ML17338B076

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Responds to NRC 790705 Ltr Re Violations Noted in IE Insp Repts 50-250/79-19 & 50-251/79-19.Corrective Actions: Existing Tech Spec Procedures Re Plastic Sleeve Implemented on 790731 & Operating Procedure 5163.1 Being Revised
ML17338B076
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 08/10/1979
From: Robert E. Uhrig
FLORIDA POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17338B075 List:
References
L-79-223, NUDOCS 7909200362
Download: ML17338B076 (6)


Text

I'. 80>i 520>00, MIAMl, F L 334> '2 Au@us>t 10, 1979 1.-79-223 Mr. James P. O'Beilly, Director, Region iX Of fice of Inspection and Enforcement U. S. Nuclear Regulatory Comm'ssion 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303

Dear Mr. O'Re'lly:

Re: RII:RVL 50-250/79-19 50-251 79-19 Florida Power h Light Company has reviewed the subj~'.ct inspection report and a response is attached.

There is no proprietary information in the repor-,.

Very truly yours, bert . U rig Vice President Advanced Systems $, Technology RE U/MAS/cph Attachment cc: Robert Low< ..'tein, Esquire P(

V909$ 00 3 6$

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ATTAC!!i~AN'1'(':

RI I: RVL 50-250/79-:9 50-251/79-;'>

Findin, A As required by .'=.~c".ion 6. 8.1 o? tl:<. "Tc <:hnica?..'.::><<-.:

procedure.: and admini.';rativ<~,'~'cies t?~~',,-.Is"'o)

<'i~.~'tm.:.'ritten the requirement,-. and recomm&naati('ns t>f S-,c ion ". I,,;"(~,j. l .)f ANSI N18. 7-1972 a>>d Appendi x "t>" of li,.NR(: ?)egula~ <t,': l.'..<]<. '?

shall be impl<sm>>,.cd.

Contrary to the al'<>ve, t,he fo~ lowing 'r'.<. exam;.-'.<".- r".?:r sent.

failure to impl=m< nt existing prcceduxo::

1) No safety evaluation was performed as require<! ?t, AP 190.15,

'Pla'nt Changes and Modi ficati ons" for the p] <<s',-. i<< I cove ."

placed over the 8 Monitor Tank over..".?ow line it.. '::3 ting i>>

siphon ef feet that, led to water of June 11, 1979.

'e unpla>>ned releas<'p,ideograph f con tamina tet

2) Recirculation of Monitor Tanks without use of 8.4 of OP 5163.1, "KDS-ctaste Cond<.nsate Tank, Polishing Demineralize:

and Monitor Tank Operation", whi ch addresses t?.i s evolution.

3) Failure to log the unplann<:-<! liauid release on flu>>c: 31, i 979, and the flu>d transfer evolution 'aking plac>> ?t:.io-release in th<. Nuclear Op<'gator's ! og bool:, s." r~'!>>irked b; paragraph 8. 4. 2. 3 of A 103. 2, "?)ut.ic:s and R~.s:.onsibiliti<:s of Operators on Shift an<'! Mainteranc- of Op<erat in.; !.:.gs an<!

Records".

Res~see The plastic sleev was remove<! from the < v<.rflo<< .'.~ <= before t.l~e end of the inspection.

To prevent recu -rence, the Plant !!a>>age has str<>nc!,y <:mphasi importance of verbatim procedure cori.-pliance i >> s; letter t<i

.c<'he plant supervisor; personnel. The lett<.r reitera: ..'ha" every supervisor 's responsibi'.'y to a sure tha",i:; uersonn<.!

it is apply verbatim -ompliance to their p< rfurma>>cc o ?t c>< edures.

Compliance was ac.'sieved on July 31, l979.

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Fin~di i B As required by l~ection 6. 8. 1 of t.he "Tecffnical Sp~:c i f c a f 2. 0I l s 3.

written procedure" and admi nis Lrative r)ol icies tha t. pI ~Q Q or ( 4 (.Q(l J

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the requirements and recomn.endations of Section an(: 5. ] <)f ANSI N18.7-1972 <<nd Appendix "A" of USNf(C Regula'<))i 4ulde 1. 33 shall be established.

Contrary to the aboveI no writ"Qn proc&< ure has j)co~ <<n, ablj shed for use in tran.;for "ing fl uid from o>>~ m ni to> t u,f. to <<not'h('l .

ROSPOll<B Operating Procedure 5163.1 (baste Disposal System ii<~ste Condensate Tanks, Polishing Demineralizer and Moni tor Tank 0:>e>'ation) w' l be revised to inc]ude instruction". related to tran~ <': rFing fluid f r".>m one monitor tank to another. The revision will. )-<::cvi ewer'y the Plant Nuclear Safety Comms ttee by S< ptembe.", 2,', ]979, at whicn time compliance wil.l have been achie.c.~".:.

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