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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C2121993-07-30030 July 1993 LER 93-004-01:on 930301,confirmed That Channel D Axial Shape Index (Asi) Being Calculated in Reverse Since 921031-930301 Due to Drawing Discrepancies Associated W/Control Channel B. Temporary Mod 92-078 & Standing Order 0-25 Revised ML20046A8691993-07-26026 July 1993 LER 93-011-00:on 930624,experienced Reactor Trip Due to Loss of Load.Caused by Lack of Proper Job Planning,Lack of Formal Decision Making Process & Incomplete Communications.Training Will Be Provided to Operations personnel.W/930726 Ltr ML20045H2561993-07-12012 July 1993 LER 93-010-00:on 930611,1 of 14 Halon Cylinders Did Not Meet Min Pressure Acceptance Criteria Listed in Semiannual Switchgear Rooms Surveillance Test.Caused by Failure of Test to Include Necessary Steps.Cylinder recharged.W/930712 Ltr ML20045D7201993-06-22022 June 1993 LER 93-009-00:on 930524,apparent Spurious Signal from Pressurizer Level Instrumentation Caused Backup Charging Pumps to Automatically Start,Due to Deterioration of Wiring. Instrument Loop Calibration Will Be performed.W/930622 Ltr ML20045D3741993-06-21021 June 1993 LER 93-008-00:on 930520,determined That TS SR Not Satisfied for Stack Flow Indicator,Per Amend 137 Issued on 910307. Caused by Lack of Attention to Detail.Calibr & Functional Test Procedures developed.W/930621 Ltr ML20044H5261993-06-0101 June 1993 LER 93-007-00:on 930430,unplanned Emergency Generator Start & Rt Signal Occurred.Caused by Inadequate Attention to Detail,Labeling of Fuse Drawers,Caution Signs & Training. Labeling & Caution Signs upgraded.W/930601 Ltr ML20044G4941993-05-26026 May 1993 LER 93-006-00:on 930118,Halon Fire Suppression Sys for Switchgear Rooms Disabled to Allow Repair/Replacement of Halon Sys Piping.On 930427,individual Responsible for Fire Watch Not Present.Individual Relieved of Responsibilities ML20044B6711993-02-22022 February 1993 LER 93-002-00:on 930122,determined That Current SG LP Signal Block Reset Values Greater than Allowed Ts.Caused by Improper Design.Test Procedures Will Be Revised by 930917 to Specify Desired Value for Block function.W/930222 Ltr ML20024G6821991-04-19019 April 1991 LER 91-007-00:on 910320,480 Volt Circuit Breaker Coordination Outside Design Basis.Caused by Deficiencies in Original Sys Design.Breaker/Fuse Coordination Study to Be Completed & Problems Will Be corrected.W/910419 Ltr ML20029C1591991-03-21021 March 1991 LER 91-004-00:on 910212,offsite Power Low Signal Outside Design Basis.Caused by Inadequate Mod Design at Time of Performance of Original Degraded Voltage Analysis. Engineering Analysis EA-FC-91-017 performed.W/910321 Ltr ML20029C1051991-03-18018 March 1991 LER 91-002-00:on 901209,ventilation Isolation Actuation Signal Generated by High Alarm on Process Radiation Monitor RM-062.Caused by Accumulation of Noncondensible Gases in Sample Piping.Valve Packing Leak repaired.W/910318 Ltr ML20029A2981991-02-0808 February 1991 LER 91-001-00:on 910109,determined That Containment Tendon Surveillances Performed in 1981 & 1985 Did Not Reflect Guidance in Tech Specs.Caused by Inadequate Administrative Controls.Testing Program Plan implemented.W/910208 Ltr ML20029A2971991-02-0606 February 1991 LER 90-022-02:on 900907,approx 460 Fire Barrier Penetration seals,60 Fire Dampers & 6 Fire Doors Declared Nonfunctional Per NRC Info Notice 88-004 Due to Lack of Documentation. Plant Outage Required to Implement Repairs/Replacements ML20028G9171990-09-28028 September 1990 LER 90-021-00:on 900829,inadvertent Reactor Protective Sys Actuation Occurred While Operator Changed Power Source. Caused by Operator Not Following Proper Procedures.Operator counseled.W/900928 Ltr ML20044B0131990-07-12012 July 1990 LER 90-018-00:on 900612,reactor Protective Sys (RPS) Trip Units for Axial Power Distribution Determined to Be Inoperable.Caused by Procedural Deficiencies.Procedure Revised & RPS Surveillance Tests reviewed.W/900712 Ltr ML20043F6301990-06-11011 June 1990 LER 90-016-00:on 900511,accident Scenarios Identified by Which Auxiliary Feedwater Piping from Discharge of Turbine Driven Auxiliary Feedwater Pump FW-10 Can Be Overpressurized.Caused by Design deficiency.W/900611 Ltr ML20043F2441990-06-0707 June 1990 LER 90-015-00:on 900507,PORV Variable Setpoints Used for Low Pressure Overpressure Protection Determined to Be Nonconservative for PORV Opening Time.Caused by Design Deficiency.Tech Spec Amend prepared.W/900607 Ltr ML20043C0991990-05-29029 May 1990 LER 90-014-00:on 900427,investigation Revealed That Component Cooling Water Piping to Reactor Coolant Pump Seal Coolers Could Be Targets of High Energy Line Break.Safety Analysis for Operability completed.W/900529 Ltr ML20042G7211990-05-10010 May 1990 LER 90-011-00:on 900402,inadvertent Actuation of Pressurizer Pressure Low Signal Occurred While Performing Calibr Procedure.Caused by Inappropriate Action by Technician Involved.Validation of Procedures reviewed.W/900510 Ltr ML20042E6871990-04-23023 April 1990 LER 90-007-01:on 900228,determined That Several Supports Would Be Overloaded During Seismic Event on Nonsafety Related & safety-related Main Steam Piping.Caused by Design Deficiency.Piping Supports modified.W/900423 Ltr ML20042E6861990-04-23023 April 1990 LER 90-009-00:on 900316,potential Overpressurization of Auxiliary Feedwater Piping Could Have Occurred During Thermal Expansion of Process Fluid Between Closed Valved. Caused by Design deficiencies.W/900423 Ltr ML20012E7641990-03-26026 March 1990 LER 90-005-00:on 900223,determined That Spent Fuel Pool Area Charcoal Filtration Unit VA-66 Was Outside Design Basis. Caused by Insufficient Airflow Into Unit.Affected Updated SAR Analysis Will Be updated.W/900326 Ltr ML20012D0121990-03-19019 March 1990 LER 90-004-00:on 900217,lift Pressures for 6 of 10 Main Steam Safety Valves Found Outside Acceptance Criteria. Caused by Overly Restrictive Operability Criteria.Valves Recalibr & License Amend Submitted to NRC.W/900319 Ltr ML20012D0101990-03-19019 March 1990 LER 90-003-00:on 900216,determined That Auxiliary Feedwater Piping Outside Normal Stress Limits of ASME Code & Design Basis Specified in Updated Sar.Caused by Design Deficiency.Valve Operators Will Be inspected.W/900319 Ltr ML20012B6361990-03-0909 March 1990 LER 89-017-01:on 890624,internal Valve Component from Check Valve Found Lying on Pump Discharge Vane.Repair or Replacement of Valve Internals Could Not Be Accomplished within Time Requirement of Tech Spec.W/900309 Ltr ML20006E1041990-02-0909 February 1990 LER 90-001-00:on 900108,fire Barrier for Wall Between Auxiliary Bldg Rooms 26 & 34 Breached But Hourly Fire Watch Patrol Not Established.Caused by Lack of Sufficient Training for Shift Supervisors.Standing Order revised.W/900209 Ltr ML20011E2691990-02-0505 February 1990 LER 89-024-00:on 891221,determined That Containment Spray Pumps & Suction Header Piping Not Constructed for Use as Backup to LPSI Sys for Shutdown Cooling.Caused by Inadequate Review of Assumptions.Firewatch established.W/900205 Ltr ML20011E2271990-02-0101 February 1990 LER 89-021-00:on 891010,util Informed by C-E of Potential Nonconservative Setpoint in Reactor Protection Sys Thermal Margin/Low Pressure Trip Unit.Caused by Error in Incorporating Transient Setpoint analyses.W/900201 Ltr ML20005F7151990-01-10010 January 1990 LER 89-023-00:on 891211,hourly Firewatch Patrol Entered Posted High Radiation Area W/O Meeting Entry Requirements for Area.Briefings on High Radiation Entry Requirements Held for Personnel W/Assigned dosimetry.W/900110 Ltr ML19354D6381989-12-20020 December 1989 LER 89-022-00:on 890805,change to Surveillance Procedure ST-CEA-1 Became Effective Which Would Have Made Both Emergency Diesel Generators Simultaneously Inoperable During Portion of Test.Change removed.W/891220 Ltr ML19332E7431989-12-0808 December 1989 LER 88-037-01:on 881214,one of Two Supply Headers Supplying Fire Suppression Headers in Auxiliary Bldg Isolated.Caused by Lack of Procedural Guidance & Inadequate Procedural Controls.Standing Order G-58 Will Be revised.W/891208 Ltr ML19332E2681989-12-0101 December 1989 LER 89-016-02:on 890616,for Unknown Period Since 890614, Auxiliary Feedwater Pump FW-10 Operated Outside Design Basis for Certain Accident Conditions.Caused by Inoperable Speed Control Loop.Action Plan implemented.W/891201 Ltr ML19351A4541989-11-22022 November 1989 LER 89-020-00:on 891012,determined That Two of Four Component Cooling Water HXs Simultaneously Inoperable for More than 24 H.Caused by Inadequate Controls Re Return of Equipment to Svc.Standing Order revised.W/891122 Ltr ML19327B5481989-10-24024 October 1989 LER 89-019-00:on 890924,indication of High Temp for Reactor Coolant Pump RC-3A Upper Motor Thrust Bearing Received in Control Room.Caused by Damaged Cable for Bearing Resistive Temp Device.Damaged Cable replaced.W/891024 Ltr ML19325D2471989-10-13013 October 1989 LER 89-012-01:on 890502,main Feedwater Isolation Valve to Steam Generator a Found Inoperable Due to Improperly Set Torque Switch.Caused by Inadequate Program for Maint of Motor Operated Valves.Torque Switches reset.W/891013 Ltr ML20028C7711983-01-0606 January 1983 LER 82-020/03L-0:on 821207,during Main Steam Safety Valve Test,Four Main Steam Safety Valves Had Lift Setpoints Out of Tolerance.Caused by Normal Drift of Valves Over Operating Cycle.Valves Readjusted ML20028B5451982-10-28028 October 1982 LER 82-019/03L-0:on 821024,MSIVs HCV-1041A & HCV-1042A Stopped Three to Four Degrees Off Seat When Signaled to Close.Caused by Binding Between Valve Packing & Shaft. Packings Sprayed W/Penetrant Oil ML20052J0631982-04-27027 April 1982 LER 82-009/03L-0:on 820411,while Exchanging Component Cooling Water Heat Exchangers,Associated Outlet Valves HCV-490B,HCV-491B & HCV-492B Failed to Open.Cause Not stated.HCV-491B Reassembled & Tested ML20052B2361982-04-0707 April 1982 LER 82-006/03L-0:on 820323,during Surveillance Test ST-ISI- WD-1,F.1,valve HCV-506A Failed to Close Via Control Room Switch.Caused by Solenoid Valve Malfunction.Solenoid Valve Disassembled,Cleaned & Reassembled ML20052D9291982-04-0606 April 1982 LER 82-008/03L-0:on 820330,during Performance of ST-FW-1, F.2(b)(6)per Tech Spec 3.9,steam Driven Auxiliary Feedwater Pump Failed to Start.Caused by Back Pressure Trip Lever in Tripped Position.Lever Reset ML20041G1291982-02-22022 February 1982 LER 82-005/03L-0:on 820210,at 98% Power,Control Element 24 Inserted Into Core.Emergency Procedure EP-13,CEDM Malfunctions,Implemented & Power Stabilized at 88%.Caused by Erroneous Operating Instruction.Instruction Changed ML20041F7481982-02-17017 February 1982 LER 82-003/03L-0:on 820203,containment Isolation Valve Associated W/Gas Vent Header HCV-507A Failed to Close on Demand.Caused by Solenoid Valve Plunger Sticking in Energized Position.Plunger Freed ML20041F6251982-02-0505 February 1982 LER 82-004/03L-0:on 820203,small Quantity of Radioactive Gas/Particulate Released to Auxiliary Bldg During Routine Operation.Caused by Failure of Stack Gas Monitor RM-062 to Alarm at Appropriate Setpoint Due to Faulty Alarm Module ML20041B1051982-01-28028 January 1982 LER 82-002/03L-0:on 820114,at 99% Power,Lockout Relay 86B1, Containment Radiation High Signal,Failed to Actuate on Demand by Plant Radiation Monitoring Sys.Caused by Burnt Coil on Lockout Relay.Coil Replaced & Tested Satisfactorily ML20041B1171982-01-19019 January 1982 LER 82-001/03L-0:on 820111,during Normal Operation,Two Fire Barrier Penetrations Found Nonfunctional.Shift Supervisor Immediately Notified;However,Fire Watch Not Posted.Insp & Supervisor Personnel Instructed on Proper Actions ML20039B4561981-12-11011 December 1981 LER 81-011/03L-0:on 811113,containment Isolation Valves Opened & Ventilation Process Initiated W/Containment Air Monitor RM-050/051 Inoperable.Caused by Personnel Error. Valves Closed ML20010H8581981-08-27027 August 1981 LER 81-008/03L-0:on 810813,86B/CRHS (Containment Radiation High Signal) Lockout Relay Failed to Actuate When RM-062 Was Placed in Alarm,Resulting in Failure of 86B1/CRHS Relay to Actuate.Caused by Dirt in Relay Latching Mechanism ML20041F6291981-08-27027 August 1981 LER 81-008/03L-1:on 810813,containment Radiation High Signal 86B Lockout Relay Failed to Actuate When Radiation Monitor RM-062 Placed in Alarm.Caused by Bound Relay Latching Mechanism Due to Dirt & Grease.Latch Cleaned ML20010C2271981-07-0707 July 1981 LER 81-006/03L-0:on 810624,reactor Protection Sys Nuclear Power Recorder Channel B Trip Setpoints Determined to Be Nonconservative.Caused by Faulty Temp Change Power Calculation Due to Grounded Hot Leg Temp Loop ML20004B1111981-05-0606 May 1981 LER 81-005/03L-0:on 810423,dc Sequencer Timers AC-3A (Component Cooling Water Pump) & AC-102A (Raw Water Pump) Failed to Time Out within Prescribed Limit.Cause Unknown Mechanisms Satisfactorily Inspected 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046C2121993-07-30030 July 1993 LER 93-004-01:on 930301,confirmed That Channel D Axial Shape Index (Asi) Being Calculated in Reverse Since 921031-930301 Due to Drawing Discrepancies Associated W/Control Channel B. Temporary Mod 92-078 & Standing Order 0-25 Revised ML20046A8691993-07-26026 July 1993 LER 93-011-00:on 930624,experienced Reactor Trip Due to Loss of Load.Caused by Lack of Proper Job Planning,Lack of Formal Decision Making Process & Incomplete Communications.Training Will Be Provided to Operations personnel.W/930726 Ltr ML20045H2561993-07-12012 July 1993 LER 93-010-00:on 930611,1 of 14 Halon Cylinders Did Not Meet Min Pressure Acceptance Criteria Listed in Semiannual Switchgear Rooms Surveillance Test.Caused by Failure of Test to Include Necessary Steps.Cylinder recharged.W/930712 Ltr ML20045D7201993-06-22022 June 1993 LER 93-009-00:on 930524,apparent Spurious Signal from Pressurizer Level Instrumentation Caused Backup Charging Pumps to Automatically Start,Due to Deterioration of Wiring. Instrument Loop Calibration Will Be performed.W/930622 Ltr ML20045D3741993-06-21021 June 1993 LER 93-008-00:on 930520,determined That TS SR Not Satisfied for Stack Flow Indicator,Per Amend 137 Issued on 910307. Caused by Lack of Attention to Detail.Calibr & Functional Test Procedures developed.W/930621 Ltr ML20044H5261993-06-0101 June 1993 LER 93-007-00:on 930430,unplanned Emergency Generator Start & Rt Signal Occurred.Caused by Inadequate Attention to Detail,Labeling of Fuse Drawers,Caution Signs & Training. Labeling & Caution Signs upgraded.W/930601 Ltr ML20044G4941993-05-26026 May 1993 LER 93-006-00:on 930118,Halon Fire Suppression Sys for Switchgear Rooms Disabled to Allow Repair/Replacement of Halon Sys Piping.On 930427,individual Responsible for Fire Watch Not Present.Individual Relieved of Responsibilities ML20044B6711993-02-22022 February 1993 LER 93-002-00:on 930122,determined That Current SG LP Signal Block Reset Values Greater than Allowed Ts.Caused by Improper Design.Test Procedures Will Be Revised by 930917 to Specify Desired Value for Block function.W/930222 Ltr ML20024G6821991-04-19019 April 1991 LER 91-007-00:on 910320,480 Volt Circuit Breaker Coordination Outside Design Basis.Caused by Deficiencies in Original Sys Design.Breaker/Fuse Coordination Study to Be Completed & Problems Will Be corrected.W/910419 Ltr ML20029C1591991-03-21021 March 1991 LER 91-004-00:on 910212,offsite Power Low Signal Outside Design Basis.Caused by Inadequate Mod Design at Time of Performance of Original Degraded Voltage Analysis. Engineering Analysis EA-FC-91-017 performed.W/910321 Ltr ML20029C1051991-03-18018 March 1991 LER 91-002-00:on 901209,ventilation Isolation Actuation Signal Generated by High Alarm on Process Radiation Monitor RM-062.Caused by Accumulation of Noncondensible Gases in Sample Piping.Valve Packing Leak repaired.W/910318 Ltr ML20029A2981991-02-0808 February 1991 LER 91-001-00:on 910109,determined That Containment Tendon Surveillances Performed in 1981 & 1985 Did Not Reflect Guidance in Tech Specs.Caused by Inadequate Administrative Controls.Testing Program Plan implemented.W/910208 Ltr ML20029A2971991-02-0606 February 1991 LER 90-022-02:on 900907,approx 460 Fire Barrier Penetration seals,60 Fire Dampers & 6 Fire Doors Declared Nonfunctional Per NRC Info Notice 88-004 Due to Lack of Documentation. Plant Outage Required to Implement Repairs/Replacements ML20028G9171990-09-28028 September 1990 LER 90-021-00:on 900829,inadvertent Reactor Protective Sys Actuation Occurred While Operator Changed Power Source. Caused by Operator Not Following Proper Procedures.Operator counseled.W/900928 Ltr ML20044B0131990-07-12012 July 1990 LER 90-018-00:on 900612,reactor Protective Sys (RPS) Trip Units for Axial Power Distribution Determined to Be Inoperable.Caused by Procedural Deficiencies.Procedure Revised & RPS Surveillance Tests reviewed.W/900712 Ltr ML20043F6301990-06-11011 June 1990 LER 90-016-00:on 900511,accident Scenarios Identified by Which Auxiliary Feedwater Piping from Discharge of Turbine Driven Auxiliary Feedwater Pump FW-10 Can Be Overpressurized.Caused by Design deficiency.W/900611 Ltr ML20043F2441990-06-0707 June 1990 LER 90-015-00:on 900507,PORV Variable Setpoints Used for Low Pressure Overpressure Protection Determined to Be Nonconservative for PORV Opening Time.Caused by Design Deficiency.Tech Spec Amend prepared.W/900607 Ltr ML20043C0991990-05-29029 May 1990 LER 90-014-00:on 900427,investigation Revealed That Component Cooling Water Piping to Reactor Coolant Pump Seal Coolers Could Be Targets of High Energy Line Break.Safety Analysis for Operability completed.W/900529 Ltr ML20042G7211990-05-10010 May 1990 LER 90-011-00:on 900402,inadvertent Actuation of Pressurizer Pressure Low Signal Occurred While Performing Calibr Procedure.Caused by Inappropriate Action by Technician Involved.Validation of Procedures reviewed.W/900510 Ltr ML20042E6871990-04-23023 April 1990 LER 90-007-01:on 900228,determined That Several Supports Would Be Overloaded During Seismic Event on Nonsafety Related & safety-related Main Steam Piping.Caused by Design Deficiency.Piping Supports modified.W/900423 Ltr ML20042E6861990-04-23023 April 1990 LER 90-009-00:on 900316,potential Overpressurization of Auxiliary Feedwater Piping Could Have Occurred During Thermal Expansion of Process Fluid Between Closed Valved. Caused by Design deficiencies.W/900423 Ltr ML20012E7641990-03-26026 March 1990 LER 90-005-00:on 900223,determined That Spent Fuel Pool Area Charcoal Filtration Unit VA-66 Was Outside Design Basis. Caused by Insufficient Airflow Into Unit.Affected Updated SAR Analysis Will Be updated.W/900326 Ltr ML20012D0121990-03-19019 March 1990 LER 90-004-00:on 900217,lift Pressures for 6 of 10 Main Steam Safety Valves Found Outside Acceptance Criteria. Caused by Overly Restrictive Operability Criteria.Valves Recalibr & License Amend Submitted to NRC.W/900319 Ltr ML20012D0101990-03-19019 March 1990 LER 90-003-00:on 900216,determined That Auxiliary Feedwater Piping Outside Normal Stress Limits of ASME Code & Design Basis Specified in Updated Sar.Caused by Design Deficiency.Valve Operators Will Be inspected.W/900319 Ltr ML20012B6361990-03-0909 March 1990 LER 89-017-01:on 890624,internal Valve Component from Check Valve Found Lying on Pump Discharge Vane.Repair or Replacement of Valve Internals Could Not Be Accomplished within Time Requirement of Tech Spec.W/900309 Ltr ML20006E1041990-02-0909 February 1990 LER 90-001-00:on 900108,fire Barrier for Wall Between Auxiliary Bldg Rooms 26 & 34 Breached But Hourly Fire Watch Patrol Not Established.Caused by Lack of Sufficient Training for Shift Supervisors.Standing Order revised.W/900209 Ltr ML20011E2691990-02-0505 February 1990 LER 89-024-00:on 891221,determined That Containment Spray Pumps & Suction Header Piping Not Constructed for Use as Backup to LPSI Sys for Shutdown Cooling.Caused by Inadequate Review of Assumptions.Firewatch established.W/900205 Ltr ML20011E2271990-02-0101 February 1990 LER 89-021-00:on 891010,util Informed by C-E of Potential Nonconservative Setpoint in Reactor Protection Sys Thermal Margin/Low Pressure Trip Unit.Caused by Error in Incorporating Transient Setpoint analyses.W/900201 Ltr ML20005F7151990-01-10010 January 1990 LER 89-023-00:on 891211,hourly Firewatch Patrol Entered Posted High Radiation Area W/O Meeting Entry Requirements for Area.Briefings on High Radiation Entry Requirements Held for Personnel W/Assigned dosimetry.W/900110 Ltr ML19354D6381989-12-20020 December 1989 LER 89-022-00:on 890805,change to Surveillance Procedure ST-CEA-1 Became Effective Which Would Have Made Both Emergency Diesel Generators Simultaneously Inoperable During Portion of Test.Change removed.W/891220 Ltr ML19332E7431989-12-0808 December 1989 LER 88-037-01:on 881214,one of Two Supply Headers Supplying Fire Suppression Headers in Auxiliary Bldg Isolated.Caused by Lack of Procedural Guidance & Inadequate Procedural Controls.Standing Order G-58 Will Be revised.W/891208 Ltr ML19332E2681989-12-0101 December 1989 LER 89-016-02:on 890616,for Unknown Period Since 890614, Auxiliary Feedwater Pump FW-10 Operated Outside Design Basis for Certain Accident Conditions.Caused by Inoperable Speed Control Loop.Action Plan implemented.W/891201 Ltr ML19351A4541989-11-22022 November 1989 LER 89-020-00:on 891012,determined That Two of Four Component Cooling Water HXs Simultaneously Inoperable for More than 24 H.Caused by Inadequate Controls Re Return of Equipment to Svc.Standing Order revised.W/891122 Ltr ML19327B5481989-10-24024 October 1989 LER 89-019-00:on 890924,indication of High Temp for Reactor Coolant Pump RC-3A Upper Motor Thrust Bearing Received in Control Room.Caused by Damaged Cable for Bearing Resistive Temp Device.Damaged Cable replaced.W/891024 Ltr ML19325D2471989-10-13013 October 1989 LER 89-012-01:on 890502,main Feedwater Isolation Valve to Steam Generator a Found Inoperable Due to Improperly Set Torque Switch.Caused by Inadequate Program for Maint of Motor Operated Valves.Torque Switches reset.W/891013 Ltr ML20028C7711983-01-0606 January 1983 LER 82-020/03L-0:on 821207,during Main Steam Safety Valve Test,Four Main Steam Safety Valves Had Lift Setpoints Out of Tolerance.Caused by Normal Drift of Valves Over Operating Cycle.Valves Readjusted ML20028B5451982-10-28028 October 1982 LER 82-019/03L-0:on 821024,MSIVs HCV-1041A & HCV-1042A Stopped Three to Four Degrees Off Seat When Signaled to Close.Caused by Binding Between Valve Packing & Shaft. Packings Sprayed W/Penetrant Oil ML20052J0631982-04-27027 April 1982 LER 82-009/03L-0:on 820411,while Exchanging Component Cooling Water Heat Exchangers,Associated Outlet Valves HCV-490B,HCV-491B & HCV-492B Failed to Open.Cause Not stated.HCV-491B Reassembled & Tested ML20052B2361982-04-0707 April 1982 LER 82-006/03L-0:on 820323,during Surveillance Test ST-ISI- WD-1,F.1,valve HCV-506A Failed to Close Via Control Room Switch.Caused by Solenoid Valve Malfunction.Solenoid Valve Disassembled,Cleaned & Reassembled ML20052D9291982-04-0606 April 1982 LER 82-008/03L-0:on 820330,during Performance of ST-FW-1, F.2(b)(6)per Tech Spec 3.9,steam Driven Auxiliary Feedwater Pump Failed to Start.Caused by Back Pressure Trip Lever in Tripped Position.Lever Reset ML20041G1291982-02-22022 February 1982 LER 82-005/03L-0:on 820210,at 98% Power,Control Element 24 Inserted Into Core.Emergency Procedure EP-13,CEDM Malfunctions,Implemented & Power Stabilized at 88%.Caused by Erroneous Operating Instruction.Instruction Changed ML20041F7481982-02-17017 February 1982 LER 82-003/03L-0:on 820203,containment Isolation Valve Associated W/Gas Vent Header HCV-507A Failed to Close on Demand.Caused by Solenoid Valve Plunger Sticking in Energized Position.Plunger Freed ML20041F6251982-02-0505 February 1982 LER 82-004/03L-0:on 820203,small Quantity of Radioactive Gas/Particulate Released to Auxiliary Bldg During Routine Operation.Caused by Failure of Stack Gas Monitor RM-062 to Alarm at Appropriate Setpoint Due to Faulty Alarm Module ML20041B1051982-01-28028 January 1982 LER 82-002/03L-0:on 820114,at 99% Power,Lockout Relay 86B1, Containment Radiation High Signal,Failed to Actuate on Demand by Plant Radiation Monitoring Sys.Caused by Burnt Coil on Lockout Relay.Coil Replaced & Tested Satisfactorily ML20041B1171982-01-19019 January 1982 LER 82-001/03L-0:on 820111,during Normal Operation,Two Fire Barrier Penetrations Found Nonfunctional.Shift Supervisor Immediately Notified;However,Fire Watch Not Posted.Insp & Supervisor Personnel Instructed on Proper Actions ML20039B4561981-12-11011 December 1981 LER 81-011/03L-0:on 811113,containment Isolation Valves Opened & Ventilation Process Initiated W/Containment Air Monitor RM-050/051 Inoperable.Caused by Personnel Error. Valves Closed ML20010H8581981-08-27027 August 1981 LER 81-008/03L-0:on 810813,86B/CRHS (Containment Radiation High Signal) Lockout Relay Failed to Actuate When RM-062 Was Placed in Alarm,Resulting in Failure of 86B1/CRHS Relay to Actuate.Caused by Dirt in Relay Latching Mechanism ML20041F6291981-08-27027 August 1981 LER 81-008/03L-1:on 810813,containment Radiation High Signal 86B Lockout Relay Failed to Actuate When Radiation Monitor RM-062 Placed in Alarm.Caused by Bound Relay Latching Mechanism Due to Dirt & Grease.Latch Cleaned ML20010C2271981-07-0707 July 1981 LER 81-006/03L-0:on 810624,reactor Protection Sys Nuclear Power Recorder Channel B Trip Setpoints Determined to Be Nonconservative.Caused by Faulty Temp Change Power Calculation Due to Grounded Hot Leg Temp Loop ML20004B1111981-05-0606 May 1981 LER 81-005/03L-0:on 810423,dc Sequencer Timers AC-3A (Component Cooling Water Pump) & AC-102A (Raw Water Pump) Failed to Time Out within Prescribed Limit.Cause Unknown Mechanisms Satisfactorily Inspected 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217B5401999-10-0606 October 1999 Safety Evaluation Supporting Amend 193 to License DPR-40 ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data LIC-99-0096, Monthly Operating Rept for Sept 1999 for Fcs,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Fcs,Unit 1.With ML20211J9321999-09-0202 September 1999 Safety Evaluation Concluding That Licensee Proposed Alternatives Provide Acceptable Level of Quality & Safety. Proposed Alternatives Authorized for Remainder of Third ten- Yr ISI Interval for Fort Calhoun Station,Unit 1 LIC-99-0084, Monthly Operating Rept for Aug 1999 for Fort Calhoun Station.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Fort Calhoun Station.With ML20216E6431999-08-26026 August 1999 Rev 19 to TDB-VI, COLR for FCS Unit 1 ML20210R1961999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Fcs,Unit 1 ML20210G2181999-07-27027 July 1999 Safety Evaluation Supporting Amend 192 to License DPR-40 ML20210D9951999-07-22022 July 1999 Safety Evaluation Supporting Amend 191 to License DPR-40 ML20216E6361999-07-21021 July 1999 Rev 18 to TDB-VI, COLR for FCS Unit 1 ML20210R2081999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Fcs,Unit 1 LIC-99-0065, Monthly Operating Rept for June 1999 for Fort Calhoun Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Fort Calhoun Station,Unit 1.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20210P5461999-06-0808 June 1999 Rev 0,Vols 1-5 of Fort Calhoun Station 1999 Emergency Preparedness Exercise Manual, to Be Conducted on 990810. Pages 2-20 & 2-40 in Vol 2 & Page 4-1 in Vol 4 of Incoming Submittal Not Included ML20195B4581999-05-31031 May 1999 Rev 3 to CE NPSD-683, Development of RCS Pressure & Temp Limits Rept for Removal of P-T Limits & LTOP Requirements from Ts ML20207H7401999-05-31031 May 1999 Performance Indicators Rept for May 1999 LIC-99-0053, Monthly Operating Rept for May 1999 for Fort Calhoun Station,Unit 11999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Fort Calhoun Station,Unit 1 ML20195B4521999-05-17017 May 1999 Technical Data Book TDB-IX, RCS Pressure - Temp Limits Rept (Ptlr) ML20206L4241999-05-10010 May 1999 Safety Evaluation Supporting Corrective Actions to Ensure That Valves Are Capable of Performing Intended Safety Functions & OPPD Adequately Addressed Requested Actions Discussed in GL 95-07 ML20206M2601999-05-0606 May 1999 SER Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & IPEEE Results Reasonable Given FCS Design,Operation & History LIC-99-0047, Monthly Operating Rept for Apr 1999 for Fort Calhoun Station Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Fort Calhoun Station Unit 1.With ML20195E8621999-04-30030 April 1999 Performance Indicators, for Apr 1999 ML20205Q5831999-04-15015 April 1999 Safety Evaluation Supporting Amend 190 to License DPR-40 ML20210J4331999-03-31031 March 1999 Changes,Tests, & Experiments Carried Out Without Prior Commission Approval for Period 981101-990331.With USAR Changes Other than Those Resulting from 10CFR50.59 ML20206G2641999-03-31031 March 1999 Performance Indicators Rept for Mar 1999 LIC-99-0034, Monthly Operating Rept for Mar 1999 for Fcs,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Fcs,Unit 1.With ML20205J8181999-02-28028 February 1999 Performance Indicators, for Feb 1999 LIC-99-0025, Monthly Operating Rept for Feb 1999 for Fort Calhoun Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Fort Calhoun Station,Unit 1.With ML20207F3291999-01-31031 January 1999 FCS Performance Indicators for Jan 1999 ML20203B0991998-12-31031 December 1998 Performance Indicators for Dec 1998 LIC-99-0026, 1998 Omaha Public Power District Annual Rept. with1998-12-31031 December 1998 1998 Omaha Public Power District Annual Rept. with LIC-99-0003, Monthly Operating Rept for Dec 1998 for Fort Calhoun Station.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Fort Calhoun Station.With ML20198S3771998-12-31031 December 1998 Safety Evaluation Supporting Amend 189 to License DPR-40 ML20198S4831998-12-31031 December 1998 Safety Evaluation Supporting Amend 188 to License DPR-40 ML20196G2251998-12-18018 December 1998 Rev 2 to EA-FC-90-082, Potential Over-Pressurization of Containment Penetration Piping Following Main Steam Line Break in Containment ML20198M3141998-11-30030 November 1998 Performance Indicators Rept for Nov 1998 LIC-98-0172, Monthly Operating Rept for Nov 1998 for Fort Calhoun Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Fort Calhoun Station,Unit 1.With LIC-98-0160, Special Rept:On 981113,MSL RM RM-064 Was Declared Inoperable Due to Leakage Past Isolation Valve HCV-922.Troubleshooting Has Indicated That Leakage Has Stopped & Cause of Leak Continues to Be Investigated1998-11-25025 November 1998 Special Rept:On 981113,MSL RM RM-064 Was Declared Inoperable Due to Leakage Past Isolation Valve HCV-922.Troubleshooting Has Indicated That Leakage Has Stopped & Cause of Leak Continues to Be Investigated ML20203B0721998-11-16016 November 1998 Rev 6 to HI-92828, Licensing Rept for Spent Fuel Storage Capacity Expansion ML20196E4981998-10-31031 October 1998 Performance Indicators Rept for Oct 1998 ML20196G2441998-10-31031 October 1998 Changes,Tests & Experiments Carried Out Without Prior Commission Approval. with USAR Changes Other than Those Resulting from 10CFR50.59 LIC-98-0154, Monthly Operating Rept for Oct 1998 for Fort Calhoun Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Fort Calhoun Station,Unit 1.With ML20154M4881998-10-19019 October 1998 Safety Evaluation Supporting Amend 186 to License DPR-40 ML20154N2411998-10-19019 October 1998 Safety Evaluation Supporting Amend 187 to License DPR-40 LIC-98-0136, Monthly Operating Rept for Sept 1998 for Fort Calhoun Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Fort Calhoun Station,Unit 1.With ML20155G4261998-09-30030 September 1998 Performance Indicators for Sept 1998 ML20154A1251998-08-31031 August 1998 Performance Indicators, Rept for Aug 1998 LIC-98-0122, Monthly Operating Rept for Aug 1998 for Fort Calhoun Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Fort Calhoun Station Unit 1.With ML20238F7231998-08-17017 August 1998 Owner'S Rept for Isis ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency 1999-09-30
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Omaha Public Power District P.O. Box 399 Hwy.75- North of Ft.Calhoun Fort Calhoun, NE 68023-0399 402/636-2000 February 22, 1993 LIC-93-0049 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Station PI-137 Washington, DC 20555 i
Reference:
Docket No. 50-285 :
Gentlemen:
Subject:
Licensee Event Report 93-002 for the Fort Calhoun Station Please find attached Licensee Event Report 93-002 dated February 22, 1993.
This report is being submitted pursuant to 10 CFR 50.73(a)(2)(i)(B). If you should have any questions, please contact me.
Sincerely, M/, E &
W. G. Gates l Vice President l l
WGG/jrg j Attachment c: J. L. Milhoan, NRC Regional Administrator, Region IV S. D. Bloom, NRC Project Manager R. P. Mullikin, NRC Senior Resident Inspector INPO Records Center I
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9303010164 930222 45.5129 PDR S ADOCK 05000285 PDR
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Fort Calhoun Station Unit No. 1 05000285 1 OF 5 Tm.E n Inappropriate Steam Generator Low Pressure Signal Block Reset Values EVENT DATE (5) LER NUMBER (6) REPORT NUMBER (7) OTHER FACluTIES INVOLVED (B)
MONTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER 05000 01 22 93 93 002 00 02 22 93
]0b"0 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REOUIREMENTS OF 10 CFR 8: (Check one or more) (11) 1 MODE (9) 20.402(b) 20.405(c) 50.73fa)(2)(iv) 73.71(b)
S ER 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)
UNEL (10) 100 20 405(O(1)Ci) 50 36(e)(2) 50.73(a)(2)Mi) OTHER 20.405(a)(1)(iii) X 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) (Specify in Abstract 20.405(a)(1)(lv) 20.405(a)(1)(v) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(viii)(B) "(("
50.73(a)(2)(x)
UCENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBEst (mesvoe Area Code)
Calvin C. Taylor, Shift Technical Advisor (402) 533-6754 COMPLETE ONE UNE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM CouPONENT MANUFACTURER CAUSE O SYSTEM COMPONENT MANUFACTURER TO RS SUPPLEMENTAL REPORT EXPECTED (14) MCMH DAY YEAR EXPECTED YEB SUBMISSION (If yes. cornp6ete EXPECTED SUBM!SSION DATE) )( NO DATE (15)
ABSTRACT (Umit to 1400 spaces, i.e., approximately 15 singte-spaced typewritten hnes) (16)
During a review of calibration procedures for the Steam Generator Pressure Loops, it was determined that the current Steam Generator Low pressure Signal (SGLS) block reset values, for all four channels of both steam generators, were greater than that allowed by Technical Specification (TS) 2.14, Table 2-1. This TS allows SGLS to be bypassed (manually) below 550 psia, however, the block reset values were found to range from 562 to 566.5 psia. This condition has existed since the 1988-89 (Cycle 13) Refueling Outage. SGLS was not in a bypassed condition at the time of discovery of this event.
The root cause of this event has been determined to be improper design of the pressure indicating controllers.
An operability evaluation has been completed and procedures have been revised to ensure manual reset of SGLS prior to exceeding 550 psia. Additional corrective actions include revising surveillance tests and submitting a TS amendment request.
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NUMBER NUMDER -
Fort Calhoun Station Unit No. 1 05000285 2OF5 !
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i BACKGROUND j
'A main steam line break would result in an abnormally high rate of steam flow from t either steam generator, accompanied by a marked decrease in steam pressure. To protect against the adverse reactivity consequences of a main steam line break, a reactor trip ,
is initiated by low Steam Generator (SG) pressure. Four pressure transmitters on each !
SG provide input to the reactor protective system to initiate a reactor trip if either i SG's pressure drops below the trip setpoints on two-out-of-four channels. The trip !
setpoints are required to be greater than or equal to 500 psia. .
These SG pressure transmitters also provide input to Pressure Indicating Controllers '
(PICS). The PICS serve as inputs for two-out-of-four coincidence matrices (independent I of the reactor protective system) that generate a Steam Generator Low pressure Signal (SGLS). The two SGLS matrix outputs serve as inputs to two Steam Generator Isolation l Signal (SGIS) logic circuits. The setting limit for steam line isolation is greater 7 than or equal to 500 psia. ,
SGIS automatically isolates the SGs to minimize the blowdown of the SG(s) in the event [
of a main steam line break outside containment and to limit containment pressurization "
during a break inside containment. Two channels of SGIS are derived from a logical '
combination of a Containment Pressure High Signal (CPHS) or a SGLS because either !
condition is symptomatic of a main steam line break. The combining logic for SGIS is arranged such that either channel of SGLS or CPHS will initiate SGIS signals, isolating both SGs. Isolation is accomplished by automatic closure of the main steam isolation i and bypass valves, both feedwater isolation valves, the backup feedwater isolation ,
valves, and both feedwater bypass valves.
A key-operated bypass switch allows SGLS to be manually blocked when SG pressure is less than the block permissive setpoint. This blocks a SGIS actuation due to a SGLS but does -
not inhibit a CPHS from actuating SGIS. This block capability accommodates a controlled plant cooldown. This SGLS block is automatically removed when pressure rises above a reset value. The pressure difference between the block permissive setpoint and the block reset value (reset being higher than permissive) is the reset span. '
Fort Calhoun Station Technical Specification 2.14, Table 2-1, " Engineered Safety !
Features System Initiation Instrument Setting Limits", establishes the Low Steam ;
Generator Pressure setting limit as greater than or equal to 500 psia for steam line isolation. Note (2), on page 2-64a of the Technical Specifications, is associated with ;
the steam line isolation setting limit. This note states: "May be bypassed below 550 ;
psia and is automatically reinstated above 550 psia." The intent of this note is that !
SGLS is to be active above 550 psia. This is to be ensured by the automatic reset
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NUMBER NUMBER J Fort Calhoun Station Unit No. 1 05000285 3 OF 5 ;
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EVENT DESCRIPTION !
i Modification MR-FC-85-136 replaced the existing Sigma PICS with Dixson PICS during the i 1988-89(Cycle 13)RefuelingOutage. The Dixson PICS were to have a ten psi reset span for the block permissive function, and an adjustable block permissive setpoint.. A 10 psi reset span would result in a block reset value of 550 psia or below if the block permissive setpoint is 540 psia or below; a larger reset span would require the block t permissive setpoint to be correspondingly lower than 540 psia in order for the block !
reset value to be maintained at 550 psia or below. ;
On January 22, 1993 at 0800, while in Mode 1 at 100% power, it was determined that SGLS !
block reset values were greater than 550 psia on all four channels of both SGs, with values ranging from 562 to 566.5 psia. This condition was discovered as a result of a review of calibration procedures for the Steam Generator Pressure Loops. This review
'had been initiated to evaluate procedural guidance on setting the block permissive j setpoints. :
I With the block reset values between 562 and 566.5 psia, the SGLS had been allowed to be !
in a bypassed condition at pressures greater than 550 psia during recent SG l pressurizations fellowing plant shutdowns. This was determined to be in conflict with i TS 2.14, Table 2-1, Note (2), and therefore reportable pursuant to 10 CFR 50.73(a)(2)(i)(B). SGLS was not in a bypassed condition at the time of discovery l
. of this event. i i
SAFETY ASSESSMENT !
This event was found to have~no safety significance. An operability evaluation found the consequences of a main steam line break-(with SGLS bypassed between 550 and 566 l psia) to be bounded by the hot full power and hot zero power cases. The event did not ;
affect the ability of the reactor protective system to perform its design function. !
Also, the short amount of time spent with the SG pressure in the range of 550-566 psia {
results in a low probability of occurrence of a main steam line break in this condition. .
-Finally, Emergency Operating Procedure E0P-05, " Uncontrolled Heat Extraction", instructs !
operatorstoensuretheappropriatevalvesareisolated(closed)intheeventtheSGIS is not present. l f
Several licensed Combustion Engineering plants have SGLS block reset limits which are j 100 psi greater than the trip setpoint limit. Applying similar criteria'to the Fort i Calhoun Station' limits would result in a block reset limit of 600 psia. j I
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TEXT CONTINUATION h
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MANAGEMENT AND DUDGET, WASHINGTOtt DC 20503, FADLmf NAME(t) DDOMET NUMBER R LER NUMBE R PAGE R
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NUMDER NUMBER Fort Calhoun Station Unit No. 1 05000285 4 OF 5 l 93 --
002 -- 00 ,
i TBCT (W more opmos is requ6 red, use addh6onal copies at NRC Form 30GA} 07)
-CONCLUSIONS The root cause of this event has been determined to be an inadequate design of the PICS.
OPPD provided specifications for the PICS requiring a 10 psi tolerance for the block
, permissive reset span and an adjustable block permissive setpoint. The manufacturer :
supplied PICS with non-adjustable block permissive setpoints and reset spans of :
approximately 26 psi. !
A contributing factor was inadequate calibration procedures, in that there were no-provisions for verifying the block reset value. Since the modification used inadequate i calibration procedures, post-modification testing was also deemed inadequate. !
The Pressurizer Pressure Low Signal (PPLS) circuitry includes similar provisions for i manual bypass and automatic reset. The PPLS PICS were checked and found to have ,
i appropriate block reset values. ;
- CORRECTIVE ACTIONS The following corrective actions have been or will be taken: :
- 1. A caution tag has been placed by the PICS, instructing control room operators to manually reset the block permissive prior to exceeding 550 psia.
Procedures that address verification of the reset function have been revised ,
to ensure manual reset prior to 550 psia.
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- 2. The supplier has been contacted regarding the discrepancy with the PICS. A !
NUPIC Joint Audit of the supplier was conducted in January 1992. The Audit 1 established that the company is implementing an effective program which meets l the requirements of 10 CFR 50, Appendix B. )
- 3. Actions have been taken since installation of MR-FC-85-136 to improve the i post-modification testing program (reference LER 92-006-01). These actions :
included a procedure change, training and a review of the post-modification '
testing specified for a sample of modifications. It was concluded that there was not a generic problem with post-modification testing.
- 4. Surveillance Tests IC-ST-MS-0026 through 0033 (procedures for calibration of '
SG pressure loops) will be revised by September 17, 1993, to specify a desired I value and tolerance range for the block reset function. ,
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TEXT CONTINUATION AND RECORDS MANAGEMENT BFWWCH (MNBB m4). U.S. NUCLEAR ,
REGIA.ATORY ODMMiBBON WASHINGTON DC 202Mio01. AND TO ;
THE PAPERWORK REDUCTON PRalEC.T 015:>0104). OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON,0C 20$03.
FADUfY NAME(1) DOOMET NUMBER R LER NUMBER R PAGE R SEQUENT AL FIEVlfAION I NUMBER NUMBER Fort Calhoun Station Unit No. 1 05000285 93 -- 002 -- 00 mr e . % .a. o .oa.n.i a,F.- a NaC rm ini i
- 5. A Technical Specification amendment request, to allow higher values for the :
SGLS block permissive / block reset function, will be submitted by :
June 15, 1993.
-PREVIOUS SIMILAR EVENTS l LER 91-005 discusses a previous event involving a Technical Specification violation associated with SGLS. This LER, however, was not associated with the SGLS block permissive / block reset function.
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