ML20055A972

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Final Deficiency Rept Re Setpoints for Relief Valves on Fuel Pool Cooling & Cleanup Sys Heat Exchangers,Initially Reported on 820528.Deficiency Determined Not Reportable Per 10CFR50.55e
ML20055A972
Person / Time
Site: Grand Gulf  Entergy icon.png
Issue date: 07/09/1982
From: Reaves T
MISSISSIPPI POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
10CFR-050.55E, 10CFR-50.55E, NUDOCS 8207200203
Download: ML20055A972 (4)


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. o MEMO TO: File f/

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FROM: T. E. Reaves, Jr., Manager of Quality Assu& y e i

SUBJECT:

PRD-82/31, Setpoints for Relief Valves on the' Ff(kU System

! Heat Exchangers t

i FILE: 0290/0490/15525/15526

PMI-82/4172
On May 28, 1982, Mississippi Power and Light notified the NRC of a Potentially l ,

Reportable Deficiency (PRD) concerning setpoints for relief valves on the Fuel

! Pool Cooling and Cleanup (FPCCU) System Heat Exchangers.

On June 22, 1982, MP&L QA received a letter, PMI-82/3815 (dated 6/21/82), from MP&L Nuclear Plant Engineering stating that thic potential deficiency would not adversely effect the safety of operations of GGNS. On June 23, 1982, QA informed the NRC that MP&L had determined that this potential deficiency was not reportable under the provisions of 10CFR50.55(e). The PRD was withdrawn with the understanding that a formal report would be submitted if requested by

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the NRC at a later date.

! On July 1, 1982, Mr. R. Butcher, NRC Region II, conducted an exit interview at GGNS. He informed MP&L that during his inspection he reviewed MP&L's

' rationale concerning the reportability of the deficiency. He stated that he believed the deficiency to be reportable and that MP&L should submit a formal report to the NRC. As a result, on July 2,1982 MP&L telephoned Mr. Butcher to request and was granted an extension for submission of a written report until July 9, 1982.

On July 7,1982, Mr. Butcher called MP&L QA and stated that per further conversations with members of the NRC Region 11 staf f, PRD-82/31 would not need to be reported to the NRC in a formal report. The PRD would, therefore,

, be considered withdrawn.

This PRD is considered closed.

T. E. R.

7/9/82 g[()N RDC:d1 9 01 @ JL

Attachment:

A - PRD-82/31 g M cc: Mr. N. L. Stampley, w/o Mr. J. W. Yelverton, w/o i Mr. J. P. McGaughy, Jr. , w/o PRD-82/31, w/a >

Mr. L. F. Dale, w/o Manual File, w/a Mr. C. K. McCoy, w/o '

j Mr. J. F. Pinto, w/o , ,

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Mr. C. C. Hayes, w/o  ; . , ,yg , , q.]gy <

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% , 8207200203 DR ADOCK 05000 020709 n ,

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! MISSISSIPPI POWER & LICllT COMPANY POTENTIALLY REPORTABLE DEFICIENCY ( PRD')'~ PRD # 82/31

1. DESCRIPTION: Nonconformance Document Number Deficiency Af fects:

, Unit I? X

,' SEE ATTACllMENT "A" Yes No Unknow j Unit 27 X i Date: 5/26/82 Yes No Unknor

{ Identifier S. E. Thomas Organization NPE i i II. DETERMINATION OF EFFECT ON SAFE OPERATION OR SUBSTANTIAL SAFETY HAZARD:

Could have adversely af fected the safe operation of the plant or is a substantial safety hazard.

ii.

. Could not have adversely af fected the safe operation of the

] plant or is not a substantial safety hazard.

X Unable to determine.

Engineering Organization NPE Documentation PMI-82/3196 5/26/82 III. POTENTIALLY REPORTABLE? .

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! X Yes i

No Signature MViager of QA M Date [ -

IV. NOTIFICATION TO NRC:

10CFR50.55(e) 10CFR21 Person Notified: Butcher How Notified: Person Notified: How Notified:

Telephone Notified By: A. Smey Date: May 26, 1982 Notified By: Date:

(CIRCLE ONE)

V. EVALUATION OF 10CFR50.55(e) REPORTABILITY: Reportable per 10CFR50.55(e)? YES

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Date

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VI. EVALUATION OF 10CFR21 REPORTABILITY: (CIRCLE ONE)

Received Component? [g J Reportable per 10CFR21?

Failure to Comply? ,

YESh fee, P M - k R/3g/,r//e?.

Signature / Signature _

Date "

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VII. F.ECEIPT OF 10CFR21 INFORMATION - Assistant Vice President use only Signature Date Time

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I. QUALITY ASSURANCE FORM 16.20(A),

M .q Rev.' 8 . 2/28/82.' Page ' 1 of 'I ._--i

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' Attachment A to PRD-82/31 Page 1 of 1 DESCRIPTION i

The Fuel Pool Cooling and Cleanup (FPCCU) Heat Exchangers (Q1G41B001A&B) are l fitted with relief valves set in excess of the design pressure. The equipment

,t is designed under ASME Section III, Subsection ND (Class 3). ND-7511, Set i

Pressure Limitations, states that the set pressure of at least one pressure (1'

relier device connected to the system shall not be greater than the design pressure of the system at design temperature. GE Document 21A9520AB Rev. 7, i Fuel Pool Heat Exchanger Data Sheet, states the design pressure as 250 psig and 150 psig for the shell and tube sides of the heat exchanger, respectively. GE drawing VPF 5202-1-7 shows the set pressures at 275 psig and 165 psig. The vendor is Atlas Industrial Manufacturing Co., 81 Somerset

, j Place, Clif ton, N.J.

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