXES:

i l TAG # DESCRIPTION LOCATION l JB-122T JB FOR VA-161F,VA-161G 0FTD-45'9 1011 l JB-58T JB FOR LA-1197A, LA-11978 IFTAl-0F09 1011 JB-59T JB FOR LA-11978, LA-1197D lE'TAl-0W9 1011 l l JB-16T JB FOR LC-963A, LCV-963A 19FA-5W8 1011

[ JB-17T JB FOR LC-9638, LCV-9638 OWTB-IS'8 1017 )

JB-15T JB FOR LC-967A, LCV-967B 0rTC-Or8 1017 3

JB-14T JB FOR LC-967A, LCV-967A 0WTC-0N'8 1017 i JB-166T J8 FOR SEPERATOR DRAIN TANK NO. 3 AND 4 2WTC-Or7X 1017 i

j JB-151T JB FOR RCV-978, RCV-979, RCV-979 3E'TD-6r7X 1011 i

JB-180T UENOWN f 1011

JB-170T JB FOR DV-3, DV-4 3FB-8r6X 1011 JB-TB6 EAST OF TURNING GEAR OIL PUMP LO-3 1011 i JB-164T JB FOR LO-14A, LO-148, LO-14C 4E'TE-3r8 1011 l JB-TB8 NORTH OF BEARING LIFT PUMPS 1011 .

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JB-31T JB FOR SV-1/2/3/4 IFTD-Sr8 1011 1 JB-167 JB FOR SEPERATOR NO. 1 AND 2 2E'TE-Or7X 1011 i

a i PUSH BUTTON STATIONS:

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} PUSH BUTTON SWITCH TYPE DESCRIPTION l OM/15 JB-122T (CABLE 8688) 0M/15 JB-122T (CABLE 8680)

OM/2 JB-17T OM/2 JB-151T FOR RCV-978 OM/l JB-164T FOR 2 STATIONS (AND CABLE B2635 FOR 1) l OM/38 JB-31T FOR WR-598C-DS

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MWR 9701367 - ATTACMENT 1 -

TERMINAL BOXES AND PUSH BUTTON STATIONS MOISTURE INTRUSION INSPECTION i

'1036' LEVEL: ,

1 TERMINAL BOXES:

TAG # DESCRIPTION LOCATION I

JB-155T JB FOR VA-165A 10WTAl-6N8X 1036 JB-TB1 EAST SIDE OF TURBINE FRONT STANDARD 1036 JB-154T JB FOR VA-165E 2W'TE-6N'8X 1036 l

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t OETAGE RECOVERY EFFORT l l

MATRIX l

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1 i Note: This matrix is dynamic and will be updated frequently. The Manager - System l Engineering will keep the most up-to-date copy of this matrix with the master copy of the Damage Assessment Repon.

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System Engineering FCS OUTAGE RECOVERY EFFORT 1430 nrs, uay 12,199 MWR MWD SE fCRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS ARCHITECTURAL (AE)

N/A N/A JMS SE AE Perform Procedure COMPLETE. No problems associated with SE-PM-AE 1003, Turbine the steam line rupture were Building Structure noted.'

Inspection.

9701666 MWD Required JMS PE AE Suspend a scaffolding at MWD Required.

approximately the 1029' To be done on line.

level of the mezzanine level in the Turbine Building to assist plant cleanup.

9701765 MWD Required JMS GM AE Handrail sections for access MWD Required.

to valves MS-172 and To be done on line.

MS-173 blew away and were bent during the steam line rupture event. Repair /

reinstall handrails. Repair toe plates and handrail i sockets.

l SYSTEM.TBL Page 1 of 34.

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,191 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS AUX 1UARY STEAM (AS) 9701411 MWO 971521 CHF PE VA-161G Clean Aux Steam unit Performing on-line. N/A heaters.

9701367 MMO 971548 WBP EM VA-181G Replace thermostat. COMPLETE. Thermostat shorted due to water and debris as a result of steam line break. Repiaced thermostat.

9701336 MWO 971313 DGF EM .RCV-978 Replace conduits and COMPLETE. Conduit was damaged.

cables as required for 8th Cables were meggered satis-stage extraction steem to factorily. Conduit was Aux!liary Steam Radiation replaced.

Control Valve RCV-978.

97G1890 MMO 971687 CHF EM ' RCV-978-PB inspect / clean / repair and/or COMPLETE. Switch was dirty. Cleaned replace the stop push switch, lubricated and tested button for RCV-978. volve with switch satisfac-torily.

SYSTEM.TBL Page 2 of 3

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l System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,199f MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS REStsLTS ELECTRICAL (EE) 9701367 MWO 971351 DGF EM EE Inspect sample of junction COMPLETE. :See explanation of results boxes and pushbotton pelow.)

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(RESULTS OF MWO 971351):

The following Terminal Boxes were inspected on the 990' Elevation of the Turbine Building for signs of moisture intrusion, and no sign detected:

JB-116T JE 54T JB-55T JB-142T JB-153T JB-41T JB-140T JS-53T JB-141T The following Push Button Stations were inspected on the 9e0' Elevation of the Turbine Building for signs of moisture intrusion, and no were detected: '

OM/48 (2) OM/15 ON JS-IIST (2) 'OM/1 (2) OM/11 OM/3 OM/38

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t The following moisture Terminal Boxes were Inspected on the 1011' and 1017' Elevations of the Turlbine Building for signs of moisture intru were detected:

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JB-122T ' JB-16T JB-17T JB-186T .JB-151Ti JB-180T JB-TB6 JB-164T - JB-TBS , . .JB-167 The following six Terminal Boxes were inspected on the 1011' and 1017' Elevations of the Turbine Building for signs of moisture in

moisture intrusion were detected. The Terminal Boxes were air blosmldryi.j

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LJB-SST.. 1 JB-59T JB-15T JB-14T ' .B-17075 JB-31T The following Push Button Sta3ons were inspected on the 1011' Elevation of the Turbine Building for signs of moisture intrusion, and n were detected: '

OM/15 ON JB-122T OM/15 ON JB-122T OM/2 ON J3-17T; OM/2 ON JB-151T OM/1 ON JB-164T- OM/38 ON JB-31T The following Terminal Boxes were inspected on the 1036' Elevetiert of the Turbine Building for signs of moisture intrusion, and no signs of JB-1557 JB-TB1 JB-154T l

SYSTEM.TBL Page 3 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,199 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS

_ ELECTRICAL (EE) (Contmuod) 9701524 MMO 971510 DGF EM ELP-5 Inspect and test emergency COMPLETE. Emergency lights tested lighting in Turbine Building satisfactorily, per EM-ST+EE-0011. -

9701366 MWO 971574 RDG- l&C EE Inspect instrumentation on COMPLETE. (See explanation of results turbine mezzanine and ' below.)

basement.

(RESULTS OF MWO 971574) The assessments were conducted by Senior I&C Technicians and I&C Coordinators between April 27 and May 1,1997. The Essessments were performed as directed by MWO 971574 which allowed the opening / removal of covers, etc., on applicable instrumontation. The pnmary inspections were conducted to evaluate the effects of steam impingement on the units as well as moisture intrusion caused either by the deluge system or the washing of areas during asbestos abatement.

The following table highlights those instruments inspected / opened during the pedod and documents condition. Those devices showing possible damage er excessive exposure will require attention per work documents accordingly identified.

The following instruments were found and swelueled to be acceptable and require no additional review:

PT-941 PT-910 LA-1197C ;LT-1197A LT-11978 LC-1197D LC-11978 '. L LC-1197C LC-11968 LC-1196A PT-1141 LT-1196A LC-1196A LA-1196C LA-11968 LA-1196D LT-11968 LC-1196C LC-1196A LC-11968 LC-11960 LC-9598 LC-959A PT-966 PT-920 PT-945 PT-944 PT-943 t PT-939 JB-59T-The following instruments were found and twelueled to have possibly been impacted du;1ng the event and, as such, have had work documents genereted ?

to evaluate and perform function tests / calibrations accordingly:

LA-1197D WP003393 PT-958 . WP003424 LA-1197A MWR 9701567 PT-962 WP003425 LA-11978 MWR 9101568 PT-946A ' WP003423 PT-947 WP005136 PT-919 WP003421 N/A WP 005662 DGF' EM' ELP inspect emergency lightinn COkWLETE. All lighting lantems were l PMO 9703693 < lantems in the Turbine, inspected satisfactorily. l Service and Auxiiiery buildings.

SYSTEM.TBL Page 4 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,199; MWR MWD SE CRAFT TAG NO. PROBEM DESCRIPTION STATUS RESULTS ELECTRICAL (EE) (Continued) 9701665 MMO 971671 DGF EM EE Repair or replace the light Ready to work.

fixtures in the Turbine To be done on line.

Building near CV-1 that were damaged during the steam line rupture.

SYSTEM.TBL Page 5 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,19T

=

MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS TURBINE ROOM MOTOR CONTROL CENTERS (MCC) 9701320 MWO 971276 SRM EM MCC-4CS Clean and inspect MCC-4C5 COMPLETE. (See explanation of results using EM-PM-EX-1100. below.)

(RESULTS OF MWO 971276):

Back panel doors open and deformed.

Panel doors were straightened and rehung.

Three door sills in the back broken.

New door silis were made and installed.

A small portion of the bus insulation in the second vertical section damaged.

The bus insulation was repaired.

MCC structure was pushed out of plumb (6 to 8 inches).

No repairs required; bus is sound.

A representative from General Electric performed a field inspection of MCC-4C5 and concurred with OPPD's conclusion that the MCC could be retumed to service.

Conduits attached to top of the MCC suffered minimal deformation.

No repairs required.

The breaker for seal oil pump LO-12A tripped and could not be rec!osed.

The breaker was replaced using MWO 971479.

Powdered pipe insulation material was blown throughout the MCC, coating exterior and interior components.

The entire MCC was cleaned up.

9701321 - MWO 971278 SRM EM MCC-4C3 Clean and inspect MCC-4C3 COMPLETE. All MCC cubicles and buses using EM-PM-EX-1100. were cleaned and inspected.

No deficiencies found attributable to the event.

SYSTEM.TBL Page 6 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,19s MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS TURBINE ROOM MOTOR CONTROL CENTERS (MCC) (Continued) 9701424 MWO 971418 SRM EM MCC-482 Clean and inspect MCC-482 COMPLETE. All MCC cubicles and buses using EM-PM.EX-1100. were cleaned and inspected.

No deficiencies found attributable to the event.

9701332 MWO 971289 SRM EM MCC-4C5 Megger cables associated COMPLETE. No cable damage detected by with MCC-4C5. meggering except for cable 600 to be repaired by MWO 971558.

9701330 MMO 071291 SRM EM MCC-4C5 Inspect cable trays and COMPLETE. No work performed.

conduit associated with MCC-4C5. (May be covered by MWO 971363.)

9701396 MWO 971396 SRM EM MCC-4C5 Clean and inspect aux COMPLETE. All Auxiliary relays in relays in MCC-4C5. compartments were cleaned and function checked. No deficiencies found.

9701472 MWO 971558 SRM EM MCC-4C5-A05 Replace / repair cable 600 COMPLETE. Cable 600 insulation repaired (supply to welding with Raychem sleeves.

receptacles).

9701494 MWO 971479 SRM EM MCC-4C5-G04 Replace breaker in . COMPLETE. Breaker would not close.

MCC-4C5-G04 for LO-12A Breaker was replaced. The Saino ECH 97-148. failure was due to the steam

~

leak.

9701511' MMO 971482 SRM EM MCC-4C5- Perform Procedure Cai1PLETE. No deficiencies noted A02U EM-PM-EX-0203. attributed to steam leak event.

9701511- MMO 971487 SRM EM MCC-4C5-A05 Perform Procedure COMPLETE. No deficiencies noted EM-PM-EX-0203, attrib.4ed to steam leak event.

SYSTEM.TBL Page 7 of 3

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,19 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS

==

TURBINE ROOM MOTOR CONTROL CENTERS (MCC) (Continued) 9701511 MMO 971489 SRM EM M CC-4C5-803 Perform Procedures COMPLETE. No deficiencies noted EM-PM-EX-0203 and attributed to steam leak EM-CP-08-1600. event.

9701511 MMO 971496 SRM EM MCC-4C5-CO3 Perform Procedures COMPLETE. No deficiencies noted EM-PM-EX-0203 and attributed to steam leak EM-CP-08-1600. event.

9701511 MMO 971497 SRM EM MCC-4C5-D03 Perform Procedures COMPLETE. No deficiencies noted EM-PM-EX-0203 and attributed to steam leak EM-CP-08-1600. event.

9701511 MMO 971500 SRM EM M CC-4C5-E03 Perform Procedures COMPLETE- No deficiencies noted EM-PM-EX-0203 and attributed to steam leak EM-CP-08-1600. event. '

9701511 MMO 971502 SRM EM MCC-4C5-F03 Perform Procedures COMPLETE. No deficiencies noted EM-PM-EX-0203 and attributed to steam leak -

EM-CP-08-1600. event.

9701511 MMO 971515 SRM- EM MCC-4C5-G03 Perform Procedures COMPLETE. No deficiencies noted EM-PM-EX-0203 and attributed to steam leek EM-CP-08-1600. event.

9701324 MWO 971320 DGF. EM EE-11 Megger power cable from COMPLETE. All meggered cables are affected MCCs 3B2,4C3 acceptable. Lowest reading and 4C5. was 1000 M Ohms. Most read m.

9701497 MMO 971480 JMS PE MCC-4C5 Dismantle scaffolding. COMPLETE. Scaffolding dismantled.

9701320 MMO 971536 SRM EM MCC-4C5 Replace front panel covers COMPLETE. Front panel covers replaced.

on MCC-4C5 (discarded during asbestos abatement).

SYSTEM.TBL Page 8 of 3

Systera Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,191 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS TURBINE ROOM MOTOR CONTROL CENTERS (MCC) (Continued) 9701320 MMO 971577 SRM EM MCC-4C5 Fabricate and install bus COMPLETE. Bus connection fabricated connection piece for and installed. Not believed MCC-4C5. to be'due to steem leak.

9701497 MMO 971665 JMS GM MCC-4C5 Erect / dismantle scaffolding VOlc. MWO 971665 was voided.

to access cable trays on the east side of MCC-4CS.

SYSTEM.TBL Page 9 of 3<

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,191 MWR MWD SE CRAFT TAG NO. PROBEM DESCRIPTION STATUS RESUt.TS CABLE SYSTEMS 9701508 MWO 971481 DGF EM EE Repair / replace damaged in progress - 5/12/97.

cable tray and unistrut support for the cable tray "

near Main Steam Control Valve CV-1.

9701510 MWO 971520 DGF~ EM EE Inspect, adjust and repair COMPLETE. Straightened and realigned cable tray supports, covers cable tray supports. Adjusted and tray dividers on the chairs of the trays and cable trays east of building reinstalled covers. Inspected coiumn T6. all trays for defects.

Realigned tray dividers.

Repaired horn and orange emergency flashing light.

9701364 MWO 971363 DGF'- . EM EE-11 A Inspect conduits and cable COMPETE. Replaced unistrut straps for trays in Turbine Building. two conduits coming out of MCC-4B2. Replaced screws for junction box cover for the main steam stop valves.

9701324 MMO 971570 DGF EM? EE-11 Megger cables in Cable Tray COMPETE. All cables meggered T5. satisfactorily (at or above .

2000 M ohms).

9701324 MMO 971571 DGF1 EM.i EE-11 Perform visual inspection of - COMPETE. No problems noted.

cables in Cable Tray T5.

9701324 MMO 971572 DGF. EM- EE-11 Perform visual inspection of COMPETE. No problema noted.

cables in Cable Tray.T6.

SYSTEM.TBL Page 10 of 3

System Engineering FCS OUTAGE RECOVERY EFFORT i430 hrs, uay 12, i997 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS EXTRACTION STEAM 9701419 MMO 971388 JMS GM FW-15A Erect / dismantle scaffold to in progress - 5/12/97.

support erosion / corrosion inspection.

  • 9701420 MMO 971389 JMS GM FW-15B Erect / dismantle scaffold to in progress - 5/12/97.

support erosion / corrosion inspection.

9701421 MMO 971390 JMS GM FW-16A Erect / dismantle scaffold to in progress - 5/12/97.

support erosion / corrosion inspection.

9701422 MMO 971391 JMS GM FW-168 Erect / dismantle scaffold to CORAPLETE.

support erosicn/ corrosion -

inspection.

  • 9701426 MMO 971394 JMS? GM ~ AE Erect / dismantle scaffold to- C(MAPLETE.

support erosion / corrosion .

inspechon.

9701443 MWO 971404 MWN PE ST-1 If necessary, replace the TO BE VOIDED. Based upon inspection third 90* elbow on 2nd stage results, the 90* elbow at Site extraction header. S-38 does not need to be replaced.

9701445 MWO 971410 MWN. PE ST-1 Replace third 45' elbow on : C(EAPLETE. The 45' elbow at Site S-53 east and west 6th stage end the " pup-piece' at Site extraction header and the S-54 were replaced.

second pup piece down-stream of the second 45*

elbow on ihe west extraction header. Third 45' elbow is .

also to be replaced.

9701299 MMO 971267 MWN. CH. ST-1 Clean up insulation from CORAPLETE.

Turbine Building.

SYSTEM.TBL Page 11 of 34 '

System Engineering FCS OUTAGE. RECOVERY EFFORT i4ao hrs May 12, i9s MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESUt_TS EXTRACTION STEAM (Continued) 9701329 MWO 971400 MWN CM ST-1 If necessary, replace the 7th COMPLETE. Elbow replaced.

elbow downstream of ST-1 on the 4th stage extraction header. '

9701464 N/A. MWN IAC PT-962 If necessary, remove / replace VOIDED. MWR 9701464 Voided pressure transmitter to because pine was not support pipe replacement. replaced.

9701466 MMO 971456 MWN l&C TE-961 Remove temperature - COMPLETE. Based upon inspection element, cePhrste it, results et Sites S-28, S-29, and reinstallit when MWC and S-32, this instrument was 971397 is cornplete. removed, calibrated and then replaced to allow for pipe repiecement..

9701467 MMO 971455 MWN l&C TE-957 If necessary, remove / replace TO BE VOIDED. MMO 971455 Voided because temperature element to pipe was not replaced under support pipe replacement. MWO 971405.

9701491 MMO 971449 'JMS GM AE Erect /diamentle' scaffold to COMPtETE. Scoffolding erected, then inspect onIrection steem dismantled.

piping.'

9701516 MMO 971498 JMS PE FW-16A Erect / dismantle scaffold to in progress - 5/12/97.

inspect extraction steam piping.

9701517 MWO 971485 - MWN PE FW-168 Remove insulation from first VOIDED. MWO 971485 Voeded and second bonds down-stream of FW-ISB.

9701525 'N/A MWN PE MS Need to tehdchromium COMPLETE. Chromium content values content in the Alh stage, were not unreasonable.

Values were expected.

SYSTEM.TBL Page 12 of 3 !

_ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _-____-___-__-____-__-_L

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,1997 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS EXTRACTION STEAM (CDntinued) 9701565 MMO 971537 CHF PE FW-I SA Need to support the COMPLETE. N/A grinding & NDE testing of areas identified by Engi-neering.

9701586 N/A MWN PE MS Flemove the 45' elbow from VOIDED. Void - Work completed inspection Site S-53 on the under 971410.

18" extraction header and inspect.

9701319 MMO 971269 JMS GM AE Erect / dismantle scaffold to COMPLETE.

support erosion / corrosion inspection.

9701443 MWO 971405 MWN PE ST-1 If necessary, remove fourth TO BE VOIDED. Based upon inspection 90* elbow on 2nd stage results, the 45* elbow at extraction header. Site S-42 does not require replacement.

9701443 MWO 971406 MWN PE ST-1 If necessary, remove fifth TO BE VOIDED. Based upon inspection 90* elbow on 2nd stage results, the 90* elbow at Site extraction header. F-17 does not require replacement.

9701443 MWO 971407 MWN PE ST-1 If necessary, remove sixth TO BE VOIDED. Based upon inspection 90* elbow on 2nd stage results, the 90* elbow at Site extraction header. F-13 does not require replacement.

9701491 MWO 971459 MWN PE MS Perform visual inspection of COMPLETE. Generated MWO 971560 for 4th stage extraction steam radiograph and stress relieve piping. nozzle weld on 4th stage extraction header. MWO 971560 has been completed.

SYSTEM.TBL Page 13 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,191 MWR MWD SE CRAFT TAG NO. PROBt.EM DESCRIPTION STATUS RESUtTS EXTRACTION STEAM (Continued) 9701516 MWO 971503 MWN PE FW-16A If necessary, replace first To be voided. Based upon inspection and second bends down- results, the first and second stream of FW-16A. bends downstream of FW-16A do not require replacement.

9701517 MWO 971504 MWN PE FW-168 ff necessary, replace first To be voided. Based upon inspection and second bends down- results, the first and second stream of FW-168. bends downstream of FW-168 do not require replacement.

9701329 MW 3 971273 MWN PE' ST-1 Replace third elbow COtri.ETE. The third 90* elbow at Site downstroom of ST-1 on the S-25 ruptured and was, 4th stage extraction header. replaced.

9701328 MWO 971288 MWN PE MS Remove insulation and grid in progress - 5/12/97. MWO open for reinsulation.

and U.T. piping on 2nd and Gridding and U.T. of piping 4th stage extraction steam has been completed.

header.

9701328 MWO 971325 MWNt PE MS . Remove insulation and grid C(MrtETE.

^ U.T. completed satisfactorily.

and U.T. piping on 6th stage '

extraction steam heeder.

9701329 MWO 971397 MWN PE . ST-1 Replace fourth elbow CEMrt2TE. Due to inspection results, the downstroom of ST-1 on the 90* elbow at Site S-27 was 4th stage extraction steam replaced.

header.

9701640 MMO 971627 MWN PE MS Remove insulation and U.T. COtrt2TE. U.T. performed and results downstroom or orifices and satisfactory.

elbows on equalizing line between main steem inlets to ST-1 and 2nd stage _

extraction. '

t SYSTEM.TBL Page 14 of 3 l

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,191 MWH MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS EXTRACTION STEAM (Continued) 9701641 MMO 971629 MWN PE FW-15A Remove insulation, surface COMPLETE. U.T. inspections completed prep, and grid piping for satisfactorily.

U.T. inspection. Pipe .

~

between MS-165 and LCV-963A.

9701641 MMO 971630 MWN PE FW-158 Remove insulation, surface COMPLETE. U.T. inspections completed prep, and grid piping for satisfactorily.

U.T. inspection. Pipe between MS-166 and LCV-9638.

9701645 MMO 971632 MWN PE FW-32A U.T. pipe for about 12 COMPLETE. Three parallel lines were inches downstream of recirc replaced. MWO 971650 line orifice for header drain - generated.

pump FW-5A.

9701531 MMO 971524 MWN PE MS-335 Disassemble valve and COMPLETE. MMO 971524 may not be inspect for damage due to Awaiting PMT. required.

molten slag from cutting out ruptured steam header pipe.

9701501 MMO 971460 MWN PE _AE Remove insulation with COMPLETE. -

glove bags.

9701495 MMO 971451 JMS GM AE Erect / dismantle scaffolding in progress - 5/12/97.

to support asbestos cleanup in Turbing Building base-ment.

9701651 MMO 971649 MWN PE- . FW-CD Remove insulation, buff, COMPLETE. U.T. was completed grid, and U.T. pipe at the satisfactorily.

South end of FW-14A heater.

SYSTEM.TBL Page 15 of 3

System Engineering FCS OUTAGE RECOVERY EFFORT 1430nrs,May 12, 1997 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS EXTRACTION STEAM (Continued) 9701653 MWO 971651 MWN PE FW-328 Replace eroded pipe from COMPETE. Piping replaced.

flow orifice downstream to Awaiting PMT.

1st weld on 90* L -

9701654 MWO 971652 MWN PE FW-32C Replace eroded pipe from COMPl.ETE. Piping replaced.

flow orifice downstream to Awaiting PMT.

1st weld on 90* L 9701675 MWO 971666 MWN- PE . FE-1394 U.T. 6 to 12 inches of pipe COMPT.ETE. U.T. completed.

downstream of FE-1394.

9701645 MWO 971650 MWN PE FW-32A MMO 961632 found erosion COMPETE. Piping replaced.

of the pipe from to the flow Awaiting PMT.

orifice downstream to the i

first weld on the 90* ell.

Replace this piping.

9701445: MWO 971665 MWN' ' PED ST-1 Replace 45' elbow and pop ' C(MAPLETE. All three elbows and pup piece associated with - piece were replaced.

MWO 971410.

i t

i i

i SYSTEM.TBL Page 16 of 34 i

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12, 1997 MWR MWD SE CRAFT TAG NO. f , PROBt EM DESCRIPTION STATUS RESULTS FEEDWATER (FW) 9701341 MMO 971309 MWN PE FW-139 Replace sample line. COMPLETE. Replaced sample line.

9701351 MMO 971337 MWN EM FW-30A Troubleshoot FW-4A t: earing COMPLETE. No peublems found. Possible low oil pressure alarm. moisture in MCC cubic!n.

D701352 MMO 971338 MWN EM FW-30C Troubleshoot FW-4C COMPLETE. No problems found. Possible bearing low oil pressure moisture in MCC cubicle.~

alarm.

9701409 MMO 971566 CHF PE FW-316 Replace damaged insulation Ready to work.

of condensate sample line isolation valve.

9701567 MWO 971556 MWN. I&C . LT-1197A Inspect and repair low COMPLETE. "As Found" loop check values pressure heater FW-15A.- were out of tolerence.; Loop ,

level control loop. adjusted into tolerance.-

Some tubisig and fittings were replaced.

9701568 MWO 971557 MWN l&C LT-1197B inspect and repair low ' COMPLETE. No problems found. "As .

pressure heeler FW-158 - Found" values were estis-level control loop. - factory.

N/A WP003393 ' MWN . l&C LA-1197D Calibrate loop 1197A. COMPLETE. Will not be used.': MWO 971556 to be corWed.'

9701682 MWO 971674 ' MWN PE LCV-12028 Remove ineutetion from the COMPLETE. Insulation removed.

elbow between LCV-1202B and FW 526 for erosion /. _

corrosion inspection. 4 l 9701713 MMO 971703 MWN P8 LCV-1198 Remove insulation, buff COMPLETE. U.T. completed satisinctodfy.

piping, grid piping, and u.T. s l piping. N no repears are required, reinsulate piping.

SYSTEM.TBL Page 17 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,1997 MWR MWD SE CRAFT TAG NO.' PROBLEM DESCRIPTION STATUS RESULTS FIRE PROTECTION (FP) 9701302 MWO 971332 SEC PE FP Replace basement spdnkler COMPLETE. Sprinkler heads replaced and heads. the headers are pressurized.

N/A WP001682 CJS EM Al-153 Calibrate Turbine Building in progress - 5/9/97.

PMO 9700183 Fire Detectors.

9701379 RMO 971364 CJS EM Al-153 Replace detector FD-TB-05 COMPLETE. Detector replaced.

due to trouble alarm.

C701482 RMO 971461 CJS EM Al-153 Replace detector FD-TM-29 COMPETE, , Detector replaced.

due to water damage on asbestos clean-up.

C701482 RMO 971462 CJS EM Al-153 : Troubleshoot fire detector C(MAPETE. Fire detector replaced.

which will not need the . j ventilation tdps disabled. -

l

~

9701302- MWO 971825 SEC PE .FP Replace one sprinkler head COMPLETE. .

Sprinkler head replaced and l on beoement sprinkler * '[ heet collector installed.

system and install heat collector on another spdnkler hood. ,

9701487 MWO 971477 SEC PE FP Clean fire extinguisher in progress - 5/12/97. Vendor is pressure testing TB-24 and weigh cylinder. cylinder.

97018'76 .MWO 971675 CJS EM. Al-153 : Troubleshoot the reason COMPLETE. _

Beem detector monitor that beam detector FD-To-04 module replaced.

would not alarm with push buttons or filters.

i a

I i

i SYSTEM.TBL Page 18 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,199 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATilS RESULTS FIRE PROTECTION (FP) (Continued) 9701703 MMO 971700 SEC PE AE There is a broken hanger on 'To be worked on line.

the northmost sprinkler system branch line between

  • FW-48 and FW-4C. This does not affect sprinkler system operability. Reinstall or replace the all thread for the beam clamp.

9701679 MMO 971735. SEC PE FP Tiie turbine lube oil To be worked on line.

rese voir sprinkler system needs the following items to be corrected: The heat col-lector above the thermo-static release in reservoir  !

room needs to be realigned with the thermostatic release and the dust covers need to be reinstalled on both thermostatic releases.

9701302 MWO 971441 SEC PE Inspect and repair / replace FP. COMPETE. Heat collectors and cages mezzanine level sprinkler .for the spdnkler heads were 4

heads.' Replace broken all replaced at required. All throod on beam clamp throod on beam clamp hengeron fire main piping henger was replaced.

shove the lube oil reservoir.

9701776 MWD Required SEC PE FP Uncontrolled foam seal To be worked on line.

LO-N-2 in north well of

. ladder storage room under i turbine lube oil reservoir has been damaged by acti-vation of reservoir deluge system. Repair seal.

SYSTEM.TBL Page 19 cf 34 l

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,199 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS FUEULUBE OIL (FO, LO) 9701587 MWO 971580 KKN EM LO-4-M Megger DC motor on COMPLETE. Meggering completed. No emergency bearing oil problems found.

pu m p. '

9701450 WP001024 KKN PE LO-2 Change filter element, clean COMPLETE. An excessive amount of PMO 9801045 water trap drain line, clean insulation powder was found tank, and replace bowser in the oil. LO-2 is being tank bag filters for lube oil cleaned and the filters conditioning unit LO-2. replaced.

SYSTEM.TBL Page 20 of 3<

- ~_ _ ____ __ - _______________-___________________. _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ - _ _ _ _ _ _ _ - -

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,1997 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS l GENERATOR /ALTERREX/ STATOR COOUNG j 9701468 MWO 971450 RRR I&C FIA-1288 Troubleshoot stator water COMPLETE.

i A zero shift in the transmitter coolant flow loop because was fouiid. Transmitter was the indicator is flashing on adjusted.

and off.

9701557 MWO 971610 RRR MM EE-17 Remove and replace filters COMPLETE. Alterrex filters were replaced.

on south end of Alterrex. The inside of the Alterrex fan Vacuum inside Alterrex and housing was cisaned.

fan housing. Generator field rectifier door weather stripping was repaired.

SYSTEM.TBL Page 21 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT i430 nrs, uay 12,19 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS INSTRUMENT AIR (IA) 9701378 MMO 971341 CHF PE CA-1 A Inspect instrument air COMPLETE. QC performed U.T. of joints header solder joints in the and no problems were found, affected area of the Turbine Building.

SYSTEM.TBL Page 22 of 3

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,1991 MWR MWD SE CRAFT TAG MO. PROBLEM D8. SCRIPT 10N STATUS RESULTS MAIN STEAM (MS) 9701408 MMO 971469 MWN PE M S-171, Replace damaged insulation COMPETE. Remove insulatiorr on this MS-172, on low pressure heaters MMO. Insulation will be MS-300 and FW-14A and FW-148 inlet install 6d on MMO 971681.

MS-302 and outlet valves.

9701344 MWO 971317 CHF PE MS J Remove insulation from 90* COMPLETE. Insulation removed.

- elbow at elevation 1029 on the steam dump header to the condenser.

9701344 MMO 971519 JMS PE AE Erect scaffolding for COMPLETE. MWO 971519 Voided due to MWO 971317. work performed under MWO 971522.

9701344 MWO 971522 JMS PE MS Erect scaffolding for in progress - 5/12/97.

MWO 971317.

9701344 MWO 971323 CHF PE MS Install insulation on 90* In progress - 5/12/97.

elbow associated with MWO 971317.

9701346 MMO 971431 JMS GM AEL Erect scaffolding for VOID. MMO 971431 was voided.

MWO 971343.

9701345 MWO 971343 MWN CM MSi^ Repair /repiece damaged COMPLETE. Top rod was replaced.

parts of the spdng can henger MSH-61.

9701346 MWO 971344 MWN CM MSL Repair / replace damage of COMPLETE. Top rod was replaced.

spdng can support downstream of pipe rupture.

9701347 N/A MWN PE MS- Horizontal pipe restraint COMPLETE. MWR voided to MWO 971345. i-near PT.982 has damage. '

9701347 MWO 971345

'MWN PE MS . Fabricate and instali pipe COMPETE. Pipo support fabricated and support for horizontal pipe installed.

restraint near PT-P62.

[

SYSTEM.TBL Page 23 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,1997 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS MAIN STEAM (MS) (Continued) 9701570 MMO 971553 MWN EM M S-166 Inspect limit switch. COMPLETE. Raychemed Sealtite.

N/A WP003424 KKN I&C PT-958 Calibrate 3oop 958, COMPLETE. Requested by l&C walkdown.

PMO 9704793 extraction steam inlet pressure to feedwater heaters FW-16A and FW-168.

N/A WP003423 KKN' I&C PT-946A Calibrate loop 946A, turbine COMPLETE. Requested by l&C walkdown.

PMO 9801424 first stage pressure.

N/A WP005136 KKN l&C PT-947 Calibrate loop 947, main COMPLETE. Requested by l&C walkdown.

PMO 9704792 steam chest pressure.

N/A WP003425 KKN I&C PT-962 Calibrate loop 962, COMPLETE. Requested by I&C walkdown.

PMO 9704794 extraction steam inlet pressure to feedwater heaters FW-15A and FW-158.

N/A WP003421 KKN l&C PT-919 Calibrate loop 919, turbine COMPLETE. Requested by l&C walkdown. l PMO 9702345 lirst stage pressure to l

reactor regulating system.

9701743 MMO 971717 KKN: 18C PT-953C Open the covers of the COMPLETE. Instruments were inspected.

PT-2101 instruments and irtspect for No signs of moisture and/or PS-1151D moisture and/or dust. Clean / dust intrusion were found.

dry instruments and perform Covers closed. Wiped off a applicable loop checks. light amount of dust on the MMO 971717 written per covers.

NSRG Review SRG-97-030.

SYSTEM.TBL Page 24 of 34

.7 t

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,1997 I MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS REACTOR PROTECTION SYSTEM (RPS) 9701414 MWO 971409 JRT EM SV-1-33D inspect turbine stop valve COMPLETE. Inspection completed with SV-2-33D limit switches. Awaiting PMT. satisfactory results.

SV-3-33D -

SV-4-33D i

f SYSTEM.TBL Page 25 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT i430 hrs, uay 12,199 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS MAIN TURBINE (ST) 9701337 MWO 971342 KKN ! PE CV-1 Replace bent hydraulic CORAPLETE. Hydraulic lines repaired.

lines. -

9701368 PMO 9704788 KKN TM CV-1-0 Rebuild hydraulic cylinders COtrLETE. Operator rebuilt.

on control volve CV-1.

9701338 MMO 971322 - KKN EM CV-1 Inspect conduit that has CORAPLETE. Replaced Sealtite. '

pulled away from junction

. box on CV-1. Repair /

replace as necessary.

9701369 PMO 9704788 KKN TM CV-3-0 ' Rebuild hydraulic cylinders COtrLETE. Operator rebuilt.

^

for control valve CV-3.

9701428 MMO 971415 KKN EM MOV-St-PB L Perform a visual inspection CORAPLETE. Switch blocka replaced. .

of MOV-St-PB as necessary to ensure operability.

. Repair as necessary.

9701429 MMO 971416 KKN EM MOV-S2-PB Perform a visual inspection COREPLETE. Switch blocks replaced.

of MOV-S2-PB as necessary to ensure operability.

_. Repair as necessary.

9701430 MMO 971417[ KKN EM MOV-B-PB Perform a visualinspection COASPLETE. Switch blocks replaced.

Y :of MOV-8-PB as necessary to ensure operabinty.

Repair as necessary.

. 9701375 PMO 9001044 4 KKN PE EHC 7 Desiccant replacement. C(MAPLETE. EHC-7 dessicant replaced.

9701446 MWO 971426 KKN I&C CV-1-0 Replace linear variable COedPLETE. No problems found with the differentiel transformer on - old part, but it was replaced CV-1-0. as a precaution.

9701401 MMO 971.4011 KKN GM CV-1. Erect / dismantle scaffolding CORAPLETE. ' Scaffolding erected and for CV-1, CV-2 and CV-3. dismentled.

SYSTEM.TBL Page 26 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12, ist i MWR MWD SE CRAFT TAG NO. PROBt.EM DESCRIPTION STATUS RESUtTS MAIN TURBINE (ST) (Continued) 9701406 MWO 971467 KKN PE SV-2 Replace Main Steam stop VOID. MWO 971467 was voided.

valve damaged drain lines.

9701406 MWO 971493 KKN PE SV-2 Remove Main Steam stop COMPl.ETE. Insulation removed.

valve insulation.

9701406 MWO 971532 JMS PE SV-2 Erect scaffolding for MWO in progress - 5/12/97.

971467.

9701406 MWO 971568 KKN PE SV-1 Remove Main Steam stop COMPLETE. Insulation removed.

valve insuistion.

~

9701407 MWO 971468 KKN PE SV-1 Remove Main Steam stop VOID. MWO 971468 was voided.

valve damaged drain line.

9701407  : MWO 971494 KKN PE CV-1 Remove Main Steam control COMPLETE. . insulation removed.

vsv. le CV-1 lower drain line insuladon.

9701412 MMO 971474 KKN PE CV-1 Repair / replace Main Steam in progress - 5/12/97.

control valve CV-1 insula-tion.

9701412 MMO 971475 - KKN PE CV-3 Reinstall Main Steam COMPLETE. Insulation was removed on -

control velve CV-3 insula- this MMO. Insutstion will tiorQ be reinstalled under MMO 971681. ,

N/A WP006071 ~ .KKN- TM CV-1-0 Inspect'the[ disc dump valve CORFLETE. No failures noted on CV-1 so PMO 9001816 ~ on the four control valves. only CV-1 was inspected. -

1 9701519 MWO 971526 ' KKN- I&C CV-3-0 Inspect' main steam contml COMPLETE.- No problems found with old valve CV-3 as necessary. 'part; W as precaution.

9701447 MWO 971427 KKN-- l&C CV-3-0 J4eplace Iirddr verlebte COMPLETE. No problems found with old differential transformer on part; replaced as precaution.  ;

CV-:Hl/

r i

SYSTEM.TBL Page 27 of 3 l

System Engineering FCS OUTAGE RECOVERY EFFORT i430 hrs, May 12,199 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS MAIN TURBINE (ST) (continued) 9701448 MWO 971428 KKN l&C SV-1-0 Replace linear variable COMPLETE. No problems found with old differential transformer on part; replaced as precaution.

SV-1-0. -

9701449 MWO 971429 KKN. 14C SV-2-0 Replace linear variable COMPLETE. No problems found with old differential transformer on part; replaced as precaution.

SV-2-0.

9701465 MWO 971452 KKN . l&C CV-1 Cycle conhol valses per COMPLETE. MWO 971718 written. All IC-CP-01-CV-1/2/3/4. ' other areas satisfactory.

9701471 PMO 9702245 KKNL MM' EHC Sample and test EHC fluid. COMPLETE. EHC fluid sample was satisfactory.

9701451 MMO 971471 KKN. I&C ' PI-5071 Using IC-CP-07-0001,- . . COMPLETE. PI-5071 replaced.

replace bearing oil header pressure indicator during outage or shutdown.

N/A WP003974 KKN. .M M . EHC-10A Replace Fullers earth filters COMPLETE. Filters replaced as a -

PMO 9703287 EHC-109 and others as required. precaution.

9701397 MWO 971393 KKN: PE- LO.1 Filter lobe oil per S.E.; COMPLETE. Lube oil filtered and is in n instruction. spec.

9701522 MWO 971527 KKNT .1&C; SV-1-0 Inspect main steam stop ; COMPLETE. Replaced shut-off valve as a -

~

valve SV-1 as required. precaution.

9701427 KKN" lPE 3 CIV-1 Reinsulate steam chest. VOID. MWR 9701427 volded to' MWOs 971474 and 971475.

9701431 MWO 971432 KKN, .'l&C . CV-1-20A Replace solenoid. valve due COMPLETE. No problems noted with old ;

to steem blast. pert; replaced as precaution.

9701432 MWO 971433 KKN1 l&C ~ CV-1-208 Replace solenoid valve due COMPLETE. No problems noted with old to steam blast. - part; replaced as precaution.

SYSTEM.TBL Page 28 of 34 i

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,19t MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS MAIN TURBINE (ST) (Continued) 9701433 MWO 971434 KKN l&C CV-3-20A Replace scienoid valve due COMPLETE. No problems noted with old to steam blast. part; replaced as precaution.

9701434 MWO 971435 KKN l&C CV-3-208 Replace solenoid valve due COMPl.ETE. No problems noted with old to steam blast. part; replaced as precaution.

9701435 MWO 971436 KKN I&C SV-1-20A Replace solenoid valve due COMPLETE. No problems noted with old to steam line break. part; replaced as precaution.

9701436 MVr0 971437 KKN I&C SV-1-208 Replace solenoid valve due COMPLETE. No problems noted with old to steam line rupture. part; replaced as precaution.

9701437 MWO 971438 KKn l&C SV-2-20A Replace solenoid valve due COMPIETE. No problema noted with old to steam line rupture. part; replaced as precaution.

9701438 MWO 971440 KKN l&C SV-2-20B Replace solenoid valve due COMPLETE. No problems noted witit old to steam line rupture. Awaiting PMT. past; replaced as precaution.

9701528 MMO 971538 KKN EM MOV-B-0 Megger motor and inspect COMPLETE. Meggering completed. No limit switch compartment. problems found.

9701518 MWO 9715251 KKN I&C CV-1-0 Inspect main steam control COMPLETE. No problem found. Parts valve CV-1 as required. were replaced as precaution.

9701529 MMO 971540[ KKN EM MOV-S t-0 Megger motor and inspect COMPLETE. Meggering completed. No limit switch compartment. problems found.

9701530 MMO 971541) KKN EM MOV-S2-0 Megger motor and inspect COMPLETE. Meggering completed. No limit switch compartment. problems found.

N/A WP006876 " KKN TM CV-1-0 Rebuild control valve COMPLETE. No failures found on CV-1 so PMO 9704758 hydraulic cylinders on CV-1. the other CVs were not rebuilt.

9701339 MWO 9713261 KKN I&C CV-1 Component appears to be COMPLETE. Replaced to servo valve as a charred.' preventive measure; no problems found with old part.

SYSTEM.TBL Page 29 of 3

Syttem Engineering FCS OUTAGE RECOVERY EFFORT i43o nrs, uay 12,1997l MWR MWD SE CRAFT TAG NO. PROBEM DESCRIPTION STATUS RESULTS MAIN TURBINE (ST) (Continued) 9701340 MWO 971328 KKN l&C CV-3 Component appears to be COMPETE-Repiaced to servo valve as a charred. preventive measure; no problems were found with the old part.

9701561 MMO 971562 KKN EM~ CV-1-33D inspect limit switch. COMPLETE. Found switch to be corroded and contacts burned from moisture from steam line

,. breek. Cleaned contacts and corrosion from switch.

Tested switch after cleaning.

9701452 MMO 971425 KKN EM  ; CV-1 Open junction boxes et the COMPETE. Inspected and cleaned Control Valves and Stop Control and Stop Valve Valves and inspect and. ~ junction boxes. MWR  ;

clean as required. 9701581 initiated to rebuild or '

replace switch CV-1-33D.

9701338 MMO 971322 KKN EM ' CV-1 Inspect conduits pulled) COtrETE. Replaced sealtite.

away from junction box on . j CV-1. '

9701460 . MWO 971454 KKN: l&Cl: SV-2 . Coordinate with Ops to: COMPETE. MWO 971686 written to repairL perform applicable sections'. Al-50 853 because it was not - r of IC-CP-01-SV-1,2,3,4 afterj responding.

all stop valve week ic complete.

i 9701523 MWO 971523 KKN . IAC ' SV-2-0 Inspect main steem stop COMPETE. No problem found. Old parts >

valve SV-2 as required. refurbished as a precaution.

9701520 MWO 971483 KKN PEU CV-1 Replace the bent steam VOID. MWO 971483 was voided,

~

leek-off line on main steem i-control valve CV-1.

9701407 MMO 971581 KKN CM- SV-1 Heat up piping and- COMPETE. Piping straightened. '

straighten.

SYSTEM.TBL Page 30 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,199 MWR MWD SE CRAFT TAG NO. PROBLEM DESCRIPTION STATUS RESULTS MAIN TURBINE (ST) (Continued) 9701520 MMO 971583 KKN CM CV-1 Heat up piping and COMF_E7E. Piping straightened.

straighten.

9701406 MMO 971582 KKN CM SV-2 Heat up piping and COMPLETE. Piping straightened.

straighten.

9701520 MWO 971491 KKN PE CV-1 Remove insulation from COMPLETE. Insulation removed.

CV-1 leak off line to the a

reducer fitting.

9701622 MMO 971596 KKN MM LO-1 Add 797 oil as directed by COMPLETE. Oil added.

System Engineer.

9701329 MWO 971580 MWN PE ST-1 Radiograph and stress COMPLETE. Radiograph results were re!! eve the nozzle weld to satisfactory. Nozzle weld the vertical down-comer on was stress re!!eved.

the 4th stage extraction header on ST-1.

9701520 MMO 971531 KKN PE CV-1 Erect scaffolding for MWO in progress - 5/12/97.

971483.

9701445 MMO 971606 KKN PE ST-1 Remove insulation from "Y" COMPLETE. Insulation removed.

on 8th stage extraction for i reinforcement of the 18-inch branch connection, 9701649 MMO 971640 MWN EM MOV-B Indication is not oper& ting COMPLETE. Indication repaired.

correctly. Troubleshoot a .d repair ti a Indication.

9701413 MMO 971619 KKh PE SV-2 Straighten the 3/8-inch COMPLETE. Rod hanger was threaded rod stock hanger. straightened.

9701662 N/A MWN PE MOV-B Valve will not close. Craft VOIDED. MWR 9701662 voided to

~

was able to open fully, but MWO 971656 (MWR tried to manually close valve 9701649).

j and it would not close.

SYSTEM.TBL Page 31 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 143'l hrs, May 12,1991 MWR MWD SE CRAFT TAG NO. PROBEM DESCRIPTION STATUS RESULTS MAIN TURBINE (ST) (Continued) 9701649 MWO 971656 MWN PE MOV-B Machinisits to remove and COMPETE. Crud found between stem inspect the gear box. Awaiting PMT. and stem nut. Limit switches GM/PE to disassemble the set. MOV mounting bolts valve body and make stripped during torquing.

intemal repairs as needed. MWO 971696 written.

N/A ECN 97-161 KKN' NCM MS insten reinforcing pad for coerETE. Reinforcing pod installed.

eth stage T saddle.

9701699 MWO 971886 KKN l&C ^ Al-50-B53 Troubleshoot and repair C(MPETE. Al-50.B53 adjusted.

Al-50-B53. This cord would not respond during MWO 971454.

9701898 MMO 971684 . KKN MM LO.1 Pump oil from the storege L CotrETE. Oil pumped to the bowser.

tank to the bowser.

9701689 MMO 971681 KKN PE ST-1 Reinsulate the lines directly in progress - 5/12/97.

affected by the steam line rupture.

9701329 MWO 971292 KKN. PE: ST-1 Remove insulation from CEMrETE. Insulation removed.

around the ruptured piping.

9701561 MMO 971863 - KKN; EM CV-1-33D Repiece limit swNch due to . C(MPETE. Limit switch repieced and -

' concelon and debris inside adjusted.

WE 9701700 MMO 971709 KKN EM; LO.1 Electrical panel on top of- CtMIPETE. No endence of water LO-1 needs to be opened , intrusion was found.

and inspected for evidence of waterintrusion.

9701701 MWO 971098 MWN MM? MOV-B During MWO 971958, the 1 6 Mounting bolts replaced and '

MOV mounting bolts were ? cv.inui torqued.

, overtongued and require r$71. .i".

SYSTEM.TBL Page 32 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,1997 MWR MWD SE CRAFT TAG NO. PROBEM DESCRIPTION STATUS RESULTS MAIN TURBINE (ST) (Continued) 9701714 MMO 971704 KKN MM MOV-CV Valve will operate in the COMPLETE.

close direction electrically, but it appears that the  !

torque switch is tripping I when attempting to elec-trically open the valve.

Troubleshoot and adjust as required. See Planner if extensive repair is required.

9701715 MMO 971705 KKP! MM MOV-SV-3 Valve wi!I operate in the COMPLETE.

close direction electrically, but it appears that the torque switch is tripping when attempting to elec-trically open the valve.

Troubleshoot and adjust as required. See Plannerif extensive repair is required.

9701720 N/A KKN EM MOV-SV-5 Valve only barely opens. VOlD. MWR 9701720 voided to Appears to not exhibit full MWR 9701719.

. travel.

9701744 MWO 971718 KKN l&C CV-3-20A The fast acting solenoid COMPLETE. A broken wire was found and valve on CV-3 failed during repaired.

IC-CP-01-CV-3. Trouble-shoot and/or replace CV-3-20A 9701759 MWD Required KKN AE The drip pan under the MWD Required.

control valve operators is gone due to the pipe rupture.

SYSTEM.TBL Page 33 of 34

System Engineering FCS OUTAGE RECOVERY EFFORT 1430 hrs, May 12,199 MWR MWD SE CRAFT TAG MO. PROBLEM DESCRIPTION STATUS RESUt.TS MAIN TURBINE (ST) (Contmuod) 97C1796 MWO 971755 KKN I&C ST 'Part Hold.

PS-13 (PS-3200) on the steam seal controller is leaking water from its

  • housing and is deformed.

P SYSTEM.TBL Page 34 of 34 !

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _____ __m__._______ . _ - _ _ _ _ _ _ . _ _ _ _ mm_ __m - -____ _ _ +__ _ _ _ _ _ _' -_ _-- _ _ _ _ _ _ - - -_ - m-.____