ML103020448

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IR 05000327-10-004 & 05000328-10-004, on 07/01/2010 - 09/30/2010, Sequoyah Nuclear Plant, Units 1 and 2, Heat Sink Performance, Identification and Resolution of Problems, and Event Followup
ML103020448
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 10/29/2010
From: Eugene Guthrie
Reactor Projects Region 2 Branch 6
To: Krich R
Tennessee Valley Authority
References
IR-10-004
Download: ML103020448 (33)


See also: IR 05000327/2010004

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

October 29, 2010

Mr. R. M. Krich

Vice President, Nuclear Licensing

Tennessee Valley Authority

3R Lookout Place

1101 Market Street

Chattanooga, TN 37402-2801

SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT

05000327/2010004, 05000328/2010004

Dear Mr. Krich:

On September 30, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Sequoyah Nuclear Plant, Units 1 and 2. The enclosed inspection report

documents the inspection results discussed on October 7, 2010 with Mr. C. Church and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents three NRC-identified findings of very low safety significance (Green), all

of which involved violations of NRC requirements. Additionally, a licensee-identified violation

which was determined to be of very low safety significance is listed in this report. However,

because of the very low safety significance and because they are entered into your corrective

action program, the NRC is treating these findings as non-cited violations (NCVs) consistent

with Section 2.3.2 of the NRC Enforcement Policy. If you contest any NCV in this report, you

should provide a response within 30 days of the date of this inspection report, with the basis for

your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk,

Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director,

Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-

0001; and the NRC Resident Inspector at Sequoyah Nuclear Plant.

In addition, if you disagree with the characterization of any finding in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the

Sequoyah Nuclear Plant. The information you provide will be considered in accordance with

Inspection Manual Chapter 0305.

TVA 2

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Eugene F. Guthrie, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Docket Nos.: 50-327, 50-328,72-034

License Nos: DPR-77, DPR-79,

Enclosure: Inspection Report 05000327/2010004, 05000328/2010004

w/Attachment: Supplemental Information

cc w/encl: (See page 3)

_________________________ G SUNSI REVIEW COMPLETE

OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP

SIGNATURE Via email Via email Via email CRK /RA/ EFG /RA/

NAME CYoung MSpeck WDeschaine CKontz EGuthrie

DATE 10/28/2010 10/28/2010 10/28/2010 10/29/2010 10/29/2010

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

TVA 3

cc w/encl:

C.R. Church

Vice President

Sequoyah Nuclear Plant

Tennessee Valley Authority

P.O. Box 2000

Soddy-Daisy, TN 37384-2000

K. Langdon

Plant Manager

Sequoyah Nuclear Plant

Tennessee Valley Authority

P.O. Box 2000

Soddy Daisy, TN 37384-2000

B. A. Wetzel

Manager

Licensing and Industry Affairs

Sequoyah Nuclear Plant

Tennessee Valley Authority

P.O. Box 2000

Soddy Daisy, TN 37384-2000

E. J. Vigluicci

Assistant General Counsel

Tennessee Valley Authority

6A West Tower

400 West Summit Hill Drive

Knoxville, TN 37902

County Mayor

Hamilton County

Hamilton County Courthouse

Chattanooga, TN 37402-2801

Division of Radiological Health

TN Dept. of Environment & Conservation

401 Church Street

Nashville, TN 37243-1532

Ann Harris

341 Swing Loop

Rockwood, TN 37854

TVA 4

Letter to R. M. Krich from Eugene Guthrie dated October 29, 2010

SUBJECT: SEQUOYAH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT

05000327/2010004, 05000328/2010004

Distribution w/encl:

C. Evans, RII

L. Douglas, RII

OE Mail

RIDSNRRDIRS

PUBLIC

RidsNrrPMSequoyah Resource

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.: 50-327, 50-328

License Nos.: DPR-77, DPR-79

Report Nos.: 05000327/2010004, 05000328/2010004

Licensee: Tennessee Valley Authority (TVA)

Facility: Sequoyah Nuclear Plant, Units 1 and 2

Location: Sequoyah Access Road

Soddy-Daisy, TN 37379

Dates: July 1, 2010 - September 30, 2010

Inspectors: C. Young, Senior Resident Inspector

M. Speck, Resident Inspector

W. Deschaine, Project Engineer (1R05, 1R22)

Approved by: Eugene F. Guthrie, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000327/2010004, 05000328/2010004; 07/01/2010 - 09/30/2010; Sequoyah Nuclear Plant,

Units 1 and 2; Heat Sink Performance, Identification and Resolution of Problems, and Event

Followup.

The report covered a three-month period of inspection by resident inspectors and announced

inspections by regional inspectors. Three Green findings were identified. The significance of

most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual

Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP

does not apply may be Green or be assigned a severity level after NRC management review.

The NRC's program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Criterion V, Instructions, Procedures, and Drawings, for the failure to provide

adequate documented instructions for inspection of the containment spray heat

exchangers. Preventive maintenance (PM) procedures associated with these

inspections failed to provide for an adequate inspection of the ERCW side (shell

side) of these heat exchangers. Consequently, the heat transfer capability of these

heat exchangers has not been periodically verified through either testing or

adequate visual inspection. The licensee entered this issue into their corrective

action program as PER 236318. Planned corrective actions include the

development and implementation of a single-tube method for thermal performance

testing of the heat exchangers in lieu of inspection.

The finding was determined to be greater than minor because it was associated

with the equipment performance attribute of the mitigating systems cornerstone and

affected the cornerstone objective to ensure the availability, reliability, and capability

of systems that respond to initiating events to prevent undesirable consequences,

since the heat transfer capability of these heat exchangers has not been periodically

verified through either testing or adequate visual inspection. Using IMC 0609,

Significance Determination Process, Attachment 4, Phase 1 - Initial Screening

and Characterization of Findings, the finding was determined to be of very low

safety significance (Green) since the finding did not represent an actual loss of

safety function. The cause of this finding was determined to have a cross-cutting

aspect of Corrective Action Program Issue Identification in the area of Problem

Identification and Resolution associated with the Corrective Action Program

component, in that the evaluation of PERs in 2009 on the subject of CS heat

exchanger inspection failed to identify the need to resolve the discrepancy between

the scope of the program PMs and the implementing procedure requirement for CS

heat exchanger shell side inspection. Thus, the licensee failed to completely and

accurately identify issues in the corrective action program P.1(a). (Section 1R07)

Enclosure

3

  • Green. The inspectors identified a Green non-cited violation of 10 CFR 50

Appendix B Criterion III, Design Control, for the failure to provide design control

measures for verifying the adequacy of the design calculation used to establish the

maximum RHR operating temperature limit for maintaining ECCS operability. A

design calculation yielded a non-conservative temperature limit for use in plant

operations procedures. This resulted in several occasions where ECCS operability

was in question due to the fluid temperature in the RHR system suction piping. The

licensee entered this issue into their corrective action program as PER 215434.

Corrective actions included revising operations procedures to reflect the corrected

temperature limit from a revised calculation.

The finding was determined to be greater than minor because it was similar to

example 3.j. of IMC 0612 Appendix E in that the non-conservatism in the calculation

resulted in a condition where reasonable doubt existed as to the operability of the

ECCS system. Additionally, it was associated with the procedure quality attribute of

the mitigating systems cornerstone and affected the cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences. Specifically, plant procedures for RHR

system operation contained non-conservative temperature limits for ensuring TS

operability, and actual system temperatures exceeded the revised appropriate limit

on several occasions. Using IMC 0609, Significance Determination Process,

Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, the

finding was determined to be of very low safety significance (Green) since the

finding did not represent an actual loss of safety function. No cross-cutting aspect

was identified since the issue was not reflective of current licensee performance,

since the previous calculation in question was last revised and approved in 1996.

(Section 4OA2.3)

Cornerstone: Barrier Integrity

  • Green. The inspectors identified a Green non-cited violation of Unit 2 TS 6.8,

Procedures and Programs, for the failure to take prompt action to maintain reactor

thermal power less than the licensed power limit of 3455 megawatts thermal (MWt)

in response to a transient caused by the loss of a condensate booster pump, as

required by station procedures. The licensee entered this issue into their corrective

action program as PER 259098. The licensee is currently evaluating for planned

corrective actions.

The finding was determined to be greater than minor because it was similar to

example 8.b. of IMC 0612 Appendix E. Additionally, it was associated with the

Human Performance attribute of the Barrier Integrity cornerstone and affected the

cornerstone objective relative to the fuel cladding barrier since operation above the

licensed power limit reduces analyzed margins to fuel cladding damage. Using IMC 0609, Significance Determination Process, Attachment 4, Phase 1 - Initial

Screening and Characterization of Findings, the finding was determined to be of

very low safety significance (Green) since only the fuel cladding barrier was

affected. The cause of this finding was determined to have a cross-cutting aspect

of Conservative Assumptions and Safe Actions in the area of Human Performance

Enclosure

4

associated with the Decision Making component. The decision to take no operator

action in response to the thermal power transient reflected a non-conservative

assumption that average thermal power could be allowed to exceed the licensed

limit without operator action while the feedwater control system responded to the

transient associated with the condensate pump failure H.1(b). (Section 4OA3.3)

Enclosure

REPORT DETAILS

Summary of Plant Status:

Unit 1 operated at or near 100 percent rated thermal power (RTP) for the entire inspection

period.

Unit 2 operated at or near 100 percent RTP until September 28, 2010, when power was

reduced to approximately 84 percent RTP in response to the loss of one condensate booster

pump. Unit 2 remained at 84 percent RTP while conducting repairs for the remainder of the

inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignment

Partial System Walkdown

a. Inspection Scope

The inspectors performed four partial walkdowns of the following systems to verify the

operability of redundant or diverse trains and components when safety equipment was

inoperable. The inspectors focused on identification of discrepancies that could impact

the function of the system and, therefore, potentially increase risk. The inspectors

reviewed applicable operating procedures, walked down control system components,

and determined whether selected breakers, valves, and support equipment were in the

correct position to support system operation. The inspectors also verified that the

licensee had properly identified and resolved equipment alignment problems that could

cause initiating events or impact the capability of mitigating systems or barriers and

entered them into the corrective action program (CAP). Documents reviewed are listed

in the Attachment.

train Unplanned Maintenance

Maintenance

b. Findings

No findings were identified.

Enclosure

6

1R05 Fire Protection

.1 Fire Protection Tours

a. Inspection Scope

The inspectors conducted a tour of the six areas important to safety listed below to

assess the material condition and operational status of fire protection features. The

inspectors evaluated whether: combustibles and ignition sources were controlled in

accordance with the licensees administrative procedures; fire detection and suppression

equipment was available for use; passive fire barriers were maintained in good material

condition; and compensatory measures for out-of-service, degraded, or inoperable fire

protection equipment were implemented in accordance with the licensees fire plan.

Documents reviewed are listed in the Attachment.

  • Control Building Elevation 706 (Cable Spreading Room)
  • Control Building Elevation 685 (Auxiliary Instrument Rooms)
  • Control Building Elevation 669 (Mechanical Equipment Room, 250 VDC Battery and

Battery Board Rooms)

  • Auxiliary Building Elevation 690 (Corridor)
  • Auxiliary Building Elevation 714 (Corridor)

b. Findings

No findings were identified.

.2 Annual Drill Observations

a. Inspection Scope

On July 21, 2010, the inspectors observed an unannounced fire drill in the Diesel

Generator Building Board Room 1A-A. The inspectors assessed fire alarm

effectiveness; response time for notifying and assembling the fire brigade; the selection,

placement, and use of firefighting equipment; use of personnel fire protective clothing

and equipment (e.g., turnout gear, self-contained breathing apparatus); communications;

incident command and control; teamwork; and fire fighting strategies. The inspectors

also attended the post-drill critique to assess the licensees ability to review fire brigade

performance and identify areas for improvement. Following the critique, the inspectors

compared their findings with the licensees observations and to the requirements

specified in the licensees Fire Protection report. This activity constituted one inspection

sample.

b. Findings

No findings were identified.

Enclosure

7

1R06 Flood Protection Measures

.1 Internal Flooding

a. Inspection Scope

The inspectors reviewed one internal flood protection measures sample for the Turbine

Building/Control Building interface flood barriers to verify that structures and penetrations

were consistent with the drawings and design requirements and risk analysis

assumptions and that equipment essential for reactor shutdown was properly protected

from a flood caused by pipe breaks in the turbine building. Specifically, the inspectors

reviewed the licensees drawings and walked down the barriers separating the turbine

and control buildings to verify the adequacy of common area drainage, flood detection

instrumentation, and that physical barriers were intact to ensure that a flooding event

would not impact reactor shutdown capabilities. Documents reviewed are listed in the

Attachment. The inspectors completed one sample.

b. Findings

No findings were identified.

1R07 Heat Sink Performance

a. Inspection Scope

The inspectors reviewed the licensees execution and on-line monitoring of biofouling

controls to verify whether the licensee had developed acceptance criteria for these

controls. Specifically, the inspectors reviewed SPP-9.7, Corrosion Control Program,

Revision 17, interviewed chemistry and engineering personnel, and reviewed chemistry

implementing procedures to ensure that SPP-9.7 requirements were implemented. The

inspectors also reviewed the licensees Generic Letter (GL) 89-13 commitments relating

to safety-related heat exchangers cooled by raw service water. The inspectors observed

the inspection of the shell side (raw water side) of the 1B containment spray heat

exchanger as well as documentation of the inspection of the 1A, 2A, and 2B containment

spray heat exchangers in accordance with the licensees Generic Letter 89-13 Program.

Documents reviewed are listed in the Attachment. The inspectors completed one

sample.

b. Findings

Introduction. The inspectors identified a Green non-cited violation of 10 CFR 50

Appendix B Criterion V, Instructions, Procedures, and Drawings, for the failure to

provide adequate documented instructions for inspection of the containment spray heat

exchangers. Preventive maintenance (PM) procedures associated with these

inspections failed to provide for an adequate inspection of the ERCW side (shell side) of

these heat exchangers. Consequently, the heat transfer capability of these heat

exchangers has not been periodically verified through either testing or adequate visual

inspection.

Enclosure

8

Description. On July 18, 1989, the NRC issued Generic Letter (GL) 89-13 Service

Water System Problems Affecting Safety-Related Equipment which requested licensees

to implement a program including testing and/or inspection in order to ensure adequate

heat transfer capability of applicable safety-related heat exchangers which use raw

service water for cooling. The licensees equivalent safety-related raw service water

system is the Essential Raw Cooling Water (ERCW) system. On September 22, 1995,

the licensee submitted a revised GL 89-13 program response which indicated that, for

the containment spray (CS) heat exchangers, periodic maintenance and inspection is

performed on the shell side (ERCW) for MIC, clams and mussels, silt, biofouling, and

corrosion products.

The inspectors reviewed licensee procedure 0-TI-SXX-000-146.0, Program For

Implementing NRC Generic Letter 89-13, revision 3, which required that visual

inspections of the ERCW side of the CS heat exchangers be performed via the

Preventive Maintenance (PM) Program. Specifically, PM procedures 041461000,

041481000, 041472000, and 041492000 were identified as implementing procedures for

the inspections of CS heat exchangers 1A, 1B, 2A, and 2B, respectively. In January and

March 2010, the inspectors observed the licensees performance of these PM activities.

The inspectors noted that the scope of these PMs was limited to inspection of the interior

of the ERCW inlet pipe to each heat exchanger, and that the location of the inspection

precluded observation of the condition of the shell side of the heat exchanger. The

inspectors concluded that this activity was not adequate to meet the program

requirement for heat exchanger testing/maintenance. The licensee entered this issue

into their corrective action program as PER 236318.

The inspectors also reviewed PER 165626, which documented that in March 2009, a

licensee self-assessment identified that PMs 041461000, 041481000, 041472000, and

041492000 had not been performed for greater than 5 years. This PER also identified

an action to evaluate the possibility of performing visual inspection on the shell side of

these heat exchangers. In response, the licensee evaluated the possibility of performing

boroscope inspection on the shell side, and concluded that this inspection method would

not be practicable.

The inspectors also reviewed PER 177214, dated July 2009, which was issued as a

follow-up to the above PER 165626 and identified the need to perform a functional

evaluation (FE) to assess the current operability of the CS heat exchangers and

evaluate whether the design basis required heat transfer capability was being

maintained in light of the fact that thermal performance testing and shell side inspections

were not being performed. The inspectors reviewed this FE and concluded that

reasonable assurance exists that these heat exchangers remain capable of performing

their required function based on the results of visual inspections and testing of other raw

water heat exchangers in the plant versus the allowable fouling factors associated with

the CS heat exchangers.

The inspectors were informed by the licensee that planned corrective actions include the

development and implementation of a single-tube method for thermal performance

testing of the heat exchangers in lieu of inspection.

Enclosure

9

Analysis. The licensees failure to provide adequate instructions for inspections of the

containment spray heat exchangers was a performance deficiency. The finding was

determined to be greater than minor because it was associated with the Equipment

Performance attribute of the Mitigating Systems cornerstone and affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences, since the heat transfer

capability of these heat exchangers has not been periodically verified through either

testing or adequate visual inspection. Using IMC 0609, Significance Determination

Process, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings,

the finding was determined to be of very low safety significance (Green) since the finding

did not represent an actual loss of safety function.

The cause of this finding was determined to have a cross-cutting aspect of Corrective

Action Program Issue Identification in the area of Problem Identification and Resolution

associated with the Corrective Action Program component, in that the evaluation of

PERs in 2009 on the subject of CS heat exchanger inspection failed to identify the need

to resolve the discrepancy between the scope of the program PMs and the implementing

procedure requirement for CS heat exchanger shell side inspection. Thus, the licensee

failed to completely and accurately identify issues in the corrective action program

P.1(a).

Enforcement. 10 CFR 50 Appendix B, Criterion V, required that activities affecting

quality shall be prescribed by documented instructions of a type appropriate to the

circumstances, and that instructions shall include appropriate qualitative acceptance

criteria for determining that important activities have been satisfactorily accomplished.

Procedure 0-TI-SXX-000-146.0, Program For Implementing NRC Generic Letter 89-13,

revision 3, required that visual inspections of the ERCW side of the containment spray

heat exchangers be performed via the Preventive Maintenance (PM) Program. Contrary

to this, on January 13, 2010, January 21, 2010, February 25, 2010, and March 11, 2010,

the licensee failed to provide adequate documented instructions which included

appropriate qualitative acceptance criteria for determining that activities affecting quality

have been satisfactorily accomplished. Specifically, instructions provided in PM

procedures 041461000, 041481000, 041472000, and 041492000 were not adequate to

perform the inspections of the ERCW side of the containment spray heat exchangers

identified in 0-TI-SXX-000-146.0. Consequently, the heat transfer capability of these

heat exchangers had not been periodically verified through either testing or adequate

visual inspection. Because this violation was determined to be of very low safety

significance and has been entered into the licensees corrective action program as PER

236318, it is being treated as an NCV consistent with Section 2.3.2 of the NRC

Enforcement Policy: NCV 05000327,328/2010004-01, Inadequate Inspection of Raw

Water Side of Containment Spray Heat Exchangers.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

The inspectors performed one licensed operator requalification program review. The

inspectors observed a simulator session on August 10, 2010. The training scenario

Enclosure

10

involved a reactor coolant system leak followed by a failure of the containment spray

system. Additional anomalies included a containment air return fan failure. The

inspectors observed crew performance in terms of: communications; ability to take

timely and proper actions; prioritizing, interpreting and verifying alarms; correct use and

implementation of procedures, including the alarm response procedures; timely control

board operation and manipulation, including high risk operator actions; oversight and

direction provided by shift manager, including the ability to identify and implement

appropriate Technical Specification (TS) action; and, group dynamics involved in crew

performance. The inspectors also observed the evaluators critique and reviewed

simulator fidelity to verify that it matched actual plant response. Documents reviewed

are listed in the Attachment. This activity constituted one inspection sample.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the maintenance activity listed below to verify the effectiveness

of the activities in terms of: appropriate work practices; identifying and addressing

common cause failures; scoping in accordance with 10 CFR 50.65 (b); characterizing

reliability issues for performance; trending key parameters for condition monitoring;

charging unavailability for performance; classification in accordance with 10 CFR

50.65(a)(1) or (a)(2); appropriateness of performance criteria for structure, system, or

components (SSCs) and functions classified as (a)(2); and, appropriateness of goals

and corrective actions for SSCs and functions classified as (a)(1). Documents reviewed

are listed in the Attachment.

  • PER 241570 - Sampling System Containment Isolation Valve Failures

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the four following activities to determine whether appropriate

risk assessments were performed prior to removing equipment from service for

maintenance. The inspectors evaluated whether risk assessments were performed as

required by 10 CFR 50.65 (a)( 4), and were accurate and complete. When emergent

work was performed, the inspectors reviewed whether plant risk was promptly

reassessed and managed. The inspectors also assessed whether the licensees risk

assessment tool use and risk categories were in accordance with Standard Programs

Enclosure

11

and Processes Procedure (SPP)-7.1, On-Line Work Management, Revision 12, and

Instruction 0-TI-DSM-000-007.1, Risk Assessment Guidelines, Revision 8. Documents

reviewed are listed in the Attachment. This inspection satisfied four inspection samples

for Maintenance Risk Assessment and Emergent Work Control.

  • July 9, 2010, Yellow PSA Risk - Unit 1 - Turbine-driven AFW train scheduled and

unscheduled maintenance

  • August 3, 2010, Heavy/complex lift in vicinity of U1/U2 6.9kV Unit Boards and

Condensate Demineralizer Piping

  • August 26, 2010, Unplanned Unavailability of Centrifugal Charging Pump 1B
  • September 30, 2010, Unit 1 start bus maintenance risk assessment

b. Findings

No findings were identified.

1R15 Operability Evaluations

a. Inspection Scope

For the nine operability evaluations described in the PERs listed below, the inspectors

evaluated the technical adequacy of the evaluations to ensure that TS operability was

properly justified and the subject component or system remained available, such that no

unrecognized increase in risk occurred. The inspectors compared the operability

evaluations to UFSAR descriptions to determine if the system or components intended

function(s) were adversely impacted. In addition, the inspectors reviewed compensatory

measures implemented to determine whether the compensatory measures worked as

stated and the measures were adequately controlled. The inspectors also reviewed a

sampling of PERs to assess whether the licensee was identifying and correcting any

deficiencies associated with operability evaluations. Documents reviewed are listed in

the Attachment.

  • PER 237441, EDG/ERCW cable splice submergence performance under flood

conditions

  • PER 234171, EGTS Cooldown Valve Failure
  • PER 208228, Battery Powered Light Failed Battery Test and Not Corrected Within 14

day Allowed Outage Time

  • PER 232000, ERCW Missile Shield Concrete Test Values Outside of Acceptance

Range

  • PER 246077, 1B Centrifugal Charging Pump Mechanical Seal Leakage
  • SR 243845, Vital Battery V Discharge Test Procedure Not Followed

pressure switch logic relay and flow controller failure

  • SR 252775, RWST aligned to non-safety related system on recirculation

Enclosure

12

b. Findings

No findings were identified.

1R18 Plant Modifications

.1 Temporary Modifications

a. Inspection Scope

The inspectors reviewed the temporary modification listed below and the associated 10

CFR 50.59 screening, and compared it against the UFSAR and TS to verify whether the

modification affected operability or availability of the affected system.

  • TACF 0-10-0011-082, Install Diesel Generator Fuel Tank Atmospheric Vent Screens

Following installation and testing, the inspectors observed indications affected by the

modification, discussed them with operators, and verified that the modification was

installed properly and its operation did not adversely affect safety system functions.

Documents reviewed are listed in the Attachment. The inspectors completed one

sample.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the five post-maintenance tests associated with the work orders

(WOs) listed below to assess whether procedures and test activities ensured system

operability and functional capability. The inspectors reviewed the licensees test

procedure to evaluate whether: the procedure adequately tested the safety function(s)

that may have been affected by the maintenance activity; the acceptance criteria in the

procedure were consistent with information in the applicable licensing basis and/or

design basis documents; and the procedure had been properly reviewed and approved.

The inspectors also witnessed the test or reviewed the test data to determine whether

test results adequately demonstrated restoration of the affected safety function(s).

Documents reviewed are listed in the Attachment.

Replacement

Enclosure

13

  • WO 110835968, Inspect, Clean, and Tighten 2B Diesel Generator Battery

Connection

  • WO 11325613, Evaluate and Repair 1B Centrifugal Charging Pump Mechanical Seal

Leakage

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

For the four surveillance tests identified below, the inspectors assessed whether the

SSCs involved in these tests satisfied the requirements described in the TS surveillance

requirements, the UFSAR, applicable licensee procedures, and whether the tests

demonstrated that the SSCs were capable of performing their intended safety functions.

This was accomplished by witnessing testing and/or reviewing the test data. Documents

reviewed are listed in the Attachment. The inspectors completed four samples.

Routine Surveillance Tests:

  • 0-SI-NUC-000-007.0, Measurement of the At-Power Moderator Temperature

Coefficient, Revision 16

  • 0-SI-EBT-082-238.2, Diesel Generator Battery Quarterly Operability, Revision 18
  • 2-SI-IFT-099-90.8B, Reactor Trip Instrumentation Monthly Functional Test (SSPS)

Train B, Revision 17

In-Service Tests:

  • 1-SI-SXP-063-201.B, Safety Injection Pump 1B-B Performance Test, Revision 13

b. Findings

No findings were identified.

1EP6 Drill Evaluation

a. Inspection Scope

Resident inspectors evaluated the conduct of a routine licensee emergency drill on

September 1, 2010 to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation (PAR) development activities. The

inspectors observed emergency response operations in the simulated control room to

verify that event classification and notifications were done in accordance with EPIP-1,

Emergency Plan Classification Matrix, Revision 43. The inspectors also attended the

licensee critique of the drill to compare any inspector-observed weakness with those

Enclosure

14

identified by the licensee in order to verify whether the licensee was properly identifying

deficiencies. The inspectors completed one sample.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

.1 Daily Review

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a daily screening of items entered into the

licensees CAP. This was accomplished by reviewing the description of each new PER

and attending daily management review committee meetings.

b. Findings and Observations

No findings were identified.

.2 Selected Issue Follow-up: Maintenance Rule scoping of SSCs used in EOPs

a. Inspection Scope

In August 2008, the NRC issued a Green NCV of 10 CFR 50.65(b)(2)(i) for the failure to

include a component within the scope of the maintenance rule monitoring program on

the basis that the use of the component was prescribed in emergency operating

procedures (EOPs) (this was issued in IR 05000327,328/2008003). The licensee issued

PER 142050 in response to this identified violation. In August 2009, the NRC identified

that the licensee had not taken action to determine the extent of additional components

not being monitored within the maintenance rule program which would fall under the

same scoping criteria. The NRC opened Unresolved Item (URI)

05000327,328/2009006-02, Inadequate Scoping of SSCs Used in EOPs into the

Maintenance Rule Program, in IR 05000327,328/2009006 to determine whether

additional scoping violations existed based on the licensees evaluation to be conducted.

The licensee issued PER 177211 to address this issue. The inspectors reviewed the

licensees actions, which included chartering a comprehensive evaluation study to

identify plant components used in EOPs and evaluate each for scoping into the

maintenance rule monitoring program. This effort is ongoing as of the time of this

inspection report.

Enclosure

15

b. Findings and Observations

No findings were identified. The inspectors have reviewed the scope and status of the

ongoing evaluation and determined that the licensee is taking appropriate action to

address the issue. To date, the licensee has scoped into the maintenance rule

monitoring program the steam dump valves, which were identified by the NRC as not

being previously scoped. It is not expected that any additional previously unscoped

components which may be identified as a result of this evaluation would constitute

violations of 10 CFR 50.65(b)(2)(i) of more than minor significance.

.3 Selected Issue Follow-up: Potential for RHR system suction line voiding when aligned

for ECCS injection

a. Inspection Scope

The inspectors reviewed the licensees actions to address the potential for voiding in the

RHR system suction piping whenever the fluid temperature exceeds the saturation

temperature associated with ECCS injection alignment. The inspectors reviewed the

licensees evaluation of Westinghouse Nuclear Safety Advisory Letter (NSAL) 09-8,

Presence of Vapor in Emergency Core Cooling System/Residual Heat Removal System

in Modes 3/4 Loss-of-Coolant Accident Conditions, which was issued in November

2009. The licensee issued PERs 203852 and 155933 to evaluate the concern. The

inspectors also reviewed NRC Information Notice (IN) 2010-11, Potential For Steam

Voiding Causing Residual Heat Removal System Inoperability, and verified that the

licensee had incorporated a review of this IN in their evaluation.

b. Findings and Observations

Introduction. The inspectors identified a Green non-cited violation of 10 CFR 50

Appendix B Criterion III, Design Control, for the failure to provide design control

measures for verifying the adequacy of the design calculation used to establish the

maximum RHR operating temperature limit for maintaining ECCS operability. A design

calculation yielded a non-conservative temperature limit for use in plant operations

procedures. This resulted in several occasions where ECCS operability was in question

due to the fluid temperature exceeding temperature limits in the RHR system suction

piping.

Description. The inspectors reviewed the licensees evaluation of Westinghouse

Nuclear Safety Advisory Letter (NSAL) 09-8, Presence of Vapor in Emergency Core

Cooling System/Residual Heat Removal System in Modes 3/4 Loss-of-Coolant Accident

Conditions, which was issued in November 2009. The licensee issued PERs 203852

and 155933 to evaluate the concern. The licensees evaluation documented that an

operability limit of 235F for RHR suction line temperature had been previously

determined, and was reflected in current operations procedures. The inspectors

reviewed operations procedure 0-GO-1, Unit Startup From Cold Shutdown to Hot

Standby, revision 54, which required that RHR shall be removed from service prior to

exceeding 235F to avoid operability issues. This procedure, as well as 0-GO-7, Unit

Shutdown From Hot Standby to Cold Shutdown, revision 59, and 0-SO-74-1, Residual

Enclosure

16

Heat Removal System, revision 69, stated that RHR must be considered inoperable for

ECCS if shutdown cooling is in service with RCS greater than 235F.

The inspectors reviewed the engineering design calculation which had been performed

to establish the RHR system temperature limit to maintain ECCS operability. Calculation

SQN-SQS2-0155, Safety limit and setpoint for the maximum RHR pump temperature to

avoid flashing at the pump suction when aligned to the RWST, revision 1, established

the RHR temperature limit of 235F which was then incorporated into operations

procedures as being a system operability limit. The inspectors noted that this calculation

was last reviewed and approved in November 1996. The inspectors identified that some

of the parameters used in this calculation were derived from another calculation which

had been superseded in 1999 by another calculation which had since been revised there

times. The inspectors also identified that the calculation was non-conservative in that it

failed to account for maintaining the minimum net positive suction head (NPSH) required

for the RHR pumps to operate. The licensee generated PER 215434 to evaluate these

concerns. The calculation was revised and resulted in a new operability limit of 200F.

Operations procedures were revised to reflect the new operability limit.

The inspectors identified that on a number of occasions the RHR system had been

operated at temperatures exceeding the newly determined operability limit, and that the

licensee had not evaluated this condition for potential reportability based on periods of

potential past inoperability. The inspectors identified examples of when both trains of

RHR were in service above the limit in Mode 4 and 1 train of ECCS was required by TS

LCO 3.5.3 to be operable. The inspectors also identified examples of when the in-

service train of RHR was secured above the temperature limit in Mode 4, with

subsequent Mode 3 entry, where 2 trains of ECCS were required by TS LCO 3.5.2 to be

operable. The licensee entered this concern into their corrective actions program as

PER 234373. The inspectors reviewed the licensees past operability evaluation, which

concluded that, for the most limiting example of operation of both trains above the limit in

Mode 4, reasonable assurance of system operability was demonstrated to be maintained

based on proceduralized operator actions to cool the RHR suction lines in the event of a

design basis event. For the most limiting case of securing one RHR train above the

temperature limit in Mode 4 prior to Mode 3 entry, the actual system temperature was

evaluated to have been below the maximum limit for operability at the time of the Mode

change.

Analysis. The licensees failure to provide adequate design control measures for

verifying the adequacy of the design calculation used to establish the maximum RHR

operating temperature limit for maintaining ECCS operability was a performance

deficiency. The finding was determined to be greater than minor because it was similar

to example 3.j. of IMC 0612 Appendix E in that the non-conservatism in the calculation

resulted in a condition where reasonable doubt existed as to the operability of the ECCS

system. Additionally, it was associated with the Procedure Quality attribute of the

Mitigating Systems cornerstone and affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Specifically, plant procedures for RHR system

operation contained non-conservative temperature limits for ensuring TS operability, and

actual system temperatures exceeded the revised appropriate limit on several

Enclosure

17

occasions. Using IMC 0609, Significance Determination Process, Attachment 4,

Phase 1 - Initial Screening and Characterization of Findings, the finding was

determined to be of very low safety significance (Green) since the finding did not

represent an actual loss of safety function.

No cross-cutting aspect was identified since the issue was not reflective of current

licensee performance, since the previous calculation in question was last revised and

approved in 1996.

Enforcement. 10 CFR 50 Appendix B Criterion III required, in part, that design control

measures shall provide for verifying or checking the adequacy of design, such as by the

use of calculational methods. Contrary to this, on November 4, 1996, the licensee failed

to provide adequate design control measures for verifying the adequacy of design

calculation SQN-SQS2-0155, revision 1, to meet its intended purpose of determining a

limiting parameter for maintaining the operability of a safety system. Consequently,

several instances occurred where actual system temperatures exceeded the design

temperature limit during system operating conditions. Corrective actions have been

taken to revise operations procedures to reflect the corrected temperature limit from a

revised calculation. Because this violation was determined to be of very low safety

significance and has been entered into the licensees corrective action program as PER

215434, it is being treated as an NCV consistent with Section 2.3.2 of the NRC

Enforcement Policy: NCV 05000327,328/2010004-02, Non-conservative Design

Calculation for RHR Suction Temperature Limit.

4OA3 Event Follow-up

.1 Inadvertent transfer of inventory from the spent fuel pit (SFP) to the Unit 1 refueling

water storage tank (RWST)

a. Inspection Scope

On June 8, 2010, the inspectors responded to a high level condition in the Unit 1 RWST

that resulted from an inadvertent transfer of water inventory from the SFP to the Unit 1

RWST. The SFP filter was being replaced while the Unit 1 RWST was on purification

recirculation and purification filters bypassed. This resulted in a system alignment of the

SFP cooling/purification system which established an unintended flowpath from the SFP

to the Unit 1 RWST. Operators responded to RWST Make-Up Shutoff and Spent Fuel

Pit Level High-Low alarms by promptly recognizing and correcting the condition.

Operators referenced TS LCO 3.5.5 which required that an inoperable RWST (due to

high level) be restored to operable within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, or the Unit would have to be shut down

within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. The RWST level was restored within the operable band within

approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 10 minutes. Approximately 2,800 gallons of inventory was

transferred.

The inspectors discussed the event with operations, engineering, and licensee

management personnel to gain an understanding of the event and assess follow-up

actions. The inspectors reviewed operator actions taken to determine whether they

were in accordance with licensee procedures and TS, and reviewed unit and system

Enclosure

18

indications to verify whether actions and system responses were as expected and

designed. The event was reported to the NRC as EN 45520, and documented in the

licensees CAP as PER 233652. Planned corrective actions included a revision to the

SFP cooling system operating procedure to preclude the establishment of the abnormal

system alignment that resulted in this event.

b. Findings

No findings were identified.

.2 Fire in A Intertie Transformer

a. Inspection Scope

On September 22, 2010, the inspectors responded to a fire in the A phase intertie

transformer in the switchyard, which serves as a connection between the 161-kV and

500-kV switchyards inside the sites protected area. Operators responded by

dispatching fire operations personnel to extinguish the fire. Both operating Units were

unaffected by the loss of the transformer. The inspectors discussed the event with

operations, engineering, and licensee management personnel to gain an understanding

of the event and assess follow-up actions. The inspectors reviewed operator actions

taken to determine whether they were in accordance with licensee procedures and TS,

and reviewed unit and system indications to verify whether actions and system

responses were as expected and designed. The inspectors verified that required

redundant and independent offsite power supplies to both Units remained operable, and

that no safety-related equipment was affected by the fire. The inspectors also

independently verified that the licensee had appropriately classified the event in

accordance with EPIP-1, Emergency Plan Classification Matrix, revision 44. The event

was appropriately classified as a Notice of Unusual Event for a fire within the protected

area lasting more than 15 minutes. The inspectors verified that the licensees event

classification and notifications to local authorities and NRC were performed timely. The

inspectors also reviewed the initial licensee notifications to verify that they met the

requirements specified in NUREG-1022, Event Reporting Guidelines. The event was

reported to the NRC as EN 46270, and documented in the licensees CAP as PERs

257350.

b. Findings

No findings were identified.

.3 Unit 2 Condensate Booster Pump Trip and Thermal Power Transient

a. Inspection Scope

On September 28, 2010, Unit 2 experienced a loss of one condensate booster pump.

The inspectors discussed the event with operations, engineering, and licensee

management personnel to gain an understanding of the event and assess follow-up

actions. The inspectors reviewed operator actions taken to determine whether they

Enclosure

19

were in accordance with licensee procedures and TS, and reviewed unit and system

indications to verify whether actions and system responses were as expected and

designed. The event was documented in the licensees CAP as PER 259098.

b. Findings

Introduction. The inspectors identified a Green non-cited violation of Unit 2 TS 6.8,

Procedures and Programs, for the failure to take prompt action to maintain 10-minute

average reactor thermal power less than the licensed power limit of 3455 megawatts

thermal (MWt) in response to a transient caused by the loss of a condensate booster

pump, as required by station procedures.

Description. Facility operating license DRP-79 condition 2.(C).1 stated that TVA is

authorized to operate the [Unit 2] facility at reactor core power levels not in excess of

3455 MWt. On September 28, 2010, Unit 2 operators responded to a condensate

booster pump trip by implementing the applicable portion of AOP-S.04, Condensate or

Heater Drains Malfunction, revision 15, section 2.5, Condensate Booster Pump Trip.

Step 3 of this section of the procedure required operators to monitor reactor power, and

reduce turbine load as necessary to maintain 10-minute average power less than the

3455 MWt limit. Operators noted that average power was above the licensed limit

during the transient and allowed the automatic response of the feedwater control system

to restore reactor power with no operator actions. The 10-min average of thermal power

was above the licensed limit for 8 minutes beginning 10 minutes after the pump trip, and

again for an additional 5-minute period beginning 32 minutes after the pump trip, with no

operator action taken to reduce power. Peak 10-minute average power was 3481 MWt,

and peak instantaneous power was 3515 MWt.

The inspectors reviewed Regulatory Issue Summary 2007-21, Rev. 1, Adherence To

Licensed Power Limits, which endorsed an NEI Position Statement Guidance To

Licensees on Complying with the Licensed Power Limit. This included guidance that

licensees are expected to take prompt action to reduce thermal power whenever it is

found above the licensed limit. The inspectors found the following licensee

proceduralized operating requirements:

OPDP-1, Conduct of Operations, revision 18, stated that if the unit is determined to be

operating above its licensed core thermal power limit take prompt (typically no more than

10 minutes from the time of determination) action to reduce power below the core

thermal power limit.

0-GO-5, Normal Power Operation, revision 67, stated that every effort should be made

to maintain core thermal power 10 minute average less than 3455 MWt. This procedure

further required that the 10 minute average power be trended and monitored for

increasing power trends above 3455 MWt, and if such an increasing trend is observed,

ensure prompt action is taken to decrease reactor power as necessary.

2-PI-OPS-000-022.1, Operator At The Controls Duty Station Checklists Modes 1-4,

revision 44, stated that every effort to maintain core thermal power 10 minute average

less than 3455 MWt should be made. It further required that the 10 minute average

Enclosure

20

power be monitored, and if core thermal power 10 minute average exceeds 3455 MWt

or an increasing trend which will exceed 3455 MWt is observed, then ensure prompt

action is taken to decrease reactor power as necessary.

The inspectors determined that the licensee did not meet procedural requirements to

promptly take action to decrease reactor power as necessary to maintain reactor power

below the licensed core thermal power limit.

Analysis. The licensees failure to follow procedural requirements to maintain 10-minute

average thermal power less than the licensed limit was a performance deficiency. The

finding was determined to be greater than minor because it was similar to example 8.b.

of IMC 0612 Appendix E. Additionally, it was associated with the human performance

attribute of the barrier integrity cornerstone and affected the cornerstone objective

relative to the fuel cladding barrier since operation above the licensed power limit

reduces analyzed margins to fuel cladding damage. Using IMC 0609, Significance

Determination Process, Attachment 4, Phase 1 - Initial Screening and Characterization

of Findings, the finding was determined to be of very low safety significance (Green)

since only the fuel cladding barrier was affected.

The cause of this finding was determined to have a cross-cutting aspect of Conservative

Assumptions and Safe Actions in the area of Human Performance associated with the

Decision Making component. The decision to take no operator action in response to the

thermal power transient reflected a non-conservative assumption that average thermal

power could be allowed to exceed the licensed limit without operator action while the

feedwater control system responded to the transient associated with the condensate

pump failure H.1(b).

Enforcement. Unit 2 TS 6.8.1.a required, in part, that written procedures be established,

implemented, and maintained covering the activities specified in Appendix A, Typical

Procedures for Pressurized Water Reactors and Boiling Water Reactors, of Regulatory

Guide (RG) 1.33, Quality Assurance Program Requirements (Operations), Revision 2,

dated February 1978. RG 1.33 Appendix A, Section 6.r, required procedures for

combating expected transients. Station procedure AOP-S.04, Condensate or Heater

Drains Malfunction, revision 15, was required to be implemented in response to the loss

of a condensate booster pump. Contrary to the above, on September 28, 2010, the

licensee failed to take prompt action to maintain 10-minute average thermal power less

than the applicable limit (3455 MWt) as required by AOP-S.04 section 2.5 step 3.b.

Consequently, 10-minute average thermal power was above 3455 MWt on two

occasions for a total duration of 13 minutes. Because this violation was determined to

be of very low safety significance and has been entered into the licensees corrective

action program as PER 259098, it is being treated as an NCV consistent with Section

2.3.2 of the NRC Enforcement Policy: NCV 05000328/2010004-03, Failure to Maintain

Thermal Power Less Than Licensed Limit.

Enclosure

21

.4 (Closed) LER 05000327,328/2010-001-00, Inoperability of shutdown board because of

spent fuel pool back-up pump breaker inoperability

a. Inspection Scope

On April 5, 2010, licensee maintenance personnel identified that a breaker had been

installed in the 2A1-A 480-V shutdown board without arc chutes and phase barriers

approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> prior to discovery of the condition. This resulted in the shutdown

board being declared inoperable until action could be completed to remove the affected

breaker. The licensee documented the issue in PER 224150, which included a root

cause analysis.

The inspectors discussed the event with operations, maintenance, engineering, and

licensee management personnel to gain an understanding of the conditions leading up

to the event and assess licensee actions taken following the event. Additionally, the

inspectors reviewed the root cause report to assess the detail and thoroughness of the

evaluation and the adequacy of the proposed corrective actions.

The inspectors reviewed the LER and PER 224150 to verify that the cause of the

improper breaker installation was identified and whether corrective actions were

appropriate. The cause of the event was determined to be an inadequate technical

review process which failed to identify that steps required to assemble the breaker in an

operable condition were omitted from the applicable work order. The inspectors

concluded that the licensees corrective actions to this event were appropriate.

Immediate actions included removal of the affected breaker in order to restore the

shutdown board to an operable status, and a stand-down briefing of the event to

maintenance personnel. Additional corrective actions included revision of the licensees

procedure for technical review of work order content to strengthen and clarify

requirements for technical review.

This LER is closed.

b. Findings

One licensee-identified violation was identified and is documented in section 4OA7 of

this report.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

Enclosure

22

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors normal plant status review and inspection activities.

b. Findings

No findings were identified.

.2 (Closed) Unresolved Item (URI) 05000327,328/2009006-02, Inadequate Scoping of

SSCs Used in EOPs into the Maintenance Rule Program

This URI was opened on August 28, 2009 in IR 05000327,328/2009-006 based on the

need to evaluate the potential existence of violations of 10 CFR 50.65(b)(2)(i) for plant

components which are used in EOPs not being scoped in the maintenance rule

monitoring program. The inspectors have reviewed the licensees actions to address

this issue as discussed in section 4OA2.2 of this report. This URI is closed.

4OA6 Meetings

Exit Meeting Summary

On October 7, 2010, the resident inspectors presented the inspection results to Mr. Chris

Church and other members of his staff, who acknowledged the findings. The inspectors

asked the licensee whether any of the material examined during the inspection should

be considered proprietary. No proprietary information was identified.

4OA7 Licensee-identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements that meets the criteria of Section VI of

the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

Unit 2 TS 6.8.1.a required, in part, that written procedures be established, implemented,

and maintained covering the activities specified in Appendix A, Typical Procedures for

Pressurized Water Reactors and Boiling Water Reactors, of Regulatory Guide (RG)

1.33, Quality Assurance Program Requirements (Operations), Revision 2, dated

February 1978. RG 1.33 Appendix A Section 9.a required that maintenance that can

affect the performance of safety-related equipment should be properly pre-planned and

performed in accordance with written procedures, documented instructions, or drawings

appropriate to the circumstances. Contrary to the above, on April 5, 2010, written

procedures appropriate to the circumstances were not established which adequately

prescribed the performance of maintenance that could affect the performance of safety-

related equipment. Specifically, the maintenance instructions for reassembly of the SFP

pump C-S backup breaker failed to include instructions for proper reassembly, which

resulted in the breaker being installed in the 2A1 shutdown board and restored to service

without arc chutes, causing the shutdown board to be inoperable for greater than its TS

allowed outage time. The licensee entered the issue into the corrective action program

Enclosure

23

as PERs 228519 and 228818. The finding was determined to have very low safety

significance (Green) because there was no actual loss of safety system function, and

there was no significant increase in the likelihood of a fire.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

S. Bowman, Licensing Engineer

C. Church, Site Vice President

R. Detwiler, Director Safety and Licensing

J. Dvorak, Outage and Site Scheduling Manager

D. Foster, Performance Improvement Manager

J. Furr, Quality Assurance Manager

Z. Kitts, Licensing

R. Krich, Licensing Vice President

K. Langdon, Plant Manager

T. Marshall, Maintenance and Modifications Manager

S. McCamy, Radiation Protection Manager

M. McDowell, Corporate Project Manager

W. Nurnberger, Chemistry/Environmental Manager

D. Porter, Operations Procedures

R. Proffitt, Licensing Engineer

P. Simmons, Operations Manager

R. Thompson, Emergency Preparedness Manager

B. Wetzel, Director, Safety and Licensing

K. Wilkes, Operations Superintendent

J. Williams, Site Engineering Director

S. Young, Site Security Manager

NRC personnel

W. Rogers, Region II, Senior Reactor Analyst

S. Lingam, Project Manager, Office of Nuclear Reactor Regulation

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000327,328/2010004-01 NCV Inadequate Inspection of Raw Water Side of

Containment Spray Heat Exchangers

(Section 1R07)

05000327,328/2010004-02 NCV Non-conservative Design Calculation for

RHR Suction Temperature Limit (Section

4OA2.3)05000328/2010004-03 NCV Failure to Maintain Thermal Power Less

Than Licensed Limit (Section 4OA3.3)

Attachment

2

Closed

05000327,328/2010-001-00 LER Inoperability of shutdown board because of

spent fuel pool back-up pump breaker

inoperability (Section 4OA3.4)

05000327,328/2009006-02 URI Inadequate Scoping of SSCs Used in EOPs

into the Maintenance Rule Program

(Section 4OA5.2)

LIST OF DOCUMENTS REVIEWED

Section R04: Equipment Alignment

1,2-47W803-2, Flow Diagram-Auxiliary Feedwater, Revision 64

Section R05: Fire Protection

General Engineering Specification G-73, Installation, Modifications, and Maintenance of Fire

Protection Systems and Features, Revision 5

Sequoyah Fire Drill Critique Form, Revision 5

MMTP-102, Erection of Scaffolds/Temporary Work Platforms and Ladders, Revision 4

0-SI-FPU-247-001.0, Appendix R Emergency Lighting Auxiliary Building Quarterly test, Revision

18

FPDP-1, Conduct of Fire Protection, Revision 1

0-PI-FPU-317-299.W, Fire Protection Miscellaneous Inspections, Revision 30

Section R06: Flood Protection Measures

1,2-47W853-1, Flow Diagram Station Drainage-Control/Turbine/Service Building, Revision 17

1,2-47W853-3, Flow Diagram Station Drainage-Control/Turbine Building, Revision 6

1,2-47W853-4, Flow Diagram Station Drainage-Control/Turbine Building, Revision 11

1,2-47W853-5, Flow Diagram Station Drainage-Control/Turbine Building, Revision 7

Section R07: Heat Sink Performance

SPP-9.7, Corrosion Control Program, revision 17

0-TI-SXX-000-146.0, Program for implementing NRC Generic Letter 89-13, revision 3

SPP-9.14, Generic Letter (GL) 89-13 Implementation, revision 2

WO 09-777986-000, Cntmt spray heat exch 1A clam inspection

WO 09-782086-000, Cntmt spray heat exch 2A clam inspection

WO 09-782087-000, Cntmt spray heat exch 2B clam inspection

WO 09-777985-000, Cntmt spray heat exch 1B clam inspection

Section R12: Maintenance Rule Implementation

TI-4, Maintenance Rule Performance Indicator Monitoring, Trending, and Reporting -

10CFR50.65, Revision 22

PERs 177904, 204589, 227496

Attachment

3

CDEs 2286, 2296, 2516

CDEs - System 43 and 88

Section R13: Maintenance Risk Assessments and Emergent Work Evaluation

Sentinel Risk Model runs dated July 7 and 8, 2010

0-TI-DSM-000-007.1, Risk Assessment Guidelines, Revision 9

SPP-7.3, Work Activity Risk Management Process, Revision 5

MSS Daily Schedule Report-24 hour look-ahead, dated July 7, 2010

SPP-7.2.4, Forced Outage or Short Duration Planned Outage Management, Revision 1

SPP-7.2, Outage Management, Revision 18

GOI-6, Apparatus Operations, Revision 134

0-GO-16, System Operability Checklists, Revision 9

MMTP-103A, NPG Lifting and Rigging Manual, Revision 1

MMTP-103, Nuclear Power Group Movement of Items Using Overhead Handling Equipment,

Revision 2

Sentinel Risk Model run dated July 29, 2010

PSO-SPP-10.303, System Alerts, Revision 3

PRA Evaluation Response SQN-0-10-099

NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear

Power Plants, Section 11, Assessment of Risk Resulting From Performance of maintenance

Activities

0-SI-OPS-082-007.W, AC Electrical Power Source Operability Verification, revision 17

Section R15: Operability Evaluations

FSAR Section 6.2.3, Containment Air Purification and Cleanup System

FSAR Figure 9.4.7-1, Reactor Building Air Flow

FSAR Section 3.5.5, Missile Barrier Features, Buried Piping

FSAR Section 6.3.2.2, Emergency Core Cooling System

WO 09-777416-002, Reinstall Missile Shield Concrete - Diesel Generator Building

General Engineering Specification G-2, Plain and Reinforced Concrete, Revision 8

0-SI-OPS-065-017.A, Containment Shield Building Emergency Gas Treatment System Flow

Train A, Revision 14

0-SI-OPS-065-017.B, Containment Shield Building Emergency Gas Treatment System Flow

Train B, Revision 13

0-SI-OPS-065-135.0, EGTS Cleanup Subsystem Automatic Start, Revision 17

0-SO-65-1, Emergency Gas Treatment System Air Cleanup and Annulus Vacuum, Revision 19

1-SI-SLR-062-632.B, Auxiliary Building Chemical and Volume Control System Unit 1 Train B

External Leakage, Revision 4

0-MI-MRR-062-001.0, Inspection/Repair of CVCS Centrifugal Charging Pump Seals, Revision

12

NEDP-22, Functional Evaluations, Revision 8

IEEE 450-2002, IEEE Recommended Practice for Maintenance, Testing, and Replacement of

Vented Lead-Acid Batteries for Stationary Applications

IEEE Std 404-2006, IEEE Standard for Extruded and Laminated Dielectric Shielded Cable

Joints Rated 2500V to 500,000 V

Drawing 1,2-47W454-1, Mechanical Fuel Pool Cooling and Cleaning System, revision 2

Drawing 1,2-47W454-4, Mechanical Fuel Pool Cooling and Cleaning System, revision 6

Attachment

4

Design Criteria Document SQN-DC-V-3.0, The Classification of Piping, Pumps, Valves, and

Vessels, revision 17

Calculation SCG4M01131, Scaffold wired to 1B CS Heat Exchanger Vent/Drain Line, revision 0

Drawing 1, 2-45N657-5. Wiring Diagrams Separation & Misc Aux Rlys, revision 19

Section R18: Plant Modifications

SPP-9.5, Temporary Alterations, Revision 10

1,2-47W840-1, Flow Diagram-Fuel Oil, Atomizing Air and Steam, Revision 44

WO 110842725, TACF implementation for EDG 1A

WO 110842737, TACF implementation for EDG 2A

WO 110842731, TACF implementation for EDG 1B

WO 110842751, TACF implementation for EDG 2B

Section R19: Post Maintenance Testing

0-MI-IEQ-000-001.0, EQ Maintenance for 10CFR50.49 Equipment Fluid Components, (EQ

Binder SQNEQ-IFS-001), Revision 11

MMDP-3, Guidelines for Planning and Execution of Troubleshooting Activities, Revision 5

SPP-6.5, Foreign Material Control, Revision 14

MMDP-1, Maintenance Management System, Revision 18

MMDP-3, Guidelines for Planning and Execution of Troubleshooting Activities, Revision 6

SPP-6.1, Work Order Process Initiation, Revision 8

SPP-8.1, Conduct of Testing, Revision 6

1-SI-EDC-003-180.0, Setpoint Verification and Calibration of Aux Feedwater Suction Transfer

System 3 Time Delay Relays, Revision 8

1-45W1614-12, Wiring Diagram Aux Feedwater Pump and Turbine Connection Diagrams,

Revision 1

1, 2-45N657-5, Wiring Diagrams Separation and Misc Aux Relays Schematic Diagrams,

Revision 19

MI-10.54, Diesel Generator Battery Replacement and/or Battery Bank Bus Rework, Revision 20

1-SO-3-2, Auxiliary Feedwater System, revision 44

WO 111143594, Auxiliary Feedwater Pump Flow Controller

Section R22: Surveillance Testing

SPP-8.1, Conduct of Testing, Revision 5

0-SI-NUC-000-007.0, Measurement of the At-Power Moderator Temperature Coefficient,

Revision 16

1-47W811-1, Flow Diagram Safety Injection System, Revision72

Section 4OA2: Identification and Resolution of Problems

SPP-3.9, Operating Experience Program, revision 3

Calculation MDQ0072-980034, CCP, SIP, CSP, and RHR Pump NPSH Evaluation, revision 3

NRC Information Notice 2010-11, Potential For Steam Voiding Causing Residual Heat Removal

System Inoperability

Westinghouse Nuclear Safety Advisory Letter (NSAL) 09-8, Presence of Vapor in Emergency

Core Cooling System/Residual Heat Removal System in Modes 3/4 Loss-of-Coolant Accident

Conditions

0-GO-1, Unit Startup From Cold Shutdown to Hot Standby, revision 54

0-GO-7, Unit Shutdown From Hot Standby to Cold Shutdown, revision 59

Attachment

5

0-SO-74-1, Residual Heat Removal System, revision 69

Calculation SQN-SQS2-0155, Safety limit and setpoint for the maximum RHR pump

temperature to avoid flashing at the pump suction when aligned to the RWST, revision 1

Calculation SQN-SQS2-0155, Shutdown LOCA Analysis for the ECSC System, Core Cooling,

and Containment Including RHR Pump NPSH Considerations, revision 2

Section 4OA3: Event Followup

AOP-P.06, Loss of Unit 2 Electrical Shutdown Boards, revision 15

0-SO-78-1, Spent Fuel Pit Coolant System, revision 45

2-AR-M1-B, Electrical Control Board 2-XA-55-1B, revision 19

AOP-S.04, Condensate or Heater Drains Malfunction, revision 15

OPDP-1, Conduct of Operations, revision 18

0-GO-5, Normal Power Operation, revision 67

2-PI-OPS-000-022.1, Operator At The Controls Duty Station Checklists Modes 1-4, revision 44

EPIP-1, Emergency Plan Classification Matrix, revision 44

EPIP-2, Notification of Unusual Event, revision 29

Section 4OA5: Other Activities

0-PI-SQS-000-647.W, Explosive Detector Performance Test, Revision 12

0-PI-SQS-000-643.W, X-ray Equipment Function Test, Revision 13

0-PI-SQS-000-646.W, Metal Detector Functional Test, Revision 10

Attachment