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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20043H9921990-06-22022 June 1990 Special Rept 1-90-04:on 900523,valid Diesel Generator 1B Tripped.Caused by Replaced Jacket Water Temp Switches.Onsite Calibr Procedure Revised to Provide Technique Consistent W/ Actual Operating Conditions ML20043B6001990-05-24024 May 1990 Special Rept:On 900415,loose Part Detection Sys Inoperable for More than 30 Days.Caused by Either Sensors IXE-0750 & IXE-0751 Attached to Reactor Head or pre-amplifier Located 6 Ft Away.Sensors Will Be Inspected After Next Mode 5 Entry ML20042F3781990-05-0404 May 1990 Special Rept 1-90-03: on 900415,steam Line Radiation Monitor Removed from Svc When Personnel Unable to Enter Parameters on Digital Process Module.New Circuit Board Installed on 900430 & Monitor Returned to Svc by 900501 ML20012C3371990-03-12012 March 1990 Special Rept 2-90-02-01:on 900124 & 25,Diesel Generators 2A & 2B Failed,Respectively.Caused by Air Leak from Right Bank Air Start Blocking Valve Solenoids.Air Start Distributor Filters Replaced ML20011F5621990-02-19019 February 1990 Special Rept 2-90-02:on 900124 & 25,when Start Button Depressed,Diesel Generator 2A Rolled Slowly for Approx Two Turns But Did Not Start.On 900201,when Diesel Paralleled to Grid,Low Excitation Alarm Received.Bridge Circuit Repaired ML20006B9891990-01-29029 January 1990 Special Rept 1-90-01:on 900103,when Diesel Generator 1B Started for Monthly Surveillance,Low Turbocharger Oil Pressure Annunicator Alarmed.Caused by Small Leak on Low Oil Pressure Switch.Switch Replaced & Surveillance Completed ML20006B9141990-01-29029 January 1990 Special Rept 2-90-01:on 891206-900110,containment Radiation Level high-range Monitors Inoperable.Caused by Bad Preamplifier Circuit Board Which Caused Spurious Alarms. Preamplifier Circuit Board Replaced ML19332D9051989-11-29029 November 1989 Special Rept 50-424/1989-003:on 891030,31 & 1107,tendon Grease Deficiencies Noted During Combined Tendon Surveillances.No Corrosion or Cracks Found.Tensile Test Results for Strand Samples Expected by End of Dec 1989 ML19325E2611989-10-26026 October 1989 Special Rept.On 891016,channel Calibr for Loose Part Detection Sys Not Performed as Specified in Fsar.Caused by Belief That Calibr Not Required.Channel Calibr Entered Into Tech Spec Surveillance Tracking Program 1990-06-22
[Table view] Category:LER)
MONTHYEARML20043H9921990-06-22022 June 1990 Special Rept 1-90-04:on 900523,valid Diesel Generator 1B Tripped.Caused by Replaced Jacket Water Temp Switches.Onsite Calibr Procedure Revised to Provide Technique Consistent W/ Actual Operating Conditions ML20043B6001990-05-24024 May 1990 Special Rept:On 900415,loose Part Detection Sys Inoperable for More than 30 Days.Caused by Either Sensors IXE-0750 & IXE-0751 Attached to Reactor Head or pre-amplifier Located 6 Ft Away.Sensors Will Be Inspected After Next Mode 5 Entry ML20042F3781990-05-0404 May 1990 Special Rept 1-90-03: on 900415,steam Line Radiation Monitor Removed from Svc When Personnel Unable to Enter Parameters on Digital Process Module.New Circuit Board Installed on 900430 & Monitor Returned to Svc by 900501 ML20012C3371990-03-12012 March 1990 Special Rept 2-90-02-01:on 900124 & 25,Diesel Generators 2A & 2B Failed,Respectively.Caused by Air Leak from Right Bank Air Start Blocking Valve Solenoids.Air Start Distributor Filters Replaced ML20011F5621990-02-19019 February 1990 Special Rept 2-90-02:on 900124 & 25,when Start Button Depressed,Diesel Generator 2A Rolled Slowly for Approx Two Turns But Did Not Start.On 900201,when Diesel Paralleled to Grid,Low Excitation Alarm Received.Bridge Circuit Repaired ML20006B9891990-01-29029 January 1990 Special Rept 1-90-01:on 900103,when Diesel Generator 1B Started for Monthly Surveillance,Low Turbocharger Oil Pressure Annunicator Alarmed.Caused by Small Leak on Low Oil Pressure Switch.Switch Replaced & Surveillance Completed ML20006B9141990-01-29029 January 1990 Special Rept 2-90-01:on 891206-900110,containment Radiation Level high-range Monitors Inoperable.Caused by Bad Preamplifier Circuit Board Which Caused Spurious Alarms. Preamplifier Circuit Board Replaced ML19332D9051989-11-29029 November 1989 Special Rept 50-424/1989-003:on 891030,31 & 1107,tendon Grease Deficiencies Noted During Combined Tendon Surveillances.No Corrosion or Cracks Found.Tensile Test Results for Strand Samples Expected by End of Dec 1989 ML19325E2611989-10-26026 October 1989 Special Rept.On 891016,channel Calibr for Loose Part Detection Sys Not Performed as Specified in Fsar.Caused by Belief That Calibr Not Required.Channel Calibr Entered Into Tech Spec Surveillance Tracking Program 1990-06-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
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Text
7. . , --
~i Categia Power Cbmpany
- 333 P,iutmon! Am*,ao I O. At.anta Geo;)a 30338
.M Tsephone 434 L?6 3196 Y unamm
- 40 IMirren Conter Pdway so lict 0% Box 1?95 tFrm naham. Alabama 35201 L w .n u eost u suo l
February 19, 1990 .. , , . . , , , , , , , , , ,
W. G. Hairston, Ill L
sew vce rrewi, Nant r Operahans ELV-01353 0243
[ Docket No. 50-425
- U. S. Nuclear Regulatory Commission ATTN
- Document Control Desk p Washington, D. C. 20555 Gentlemen:
V0GTLE ELECTRIC GENERATING PLANT SPECIAL REPORT VAllD DIESEL GENERATOR FAILVRES In accordance with the requirements of the Vogtle Electric Generating Plant Technical Specifications, Sections 4.8.1.1.3 and 6.8.2, Georgia Power Company is submitting the enclosed Special Report concerning valid diesel generator
- - failures.
!. Sincerely.
././ W
. G. Hairston, 111 WGH,lil/NJS/gm
Enclosure:
Special Report 2-90-02 xt: Georaia Power Comna01 Mr. C. K. McCoy Mr. G. Bockhold, Jr.
Mr. R. M. Odom Mr. P. D. Rushton NORMS U. S. Nuclear Reaulatory Commission b' Mr. S. D. Ebneter, Regional Administrator Mr. D. B. Matthews, Director, Project Directorate 11-3 Mr. R. F. Aiello, Senior Resident inspector, Vogtle i
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.9003060269 900219
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ADOCK 05000423 FDC 0
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t ENCLOSURE V0GTLE ELECTRIC GENERATING PLANT - UNIT 2 TECHNICAL SPECIFICATION SPECIAL REPORT 2-90-02 VAllD DjfSEL GENERATOR FAllDRES A. REQUIREMENT FOR REPORT n' This report is required in accordance with the Vogtle Electric Generating Plant Technical Specifications, Section 4.8.1.1.3. This section of the Technical Specifications requires that all diesel generator failures, valid or non-valid, be reported to the Commission in a Special Report pesuant to 3
Technical Specification 6.8.2.
B. DESCRIPTION OF VAllD FAILURES FOR DIESEL GENERATOR TRAIN A (1) On January 24, 1990 Diesel Generator (DG) 2A was scheduled to be started for the monthly surveillance. When the start pushbutton was depressed, the diesel rolled slowly for approximately 2 turns, but did ,
not start. One air receiver had been isolated, as required by procedure, to test independent starting. The operator noticed an air leak from one of the right bank air start blocking valve solenoids.
Assuming this to be the problem, he opened the isolated air receiver and attempted to start the diesel. The diesel was started and the surveillance completed with no further problems. Subsequent ,
investigation revealed that the leaking solenoid could not have caused the failure since it was associated with the isolated air receiver. No other cause for the failure could be found and, since the diesel was successfully started, it was declared operable. During this time, DG2A was out of service for 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> and 20 minutes. The leaking solenoid has subsequently been repaired.
(2) On January 25, 1990, DG2B was taken out of service after a successful test due to a problem with the stopping light. As a result, DG2A had to be tested again to satisfy the Technical Specification action requirements. Neither air receiver was isolated and when the start pushbutton was depressed, the diesel rolled slowly but did not start.
When operators attempted another start, the engine started and the surveillance was completed. Realizing this failure was similar to the one the day before in which one air receiver was isolated, operators did not return the diesel to service upon completion of the surveillance.
Troubleshooting included replacing the air start distributor filters and checking the operation of the governor, the fuel racks, the fuel l
system and the air start valves in the cylinders. No apparent problems were found and the engine was started 2 consecutive times with no other probl ems .
The engine was started a third time and a normal surveillance was completed. The diesel was returned to service. During this time, DG2A was out of service for 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br /> and 54 minutes. Both diesels were out of service simultaneously for a period of I hour and 56 minutes.
pr 3
ENCLOSURE (CONT'D)
V0GTLE ELECTRIC GENERATING PLANT - UNIT 2 ,
i
- TEGINICAL SPECIFICATION SPECIAL REPORT 2-90-02 i yAllD DIESEL GENERATOR FAILURES l-(3) On february 1,1990 DG2A was again started to complete Technical Specification surveillance requirements which had been increased to ,
every 7 days due to the past two valid failures. The diesel started;
, however, when paralleled with the grid, a low excitation alarm was received and reactive load exceeded stability limits. The DG output i- breaker was tripped and the generator was switched to the opposite independent rectifier bridge pe The DG was paralleled with the grid again /rndthetheoperating procedure.
surveillance was completed with no further problems. Upon satisfactory completion of the surveillance, DG2A was declared operable. The bridge circuit has subsequently been repaired. As a result of this failure, DG2A was out of service for 4
. hours and 1 minute. >
C.
SUMMARY
These were the first three valid failures on DG2A and the test frequency has been increased to once every 7 days in accordance with Table 4.8-1 of the 1 Technical Specifications. This frequency will be continued until 7 consecutive valid tests are completed and one or less valid failures have occurred in the last 20 valid tests. There have been a total of 41 valid tests of DG2A.
.