LER 90-022-02:on 900907,approx 460 Fire Barrier Penetration seals,60 Fire Dampers & 6 Fire Doors Declared Nonfunctional Per NRC Info Notice 88-004 Due to Lack of Documentation. Plant Outage Required to Implement Repairs/ReplacementsML20029A297 |
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Fort Calhoun |
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Issue date: |
02/06/1991 |
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From: |
Fritts C OMAHA PUBLIC POWER DISTRICT |
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To: |
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Shared Package |
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ML20029A296 |
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References |
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IEIN-88-004, IEIN-88-4, LER-90-022, LER-90-22, NUDOCS 9102120021 |
Download: ML20029A297 (5) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C2121993-07-30030 July 1993 LER 93-004-01:on 930301,confirmed That Channel D Axial Shape Index (Asi) Being Calculated in Reverse Since 921031-930301 Due to Drawing Discrepancies Associated W/Control Channel B. Temporary Mod 92-078 & Standing Order 0-25 Revised ML20046A8691993-07-26026 July 1993 LER 93-011-00:on 930624,experienced Reactor Trip Due to Loss of Load.Caused by Lack of Proper Job Planning,Lack of Formal Decision Making Process & Incomplete Communications.Training Will Be Provided to Operations personnel.W/930726 Ltr ML20045H2561993-07-12012 July 1993 LER 93-010-00:on 930611,1 of 14 Halon Cylinders Did Not Meet Min Pressure Acceptance Criteria Listed in Semiannual Switchgear Rooms Surveillance Test.Caused by Failure of Test to Include Necessary Steps.Cylinder recharged.W/930712 Ltr ML20045D7201993-06-22022 June 1993 LER 93-009-00:on 930524,apparent Spurious Signal from Pressurizer Level Instrumentation Caused Backup Charging Pumps to Automatically Start,Due to Deterioration of Wiring. Instrument Loop Calibration Will Be performed.W/930622 Ltr ML20045D3741993-06-21021 June 1993 LER 93-008-00:on 930520,determined That TS SR Not Satisfied for Stack Flow Indicator,Per Amend 137 Issued on 910307. Caused by Lack of Attention to Detail.Calibr & Functional Test Procedures developed.W/930621 Ltr ML20044H5261993-06-0101 June 1993 LER 93-007-00:on 930430,unplanned Emergency Generator Start & Rt Signal Occurred.Caused by Inadequate Attention to Detail,Labeling of Fuse Drawers,Caution Signs & Training. Labeling & Caution Signs upgraded.W/930601 Ltr ML20044G4941993-05-26026 May 1993 LER 93-006-00:on 930118,Halon Fire Suppression Sys for Switchgear Rooms Disabled to Allow Repair/Replacement of Halon Sys Piping.On 930427,individual Responsible for Fire Watch Not Present.Individual Relieved of Responsibilities ML20044B6711993-02-22022 February 1993 LER 93-002-00:on 930122,determined That Current SG LP Signal Block Reset Values Greater than Allowed Ts.Caused by Improper Design.Test Procedures Will Be Revised by 930917 to Specify Desired Value for Block function.W/930222 Ltr ML20024G6821991-04-19019 April 1991 LER 91-007-00:on 910320,480 Volt Circuit Breaker Coordination Outside Design Basis.Caused by Deficiencies in Original Sys Design.Breaker/Fuse Coordination Study to Be Completed & Problems Will Be corrected.W/910419 Ltr ML20029C1591991-03-21021 March 1991 LER 91-004-00:on 910212,offsite Power Low Signal Outside Design Basis.Caused by Inadequate Mod Design at Time of Performance of Original Degraded Voltage Analysis. Engineering Analysis EA-FC-91-017 performed.W/910321 Ltr ML20029C1051991-03-18018 March 1991 LER 91-002-00:on 901209,ventilation Isolation Actuation Signal Generated by High Alarm on Process Radiation Monitor RM-062.Caused by Accumulation of Noncondensible Gases in Sample Piping.Valve Packing Leak repaired.W/910318 Ltr ML20029A2981991-02-0808 February 1991 LER 91-001-00:on 910109,determined That Containment Tendon Surveillances Performed in 1981 & 1985 Did Not Reflect Guidance in Tech Specs.Caused by Inadequate Administrative Controls.Testing Program Plan implemented.W/910208 Ltr ML20029A2971991-02-0606 February 1991 LER 90-022-02:on 900907,approx 460 Fire Barrier Penetration seals,60 Fire Dampers & 6 Fire Doors Declared Nonfunctional Per NRC Info Notice 88-004 Due to Lack of Documentation. Plant Outage Required to Implement Repairs/Replacements ML20028G9171990-09-28028 September 1990 LER 90-021-00:on 900829,inadvertent Reactor Protective Sys Actuation Occurred While Operator Changed Power Source. Caused by Operator Not Following Proper Procedures.Operator counseled.W/900928 Ltr ML20044B0131990-07-12012 July 1990 LER 90-018-00:on 900612,reactor Protective Sys (RPS) Trip Units for Axial Power Distribution Determined to Be Inoperable.Caused by Procedural Deficiencies.Procedure Revised & RPS Surveillance Tests reviewed.W/900712 Ltr ML20043F6301990-06-11011 June 1990 LER 90-016-00:on 900511,accident Scenarios Identified by Which Auxiliary Feedwater Piping from Discharge of Turbine Driven Auxiliary Feedwater Pump FW-10 Can Be Overpressurized.Caused by Design deficiency.W/900611 Ltr ML20043F2441990-06-0707 June 1990 LER 90-015-00:on 900507,PORV Variable Setpoints Used for Low Pressure Overpressure Protection Determined to Be Nonconservative for PORV Opening Time.Caused by Design Deficiency.Tech Spec Amend prepared.W/900607 Ltr ML20043C0991990-05-29029 May 1990 LER 90-014-00:on 900427,investigation Revealed That Component Cooling Water Piping to Reactor Coolant Pump Seal Coolers Could Be Targets of High Energy Line Break.Safety Analysis for Operability completed.W/900529 Ltr ML20042G7211990-05-10010 May 1990 LER 90-011-00:on 900402,inadvertent Actuation of Pressurizer Pressure Low Signal Occurred While Performing Calibr Procedure.Caused by Inappropriate Action by Technician Involved.Validation of Procedures reviewed.W/900510 Ltr ML20042E6871990-04-23023 April 1990 LER 90-007-01:on 900228,determined That Several Supports Would Be Overloaded During Seismic Event on Nonsafety Related & safety-related Main Steam Piping.Caused by Design Deficiency.Piping Supports modified.W/900423 Ltr ML20042E6861990-04-23023 April 1990 LER 90-009-00:on 900316,potential Overpressurization of Auxiliary Feedwater Piping Could Have Occurred During Thermal Expansion of Process Fluid Between Closed Valved. Caused by Design deficiencies.W/900423 Ltr ML20012E7641990-03-26026 March 1990 LER 90-005-00:on 900223,determined That Spent Fuel Pool Area Charcoal Filtration Unit VA-66 Was Outside Design Basis. Caused by Insufficient Airflow Into Unit.Affected Updated SAR Analysis Will Be updated.W/900326 Ltr ML20012D0121990-03-19019 March 1990 LER 90-004-00:on 900217,lift Pressures for 6 of 10 Main Steam Safety Valves Found Outside Acceptance Criteria. Caused by Overly Restrictive Operability Criteria.Valves Recalibr & License Amend Submitted to NRC.W/900319 Ltr ML20012D0101990-03-19019 March 1990 LER 90-003-00:on 900216,determined That Auxiliary Feedwater Piping Outside Normal Stress Limits of ASME Code & Design Basis Specified in Updated Sar.Caused by Design Deficiency.Valve Operators Will Be inspected.W/900319 Ltr ML20012B6361990-03-0909 March 1990 LER 89-017-01:on 890624,internal Valve Component from Check Valve Found Lying on Pump Discharge Vane.Repair or Replacement of Valve Internals Could Not Be Accomplished within Time Requirement of Tech Spec.W/900309 Ltr ML20006E1041990-02-0909 February 1990 LER 90-001-00:on 900108,fire Barrier for Wall Between Auxiliary Bldg Rooms 26 & 34 Breached But Hourly Fire Watch Patrol Not Established.Caused by Lack of Sufficient Training for Shift Supervisors.Standing Order revised.W/900209 Ltr ML20011E2691990-02-0505 February 1990 LER 89-024-00:on 891221,determined That Containment Spray Pumps & Suction Header Piping Not Constructed for Use as Backup to LPSI Sys for Shutdown Cooling.Caused by Inadequate Review of Assumptions.Firewatch established.W/900205 Ltr ML20011E2271990-02-0101 February 1990 LER 89-021-00:on 891010,util Informed by C-E of Potential Nonconservative Setpoint in Reactor Protection Sys Thermal Margin/Low Pressure Trip Unit.Caused by Error in Incorporating Transient Setpoint analyses.W/900201 Ltr ML20005F7151990-01-10010 January 1990 LER 89-023-00:on 891211,hourly Firewatch Patrol Entered Posted High Radiation Area W/O Meeting Entry Requirements for Area.Briefings on High Radiation Entry Requirements Held for Personnel W/Assigned dosimetry.W/900110 Ltr ML19354D6381989-12-20020 December 1989 LER 89-022-00:on 890805,change to Surveillance Procedure ST-CEA-1 Became Effective Which Would Have Made Both Emergency Diesel Generators Simultaneously Inoperable During Portion of Test.Change removed.W/891220 Ltr ML19332E7431989-12-0808 December 1989 LER 88-037-01:on 881214,one of Two Supply Headers Supplying Fire Suppression Headers in Auxiliary Bldg Isolated.Caused by Lack of Procedural Guidance & Inadequate Procedural Controls.Standing Order G-58 Will Be revised.W/891208 Ltr ML19332E2681989-12-0101 December 1989 LER 89-016-02:on 890616,for Unknown Period Since 890614, Auxiliary Feedwater Pump FW-10 Operated Outside Design Basis for Certain Accident Conditions.Caused by Inoperable Speed Control Loop.Action Plan implemented.W/891201 Ltr ML19351A4541989-11-22022 November 1989 LER 89-020-00:on 891012,determined That Two of Four Component Cooling Water HXs Simultaneously Inoperable for More than 24 H.Caused by Inadequate Controls Re Return of Equipment to Svc.Standing Order revised.W/891122 Ltr ML19327B5481989-10-24024 October 1989 LER 89-019-00:on 890924,indication of High Temp for Reactor Coolant Pump RC-3A Upper Motor Thrust Bearing Received in Control Room.Caused by Damaged Cable for Bearing Resistive Temp Device.Damaged Cable replaced.W/891024 Ltr ML19325D2471989-10-13013 October 1989 LER 89-012-01:on 890502,main Feedwater Isolation Valve to Steam Generator a Found Inoperable Due to Improperly Set Torque Switch.Caused by Inadequate Program for Maint of Motor Operated Valves.Torque Switches reset.W/891013 Ltr ML20028C7711983-01-0606 January 1983 LER 82-020/03L-0:on 821207,during Main Steam Safety Valve Test,Four Main Steam Safety Valves Had Lift Setpoints Out of Tolerance.Caused by Normal Drift of Valves Over Operating Cycle.Valves Readjusted ML20028B5451982-10-28028 October 1982 LER 82-019/03L-0:on 821024,MSIVs HCV-1041A & HCV-1042A Stopped Three to Four Degrees Off Seat When Signaled to Close.Caused by Binding Between Valve Packing & Shaft. Packings Sprayed W/Penetrant Oil ML20052J0631982-04-27027 April 1982 LER 82-009/03L-0:on 820411,while Exchanging Component Cooling Water Heat Exchangers,Associated Outlet Valves HCV-490B,HCV-491B & HCV-492B Failed to Open.Cause Not stated.HCV-491B Reassembled & Tested ML20052B2361982-04-0707 April 1982 LER 82-006/03L-0:on 820323,during Surveillance Test ST-ISI- WD-1,F.1,valve HCV-506A Failed to Close Via Control Room Switch.Caused by Solenoid Valve Malfunction.Solenoid Valve Disassembled,Cleaned & Reassembled ML20052D9291982-04-0606 April 1982 LER 82-008/03L-0:on 820330,during Performance of ST-FW-1, F.2(b)(6)per Tech Spec 3.9,steam Driven Auxiliary Feedwater Pump Failed to Start.Caused by Back Pressure Trip Lever in Tripped Position.Lever Reset ML20041G1291982-02-22022 February 1982 LER 82-005/03L-0:on 820210,at 98% Power,Control Element 24 Inserted Into Core.Emergency Procedure EP-13,CEDM Malfunctions,Implemented & Power Stabilized at 88%.Caused by Erroneous Operating Instruction.Instruction Changed ML20041F7481982-02-17017 February 1982 LER 82-003/03L-0:on 820203,containment Isolation Valve Associated W/Gas Vent Header HCV-507A Failed to Close on Demand.Caused by Solenoid Valve Plunger Sticking in Energized Position.Plunger Freed ML20041F6251982-02-0505 February 1982 LER 82-004/03L-0:on 820203,small Quantity of Radioactive Gas/Particulate Released to Auxiliary Bldg During Routine Operation.Caused by Failure of Stack Gas Monitor RM-062 to Alarm at Appropriate Setpoint Due to Faulty Alarm Module ML20041B1051982-01-28028 January 1982 LER 82-002/03L-0:on 820114,at 99% Power,Lockout Relay 86B1, Containment Radiation High Signal,Failed to Actuate on Demand by Plant Radiation Monitoring Sys.Caused by Burnt Coil on Lockout Relay.Coil Replaced & Tested Satisfactorily ML20041B1171982-01-19019 January 1982 LER 82-001/03L-0:on 820111,during Normal Operation,Two Fire Barrier Penetrations Found Nonfunctional.Shift Supervisor Immediately Notified;However,Fire Watch Not Posted.Insp & Supervisor Personnel Instructed on Proper Actions ML20039B4561981-12-11011 December 1981 LER 81-011/03L-0:on 811113,containment Isolation Valves Opened & Ventilation Process Initiated W/Containment Air Monitor RM-050/051 Inoperable.Caused by Personnel Error. Valves Closed ML20010H8581981-08-27027 August 1981 LER 81-008/03L-0:on 810813,86B/CRHS (Containment Radiation High Signal) Lockout Relay Failed to Actuate When RM-062 Was Placed in Alarm,Resulting in Failure of 86B1/CRHS Relay to Actuate.Caused by Dirt in Relay Latching Mechanism ML20041F6291981-08-27027 August 1981 LER 81-008/03L-1:on 810813,containment Radiation High Signal 86B Lockout Relay Failed to Actuate When Radiation Monitor RM-062 Placed in Alarm.Caused by Bound Relay Latching Mechanism Due to Dirt & Grease.Latch Cleaned ML20010C2271981-07-0707 July 1981 LER 81-006/03L-0:on 810624,reactor Protection Sys Nuclear Power Recorder Channel B Trip Setpoints Determined to Be Nonconservative.Caused by Faulty Temp Change Power Calculation Due to Grounded Hot Leg Temp Loop ML20004B1111981-05-0606 May 1981 LER 81-005/03L-0:on 810423,dc Sequencer Timers AC-3A (Component Cooling Water Pump) & AC-102A (Raw Water Pump) Failed to Time Out within Prescribed Limit.Cause Unknown Mechanisms Satisfactorily Inspected 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046C2121993-07-30030 July 1993 LER 93-004-01:on 930301,confirmed That Channel D Axial Shape Index (Asi) Being Calculated in Reverse Since 921031-930301 Due to Drawing Discrepancies Associated W/Control Channel B. Temporary Mod 92-078 & Standing Order 0-25 Revised ML20046A8691993-07-26026 July 1993 LER 93-011-00:on 930624,experienced Reactor Trip Due to Loss of Load.Caused by Lack of Proper Job Planning,Lack of Formal Decision Making Process & Incomplete Communications.Training Will Be Provided to Operations personnel.W/930726 Ltr ML20045H2561993-07-12012 July 1993 LER 93-010-00:on 930611,1 of 14 Halon Cylinders Did Not Meet Min Pressure Acceptance Criteria Listed in Semiannual Switchgear Rooms Surveillance Test.Caused by Failure of Test to Include Necessary Steps.Cylinder recharged.W/930712 Ltr ML20045D7201993-06-22022 June 1993 LER 93-009-00:on 930524,apparent Spurious Signal from Pressurizer Level Instrumentation Caused Backup Charging Pumps to Automatically Start,Due to Deterioration of Wiring. Instrument Loop Calibration Will Be performed.W/930622 Ltr ML20045D3741993-06-21021 June 1993 LER 93-008-00:on 930520,determined That TS SR Not Satisfied for Stack Flow Indicator,Per Amend 137 Issued on 910307. Caused by Lack of Attention to Detail.Calibr & Functional Test Procedures developed.W/930621 Ltr ML20044H5261993-06-0101 June 1993 LER 93-007-00:on 930430,unplanned Emergency Generator Start & Rt Signal Occurred.Caused by Inadequate Attention to Detail,Labeling of Fuse Drawers,Caution Signs & Training. Labeling & Caution Signs upgraded.W/930601 Ltr ML20044G4941993-05-26026 May 1993 LER 93-006-00:on 930118,Halon Fire Suppression Sys for Switchgear Rooms Disabled to Allow Repair/Replacement of Halon Sys Piping.On 930427,individual Responsible for Fire Watch Not Present.Individual Relieved of Responsibilities ML20044B6711993-02-22022 February 1993 LER 93-002-00:on 930122,determined That Current SG LP Signal Block Reset Values Greater than Allowed Ts.Caused by Improper Design.Test Procedures Will Be Revised by 930917 to Specify Desired Value for Block function.W/930222 Ltr ML20024G6821991-04-19019 April 1991 LER 91-007-00:on 910320,480 Volt Circuit Breaker Coordination Outside Design Basis.Caused by Deficiencies in Original Sys Design.Breaker/Fuse Coordination Study to Be Completed & Problems Will Be corrected.W/910419 Ltr ML20029C1591991-03-21021 March 1991 LER 91-004-00:on 910212,offsite Power Low Signal Outside Design Basis.Caused by Inadequate Mod Design at Time of Performance of Original Degraded Voltage Analysis. Engineering Analysis EA-FC-91-017 performed.W/910321 Ltr ML20029C1051991-03-18018 March 1991 LER 91-002-00:on 901209,ventilation Isolation Actuation Signal Generated by High Alarm on Process Radiation Monitor RM-062.Caused by Accumulation of Noncondensible Gases in Sample Piping.Valve Packing Leak repaired.W/910318 Ltr ML20029A2981991-02-0808 February 1991 LER 91-001-00:on 910109,determined That Containment Tendon Surveillances Performed in 1981 & 1985 Did Not Reflect Guidance in Tech Specs.Caused by Inadequate Administrative Controls.Testing Program Plan implemented.W/910208 Ltr ML20029A2971991-02-0606 February 1991 LER 90-022-02:on 900907,approx 460 Fire Barrier Penetration seals,60 Fire Dampers & 6 Fire Doors Declared Nonfunctional Per NRC Info Notice 88-004 Due to Lack of Documentation. Plant Outage Required to Implement Repairs/Replacements ML20028G9171990-09-28028 September 1990 LER 90-021-00:on 900829,inadvertent Reactor Protective Sys Actuation Occurred While Operator Changed Power Source. Caused by Operator Not Following Proper Procedures.Operator counseled.W/900928 Ltr ML20044B0131990-07-12012 July 1990 LER 90-018-00:on 900612,reactor Protective Sys (RPS) Trip Units for Axial Power Distribution Determined to Be Inoperable.Caused by Procedural Deficiencies.Procedure Revised & RPS Surveillance Tests reviewed.W/900712 Ltr ML20043F6301990-06-11011 June 1990 LER 90-016-00:on 900511,accident Scenarios Identified by Which Auxiliary Feedwater Piping from Discharge of Turbine Driven Auxiliary Feedwater Pump FW-10 Can Be Overpressurized.Caused by Design deficiency.W/900611 Ltr ML20043F2441990-06-0707 June 1990 LER 90-015-00:on 900507,PORV Variable Setpoints Used for Low Pressure Overpressure Protection Determined to Be Nonconservative for PORV Opening Time.Caused by Design Deficiency.Tech Spec Amend prepared.W/900607 Ltr ML20043C0991990-05-29029 May 1990 LER 90-014-00:on 900427,investigation Revealed That Component Cooling Water Piping to Reactor Coolant Pump Seal Coolers Could Be Targets of High Energy Line Break.Safety Analysis for Operability completed.W/900529 Ltr ML20042G7211990-05-10010 May 1990 LER 90-011-00:on 900402,inadvertent Actuation of Pressurizer Pressure Low Signal Occurred While Performing Calibr Procedure.Caused by Inappropriate Action by Technician Involved.Validation of Procedures reviewed.W/900510 Ltr ML20042E6871990-04-23023 April 1990 LER 90-007-01:on 900228,determined That Several Supports Would Be Overloaded During Seismic Event on Nonsafety Related & safety-related Main Steam Piping.Caused by Design Deficiency.Piping Supports modified.W/900423 Ltr ML20042E6861990-04-23023 April 1990 LER 90-009-00:on 900316,potential Overpressurization of Auxiliary Feedwater Piping Could Have Occurred During Thermal Expansion of Process Fluid Between Closed Valved. Caused by Design deficiencies.W/900423 Ltr ML20012E7641990-03-26026 March 1990 LER 90-005-00:on 900223,determined That Spent Fuel Pool Area Charcoal Filtration Unit VA-66 Was Outside Design Basis. Caused by Insufficient Airflow Into Unit.Affected Updated SAR Analysis Will Be updated.W/900326 Ltr ML20012D0121990-03-19019 March 1990 LER 90-004-00:on 900217,lift Pressures for 6 of 10 Main Steam Safety Valves Found Outside Acceptance Criteria. Caused by Overly Restrictive Operability Criteria.Valves Recalibr & License Amend Submitted to NRC.W/900319 Ltr ML20012D0101990-03-19019 March 1990 LER 90-003-00:on 900216,determined That Auxiliary Feedwater Piping Outside Normal Stress Limits of ASME Code & Design Basis Specified in Updated Sar.Caused by Design Deficiency.Valve Operators Will Be inspected.W/900319 Ltr ML20012B6361990-03-0909 March 1990 LER 89-017-01:on 890624,internal Valve Component from Check Valve Found Lying on Pump Discharge Vane.Repair or Replacement of Valve Internals Could Not Be Accomplished within Time Requirement of Tech Spec.W/900309 Ltr ML20006E1041990-02-0909 February 1990 LER 90-001-00:on 900108,fire Barrier for Wall Between Auxiliary Bldg Rooms 26 & 34 Breached But Hourly Fire Watch Patrol Not Established.Caused by Lack of Sufficient Training for Shift Supervisors.Standing Order revised.W/900209 Ltr ML20011E2691990-02-0505 February 1990 LER 89-024-00:on 891221,determined That Containment Spray Pumps & Suction Header Piping Not Constructed for Use as Backup to LPSI Sys for Shutdown Cooling.Caused by Inadequate Review of Assumptions.Firewatch established.W/900205 Ltr ML20011E2271990-02-0101 February 1990 LER 89-021-00:on 891010,util Informed by C-E of Potential Nonconservative Setpoint in Reactor Protection Sys Thermal Margin/Low Pressure Trip Unit.Caused by Error in Incorporating Transient Setpoint analyses.W/900201 Ltr ML20005F7151990-01-10010 January 1990 LER 89-023-00:on 891211,hourly Firewatch Patrol Entered Posted High Radiation Area W/O Meeting Entry Requirements for Area.Briefings on High Radiation Entry Requirements Held for Personnel W/Assigned dosimetry.W/900110 Ltr ML19354D6381989-12-20020 December 1989 LER 89-022-00:on 890805,change to Surveillance Procedure ST-CEA-1 Became Effective Which Would Have Made Both Emergency Diesel Generators Simultaneously Inoperable During Portion of Test.Change removed.W/891220 Ltr ML19332E7431989-12-0808 December 1989 LER 88-037-01:on 881214,one of Two Supply Headers Supplying Fire Suppression Headers in Auxiliary Bldg Isolated.Caused by Lack of Procedural Guidance & Inadequate Procedural Controls.Standing Order G-58 Will Be revised.W/891208 Ltr ML19332E2681989-12-0101 December 1989 LER 89-016-02:on 890616,for Unknown Period Since 890614, Auxiliary Feedwater Pump FW-10 Operated Outside Design Basis for Certain Accident Conditions.Caused by Inoperable Speed Control Loop.Action Plan implemented.W/891201 Ltr ML19351A4541989-11-22022 November 1989 LER 89-020-00:on 891012,determined That Two of Four Component Cooling Water HXs Simultaneously Inoperable for More than 24 H.Caused by Inadequate Controls Re Return of Equipment to Svc.Standing Order revised.W/891122 Ltr ML19327B5481989-10-24024 October 1989 LER 89-019-00:on 890924,indication of High Temp for Reactor Coolant Pump RC-3A Upper Motor Thrust Bearing Received in Control Room.Caused by Damaged Cable for Bearing Resistive Temp Device.Damaged Cable replaced.W/891024 Ltr ML19325D2471989-10-13013 October 1989 LER 89-012-01:on 890502,main Feedwater Isolation Valve to Steam Generator a Found Inoperable Due to Improperly Set Torque Switch.Caused by Inadequate Program for Maint of Motor Operated Valves.Torque Switches reset.W/891013 Ltr ML20028C7711983-01-0606 January 1983 LER 82-020/03L-0:on 821207,during Main Steam Safety Valve Test,Four Main Steam Safety Valves Had Lift Setpoints Out of Tolerance.Caused by Normal Drift of Valves Over Operating Cycle.Valves Readjusted ML20028B5451982-10-28028 October 1982 LER 82-019/03L-0:on 821024,MSIVs HCV-1041A & HCV-1042A Stopped Three to Four Degrees Off Seat When Signaled to Close.Caused by Binding Between Valve Packing & Shaft. Packings Sprayed W/Penetrant Oil ML20052J0631982-04-27027 April 1982 LER 82-009/03L-0:on 820411,while Exchanging Component Cooling Water Heat Exchangers,Associated Outlet Valves HCV-490B,HCV-491B & HCV-492B Failed to Open.Cause Not stated.HCV-491B Reassembled & Tested ML20052B2361982-04-0707 April 1982 LER 82-006/03L-0:on 820323,during Surveillance Test ST-ISI- WD-1,F.1,valve HCV-506A Failed to Close Via Control Room Switch.Caused by Solenoid Valve Malfunction.Solenoid Valve Disassembled,Cleaned & Reassembled ML20052D9291982-04-0606 April 1982 LER 82-008/03L-0:on 820330,during Performance of ST-FW-1, F.2(b)(6)per Tech Spec 3.9,steam Driven Auxiliary Feedwater Pump Failed to Start.Caused by Back Pressure Trip Lever in Tripped Position.Lever Reset ML20041G1291982-02-22022 February 1982 LER 82-005/03L-0:on 820210,at 98% Power,Control Element 24 Inserted Into Core.Emergency Procedure EP-13,CEDM Malfunctions,Implemented & Power Stabilized at 88%.Caused by Erroneous Operating Instruction.Instruction Changed ML20041F7481982-02-17017 February 1982 LER 82-003/03L-0:on 820203,containment Isolation Valve Associated W/Gas Vent Header HCV-507A Failed to Close on Demand.Caused by Solenoid Valve Plunger Sticking in Energized Position.Plunger Freed ML20041F6251982-02-0505 February 1982 LER 82-004/03L-0:on 820203,small Quantity of Radioactive Gas/Particulate Released to Auxiliary Bldg During Routine Operation.Caused by Failure of Stack Gas Monitor RM-062 to Alarm at Appropriate Setpoint Due to Faulty Alarm Module ML20041B1051982-01-28028 January 1982 LER 82-002/03L-0:on 820114,at 99% Power,Lockout Relay 86B1, Containment Radiation High Signal,Failed to Actuate on Demand by Plant Radiation Monitoring Sys.Caused by Burnt Coil on Lockout Relay.Coil Replaced & Tested Satisfactorily ML20041B1171982-01-19019 January 1982 LER 82-001/03L-0:on 820111,during Normal Operation,Two Fire Barrier Penetrations Found Nonfunctional.Shift Supervisor Immediately Notified;However,Fire Watch Not Posted.Insp & Supervisor Personnel Instructed on Proper Actions ML20039B4561981-12-11011 December 1981 LER 81-011/03L-0:on 811113,containment Isolation Valves Opened & Ventilation Process Initiated W/Containment Air Monitor RM-050/051 Inoperable.Caused by Personnel Error. Valves Closed ML20010H8581981-08-27027 August 1981 LER 81-008/03L-0:on 810813,86B/CRHS (Containment Radiation High Signal) Lockout Relay Failed to Actuate When RM-062 Was Placed in Alarm,Resulting in Failure of 86B1/CRHS Relay to Actuate.Caused by Dirt in Relay Latching Mechanism ML20041F6291981-08-27027 August 1981 LER 81-008/03L-1:on 810813,containment Radiation High Signal 86B Lockout Relay Failed to Actuate When Radiation Monitor RM-062 Placed in Alarm.Caused by Bound Relay Latching Mechanism Due to Dirt & Grease.Latch Cleaned ML20010C2271981-07-0707 July 1981 LER 81-006/03L-0:on 810624,reactor Protection Sys Nuclear Power Recorder Channel B Trip Setpoints Determined to Be Nonconservative.Caused by Faulty Temp Change Power Calculation Due to Grounded Hot Leg Temp Loop ML20004B1111981-05-0606 May 1981 LER 81-005/03L-0:on 810423,dc Sequencer Timers AC-3A (Component Cooling Water Pump) & AC-102A (Raw Water Pump) Failed to Time Out within Prescribed Limit.Cause Unknown Mechanisms Satisfactorily Inspected 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217B5401999-10-0606 October 1999 Safety Evaluation Supporting Amend 193 to License DPR-40 ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data LIC-99-0096, Monthly Operating Rept for Sept 1999 for Fcs,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Fcs,Unit 1.With ML20211J9321999-09-0202 September 1999 Safety Evaluation Concluding That Licensee Proposed Alternatives Provide Acceptable Level of Quality & Safety. Proposed Alternatives Authorized for Remainder of Third ten- Yr ISI Interval for Fort Calhoun Station,Unit 1 LIC-99-0084, Monthly Operating Rept for Aug 1999 for Fort Calhoun Station.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Fort Calhoun Station.With ML20216E6431999-08-26026 August 1999 Rev 19 to TDB-VI, COLR for FCS Unit 1 ML20210R1961999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Fcs,Unit 1 ML20210G2181999-07-27027 July 1999 Safety Evaluation Supporting Amend 192 to License DPR-40 ML20210D9951999-07-22022 July 1999 Safety Evaluation Supporting Amend 191 to License DPR-40 ML20216E6361999-07-21021 July 1999 Rev 18 to TDB-VI, COLR for FCS Unit 1 ML20210R2081999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Fcs,Unit 1 LIC-99-0065, Monthly Operating Rept for June 1999 for Fort Calhoun Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Fort Calhoun Station,Unit 1.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20210P5461999-06-0808 June 1999 Rev 0,Vols 1-5 of Fort Calhoun Station 1999 Emergency Preparedness Exercise Manual, to Be Conducted on 990810. Pages 2-20 & 2-40 in Vol 2 & Page 4-1 in Vol 4 of Incoming Submittal Not Included ML20195B4581999-05-31031 May 1999 Rev 3 to CE NPSD-683, Development of RCS Pressure & Temp Limits Rept for Removal of P-T Limits & LTOP Requirements from Ts ML20207H7401999-05-31031 May 1999 Performance Indicators Rept for May 1999 LIC-99-0053, Monthly Operating Rept for May 1999 for Fort Calhoun Station,Unit 11999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Fort Calhoun Station,Unit 1 ML20195B4521999-05-17017 May 1999 Technical Data Book TDB-IX, RCS Pressure - Temp Limits Rept (Ptlr) ML20206L4241999-05-10010 May 1999 Safety Evaluation Supporting Corrective Actions to Ensure That Valves Are Capable of Performing Intended Safety Functions & OPPD Adequately Addressed Requested Actions Discussed in GL 95-07 ML20206M2601999-05-0606 May 1999 SER Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & IPEEE Results Reasonable Given FCS Design,Operation & History LIC-99-0047, Monthly Operating Rept for Apr 1999 for Fort Calhoun Station Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Fort Calhoun Station Unit 1.With ML20195E8621999-04-30030 April 1999 Performance Indicators, for Apr 1999 ML20205Q5831999-04-15015 April 1999 Safety Evaluation Supporting Amend 190 to License DPR-40 ML20210J4331999-03-31031 March 1999 Changes,Tests, & Experiments Carried Out Without Prior Commission Approval for Period 981101-990331.With USAR Changes Other than Those Resulting from 10CFR50.59 ML20206G2641999-03-31031 March 1999 Performance Indicators Rept for Mar 1999 LIC-99-0034, Monthly Operating Rept for Mar 1999 for Fcs,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Fcs,Unit 1.With ML20205J8181999-02-28028 February 1999 Performance Indicators, for Feb 1999 LIC-99-0025, Monthly Operating Rept for Feb 1999 for Fort Calhoun Station,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Fort Calhoun Station,Unit 1.With ML20207F3291999-01-31031 January 1999 FCS Performance Indicators for Jan 1999 ML20203B0991998-12-31031 December 1998 Performance Indicators for Dec 1998 LIC-99-0026, 1998 Omaha Public Power District Annual Rept. with1998-12-31031 December 1998 1998 Omaha Public Power District Annual Rept. with LIC-99-0003, Monthly Operating Rept for Dec 1998 for Fort Calhoun Station.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Fort Calhoun Station.With ML20198S3771998-12-31031 December 1998 Safety Evaluation Supporting Amend 189 to License DPR-40 ML20198S4831998-12-31031 December 1998 Safety Evaluation Supporting Amend 188 to License DPR-40 ML20196G2251998-12-18018 December 1998 Rev 2 to EA-FC-90-082, Potential Over-Pressurization of Containment Penetration Piping Following Main Steam Line Break in Containment ML20198M3141998-11-30030 November 1998 Performance Indicators Rept for Nov 1998 LIC-98-0172, Monthly Operating Rept for Nov 1998 for Fort Calhoun Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Fort Calhoun Station,Unit 1.With LIC-98-0160, Special Rept:On 981113,MSL RM RM-064 Was Declared Inoperable Due to Leakage Past Isolation Valve HCV-922.Troubleshooting Has Indicated That Leakage Has Stopped & Cause of Leak Continues to Be Investigated1998-11-25025 November 1998 Special Rept:On 981113,MSL RM RM-064 Was Declared Inoperable Due to Leakage Past Isolation Valve HCV-922.Troubleshooting Has Indicated That Leakage Has Stopped & Cause of Leak Continues to Be Investigated ML20203B0721998-11-16016 November 1998 Rev 6 to HI-92828, Licensing Rept for Spent Fuel Storage Capacity Expansion ML20196E4981998-10-31031 October 1998 Performance Indicators Rept for Oct 1998 ML20196G2441998-10-31031 October 1998 Changes,Tests & Experiments Carried Out Without Prior Commission Approval. with USAR Changes Other than Those Resulting from 10CFR50.59 LIC-98-0154, Monthly Operating Rept for Oct 1998 for Fort Calhoun Station,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Fort Calhoun Station,Unit 1.With ML20154M4881998-10-19019 October 1998 Safety Evaluation Supporting Amend 186 to License DPR-40 ML20154N2411998-10-19019 October 1998 Safety Evaluation Supporting Amend 187 to License DPR-40 LIC-98-0136, Monthly Operating Rept for Sept 1998 for Fort Calhoun Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Fort Calhoun Station,Unit 1.With ML20155G4261998-09-30030 September 1998 Performance Indicators for Sept 1998 ML20154A1251998-08-31031 August 1998 Performance Indicators, Rept for Aug 1998 LIC-98-0122, Monthly Operating Rept for Aug 1998 for Fort Calhoun Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Fort Calhoun Station Unit 1.With ML20238F7231998-08-17017 August 1998 Owner'S Rept for Isis ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency 1999-09-30
[Table view] |
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On September 7, 1990, appr0ximately 460 fire barrier penetration seals, 60 fire dampers and 6 fire doors associated with 25 fire areas were cieclared nonfunctional due to either lack of documentation to qualify non-verifiable penetration critical parameters, or penetration "as built" configurations which did not match typical configurations previously qualified by fire tests. These nonfunctional penetrations were discovered through a special design basis verification walkdown prompted by NRC Information Notice 88-04.
As required by Technical Specifications, the appropriate compensatory measures were implemeated. On November 27, 1990 and on January 2, 1991, additional barrier I penetrations were determined to be nonfunctional and the required compensatory measures were established. The compensatory measures will remain in place until the affected fire barrier penetrations are restored to functional status through engineering evaluation, repair, or replacement.
l l This report is submitted pursuant to Technical Specification 2.19(7) because most of the nonfunctional fire barrier penetrations were not restored to functional status l within 7 days. It is_being submitted also as a Voluntary LER due to, otential
- j. regulatory and industry interest.
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'v"/ "'E"N 1 P APE RWO RE o TION J 13 o O tt OF MAN &Of MENT AND Sv0GE T.W A$MINGTON. DC 20603 P ACitif V NAMS HI DOCE t Y NVMs t m 12 LIR NuWetR 80s PAGE 131 viaa "t'T.P t- W,9 1 Fort-Calhoun Station Unit No. 1 o ls 10 o j o l2 l 8l5 02 or 0 l5 rw w - N-. N ~~,o .mwac r .ma ,e 9l 0 -
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0l2 NRC Information Notice 88-04, Inadecuate Qualification and Documentation of Fire Barrier Penetration Seals, requestec utilities to verify the design basis of their fire barrier penetration seals. OmahaPublicPowerDistrict(0 PPD)begana comprehensive walkdown and assessment of all Technical Specification recuired fire barriers in April of 1990. - This walkdown and assessment effort was concucted by contrar: tor personnel under the provisions of OPPD Special Procedures SP-DEN-FP-0001, SP-DEN-FP-0002 and SP-DEN-FP-0003. The scope of the project included fire barrier penetration seals, fire doors, and fire dampers.
The walkdown portion was performed to document the "as built" condition of fire barrier penetration seals, fire doors, and fire dampers. On September 7, 1990 OPPD Systems Engineering and Design Engineering completed the assessment of fire barrier configurations as documented by the Special Procedures. These procedures required that fire barriers penetrations be considered inoperable if no prior documentation of installation was found for critical parameters that could not be field verified, or.if-any "as built" 3enetration barrier did not match a fire-tested and qualified configuration. For t11s screening, each penetration barrier was considered functional if it was considered to meet a minimum 3-hour fire rating. i Based on this assessment, the following fire barrier penetrations associated with 25 fire areas were determined to be nonfunctional:
(1) approximately 460 of 3500 penetration seals, (2) 60 of 79 fire dampers, and (3) 6 of 79 fire doors.
As a result, System Engineering initiated Fire Protection Impairment Permits for all
. areas of the plant where fire aarrier penetrations were considered to be nonfunctional. Compensatory measures required by Technical Specification 2.19(7) for inoperable fire barrier penetrations were established. Revision 0 of this report was submitted as required by the Technical Specification on October 8, 1990
- because most of the nonfunctional fire barrier penetrations were not restored to functional status within 7 days. It was submitted also as a Voluntary LER due to potential regulatory and industry interest.
A walkdown assessment of seals determined to be nonfunctional continued concurrent with a Quality Control verification of individual penetration as-built drawings.-
Consequently, additional sealing devices were identified as nonfunctional. On
. November 27, 1990, one additional barrier im)airment permit was issued and the required compensatory measures were establisled. Revision 1 of this report fulfilled the Special Report requirement of the Technical Specification for the additional nonfunctional penetrations identified.
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0f 0 l3 or 0 l5 The additional <ssessments added 92 to the total number of ino)erable seals, while another 129 seals previously identified were resolved as opera)1e, resulting in a net decrease of 37 for the total. In addition, the number of fire areas involved was increased from 25 to 26. As of the writing of Revision 1 to this report (submitted December 31,1990), the numbers of nonfunctional fire barrier penetrations were:
(1)~approximately423of3500penetrationseals, (2) 60 of 79 fire dampers, and (3) 7 of 79 f. ire doors. ,
On January 2, 1991, the walkdown inspections were completed. As a result, additional nonfunctional sealing devices were identified and appropriate compensatory measures were verified as im)lemented. This second revision fulfills the Special Report requirement of the Tec1nical Specification for the additional nonfunctional penetrations identified.
The additional assessments added 36 to the total number of inoperable seals, while another 18 seals previously identified were resolved as operable, resulting in a net increase of 18 for the total. An additional nonfunctional fire damper was discovered. As of the writing of this report revision, the numbers of nonfunctional fire barrier penetrations are:
(1) 441 of-approximately 3500 penetration seals, (2) 61 of 79 fire dampers, and (3) 7 of 79 fire doors.
The noted fire barrier penetration sealing devices were declared nonfunctional because no prior documentation existed for them, or their configurations did not match those qualified by fire testing. These criteria were used as a result of-NRC Information Notice 88-04, and were different from the criter-la utilized in performance of periodic fire barrier penetration surv6!11ances as required by TechnicalSpecification3.15(5).
Previous Technical Specification surveillances (the last completed in March of 1990) have verified that fire barrier penetrations were functional (intact) at least once per 18 months by visual ins)ection. When degraded barriers were found in the course of these surveillances, Tec1nical Specification compensatory measures were established until the barriers.were restored to functional status. Therefore, the cause of-the re)ortable nonfunctional status of the fire barrier penetrations was not an actual s1 ort term deterioration of the barriers, but the identification of design basis deficiencies in the construction and/or documentation of the barriers.
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012 014 oF 0 l5 As compensatory tetions in com>11ance with Technical Specification 2.19(7), hourly fire watches established 3ased upon verification of operable automatic fire detection on , ast one side of the affected fire barriers. These measures assure c prompt respons, the stetion tire brigade to preclude the spread of fire across any degraded fire, barrier.
As noted in the Fire Hazards Analysis, Fort Calhoun Station overall has low fixed combustible loadings within its different fire areas, with the exception of the diesel rooms and the turbine building. Tho predominant share of inoperable fire barrier penetrations were found in those areas where the total fixed combustible loading is low. In the diesel rooms, additional protection is provided by an automatic dry pipe sprinkler system. The turbine building, which adjoins the auxiliary building, is provided with automatic fire detection and automatic water sup)ression for most areas where combustible loading is high. Transient com]ustibles and hot work activities are controlled by plant administrative procedures. OPPD management personnel are required by Standing Order G-6 to perform regular plant inspections for general housekeeping. An explicit )urpose stated for this inepection is to " reduce to a minimum the amount of combustiale material stored in safe.y related areas."
Many of the fire barrier penetrations determined to be inoperable are related only to licensing commitments made in response to Appendix A to Branch Technical Position 9.5-1. These barriers do not correspond to those committed to under the Fort Calhoun Station 10CFR 50, Ap)endix R analysis, and thus are not required to preserve safe shutdown-capability. T1ese barriers do not separate redundant trains of safe shutdown equipment and, therefore, the postulated breach of these barriers by a fire would have minimal safety impact.
The results of the fire barrier walkdown and assessment effort have been handled conservatively. As immediate corrective action, applicable technical specification LC0 action statements were implemented for all fire barrier penetrations ::onsidered nonfunctional (inoperable). These measures will remain in place until the affected penetrations are restored to a functional (operable) status.
It is estimated that approximately 35 percent of the penetrations can be evaluated as functional. Guidance given in NRC Generic Letter 86-10 allows for evaluations to be performed for penetrations not sealed to the fire rating required of the boundaries. The purpose of the evaluation is to determine whether the fire area a boundaries are sufficient to withstand the hazards associated with the fire area.
. Some barrier penetrations may be evaluated as justifiable in their current configuration. This work is on-going through 1991. Restoration of these penetrations to operable status through engineering evaluation is expected to be fully complete within 2 months following the end of the 1991 "efueling outage.
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0 12 0 (5 or 0l5 The approximately 65 percent of installed fire barrier penetrations which cannot be evaluated as functional will be repaired or replaced. A modification has been initiated to perform this work. Implementationofthismodif(icationwillMR-FC-90-072) be on-going through 1991. Because certain nonfunctional penetration sealing devices are inaccessible due to plant radiological conditions and energized electrical equipment, a plant outage will be required to implement required repairs or replacements. For this reason. the modification is expected to be completed within 2 months following the end of the 1991 refueling outage.
The u)' grade of procedural controls and fire barrier as-built drawing information will )e completed concurrent with the engineering evaluations and modification iniplementation discussed above. Drawings reflecting as-built configurations for repaired or replaced penetration sealing devices will be processed as part of the modification closeout. Upgrades planned for existing procedures with respect to fire barrier configuration control will be implemented separately but concurrently
, with the activities described above.
Other 5)ecial Re) orts have been submitted because of non-related instances of inopera)1e fire Jarriers; howeveri thera have been no Special Reports or LERs submitted due to a generic cause affecting many barriers.
NaC Pero se6A 5649:
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