ML19261F250

From kanterella
Jump to navigation Jump to search
Abnormal Occurrence 50-289/74-20:on 741030,loss of Fluid in Hydraulic Shock Suppressor on Seismic Class I Sys.Caused by Improper Snubber Installation.Fitting Replaced,Reservoir Refilled,Snubber Reoriented & Lock Nut Tightened
ML19261F250
Person / Time
Site: Three Mile Island Constellation icon.png
Issue date: 11/08/1974
From: Arnold R
METROPOLITAN EDISON CO.
To:
References
GQL-0462, GQL-462, NUDOCS 7910250679
Download: ML19261F250 (4)


Text

.

  • AEC DISTRIBUTION FOR PART 50 DOCKET MATERIAL (TEMPORARY FORM) 116 0 _

CONTROL NO(

FILE:

FROM: Met. Edison Cc=pany DATE OF DOC D ATE R EC'D LTR TWX RPT OTHER Feading, Pa. 19603 o ,, .,_ a 4

~ ~~~

ll-8-Th 11-13-7h X

^T i ORIG CC OTHER SENT AEC ?DR It I'L 1 siged SENT LOCAL PDR XX CLASS UNCLASS PROPINFO INPUT NO CYS REC'D DOCKET NO:

CC< L 50-269 DESCRIPTION- Ltr adv of abnormal occurrence ENCLOSURES:

on 10-30-74 involving loss of fluid in hydrau2 ic shock suppressor en a seismic Class I systen.. ...

Abnor=alOccurrence(AO-50-289/Th-20).....

Dadiqf.Enove PLA'JT NAME: Three Mile Island Unit I 40GiiLEDN=>

FOR ACTION /INFORMATION DFL ll-15-Th SUTLER (L) SCHWENCER (L) ZIEM ANN (L) REG AN (E)

WJ Copies W/ Copies W/ Copies "'/ Copics CLARK (L) STOLZ (L) DICKER (E) E AR (L)

W/' Cop;e; W/ Copies W/ Copies W. ,opies PARR (L) VASSALLO iL) KNIGHTON (E)

W/ Copies W/ Copies W/ Copies W/ Copies KNIEL (L) PURPLE (L) YOUNGB LOOD (E)

W/ Copies W/ Copics W/ Copies W/ Copies INTERNAL DISTRIBUTION 6EG FID TECH REVIEW _D_E N T O N LIC ASST A/T IN D tsn t o r u n GRIMES B R AITro A. .

(OGC, ROO11 P E06A '/SCH RO EDE R 9AMMILL DIGGS (L) SA LTZM Ar.

h1UNTZING/STAF F /MACCARY M<ASTN E R GEARIN (L) 8. HURT p/ CASE t/KNIG HT BALLARD GOULEOURNE (L) t GI AM BUSSO /, PAWL:CKl SPANGLER KREUTZER (E) PLANS BOYD e'SHAO LEE (L) MCDON A' D MOORE (L) (BWR) t , ENVIRO MAIG RET (L) CHAPMAN DEYOUNG (L) (FWR) j/STE LLO MULLER nOUSTON REED (E) DUBE v/incut SKOVHOLT (L) .o'NOV A K DICKER SERVICE (L) E. COUPE GOLLER (L) /ROSS KNIG HTCN SHEPPARD (L)

P. CO LLINS  ;/IPPOLITO YOUNGBLOOD SLATER (E)

DENISE TEDESCO REGAN SMITH (L) th. THOMPSON (2) eKLECKER REG OPR g/LONG PROJECT LDR TEETS (L) /EISENHUT g(FILE & REGION (3) :/ LAIN AS WILLI AMS (E) if.'.1G P R I S tSENAROYA

/ H AR LESS WILSON (L)

VSTEELE i/VO LIME R ,,, c) A Q -

EXTERN AL DISTRIBUTION l4DI LM y th - LOC A, n.m Harrisbur; Pa.

p; TIC (A3ER: ATH-) i1 (2)(10) - N ATION AL LASS .___ 1 - POR SAN LA .-

fl - NSIC (3UCHAN AN) 1 - ASLSP(E.W BW Rm Sis) 1 - GROOKH AV EN' - 7 L .- c 1 - ASLS 1 - W. PE .N:NGTON Rm E 201 GT 1 - G. ULHIKSON, OP ' .

1 - Newton Ancer en 1 - B U .1 S'/. N:E R C '.0, R m E-201 GT 1 -- AG M E D (R UT H G LT2: . . ,

[5 AC c;.Al ~^  ? 0 135T 1 - CONSU LTA. :id Rm B 127 GT S. g- d5~74 N EW.',1 ARK, E LU . E;, .2 S.\3l A.Y 1 - R. D. MUE LLE R. R m E-2:i 791oGo Gy9 S

F3 (([d Reh:! ."rV

- - A7 N.C

  • w - -.~

METROPOLITAN EDISON COMPANY FCtT CF AICE SOX 542 READING. PENNSYLV ANI A 19603 TELEPHONE 2'S 3601 Nevericer 3, 1974 GQL 0462 s.x s;u.- .

~g-e4N

% \ ,

, f

] '

@ 'j e/g "y i %

Director , ,, # 1 d, i$[f .;,, 6-- ! '

'> l , -

Directorate of Licensing C. c ;, g..., [5 f .5 h(J,[-' '

U.S. Atomic Energy Com:nissiotf . M ar;& / 'f Yf Washington, D.C. 20545 .- EC U OLWS-'h k Dear Sir- ' E + ' l "\ -

Docket No. 50-289 Operating License DPR-50 In accordance with the Technical Specifications for our Three Mile Island Nuclear Station, Unit 1, we are reporting the following abnormal occurrence:

(1) Report Number: A0 50-289/74-20 (2a) Report Date: November 8, 1974 (2b) Occurrence Date: October 30, 1974 (3) Facility: Three Mile Island Nuclear Station, Unit 1 (4) Identification of Occurrence:

Title:

Loss of Fluid in a Hydraulic Shock Suppressor on a Seismic Class I System Type: An abnormal occurrence as defined by the Technical Specifications, paragraph 1.8d, in that the loss of fluid from a hydraulic shock suppressor threatened to cause an Engineered Safeguard feature or system to be incapable of performing its intended function.

(5) Conditions Prior to Occurrence: The reactor was at steady state power with major plant parameters as follows : .

Power : Core: 20% ,

Elec.: 100 W (Gross)

RC Flow: 190 x 106 lbs/hr 11G00

9 RC Pressure: 2250 psig RC Temp.: 579 F PRZR Level: 200 in PRZR Temp.: 550 F (6) Description of Occurrence:

While performing a check of the Pressurizer Relief Valve discharge lines, the engineer in charge noticed a pud 11e of hydraulic fluid on the floor. Further investigation showed that r shock suppressor (snubber) on the Pressurizer Electromatic Relief Va'.ve discharge line had rotated out of position and was lying or an adjacent pipe, and that a connector in the line connecting the attached hydraulic fluid reservoir to the shock suppressor had broken when the reservoir struck an adjacent pipe. This, in turn, allowed the hydraulic fluid to drain from the reservoir.

(7) Designation of Apparent Cause of Occurrence:

It is believed that the loss of hydraulic fluid from the snubber was caused by improper installation of the snubber. Normal operational vibration, in the present case, is thought to have freed the lock nut joining the snubber to the structural steel which supports it.

Had Loctite, or a similar substance, been used on the lo .k nut during installation of the snubber, the snubber would not have come free and would not have rotated out of position.

(8) Analysis of Occurrence:

The snubbers on the electromatic relief piping are installed for dynamic loading and the worst consequence of a failure involving such loading would be deformation of the piping. A careful examination of the discharge line from the Electromatic Relief Valve has shown the pipe to be dished-in at a point where it is in contact with a rigid support. The dished-in area has been examined both visually and with dye penetrant and the results were negative. It has been concluded from this that the loss of hydraulic fluid from the snubber in no way constituted a threat to either the health or safety of the public.

(9) Corrective Action:

Immedf ate actions were taken to replace the broken fitting, refill the cservoir with hydraulic fluid, reorient the snubber, tighten the lock nut, and it was ensured that Loctite is on order. In addition, the Architect Engineer has been directed to perform an evaluation of the deformation to further verify the integrity of the affected pipe; and no report will be submitted on the results of this investigation unless the results indicate possible adverse safety implications .

At a meeting held af ter the incident was reported, the Plant Operations Review Committee reviewed and gave its approval of these actions. As a long-term action they recommended to the Station Superintendent that the snibber seal replacement program be revised to include the use of Loctite on all snubber lock nuts. The Station Superintendent concurred with this recommendation and has taken appropriate steps to ensure its implementation.

(10) Failure Data:

a. Previous Failures:

See Abnormal Occurrence Report A0 50-289/74-14, dated August 28, 1974

b. Equipment Identification:

Brand: Grinnell Cylinder Type: Miller Valve Type: Grinnell Size: 2.5 in Stroke: 5 in Sincerely, A

L R. C ."Irnold Vice President RCA/cas File: 20.1.1/ 7.7.3.5.1 .

cc: J . P . O 'Reilly

}kh -