Abnormal Occurrence 50-289/75-30:on 750827,valve CF-V-2B of Core Flood Tank B Sample Line Isolation Failed to Close Upon Receipt of Engineered Safeguards Actuation Signal.Caused by Valve Binding Against Valve StemML19210A225 |
Person / Time |
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Site: |
Three Mile Island |
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Issue date: |
09/05/1975 |
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From: |
Arnold R METROPOLITAN EDISON CO. |
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To: |
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References |
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GQL-1482, NUDOCS 7910240938 |
Download: ML19210A225 (5) |
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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML19210A1511976-02-12012 February 1976 Abnormal Occurrence 76-7/1P:on 760212,empty Snubber Fluid Reservoir Found at Location DHH-198.Leakage Due to Damaged Seal.Snubber Removed & Replaced ML19322A4301976-02-0505 February 1976 Abnormal Occurrence 76-6/1P on 760204:radiation Leak Detection Sys Out of Svc for 22-h.No Reactor Bldg Atmospheric Samples Taken.Caused by Cover Plate to Monitor Left Open Following Insp.Procedures Reviewed W/Personnel ML19210A1581975-12-26026 December 1975 Abnormal Occurrence 50-289/75-43:on 751218,one of Six Pressure Switches Tripped at Less Conservative Limits than Tech Specs During Channels Surveillance Test.Caused by Calibr Drift in Associated Pressure Switch PS-290 ML19210A1451975-12-19019 December 1975 Abnormal Occurrence 50-289/75-42:on 751210,outside Containment Isolation Valve for Steam Generator Sample Line CA-V5B Failed to Close.Caused by Valve Manual Operator Inadvertently Left Open by Reactor Personnel ML19210A1731975-11-25025 November 1975 Abnormal Occurrence 50-289/75-40:on 751112,stuck Contacts on Diesel Generator 1A Voltage Relays Threatened Function of Engineered Safety Feature.Caused by Pitting of Relay Contact.Relays Checked at Each Startup Pending Design Mods ML19261F1481975-11-24024 November 1975 Abnormal Occurrence 50-289/75-41:on 751114,personnel Failed to Strictly Follow Drain & Blanketing Procedure.Vented Center Control Rod Drive Mechanism Allowed Radioactive Gas Into Reactor Bldg.Personnel Counseled on Proper Procedures ML19210A1831975-11-21021 November 1975 Abnormal Occurrence 50-289/75-39:on 751112,control Rod 4 in Group 7 Dropped Into Core,Resulting in Asymmetrical Rod Signal & Automatic Power Reduction.Caused by Failure of Stator Winding.Stator Winding Replaced & Tested ML19210A1891975-10-31031 October 1975 Abnormal Occurrence 50-289/75-38:on 751021,control Rod Verification Program Not in Compliance W/Tech Specs.Caused by Procedure Misinterpretation.Revised Surveillance Program Will Clearly State Requirement of Individual Rod Movement ML19210A1911975-10-31031 October 1975 Abnormal Occurrence 50-289/75-37:on 751021,blocked Strainer on Outlet to Boric Acid Mixtank Decreased Flow Rate.Plant Shutdown Followed to Replace Strainer.Improper Design Allowing for One Strainer W/No Bypass Caused Blockage ML19210A2021975-10-29029 October 1975 Abnormal Occurrence 50-289/75-36:on 751019,auxiliary Operator Failed to Obtain Radiation Work Permit & Carry Monitoring Device.Caused by Improper Administrative Procedures ML19210A1971975-10-21021 October 1975 Abnormal Occurrence 75-37:on 751021,blocked Strainer on Outlet of Boric Acid Mixtank Decreased Flow Rate.Plant Shutdown Followed to Replace Strainer.Plant Returned to Svc in 15 Minutes ML19210A2151975-10-20020 October 1975 Abnormal Occurrence 50-289/75-35:on 751010,improper Mix of Boric Acid Crystals Caused Blockage in Mix Tank.Crystals Settling to Bottom of Tank Clogged Line to Reclaimed Boric Acid Storage Tank.Mixture Mod Should Correct Failures ML19210A2211975-10-10010 October 1975 Abnormal Occurrence 75-37:on 751010,during Transfer of Boric Acid from Storage Tank to Reclaim Tank,Blockage Noticed in Outlet Line.Caused by Boric Acid Crystals Settling to Drain Due to Improper Mixture ML19210A2241975-10-0808 October 1975 Abnormal Occurrence 50-289/75-34:on 750928,inoperative Hydraulic Shock Suppressor Threatened Function of Engineered Safety Feature.Low Fluid Level in Snubber Caused Failure. All Other Snubbers Checked Satisfactorily ML19322A4371975-09-30030 September 1975 Abnormal Occurrence 75-34 Re Disconnected Hydraulic Snubber within Reactor Bldg Secondary Shield.Investigation of Circumstances Incomplete.Snubber Replaced During Ongoing Seal Replacement Program ML19210A2461975-09-26026 September 1975 Abnormal Occurrence 50-289/75-31:on 750917,core Flood Tank Water Level Below Tech Specs Requirements.Caused by Incorrect Reading on Lower Reading Channel CF2-LT3.Channel Will Now Be Monitored & Personnel Informed on Procedures ML19210A2411975-09-26026 September 1975 Abnormal Occurrence 50-289/75-33:on 750917,de-ice Makeup Valve NR-V-4A Failed in Open Position.Failure Caused by High Resistance Contact in Closing Control Circuit Not Fully Energizing.All Control Contacts to Be Checked & Cleaned ML19210A2391975-09-26026 September 1975 Abnormal Occurrence 50-289/75-32:on 750918,incorrect Open Position of Air Supply Valves PP-V-47 & 179 Could Have Prevented Proper Functioning of Door Seals in Event of Emergency Safeguards Actuation.Jj Colitz Encl ML19210A2451975-09-19019 September 1975 Abnormal Occurrence 75-33 Re Failure of de-ice Makeup Valve NR-V-4A to Close Using Control Room Remote Pushbutton.Caused by High Resistance Contact in Closing Control Circuit. Contact Cleaned,Tested & Returned to Svc ML19322A4361975-09-18018 September 1975 Abnormal Occurrence 75-31 Re Low Borated Water Level in Core Flood Tank B.Caused by Improper Level Channel Transmitter LT3 Readout.Transmitter Adjusted ML19210A1791975-09-0505 September 1975 Abnormal Occurrence 50-289/75-29:on 750827,reactor Bldg Purge Supply Valve AH-V-1D Failed to Close Prior to Engineered Safeguards Test.Caused by Corroded Robotarm Actuator.Robotarm Actuator Lubricated ML19210A2251975-09-0505 September 1975 Abnormal Occurrence 50-289/75-30:on 750827,valve CF-V-2B of Core Flood Tank B Sample Line Isolation Failed to Close Upon Receipt of Engineered Safeguards Actuation Signal.Caused by Valve Binding Against Valve Stem ML19210A1811975-09-0202 September 1975 Abnormal Occurrence 50-289/75-28:on 750823,MS-V-13A Valve Turbine Drive Emergency Feed Pump Failed to Remain Open. Caused by Control Circuit Pressure Switch Failure,Due Possibly to High Ambient Temp ML19210A1871975-08-29029 August 1975 Abnormal Occurrence 50-289/25-27:on 750821,crack & Leak Found in Auxiliary Makeup Pump a Suction Vent.Caused by Fatigue Due to Vibration.Cracks Repaired & Hydrostatically Tested.Failed Pipe Section Replaced ML19322A4351975-08-28028 August 1975 Abnormal Occurrence 75-30:on 750827,core Flood Tank B Sample Line Isolation Valve CF-V2B Failed to Close Following Engineered Safeguards Signal.Valve Manually Closed Using Handwheel ML19210A1861975-08-27027 August 1975 Abnormal Occurrence 75-29:on 750827,reactor Bldg Supply Valve AH-V-1D Failed to Fully Close.Investigation Into Cause Underway ML19210A1841975-08-23023 August 1975 Abnormal Occurrence 75-28:on 750820,during Test of Turbine Drive Emergency Feed Pump,Associated Valve Failed to Remain Open.Caused by Failed Pressure Switch ML19210A1901975-08-21021 August 1975 Abnormal Occurrence 75-27 on 750821:leaks Found in Socket Weld Joint at Makeup Pump a & Suction Line Connection W/Pump Suction Header.Cause of Problem Under Investigation ML19210A1941975-08-0101 August 1975 Abnormal Occurrence 50-289/75-26:on 750724,high Reactor Coolant Pressure Trip Set Points Less Conservative than Tech Specs.Caused by Calibr Drift.Specs Will Be Changed to Account for Instrument Error ML19210A1951975-07-31031 July 1975 Abnormal Occurrence 50-289/75-25:on 750721,failure of Diesel Generator a Frequency Relay to Actuate,Threatening Nonperformance of Diesel Generator.Cause Presently Unknown ML19210A2001975-07-25025 July 1975 Abnormal Occurrence 50-289/75-23:on 750716,auxiliary Relay to Generator 1B Failed to Energize on Demand.Caused by Mfg Defect.Failed Relay Replaced & Remaining Relays Inspected ML19210A2071975-07-25025 July 1975 Abnormal Occurrence 50-289/75-24:on 750716,during Removal of River Water Pump NR-P1B from Svc,Discharge Valve Failed to Close.Caused by Open Phase on Winding Due to Severe Heat Resulting in Single Phasing of Other Windings ML19210A1991975-07-22022 July 1975 Abnormal Occurrence 75-25:on 750722,three Frequency Relays to Steam Generator a Found in Dropped Out State.Relays Replaced & Returned to Svc.Cause of Failure Yet to Be Determined ML19210A2171975-07-21021 July 1975 Abnormal Occurrence 50-289/75-22:on 750711,leaks Found in Socket Weld Joints of Makeup Pump Suction Vent Line MU-PIA Leading to Valve MU-V156A.Caused by Improper Spacing Between Moving Anchor & First Pipe Restraint ML19210A2051975-07-18018 July 1975 Abnormal Occurrence 75-23:on 750716,one of Three Auxiliary Relays of Diesel Generator 1B Breaker G11-02 Failed. Remaining Relays Tested Satisfactorily.Cause of Failure Under Investigation ML19210A2121975-07-18018 July 1975 Abnormal Occurrence 75-24:on 750716,river Water Pump Discharge Valve Failed Due to Low Valve Motor Winding Resistance & Winding Motor Overheating ML19210A2221975-07-11011 July 1975 Abnormal Occurrence 75-22:on 750711,leaks Found in Socket Weld Joints of Makeup Pump a Suction Line Vent.Caused by Pump Vibration ML19210A2311975-07-0303 July 1975 Abnormal Occurrence 50-289/75-21:on 750625,coolant Temp Trip Bistable Channel C Failed to Trip During Test of Reactor Protection Sys.Caused by Defective Printed Circuit Board Solder Joint in Signal Converter ML19210A2371975-06-27027 June 1975 Abnormal Occurrence 50-289/75-19:on 750618,variable Low Reactor Coolant Sys Pressure Trip Setpoints Less Conservative than Tech Specs.Caused by Channel C Trip Setpoint Out of Calibr Due to Instrument Drift ML19210A2301975-06-27027 June 1975 Abnormal Occurrence 75-03:on 750626,noble Gas Released to Auxiliary Bldg.Probable Cause:Evaporator Malfunction While Filling Makeup Tank or Coolant Bleed Tank.No Tech Specs Exceeded ML19210A1621975-06-27027 June 1975 Abnormal Occurrence 50-289/75-18:on 750615,QA Documentation from Vendor Found Inadequate for Repaired Decay Heat River Water Pump Motor Shaft.Caused by Lack of Administrative Controls ML19210A2351975-06-25025 June 1975 Abnormal Occurrence 75-21:on 750625,reactor Protection Sys Channel C Failed During Surveillance Test.Caused by Coolant Temp Trip Bistable Failure to Trip Due to Component Failure in Signal Converter ML19210A1721975-06-25025 June 1975 Abnormal Occurrence 50-289/75-17:on 750615,reactor Bldg Purge Isolation Valve Failed Local Leak Rate Test.Caused by Improper Valve Adjustment Procedures & Matl Defects Not Allowing Long Term Retention of Adjustment ML19308A5371975-06-23023 June 1975 Abnormal Occurrence 75-20:on 750622,while Returning to Full Power Operation After Forced Power Reduction,Reactor Power Increased Above Power Level Cutoff Before Xenon Reactivity Approached Stability.Procedures Under Review ML19210A2431975-06-19019 June 1975 Abnormal Occurrence 75-19:on 750618,less Conservative Variable Low Reactor Coolant Sys Pressure Trip Setpoint for One Channel of Reactor Protection Sys Violated Tech Specs. Caused by Instrument Drift for Channel C Setpoint Calibr ML19210A1661975-06-17017 June 1975 Abnormal Occurrence 75-18:on 750615,repaired Motor Shaft to Decay Heat River Water Pump Not Returned W/Proper QA Documentation.Caused by Lack of Administrative Control ML19210A1751975-06-17017 June 1975 Abnormal Occurrence 75-17:on 750615,during Test of Reactor Bldg Purge Isolation Valve Local Leak Rate Test,Two Exhaust Valves Would Not Pressurize to Required Test Pressure.Caused by Valve AH-V1A Failing to Fully Close ML19210A1771975-06-16016 June 1975 Abnormal Occurrence 50-289/75-16:on 750605,variable Low Reactor Coolant Sys Pressure Trip Setpoints Less Conservative than Tech Specs.Specific Cause Not Established. Setpoints Will Be Checked to Assure Proper Calibr ML19291B5291975-06-13013 June 1975 Abnormal Occurrence 50-289/75-15:on 750605,pressure Transmitter Trip Setpoint of Reactor Protection Sys Channel B Tested Out of Calibr.Caused by Trip Setpoint Calibr Drift ML19210A1801975-06-0606 June 1975 Abnormal Occurrence 75-16:improper Trip Setpoints on Variable Low Reactor Coolant Sys Pressure Sys Violated Tech Specs 1976-02-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1001999-10-14014 October 1999 Errata to Safety Evaluation Supporting Amend 215 to FOL DPR-50.Credit Given for Delay in ECCS Leakage ML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20216F9231999-09-22022 September 1999 Safety Evaluation Supporting Amend 216 to License DPR-50 05000289/LER-1999-010, :on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With1999-09-21021 September 1999
- on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With
ML20211H5111999-08-31031 August 1999 Non-proprietary Rev 1 to MPR-1820(NP), TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20211E8731999-08-24024 August 1999 Safety Evaluation Supporting Amend 215 to License DPR-50 ML20211B1931999-08-19019 August 1999 Safety Evaluation Supporting Amend 214 to License DPR-50 ML20210R4791999-08-13013 August 1999 Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2 ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With 05000289/LER-1999-009, :on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced1999-07-22022 July 1999
- on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced
ML20210K7651999-07-0909 July 1999 Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp Loca ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20212H9101999-06-21021 June 1999 Safety Evaluation Supporting Amend 212 to License DPR-50 05000289/LER-1999-007, :on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed1999-06-18018 June 1999
- on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed
ML20195J9401999-06-15015 June 1999 Safety Evaluation Supporting Amend 211 to License DPR-50 05000289/LER-1999-005, :on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With1999-06-14014 June 1999
- on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With
ML20195H0751999-06-0808 June 1999 Drill 9904, 1999 Biennial Exercise for Three Mile Island ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20209G0351999-05-31031 May 1999 TER on Review of TMI-1 IPEEE Submittal on High Winds,Floods & Other External Events (Hfo) ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 05000289/LER-1999-003-01, :on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open1999-05-0707 May 1999
- on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open
ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20205Q6111999-04-15015 April 1999 Safety Evaluation Supporting Amend 210 to License DPR-50 ML20205Q5981999-04-13013 April 1999 Safety Evaluation Supporting Amend 209 to License DPR-50 ML20206P2841999-04-12012 April 1999 SER Approving Transfer of License for Tmi,Unit 1,held by Gpu Nuclear,Inc to Amergen Energy Co,Llc & Conforming Amend, Per 10CFR50.80 & 50.90 ML20209G0071999-03-31031 March 1999 Submittal-Only Screening Review of Three Mile Island,Unit 1 Individual Plant Exam for External Events (Seismic Portion) ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With 05000289/LER-1999-002, :on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With1999-03-14014 March 1999
- on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With
ML20210C0161999-03-0101 March 1999 Forwards Corrected Pp 3 of SECY-98-252.Correction Makes Changes to Footnote 3 as Directed by SRM on SECY-98-246 ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With 05000289/LER-1999-001-01, :on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys1999-02-19019 February 1999
- on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys
ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits 05000289/LER-1998-014-01, :on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With1999-01-11011 January 1999
- on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With
ML20196G4661998-12-31031 December 1998 British Energy Annual Rept & Accounts 1997/98. Prospectus of British Energy Share Offer Encl ML20207A9291998-12-31031 December 1998 1998 Annual Rept for TMI-1 & TMI-2 ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20203G1211998-10-30030 October 1998 Informs Commission About Staff Preliminary Views Concerning Whether Proposed Purchase of TMI-1,by Amergen,Inc,Would Cause Commission to Know or Have Reason to Believe That License for TMI-1 Would Be Controlled by Foreign Govt 05000289/LER-1998-013, :on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance1998-10-15015 October 1998
- on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance
ML20155E7511998-10-15015 October 1998 Rev 1 to Form NIS-1 Owners Data Rept for Isi,Rept on 1997 Outage 12R EC Exams of TMI-1 OTSG Tubing 05000289/LER-1998-010-01, :on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued1998-10-0909 October 1998
- on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued
ML20154L5541998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for TMI Unit 1.With 05000289/LER-1998-011, :on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge1998-09-23023 September 1998
- on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge
1999-09-30
[Table view] |
Text
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INCIDEfr NRC DISTRIBUTION FOR PART 50 DOCKE " MATERI AL (TEMPORARY FORM)
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A/O 4 75-30, en 5-27-75, Ccncerning Failure of Core Flood Tank "3" Sanple line Isolatica Valve (CF-7-23) to close on an Engineered Safeguards x
Actuation Signal....
(1 Copy Enclosure Feceived)
PLANT NAME:
Three Mle Island FOR ACTION /INFORMATION SA3 0-12-75 BUTLER (L)
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Docket No. 50-289 Cperating License No. DPR-50
Dear Sir:
In accordance with the Technical Specifications of cu-Three Mile Island Nuclear Station Unit 1 (3I-1), we are reperting the folleving abncr=al occurrence.
/
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5 (1) Report Number: A0 50-209/75-30
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Identification of Occurrence:
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Title:
Failure of Core Flecd Tank "B" Sample line Iselaticn Valve (CF-7-23) to close on an Engineered Safeguards Actuation Signal Type:
An abncr=al occurrence as defined by the Technical Specificaticns, paragraph 1.8d, in that fail re of CF-7-23 to close constituted a failure of one ec=penent of an engineered safety feature that threatened to cause that feature to ce incapable of performing its intended function.
(5) Canditiens Pricr to Occurrence:
Power: Core:
99",
Elect.. 326 Mwe (Grces)
F RC Flev:
139x10' lb/hr 306 259 RC Fress:
2155 psig RC temp:
580*T
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.TO: Directcr Division of eeacter Licensing U. S..'iuclear Eegulatcry Cc==issicn FRZR level:
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r (6) Cescription of Cecurrence:
At 1130 hcurs en August 27, 1975 while perfer=ing the Reactor Building Cooling and Isolation Cc=penent and Lcgic Surve.llance Test, CF-V-23 (Cere Flced Tank "3" Sample Line Isolation Valve) failed te close upcn receipt of an Engineered Safeguards actuation signal.
I:=ediately pricr to this failure, the valve operated satisfactcrily upon receipt of two separate auto Engineered Safeguards test actuaticn signals.
An attempt was made to close CF-V-23 using the re=cte pushbutton, but the valve failed to close.
CF-V-23 was then clcsed locally by use of its handwheel, after which the valve cycled prcperly using the re=cte pushbutton.
The redundant isolaticn valve for the sa=ple line CF-V-23 was cycled to verify its operability.
CF-V-2B was manually cycled and the valve stem lubricated. An inspection was made of the valve's auxiliary contact b1ceks to deternine if they were binding the opening and closing contacters in any way.
(7) Designatien cf Apparent Cause of cecurrence:
Initial investigation indicated CF-V-23 failed to close as a result of the valve packing binding against the valve stem, causing it to stcp travel by cpening the clcsing terque switch prematurely.
Further troubleshcoting revealed that CF-V-23 may have failed to close due to the closing torque switch apparently physically being held cpen intermittently by splice insulating caps asscciated with viring located next to the switch. The viring adjacent to the switch provides 120 VAC to the valve limit switch cc=partment heater which is used to re=cve moisture. Excess vire asscciated with the heater was coiled in close prcximity to the valve cicsing torque switch contacts, hence the interference of the wire insulating caps with the switch contacts may have in turn caused the valve not to fully close. It is postulated that either cne or both of the above proble=s caused the closing torque switch contacts to open early, preventing CF-V-23 frc= cicsing.
g76 200
' 'TO : Directcr Divisicn of Eeacter Licensing U. S. Nuclear Regulatcry Cennissicn
- (8) Analysis of Occurrence:
It is believed that the failure of CF-7-23 did not represent a threat to the health and safety of the public in that:
a.
Cne containment isolatien valve is sufficient to isolate the Core Flood Tank "3" Sample Line in the event of a less of ecolant accident.
b.
The redundant centain=ent isolation valve for the Cere Flced Tank "3" Sa=ple Line was cperable.
c.
The redundant isolatien valve was closed at the ti=e of the occurrence.
(9) Corrective Acticns:
In additicn to the corrective actions =entioned abcVe 1cng term corrective actions were:
CF-V-23's torque switch settings have been increased, yet a.
are within acceptable linits, and any wires that '.culd possibly interfere with proper torque switch contact operation have been relecated.
b.
The valve CF-7-23 vill be repacked to further reduce the possibility of any abncr=al binding.
The Plant Opersticus Review Cenmittee and the Station Superintendent have reviewed and approved the above listed ccrrective acticns and have taken steps to ensure cc=pletion of the yet to be ec=pleted long tern corrective actions.
(10) Failure Data:
Valve Cperatcr:
Limitorque SME-000 Valve:
Ecekvell 362h(F316)JM Type-Globe 1,
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'"C : Director Division of Reactcr Licensing U. S. Nuclear Regulatory Cc=issien
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