ML18005A229

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LER 87-063-00:on 871108,plant Tripped Due to Loss of Main Feedwater.Caused by Mispositioned Condensate Recirculation Valve Due to Personnel Error.Operating Procedure Revised to Include Lessons from Event & Crews briefed.W/871207 Ltr
ML18005A229
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 12/07/1987
From: Schwabenbauer, Watson R
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
HO-870563-(O), LER-87-063, NUDOCS 8712090208
Download: ML18005A229 (5)


Text

,,A~ CELERY'J'ED 'DI&'I'RIBUTION DEMONSTRATION SYSTEM 0 ~

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8712090208 DOC.DATE: 87/12/07 NOTARIZED:'NO DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH. NAME AUTHOR AFFILIATION SCHWABENBAUER Carolina Power & Light Co.

WATSON,R.A. Carolina Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 87-063-00:on 871108,plant feedwater.

trip due to loss of main W/8 DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ENCL TITLE: 50.73 Licensees Event Report (LER), Incident Rpt, etc.

W SIZE-NOTES:Application for permit renewal filed. 05000400 g RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-1 LA 1 1 PD2-1 PD 1 1 A BUCKLEY,B 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 AEOD/DOA 1 1 AEOD/DSP/NAS 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 ARM/DCTS/DAB 1 1 DEDRO 1 1 NRR/DE ST/ADS 1 0 NRR/DE ST/CEB 1 1 NRR/DEST/ELB 1 1 NRR/DEST/I CS B 1 1 NRR/DEST/MEB 1 1 NRR/DEST/MTB 1 1 NRR/DEST/PS B 1 1 NRR/DEST/RS B 1 1 NRR/DEST/SGB 1 1 NRR/DLPQ/HFB 1 1 NRR/DLPQ/QAB 1 1 NRR/DOEA/EAB 1 1 NRR/DREP/RAB 1 1 NRR/DREP/RPB 2 2 PRR- S SIB 1 1 NRR/PMAS/I LRB 1 1 l G ILE 02 1 1 RES DEPY GI 1 1 ORD,J 1 1 RES/DE/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: EG&G GROH,M 5 5 FORD BLDG HOY i A 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC HARRIS,J 1 1 NSIC MAYS,G 1 1 S

j TOTAL NUMBER OF COPIES REQUIRED: LTTR 46 ENCL 45

NRC Form 356 U.S. NUCLEAR REOULATORY COMMISSION (94)3)

APPROVED OMB NO. 31604104 LICENSEE EVENT REPORT (LER) EXPIRES: 8/31/88 FACILITYNAME (1) DOCKET NUMBER l2) PACiE 31 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 PLANT TRIP DUE TO THE LOSS OF MAIN FEEDWATER CAUSED BY A MISPOSITIONED CONDENSATE 050004001'OF 03 RECIRCULATION VALVE EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)

EEQUEIITIAL MONTH OAY YEAR YEAR 5PÃ3 NUMBER N. NIIMSSR MONTH DAY YEAR FACILITYNAMES DOCK ET NUMB E R(S) 0 5 0 0 0 11 08 8 7 8 7 6 3 001 20 7 87 0 5 0 0 0 OPERATINO THIS REPORT IS SUBMITTED PURSUANT TO THE REOUIREMENTS OF 10 CFR (): (Check onr or morr of the foilovfingf ill)

MODE (9) 20A06(e) X 60 73(s)l2)(iv) 73.71(h)

POWER 20.405( ~ l(1) (I) EOM(c) (I) 50.73(el(2)(vl 73.71(cl LEVEL 20.405 ( ~ ) (1) (8) EOM(c)(2) 50.73(a) (2) (rg) OTHER fSueclfy In Abstract hrrow coif In Test, NRC Ferns 20.406(e l(llliii) 50.73(e) (2)(I) 60.73(e)(2)(riii) (Al 366AJ y 20AOS le) (I ) (Iv) 50.73(a l(21(8) 50.73(e) (2) I viiil(8) 20.405 (e) l I I (vl 50.73(el(2)(iii) S0.73(el(2)(al LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMBER R. SCHWABENBAUER REGULATORY COMPLIANCE TECHNICIAN AREA CODE CAUSE SYSTEM COMPONENT MANUFAC.

TURER EPORTABLE

v COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 9 c mr r

CAUSE SYSTEM COMPONENT l\3)

MANUFAC.

TURER EPORTABLE NPRDS vtN'O

.r .

SUPPLEMENTAL REPORT EXPECTED (14)

EXPECTED MONTH 5%& DAY YEAR SU 8 M I SS ION YES flfyer, complrte EXPECTED SVSMISSION OATH NO DATE (15)

ABSTRACT fLImft to 1400 spaces, I 6, epproalmetrry fiftern alnrrerpecr typrwrfrten lined l16)

The plant was operating in Mode 1, Power Operation, at 22 percent reactor power on November 8, 1987. The plant was in the start-up process following a scheduled outage and was preparing to increase power from 100 MWe to 150 MWe with only the 'lA'eedwater train in service. 1A Condensate Pump tripped on low discharge pressure which caused 1A Condensate Booster Pump and 1A Main Feedwater Pump to trip, which resulted in a total loss of Main Feedwater. The reactor and turbine were then manually tripp'ed at 1625 hours0.0188 days <br />0.451 hours <br />0.00269 weeks <br />6.183125e-4 months <br />. The Hain Steam Isolation Valves were shut in order to limit pl.ant cool, down and the Auxiliary Feedwater System actuated to restore Steam Generator water levels. All plant systems responded as required.

The immediate cause of the event was the condensate recirculation valve was in the "OPEN" position rather than "MODULATE" position as required by normal O plant operation. This caused the Condensate Pump and Condensate Booster Pump OR to be operating at near run out condition and eventually tripped the ~

OOR Condensate Pump on low discharge pressure. The root cause of the event was r'I o wO personnel error as plant operators were not fully aware of all plant W(A COO conditions. (i.e., the recirculation valve being in the open position.)

co& Corrective actions are Operating Procedure (OP)-134, Condensate System, has OCJ been revised incorporating lessons of this event, and operating shifts were C'2 O OR briefed on the causes and consequences of this event, and Post"Turnover 0 <<3:

briefings are being conducted to ensure understanding of plant conditions for C'a mCZ the operating crew.

Nu CO@ CO This event is being reported in accordance with IOCFR50.73(ai(2)(ivl as an Engineered Sateguards System Feature and Reactor Protection System Actuation. /(

NRC Form 366 ror.nv I

NRC Form 348A U.S. NUCLEAR REOULATORY COMMISSION (083 l LICENSEE EVENT REPORT ILERI TEXT CONTINUATION APPROVED OMS NO. 3(50&(04 EXPIRES: 8/31/88 FACILITYNAME III DOCKET NUMSER lll LER NUMSER (Sl IIAOE (3) yEAR 58r $ 4QUENTIAL oI rrevrercN NUM44rr ..8 NvM err SHEARON HARRIS NUCLEAR POWER PLANT ~

UNIT 1 TEXT /I/more 4/reoe 14 err/'rrrrf, voe NIN/orNIA/RC %%drre 38$ AS/ (171 o s o o o4 00 87 06 3 0 0 02>> 0 3 DESCRIPTION The plant was operating in Mode 1, Power Operation, at 22 percent reactor power on November 8, 1987. The plant was in the start-up process following a scheduled outage. The Turbine Generator (EIIS:TA) output was to be increased from 100 MWe to 150 MWe at a rate of 3MW/min. Due to the power range at this time, only the '1A'ain Feedwater (EIIS:SJ) train was in service.

As the load increase was started, the operator noted that the lA Condensate Booster Pump (CBP)(EIIS:SD)'Controller was in the maximum demand posit'.on. 1A Main Feedwater Pump (MFP)(EIIS:SJ) suction pressure and 1A CBP discharge pressure were approximately 430 psig'1A Condensate Pump (CP)(EIIS:SD) discharge pressure was approximately 200 psig. It was noted that the Condensate Recirculation Valve, 1CE-293, was in the "OPEN" position rather than the "MODULATE" (MODU) position as required by normal plant operation. In effect, the 1A CBP and the 1A CP were operating at near pump "run out" condition. The Shift Foreman determined that the safest way to avoid a flow disturbance', which would cause a CP or CBP trip, would be to slowly close the manual recirculation path isolation valve, 1CE-294. An operator was dispatched to do this; however, there was no attempt to halt the turbine power increase process.

As turbine power approached 10S MWe, before any possible operator action on the manual recirculation path isolation valve could be made, 1A CP discharge pressure fell below the trip setpoint of 195 psig. After the S second trip delay, the 1A CP tiipped and initiated the trip of the 1A CBP and 1A MFP resulting in a total loss of Main Feedwater. Since feedwater flow could not be immediately restored, the reactor and the turbine were manually tripped at 1625 hours0.0188 days <br />0.451 hours <br />0.00269 weeks <br />6.183125e-4 months <br />. The Main Steam Isolation Valves (EIIS:SB) were shut in order to limit plant cooldown and Steam Generator (EIIS:TB) water levels were restored with the automatic actuation of the Auxiliary Feedwater System (AFW)

(EIIS:BA). All plant systems responded as required and the plant was stabilized in Mode 3, Hot Standby.

CAUSE:

The immediate cause of the event was that Condensate Recirculation Valve 1CE-293, was in the open position rather than the moduLate position as required for normal plant operation. This resulted in the lA CP and 1A CBP to be operating at near run out condition and eventually tripping 1A CP on Low discharge pressure.

The root cause of the event was personnel error as plant operators were not fully aware of all pl.ant conditions (i.e., the recirculation vaLve being in the open position). Shift turnover notes did indicate that valve 1CE-293 was N/IC FD/IM 344*

(043( e U.S.OPO:108~824 538/455

NRC Potm 264A U.S. NUCLEAR REGULATORY COMMISSION (94L) I LlCENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMB NO. 2150&104 EXPIRES: 8/21/88 PACILI'TY NAME ill OOCKET NUMBER 12) LER NUMBER 16) PAGE IS)

YEAR SEOVSNTIAL R>5 II4 V IS IO N SHEARON HARRIS NUCLEAR POWER PLANT NVMSSII NVM SA UNIT 1 o s o o o4 00 8. 70 3 0 0 3 oF0 3 TEXT //I IINrp Spree /I Irovked, vrr 4/4/SAI/NRC Pr/m 6//$ 4'4/ 117)

CAUSE: (continued) in an abnormal condition. The position resulted from secondary plant chemistry operations conducted earlier in the week. The plant had been in a long path recirculation mode for the purpose of establishing secondary plant chemistry control prior to plant start-up. In this mode, Operation Procedure (OP)-134, Condensate System, permits placing valve 1CE-293, in the "OPEN" position in order to increase recirculation flow. The procedure did not specifically address returning the valve switch to the "MODULATE" position, which is the assumed position for normal pl.ant operation, when returning to the normal or short path recirculation moce.

ANALYSIS:

This event is being reported in accordance with 10CFR50.73(a)(2)(iv) as an Engineered Safeguards System Feature and Reactor Protection System Actuation.

There were no safety consequences as a result of this event; although operation of a safety system was challenged (AFW). The AFW system started as required upon loss of Main Feedwater to maintain vater levels in the Steam

'enerators.

Other events reported where the loss of Main Feedwater resulted, in a plant trip vere reported in LERs.'7-005-00, 87-008-00, 87-013-00, 87-017-00,87-018"00, 87-019-00, 87-024-00, 87-025-00, 87-028-00, 87"031-00, 87-037-00.

CORRECTIVE ACTIONS/ACTIONS TO PREVENT RECURRENCE:

1. The Shift Turnover process has been enhanced. Previously, the turnover process included a briefing by the off going Shift Foreman and a one-on-one turnover of each position. Plant direction has been issued through a Night Order to require a Post-Turnover briefing by the Balance of Plant (BOP), Reactor Operator (RO), Senior Control. Operator (SCO),

each Auxiliary Operator (AO), and the Shift Foreman (SF) to ensure the operating crew has a ful.l understanding of plant conditions.

Operations Management Manual (OMM)-001, Operations-Conduct of Operations, is being revised to incorporate this action.

2. Operating Procedure (OP)-134, Condensate System, has been revised incorporating the lessons of this event.
3. Following the event operating shifts were briefed on the causes and consequences of this Ievent.

NRC SORM SSSA 19421

  • U.S.GPO:1986.0 624 558/455

Carolina Power 8 Light Company HARRIS NUCLEAR PROJECT P.O. Box 165 New Hill, NC 27562 DEC 0 7

~98'ile

.Number'SHF/10-13510C Letter Number.'HO-870563 (0)

U.S. Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 87-063-00 Gentlemen'.

In accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted. This report fulfills the requirement for a written report within thirty (30) days of a reportable occurrence and is in accordance with the format set forth in NUREG-1022, September, 1983.

Very truly yours, SF/W~~>

R. A. Watson Vice President Harris Nuclear Project RAW'lkd Enclosure cc.'Dr. J. Nelson Grace (NRC RII)

Mr. B. Buckley (NRR)

Mr: G. Maxwell (NRC SHNPP)

MEM/LER-87-063/1/OS1