ML043020589

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IR 05000237-04-010, 05000249-04-010; on 07/01/2004 - 09/30/2004; Dresden Nuclear Power Station, Units 2 & 3; Flood Protection, Outage Activities, Radiological Environmental Monitoring and Radioactive Material Control Program, and Event Foll
ML043020589
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 10/27/2004
From: Ring M
Division Reactor Projects III
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
Download: ML043020589 (55)


See also: IR 05000237/2004010

Text

October 27, 2004

Mr. Christopher M. Crane

President and Chief Nuclear Officer

Exelon Nuclear

Exelon Generation Company, LLC

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3

NRC INTEGRATED INSPECTION REPORT 05000237/2004010;

05000249/2004010

Dear Mr. Crane:

On September 30, 2004, the NRC completed an inspection at your Dresden Nuclear Power

Station, Units 2 and 3. The enclosed report presents the inspection findings which were

discussed with Mr. D. Bost and other members of your staff on October 8, 2004.

The inspection examined activities conducted under your license as they relate to safety and to

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, five NRC identified findings and four self-revealed

findings of very low safety significance were identified. Seven of these findings were

determined to involve violations of NRC requirements. However, because of the very low safety

significance and because they were entered into your corrective action program, the NRC is

treating these seven findings as Non-Cited Violations, in accordance with Section VI.A.1 of the

NRCs Enforcement Policy. Additionally, a licensee-identified violation which was determined to

be of very low safety significance is listed in Section 4OA7 of this report.

If you contest any Non-Cited Violation in this report, you should provide a response with the

basis for your denial, within 30 days of the date of this inspection report, to the Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-001; with

copies to the Regional Administrator, Region III; the Director, Office of Enforcement, United

States Nuclear Regulatory Commission, Washington, DC 20555-001; and the NRC Resident

Inspector at the Dresden facility.

C. Crane -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter

and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRC's

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 50-237; 50-249

License Nos. DPR-19; DPR-25

Enclosure: Inspection Report 05000237/2004010; 05000249/2004010

w/Attachment: Supplemental Information

cc w/encl: Site Vice President - Dresden Nuclear Power Station

Dresden Nuclear Power Station Plant Manager

Regulatory Assurance Manager - Dresden

Chief Operating Officer

Senior Vice President - Nuclear Services

Senior Vice President - Mid-West Regional

Operating Group

Vice President - Mid-West Operations Support

Vice President - Licensing and Regulatory Affairs

Director Licensing - Mid-West Regional

Operating Group

Manager Licensing - Dresden and Quad Cities

Senior Counsel, Nuclear, Mid-West Regional

Operating Group

Document Control Desk - Licensing

Assistant Attorney General

Illinois Department of Nuclear Safety

State Liaison Officer

Chairman, Illinois Commerce Commission

DOCUMENT NAME: G:\dres\ML043020589.wpd

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE RIII N RIII E

NAME PPelke/dtp MRing

DATE 10/27/04 10/27/04

OFFICIAL RECORD COPY

C. Crane -3-

ADAMS Distribution:

AJM

DFT

MXB

RidsNrrDipmIipb

GEG

HBC

DRC1

CAA1

C. Pederson, DRS (hard copy - IRs only)

DRPIII

DRSIII

PLB1

JRK1

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-237; 50-249

License Nos: DPR-19; DPR-25

Report No: 05000237/2004010; 05000249/2004010

Licensee: Exelon Generation Company

Facility: Dresden Nuclear Power Station, Units 2 and 3

Location: 6500 North Dresden Road

Morris, IL 60450

Dates: July 1, 2004, through September 30, 2004

Inspectors: C. Phillips, Senior Resident Inspector

M. Sheikh, Resident Inspector

P. Pelke, Reactor Engineer

W. Slawinski, Senior Radiation Specialist

B. Palagi, Senior Operations Engineer

J. Neurauter, Reactor Engineer

B. Dickson, Senior Resident Inspector, Clinton

D. Eskins, Resident Inspector, LaSalle

R. Schulz, Illinois Emergency Management Agency

Approved by: M. Ring, Chief

Branch 1

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000237/2004010; IR 05000249/2004010, 07/01/2004 - 09/30/2004, Exelon Generation

Company, Dresden Nuclear Power Station, Units 2 and 3; Flood Protection, Outage Activities,

Radiological Environmental Monitoring and Radioactive Material Control Program, and Event

Followup.

This report covers a 3-month period of baseline resident inspection and announced baseline

inspection of radiation safety. The inspection was conducted by Region III inspectors and the

resident inspectors. The inspection identified nine Green findings, seven of which involved

Non-Cited Violations. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter 0609, Significance Determination

Process (SDP). Findings for which the SDP does not apply may be Green or be assigned

severity level after NRC management review. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 3, dated July 2000.

A. Inspector Identified Findings

Cornerstone: Initiating Events

Green. A self-revealed finding of very low safety significance was identified involving

several performance issues which resulted in the initiation of a Unit 2 manual scram on

April 24, 2004, due to failure of the 2A recirculation pump motor. The performance

issues included an inadequate process for rewinding the 2A recirculation pump motor

when it was installed in 1999, an inadequate evaluation of the testing of the motor

before installation, and the failure to perform post maintenance testing of the reactor

building closed cooling water system piping to identify leakage. This failure resulted in

the deposit of a conductive substance inside the motor. The licensee identified a

number of corrective actions including replacing the 2A recirculation pump motor and

revising Exelon Nuclear Engineering Standard NES-EIC-40.01 to include enhanced

testing requirements.

The finding was more than minor because it affected the initiating events cornerstone

objective to limit the likelihood of an initiating event. The finding was determined to be

of very low safety significance because all equipment and systems operated as

designed during the scram. (Section 4OA3)

Cornerstone: Mitigating Systems

Green. A finding of very low significance was identified by the inspectors on

June 5, 2004, involving a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings. The abnormal operating procedure

instructions for response to external flooding, and surveillance test procedure for the

diesel driven pump necessary to provide make-up to the isolation condenser for

response to external flooding, were not adequate for the circumstances. The licensee

planned to change the surveillance test procedure and perform a full flow test of the

4 Enclosure

pump in the near future. The licensee planned to review the abnormal operating

procedure and revise the procedure as appropriate.

This finding was more than minor because it affected the equipment performance and

procedure quality attributes of the mitigating systems cornerstone, and affected the

cornerstone objective of ensuring the reliability and capability of systems that respond to

initiating events to prevent undesirable consequences. The issue was of very low safety

significance based on the low initiating event probability, and because of the slow onset

of the flooding and the reduced decay heat in the reactor core at the time recovery

actions would be necessary, the licensee would be able to reasonably perform recovery

actions that would prevent core damage. (Section 1R06)

Green. A finding of very low significance was identified on July 1, 2004, by the

inspectors involving a Non-Cited Violation of Technical Specification 3.3.1.1. The

licensee failed to take adequate corrective actions to prevent recurrence of inoperable

condenser low vacuum reactor protection system switches, failed to recognize the

switches were inoperable, and failed to enter the appropriate Technical Specification

Limiting Condition for Operation when the 3C and 2A turbine main condenser low

vacuum reactor protection system scram channels were inoperable. The primary cause

of the violation was related to the cross-cutting area of Problem Identification and

Resolution.

The finding was more than minor because it affected the mitigating systems cornerstone

objective by affecting the reliability of the reactor protection system. The finding was

determined to be of very low safety significance (Green) because one inoperable

channel would not prevent the reactor to scram on low condenser vacuum. Corrective

actions by the licensee included installing temporary vent valves on the 3C and 2A

sensing lines, enhancing operations training materials, revising the operationss

procedure, and performing internal and external condenser walkdowns during the next

outage on Unit 2 and Unit 3. (Section 4OA3)

Green. A finding of very low safety significance was identified by the inspectors

involving a Non-Cited Violation of Technical Specification 5.4.1. Operators failed to lock

manual feedwater isolation Valve 2-220-57B when returning the valve to service. This

valve was downstream of where the high pressure core injection (HPCI) system taps

into the feedwater line. The inspectors identified this issue during the drywell closeout

after the maintenance outage on September 23, 2004. The operators were counseled

and the licensee will require out-of-service checklists to be brought into the drywell in the

future. The primary cause of this violation was related to the cross-cutting issue of

Human Performance.

This issue was more than minor because it was repetitive. Other valves were found

unlocked inside the drywell by the inspectors during the drywell close out after the last

Unit 2 refueling outage in November 2003. The issue was of very low safety

significance because the valve was in the correct position. (Section 1R20)

Green. A self-revealed finding of very low safety significance involving a Non-Cited

Violation of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, was identified. Inadequate procedural guidance resulted in the failure of

5 Enclosure

electricians to properly set the open torque switch bypass on Valve 2-1301-3, Isolation

Condenser Outboard Condensate Return Valve, on October 8, 1999. This resulted in

the failure of the valve to open during an event that occurred on April 24, 2004. The

licensee counseled the individuals and revised the maintenance procedure.

This finding was more than minor because it involved the equipment performance

attributes of the mitigating systems cornerstone and affected the cornerstone objective

of availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. This issue was of very low safety significance in

that the isolation condenser was only being used for pressure control at the time of the

event and other methods of pressure control were available, and in addition, the

licensee could have manually opened the valve if necessary. (Section 4OA3)

Cornerstone: Barrier Integrity

Green. A finding of very low safety significance was identified by the inspectors involving

a Non-Cited Violation of 10 CFR 50.65, Maintenance Rule, requirements. The

licensee failed to identify that the number of functional failures for the reactor building

ventilation system had exceeded the established performance criteria and did not move

the reactor building ventilation system into the a(1) category. Once identified, the

reactor building ventilation system was moved into the a(1) category on October 8,

2004. The licensee had not yet determined system goals or established corrective

actions by the close of the inspection period. The primary cause of the violation was

related to the cross-cutting area of Problem Identification and Resolution in that

functional failures of the system were not properly entered into the corrective action

program.

This issue was more than minor because it involved the design control and barrier

performance attributes of the barrier integrity cornerstone; and affected the cornerstone

objective of providing reasonable assurance that physical design barriers protect the

public from radionuclide releases caused by accidents or events. The issue was of very

low safety significance because the licensee was still able to maintain secondary

containment. (Section 1R12)

Green. A self-revealed finding of very low safety significance involving a Non-Cited

Violation of Technical Specification 3.7.4 was identified on April 28, 2004. The licensee

failed to correctly restore the control room emergency ventilation system to operable

status following maintenance. This left the control room emergency ventilation system

inoperable for greater than its Technical Specification allowed outage time. This finding

was self-revealed when the system did not operate properly several days later during a

routine system realignment. As corrective action, the licensee revised a procedure to

give better guidance on how to remove the temporary modification.

The issue was more than minor because it affected the Barrier Integrity Cornerstone

attributes of design and configuration control and the cornerstone objective of protecting

persons in the control room from radionuclide releases caused by accidents or events.

The issue was of very low safety significance due to the short duration of the condition

of the system. (Section 4OA3)

6 Enclosure

Green. A finding of very low safety significance was identified on August 3, 2004, by the

inspectors during the walkdown of a corrective action for a previous event. The licensee

had an abnormal operating procedure requirement to have tools and equipment staged

to install a temporary modification to keep the control room emergency ventilation

system dampers open in the event of an accident. The equipment necessary to install

the temporary modification was in various stages of disarray. Some equipment was not

labeled and some necessary tools were missing. The licensee identified a number of

corrective actions including properly packaging the necessary tools and equipment,

revising procedures, and initiating a training request to ensure operations personnel are

properly trained in the use of the tools and equipment.

The finding was more than minor because it affected the Barrier Integrity Cornerstone

attributes of configuration control and the cornerstone objective of protecting persons in

the control room from radionuclide releases caused by accidents or events. The issue

was of very low safety significance due to it only impacting the radiological barrier

function of the control room emergency ventilation system. This was not a violation of

regulatory requirements. (Section 40A3)

Cornerstone: Public Radiation Safety

Green. A self-revealed finding of very low safety significance involving a Non-Cited

Violation of 10 CFR 20.1501 was identified on October 16, 2003, following a gatehouse

radiation monitor alarm at the Braidwood Nuclear Station upon detecting a discrete

radioactive particle (DRP) on a workers boot. The DRP was attributed to the workers

activities at the Dresden facility approximately 1 year earlier. The DRP was not

identified at the Dresden Station due to an inadequate radiation survey of the worker

following a personnel contamination monitor alarm and also because of limitations with

the radiation monitoring instrumentation used at the licensees egress to the

radiologically controlled area (RCA).

Corrective actions for this finding included tailgate training to radiation protection

staff that respond to contamination monitor alarms, improvements to automated

radiation monitoring capabilities at the main RCA egress, and actions to enhance

gamma-sensitivity of those automated radiation monitors located in alternate egress

areas and at the protected area gatehouse.

The finding was more than minor because it was associated with the Program and

Process and Human Performance attributes of the Public Radiation Safety

Cornerstone, and affected the cornerstone objective that ensures adequate protection of

public health and safety from exposure to radioactive materials that are released into the

public domain. The issue represents a finding of very low safety significance because

public radiation exposure resulting from the problem was not greater than 0.005 rem

total effective dose equivalent, the licensee did not have greater than five radioactive

material control occurrences in the previous eight quarters and the dose to the involved

worker was approximately one percent of the regulatory (10 CFR 20.1201) occupational

dose limits for adults. An associated Non-Cited Violation of 10 CFR 20.1501 was

identified for the failure to conduct an adequate survey to ensure proper control of

7 Enclosure

radioactive material as required by 10 CFR Part 20, Subpart I, Storage and Control of

Licensed Material (Section 2PS3).

B. Licensee-Identified Violation

A violation of very low safety significance which was identified by the licensee has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and corrective

actions are listed in Section 4OA7 of this report.

8 Enclosure

Report Details

Summary of Plant Status

Unit 2 began the inspection period at 912 MWe (100 percent of rated electrical capacity).

  • On August 13, 2004, a controlled shutdown began for a forced outage for the purpose

of repairing a crack on the generator footing. The unit was returned online

August 21, 2004. The unit did not achieve full power because of vibration on the

  1. 9 turbine bearing.
  • On September 18, 2004, a controlled shutdown began for a forced outage for the

purpose of repairing the main turbine generator. The unit was returned online

September 25, 2004.

Unit 3 began the inspection period at 912 MWe (100 percent of rated electrical capacity).

  • On several occasions throughout the inspection period, load was reduced to perform

control rod adjustments, with the unit returning to full load during the same day.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R04 Equipment Alignment (71111.04Q&S)

.1 Partial System Walkdowns

a. Inspection Scope

The inspectors selected a redundant or backup system to an out-of-service or degraded

train, reviewed documents to determine correct system lineup, and verified critical

portions of the system configuration. Instrumentation valve configurations and

appropriate meter indications were also observed. The inspectors observed various

support system parameters to determine the operational status. Control room switch

positions for the systems were observed. Other conditions, such as adequacy of

housekeeping, the absence of ignition sources, and proper labeling were also

evaluated.

The inspectors performed partial equipment alignment walkdowns of the:

9 Enclosure

b. Findings

No findings of significance were identified.

.2 Complete System Walkdown

a. Inspection Scope

The inspectors performed one complete semiannual walkdown of the Unit 3 control rod

drive system. The inspectors reviewed the electrical and mechanical system checklist

and drawings to ensure all vital components in this system were energized. The

inspectors reviewed outstanding work orders associated with the system to determine

whether there were any deficiencies that could affect the ability of the system to perform

its safety-related function. The inspectors also reviewed all temporary modifications and

operator workarounds to verify the operational impact on the system. The inspectors

reviewed licensee condition reports (CRs) and issue reports (IRs), to verify past issues

that had been identified and their corrective actions.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Routine Inspection (Quarterly)

a. Inspection Scope

The inspectors toured plant areas important to safety to assess the material condition,

operating lineup, and operational effectiveness of the fire protection system and

features. The review included control of transient combustibles and ignition sources, fire

suppression systems, manual fire fighting equipment and capability, passive fire

protection features, including fire doors, and compensatory measures. The following

areas were walked down:

  • Unit 2 reactor building, elevation 589' isolation condenser area,

(Fire Zone 1.1.2.5.A);

  • Unit 3 reactor building, elevation 589' isolation condenser area,

(Fire Zone 1.1.1.5.A);

  • Unit 2 turbine building, elevation 469'-6" condensate pumps (Fire Zone 8.2.1.A);
  • Unit 2 turbine building, elevation 495' containment cooling service water pumps

(Fire Zone 8.2.2.A);

  • Unit 2 turbine building, elevation 517' diesel generator (Fire Zone 9.0A);
  • Unit 3 turbine building, elevation 495' containment cooling service water pumps

(Fire Zone 8.2.2.B);

  • Unit 3 turbine building, elevation 469'-6" condensate pumps (Fire Zone 8.2.1.B);
  • Unit 2 reactor building, isocondenser pipe chase (3 valve room), elevation

545'-6" (Fire Zone 1.1.2.5.c); and

  • Unit 3 reactor building, elevation 545'-6" (Fire Zone 1.1.1.3).

10 Enclosure

b. Findings

No findings of significance were identified.

.2 Weekly Fire Marshal Walkdown

a. Inspection Scope

The inspectors accompanied the Unit 3 field supervisor during a weekly fire marshal

walkdown of the Unit 2 and Unit 3 reactor and turbine buildings. The inspectors

observed that the field supervisor checked hot work activities in progress, general fire

protection housekeeping, fire protection equipment was not blocked and appeared to be

in good working order, fire doors and dampers were in good condition, and emergency

lights appeared to be in good working order.

b. Findings

No findings of significance were identified.

1R06 Flood Protection (71111.06)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report flood analysis

documents and reviewed the licensees procedures for external flooding. The

inspectors reviewed the licensees procedures for external flooding for ensuring proper

safe shutdown of the plant, and reviewed the licensees previously implemented

corrective actions for deficiencies associated with flood protection.

b. Findings

Introduction: The inspectors identified a Non-Cited Violation of 10 CFR 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, having very low safety

significance (Green) for the failure to develop adequate surveillance test and operating

procedures for equipment that was the sole source of makeup water to the isolation

condensers for both units during a design basis flood.

Description: Dresden Updated Final Safety Analysis Report (UFSAR) Section 2.4.3

stated that the NRC concluded in Systematic Evaluation Program (SEP) Topic II-3.B

that a flow of 490,000 cubic feet per second in the Illinois River would result in a still

water flood elevation of 525 feet. Adding wave runup to the stillwater flood elevation

yields a site probable maximum flood (PMF) elevation of 528 feet. This is about 11 feet

above grade. Water at this height puts all emergency core cooling system equipment

under water. Therefore, the sole sources of decay heat removal for both units would be

the isolation condensers. After initiation, make up water eventually needs to be added

to the shell side of the isolation condenser.

The UFSAR Section 3.4.1.1, External Flood Protection Measures, stated that if

forecasted flood levels exceed 517 feet, 150 gallon per minute emergency makeup

11 Enclosure

pumps are connected to the fire system. The UFSAR did not say why the pumps were

to be connected. Procedure DOA 0010-04, Floods, Revision 16, stated that a portable

diesel driven pump will be brought into the reactor building, hoisted into the air, and

connected to the fire main system to supply makeup water to the isolation condensers.

The inspectors reviewed the 10 CFR 50.59 screening performed for the procedure

change that went from four gasoline powered pumps to one diesel driven pump. The

10 CFR 50.59 screening did not address the change in the number and type of pumps.

This is an unresolved item pending NRC review of the licensees planned corrective

action to perform a 10 CFR 50.59 evaluation and subsequent revision to UFSAR

Section 3.4.1.1. (URI 05000237/2004010-01; 05000249/2004010-01)

Calculation DRE99-0035, Capacity and Discharge Head For Portable Isolation

Condenser Make-up Pump To Be Used During Flood Conditions, Revision 2,

conservatively assumes that the portable make-up pump to the isolation condensers

would be required to remove the decay heat 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> after reactor shutdown is reached.

The calculation concludes that, in order to supply sufficient makeup flow, the portable

pump must be able to supply 174 gallons per minute per reactor at a discharge head of

263 feet. The vendor manual DRE VTIP MANL GC43-001, Godwin Pumps HL80 M

Dri-Prime Pump Operating and Maintenance Manual, Revision 3, shows in Figure 6

that the pump can produce this amount of flow at the required head, but only at a speed

of 2400 rpm.

The NRC identified on June 5, 2002, that this pump was not routinely tested; and

therefore, its capability to perform its function during a flood was suspect. This was

identified in CR 111005. Assignment 5 from CR 111005 was to evaluate the

preventative maintenance and surveillances that should be performed relating to the

emergency diesel pump and other activities associated with DOA 0010-04. This was

completed on September 10, 2002. The licensee developed and implemented

DOS 1300-04, Operation Of The Isolation Condenser External Flood Emergency

Make-up Pump, on April 24, 2003. Per the surveillance test, DOS 1300-04, Revision 2,

Step I.2.g, the pump is run at a speed of 1800 rpm. Therefore the surveillance test does

not evaluate the ability of the pump to run at the speed (2400 rpm) necessary for the

pump to perform its function.

Page 9 of Calculation DRE99-0035 states that the timetable for the licensing basis flood

is given in Technical Evaluation Report (TER) C5257-421, Hydrological

Considerations, dated May 7, 1982. The report concludes that the flood waters will rise

from 509 feet to 517 feet in 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> assuming dam gates open to 16 feet. The

Technical Requirements Manual and Procedure DOA 0010-04 both require that both

units shutdown when the river elevation reaches 509 feet. Therefore, the amount of

water needed for the isolations condensers is based on decay heat 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> after

shutdown.

As mentioned above, the required amount of flow to the isolation condenser to remove

decay heat 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> after shutdown would require a diesel driven pump speed of

2400 gpm. Procedure DOA 0010-04 has no mention as to what speed the diesel driven

pump should or can be run. Procedure DOA 0010-04, Step D.14.f stated, adjust the

throttle to increase flow. The inspectors conducted an interview with members of the

12 Enclosure

non-licensed operator training staff that conducted training on the diesel driven pump to

be used during a flood. The inspectors asked if given the flood scenario, at what speed

would you operate the pump? One trainer stated that given the surveillance (DOS

1300-04) has the operator test the pump at 1800 rpm he would run the pump at that

speed. The inspectors asked if no water was flowing at that speed what would you do?

Both trainers responded that the pump would be secured and a valve lineup would be

performed.

Procedure DOA 0040-02, Localized Flooding In Plant, Revision 15, Step A.1.a, stated

that for the isolation condenser external flood emergency make-up pump, The

maximum vertical suction lift from water source to pump impeller cannot be in excess of

27 feet. The inspectors requested that system engineering personnel check the length

of the suction hose. The system engineer informed the inspectors that the suction hose

was 30 feet long. Procedure DOA 0010-04, Step D.9.i, states, Using the Rx Building

Crane, raise the emergency make-up pump to between 12 and 15 feet above the floor;

and Step D.17, states, WHEN water recedes to below EL 518 ft, THEN relocate suction

hose from diesel-driven emergency make-up pump to draw water from the nearest

ECCS [emergency core cooling system] corner room. The inspectors verified that the

distance between the location of the pump impeller when the pump is hoisted into the air

and the ECCS corner room was greater than 30 feet. This means there would be no

suction source for the pump once the water started to recede.

Technical Evaluation Report (TER) C5257-421 was prepared for the NRC by the

Franklin Research Center to evaluate the effects of flooding on Dresden Unit 2. This

TER points out that normal reactor cooling procedures will not ensue immediately

following the time flood waters drop below elevation 509, consequently the operation of

the gasoline-driven pumps will be required for a significant period of time, i.e., more than

3 days. The licensee did not estimate how long the diesel driven pump may be

needed; and therefore, did not estimate how much fuel for the diesel driven pump

needed to be pumped into barrels and staged in the reactor building in advance. The

licensee does not know how long the flooding might impact the site and how much fuel

might be needed to be staged in advance.

Analysis: The inspectors determined that the failure to implement adequate surveillance

test and abnormal operating procedures that provided instructions to ensure an

adequate supply of make-up water to the isolation condenser during flood conditions to

prevent core damage was a performance deficiency warranting a significance evaluation

in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, issued on June 20, 2003. The inspectors determined that the finding was

more than minor because it (1) involved the equipment performance and procedure

quality attributes of the mitigating systems cornerstone and (2) affected the cornerstone

objective of ensuring the reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. The inspectors also determined that the

failure to implement an adequate surveillance test procedure after it was identified that

there was no test procedure in 2002, also affected the cross-cutting area of Problem

Identification and Resolution.

The inspectors determined that the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, Appendix A, dated

13 Enclosure

September 10, 2004, because the finding was associated with the reliability of a

mitigating system. The inspectors concluded that the diesel driven make-up pump

would be a mitigating system in the case of the PMF. For the Phase 1 screening, the

inspectors answered No to the first four questions under the mitigating systems

column. The inspectors then went to the Phase 1 worksheet for Seismic, Fire, Flooding,

and Severe Weather Criteria. Question 1 was answered Yes. Question 2.c was

answered Yes. Returning to Question 5 under the mitigating systems on the Phase 1

screening sheet this question was answered Yes and referred to the Regional Office

for a Phase 3 analysis. The Phase 3 analysis performed by the Senior Reactor Analyst

(SRA) concluded that the safety significance of this finding based on the change in core

damage frequency to be Green. The Phase 3 analysis reviewed the potential failure

probabilities based on the procedure and equipment inadequacies. The SRA, in

discussions with the licensee and the resident inspectors, determined that based on the

low initiating event probability, and because of the slow onset of the flooding and the

reduced decay heat in the reactor core at the time recovery actions would be necessary,

the licensee would be able to reasonably perform recovery actions that would prevent

core damage. A Green finding represents a finding of very low safety significance.

Enforcement: The inspectors identified that the licensee did not have procedures

appropriate to the circumstances of external plant flooding on June 5, 2004. The failure

to have procedures appropriate for the circumstances of a PMF was a violation of

10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, which

states in part, Activities affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances...

Contrary to the above, on June 5, 2004, (1) surveillance procedure DOS 1300-04,

Revision 2, for the portable diesel driven isolation condenser make-up pump did not test

the diesel at the speed (2400 rpm) necessary to deliver the minimum amount of flow to

make up to the isolation condensers in the event of a flood; (2) abnormal operating

procedure DOA 0010-04, Revision 16, did not specify the minimum required speed of

the diesel driven make-up pump for the operators; (3) the suction hose from the pump

was too short to successfully accomplish the step in procedure DOA 0040-02,

Revision 15, that directed the operators to move the suction hose to the nearest corner

room when the flood waters started to recede; and (4) none of the procedures specified

how much fuel oil was necessary to be staged on the 545 foot level of the reactor

building prior to the onset of flooding. The licensee planned to change the surveillance

test procedure DOS 1300-04 to run the pump at 2400 rpm and perform a full flow test of

the pump in the near future. The licensee planned to review DOA 0010-04 and revise

the procedure as appropriate. Because this issue is of very low safety significance and

has been entered into the licensees corrective action program (Issue Reports, 246038

and 261167), this violation is being treated as a Non-Cited Violation, consistent with

Section VI.A., of the NRC Enforcement Policy. (NCV 05000237/2004010-02;

05000249/2004010-02)

14 Enclosure

1R11 Licensed Operator Requalification (71111.11Q)

a. Inspection Scope

The inspectors observed an evaluation of an operating crew on September 27, 2004.

The scenario consisted of a recirculation flow controller failure, a reactor building closed

cooling water pump trip, an instrument line break in the drywell which required flooding

of the reactor pressure vessel, and a failure of a core spray pump. The inspectors

verified that the operators were able to complete the tasks in accordance with applicable

plant procedures and that the success criteria as established in the job performance

measures were satisfied. The inspectors observed the licensees evaluators to ensure

that no inappropriate cues were provided by the evaluators while assessing the

operators' performance. In addition, the inspectors verified that condition reports written

regarding licensed operator requalification training were entered into the licensees

corrective action program with the appropriate significance characterization.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed the licensees overall maintenance effectiveness for

risk-significant mitigating systems. The inspectors also reviewed whether the licensee

properly implemented the Maintenance Rule, 10 CFR 50.65, for the systems.

Specifically, the inspectors determined whether:

  • performance problems constituted maintenance rule functional failures;
  • the systems have been assigned the proper safety significance classification;
  • the systems were properly classified as (a)(1) or (a)(2); and
  • the goals and corrective actions for the systems were appropriate.

The above aspects were evaluated using the maintenance rule program. The

inspectors also verified that the licensee was appropriately tracking reliability and/or

unavailability for the systems.

The inspectors reviewed the following systems:

b. Findings

Introduction: The inspectors identified a Non-Cited Violation (NCV) of 10 CFR 50.65

having very low safety significance (Green) for failing to adequately implement the

15 Enclosure

maintenance rule. The licensee failed to move the reactor building ventilation system to

category (a)(1) monitoring of 10 CFR 50.65 after exceeding the performance criteria

established for reliability of four functional failures in 2 years.

Description: The licensee was not able to maintain a .25-inch vacuum in the secondary

containment relative to atmosphere on June 19, 2002, June 24, 2002, July 31, 2002,

October 24, 2003, March 7, 2004, April 24, 2004, and July 22, 2004. On each date the

differential pressure was positive for less than the Technical Specification (TS) 3.6.4.1.1

Limiting Condition For Operation time. The licensees maintenance rule program

considered a positive pressure in the secondary containment as a functional failure of

the reactor building ventilation system. These events were not properly addressed by

the licensees corrective action program. The July 31, 2002 event was documented in

the operators logs but no condition report was written. The April 24, 2004 event was

entered into the corrective action program as CR 216750, and was coded as a

maintenance rule functional failure but was not counted as a maintenance rule

functional failure.

The licensee had not established a repair or replacement program for the reactor

building ventilation exhaust fan back-draft damper actuator springs. The springs

provided the motive force for the back-draft dampers. The damper vendor

recommended replacement of the springs within 10 years. The actuator springs were

18 years old. As a result of spring relaxation, the Unit 2A and 2C exhaust fan back-draft

dampers would only open about 5 percent, resulting in a failure to maintain the .25 inch

vacuum.

The licensees performance criteria for the reactor building ventilation system,

established in the maintenance rule database program, stipulated that more than four

functional failures in 2 years required transfer of the reactor building ventilation system

to 10 CFR 50.65 Section (a)(1) monitoring from Section (a)(2). The licensee had five

functional failures between July 31, 2002, and July 22, 2004, and six functional failures

between June 19, 2002, and April 24, 2004. The licensee did not move the reactor

building ventilation system to (a)(1).

Analysis: The inspectors determined that the failure to correctly enter the events into

the corrective action program which resulted in the failure to move the reactor building

ventilation system from 10 CFR 50.65 Section (a)(2) to (a)(1) was a performance

deficiency warranting a significance evaluation in accordance with IMC 0612, Power

Reactor Inspection Reports, Appendix B, Issue Screening, issued on June 20, 2003.

The inspectors determined that the finding was more than minor because it:

(1) involved the design control and barrier performance attributes of the barrier integrity

cornerstone; and (2) affected the cornerstone objective of providing reasonable

assurance that physical design barriers protect the public from radionuclide releases

caused by accidents or events. The inspectors determined that the finding also affected

the cross-cutting area of Problem Identification and Resolution.

The inspectors determined that the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, Appendix A,

Determining the Significance of Reactor Inspection Findings for At-Power Situation,

dated September 10, 2004, because the finding was associated with a degraded reactor

16 Enclosure

building containment barrier. For the Phase 1 screening, the inspectors answered Yes

to Question 1 under the Containment Barriers Cornerstone column because the finding

only represents a degradation of the radiological barrier function of the reactor building.

The finding screened as Green.

Enforcement: Section (a)(2) of 10 CFR 50.65 stated, in part, that monitoring as

specified in paragraph (a)(1) is not required where it has been demonstrated that the

performance of a structure, system, or component is being effectively controlled through

the performance of appropriate preventive maintenance, such that the structure,

system, or component remains capable of performing its intended function. The

licensees performance criteria for the reactor building ventilation system, established in

the maintenance rule database program, stipulated that more than four functional

failures in 2 years required transfer of the reactor building ventilation system to 10 CFR

50.65 Section (a)(1) monitoring from Section (a)(2). The licensee had five functional

failures between July 31, 2002 and July 22, 2004 and six functional failures between

June 19, 2002 and April 24, 2004. The functional failures were due to inappropriate

preventative maintenance. The licensee did not move the reactor building ventilation

system to (a)(1) until the inspectors identified this issue. The licensee convened a

maintenance rule evaluation panel on October 8, 2004, and moved the reactor building

ventilation system to (a)(1). System goals have not yet been established. Because this

violation was of very low safety significance and because it was entered into the

corrective action program (Issue Report 256499), this violation is being treated as a

Non-Cited Violation, consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000237/2004010-03; 05000249/2004010-03)

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors evaluated the effectiveness of the risk assessments performed before

maintenance activities were conducted on structures, systems, and components and

verified how the licensee managed the risk. The inspectors evaluated whether the

licensee had taken the necessary steps to plan and control emergent work activities.

The inspectors also verified that equipment necessary to complete planned contingency

actions was staged and available. The inspectors completed evaluations of

maintenance activities on the:

  • Unit 3, 250 VDC battery jumpering of cell 113;
  • Unit 2, Div I, LPCI, replace/regrease auxiliary contact in MCC 28-1,

Valves 2-1501-3A/2-1501-18A/2-150138A;

  • Unit 2/3, B train, standby gas treatment planned maintenance; and

b. Findings

No findings of significance were identified.

17 Enclosure

1R15 Operability Evaluations (71111.15)

.1 Routine Operability Evaluation (OE) Reviews

a. Inspection Scope

The inspectors reviewed operability evaluations to ensure that operability was properly

justified and the component or system remained available, such that no unrecognized

increase in risk occurred. The review included issues involving the operability of:

Some Safe Shutdown Events Assumed in the Licensing Basis Due to Water

Intrusion into the HPCI Steam Line (OE 04-002);

  • Unit 3 Containment Cooling Service Water Back-Up Keep Fill Line is not

Supported per Code Allowance (OE 04-006);

  • Units 2 & 3 CR105X Dried Grease Could Degrade Operation of Contactor

(OE 04-004);

  • Units 2 & 3 Electromatic Relief Valve Discharge Flanges (OE 03-013, Rev. 1);
  • IR 00245395, "NRC Concern With Reactor Level Density Error;"
  • Low Unit 2 Switchyard Voltage on August 23, and September 14, 2004;
  • Unit 2 & 3 2A and 3C Condenser Bay Vacuum Indication/Switch Sometimes

Indicates a Non-conservative Value after a Flow Reversal to East-to-West Flow

(OE 04-008, Revision 1).

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modification (7111.17A)

a. Inspection Scope

The inspectors reviewed one permanent plant modification to verify the design

adequacy to ensure licensing and design bases were maintained, and to ensure

functionality of interfacing structures, systems, and components. The modification

reviewed included the following:

  • Replacement of Standby Gas Treatment Solenoid Valve 2/3-7541-43B on

AO-7510-B.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing (71111.19)

18 Enclosure

a. Inspection Scope

The inspectors reviewed post-maintenance test results to confirm that the tests were

adequate for the scope of the maintenance completed and that the test data met the

acceptance criteria. The inspectors also reviewed the tests to determine if the systems

were restored to the operational readiness status consistent with the design and

licensing basis documents. The inspectors reviewed post-maintenance testing activities

associated with the following:

  • Unit 3, 250 VDC Battery Jumpering of Cell 113;
  • Testing of the 3B Core Spray Following 2Y EQ GE Pump Motor Maintenance;
  • Unit 2/3, B train, Standby Gas Treatment, Testing of Valve Operator 2/3-7507-

B Following Preventive Maintenance on Limitorque; and

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities (71111.20)

.1 Unit 2 Forced Maintenance Outage August 2004

a. Inspection Scope

On August 14, 2004, the licensee commenced a 6-day forced maintenance outage.

The licensee identified a crack on a weld on one of the main turbine generator support

footings. General Electric, while performing a review of Unit 2 main turbine vibrations,

informed the station of a concern that the crack could propagate into the generator

housing. Since the generator is cooled by hydrogen the result could have possibly led

to an escape of hydrogen leading to the potential for a fire and/or explosion. General

Electric recommended the shutdown of Unit 2 until the crack could be repaired.

The inspectors verified that the licensee effectively conducted the shutdown, managed

elements of risk pertaining to reactivity control during and after the shutdown, and

implemented decay heat removal system procedure requirements as applicable.

The inspectors performed the following activities daily:

  • attended control room operator turnover meetings to verify that the current

shutdown risk status was well understood and communicated;

  • performed walkdowns of the main control room to observe the alignment of

systems important to shutdown risk;

  • reviewed selected issues that the licensee entered into its corrective action

program to verify that identified problems were being entered into the program

with the appropriate characterization and significance;

  • ensured that the licensee appropriately considered risk factors during the

development and execution of planned activities;

19 Enclosure

  • monitored licensees troubleshooting efforts for emergent plant equipment

issues;

  • performed plant walkdowns to observe ongoing work activities;
  • conducted in-office reviews of selected issues that the licensee entered into its

corrective action program to verify that identified problems were being entered

into the program with the appropriate characterization and significance;

  • observed control rod withdrawals and initial transition to criticality; and
  • monitored mode switch changes and observed portions of power ascension.

b. Findings

No findings of significance were identified.

.2 Unit 2 Maintenance Outage September 2004

During the Unit 2 outage in August 2004, the licensee attempted to reduce vibrations on

the number 9 turbine bearing by realigning the main generator. That effort was

unsuccessful. Unit 2 generator vibrations were still high at a lower power level than

those seen previous to the August outage. Unit 2 was shutdown again on

September 18, 2004, for a scheduled 26 day outage in order to send the generator

offsite to be rewound. Testing during the shutdown convinced licensee management

that the actual problem causing the high vibration was soft foot conditions (foundation

not as firm as it should be) under three of the eight generator support structures. The

licensee repaired the soft conditions and added balancing weights to the main generator

rotor. The unit was restarted and returned to full power on September 26, 2004.

The inspectors performed the following activities daily:

  • attended control room operator turnover meetings to verify that the current

shutdown risk status was well understood and communicated;

  • performed walkdowns of the main control room to observe the alignment of

systems important to safe/shutdown risk condition;

  • monitored licensees troubleshooting efforts for emergent plant equipment

issues, specifically the failure of 2-2301-7, high pressure coolant injection (HPCI)

testable discharge check valve to pass its cold shutdown surveillance;

  • performed a drywell closeout walkdown;
  • observed control rod withdrawals and initial transition to criticality; and
  • monitored mode switch changes and observed portions of power ascension.

b. Finding

Introduction: The inspectors identified a Non-Cited Violation (NCV) of TS 5.4.1 having

very low safety significance (Green) for failing to lock open Valve 2-0220-57B,

Feedwater Manual Isolation Valve.

Description: The inspectors identified during a drywell closeout of Unit 2, on

September 23, 2004, that Valve 2-0220-57B was not locked open as required by

out-of-service checklist 31383 performed on September 22, 2004. The licensee had

taken 2-0220-57B out-of-service closed during the outage to perform corrective

20 Enclosure

maintenance on the 2-2301-7, high pressure coolant injection (HPCI) discharge check

valve. The inspectors verified that 2-220-57B was open, but the locking device was

wrapped around the valve yoke and not the valve handwheel. Valve 2-220-57B was in

the flow path for HPCI injection and B train of feedwater.

Analysis: The inspectors determined that failing to lock the valve open was an operator

performance deficiency warranting a significance evaluation in accordance with

IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition

Screening, issued on June 20, 2003. The inspectors determined that the finding was

more than minor because it affected the configuration control and human performance

attributes of the Mitigating Systems cornerstone; and affected the cornerstone objective

of ensuring the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. In addition, this was not the first time the

NRC identified drywell valves that were in the correct position but not locked per

licensee procedure. During the Unit 2 refueling outage drywell close out on

November 9, 2003, the inspectors identified that the two reactor head vent valves

2-0299-59 and 2-0299-60 were closed but not locked closed per licensee procedure.

This was documented in Condition Report 185823. Regarding Valve 2-220-57B,

licensee management personnel stated that, when interviewed, the operators stated that

the valve was difficult to open and when they finished they forgot to lock the valve. The

individuals did not have a copy of the clearance order checklist with them in the drywell

in an effort to reduce dry active waste. However the operators were briefed prior to the

task and the clearance checklist clearly stated the valve was to be locked. Therefore,

this finding also affected the cross-cutting area of Human Performance.

The inspectors completed a significance determination of this issue using IMC 0609,

Significance Determination Process (SDP), Appendix A, Determining the Significance

of Reactor Inspection Findings for At-Power Situations, dated September 10, 2004. For

Phase I screening the inspectors answered No to Question 1 under Mitigating Systems

Cornerstone because the finding did not result in a loss of function for either the

feedwater or HPCI systems. The finding screened as Green.

Enforcement: Technical Specification 5.4.1 required, in part, that written procedures

shall be established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, Paragraph 1.c

recommends procedures for equipment control (e.g., locking and tagging). One of the

equipment control procedures that implemented this TS was OP-MW-109-101,

Clearance and Tagging, Revision 2. Step 10.4.1.5.A, stated, PLACE equipment in

the positions/conditions specified on the clearance checklist. Clearance Checklist

31383 Step 18, required valve 2-220-57B to be locked in the open position. The

operators opened but did not lock the valve in the required position. The valve was in

the open but unlocked position for less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The non-licensed operators were

temporarily removed from shift duties and a fact finding review was scheduled for

completion after the end of the inspection period. The individuals were counseled. The

licensee planned to require carrying clearance checklists into the drywell in the future.

Because this violation was of very low safety significance and it was entered into the

licensees corrective action program (Issue Report 256029), this violation is being

21 Enclosure

treated as a Non-Cited Violation, consistent with Section VI.A of the NRC Enforcement

Policy. (NCV 05000237/2004010-04)

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors observed surveillance testing on risk-significant equipment and reviewed

test results. The inspectors assessed whether the selected plant equipment could

perform its intended safety function and satisfy the requirements contained in TSs.

Following the completion of each test, the inspectors determined that the test equipment

was removed and the equipment returned to a condition in which it could perform its

intended safety function.

The inspectors observed surveillance testing activities and/or reviewed completed

packages for the tests, listed below, related to systems in the Initiating Event, Mitigating

Systems, and Barrier Integrity Cornerstones:

  • DIS 0500-06, Rev. 20, Condenser Low Vacuum Pressure Switches Channel

Calibration and Channel Functional Test;

Functional Testing;

  • Emergency Relief Valve Pressure Switches; and
  • Unit 2/3, B Train, Standby Gas Treatment, Preventative Maintenance

Surveillance on Limitorque Valve Operator 2/3-7504-B.

1R23 Temporary Modification (71111.23)

a. Inspection Scope

The inspectors screened three active temporary modifications and assessed the effect

of the temporary modifications on safety-related systems. The inspectors also

determined if the installation was consistent with system design:

  • Temporary Configuration Change Package No. 347984, Revision 1, Install

Temporary Recorder to Monitor Unit 2 Steam Dryer Parameters;

  • Control room ventilation system as called for in DOA 5750-01; and
  • Temporary Configuration Change Package No. 349028, Revision 0, Install

Bleeder Valve on the Unit 3 C Condenser Hood Low Vacuum Sensing Line to

Prevent Moisture Buildup.

b. Findings

No findings of significance were identified.

22 Enclosure

1EP6 Drill and Training Evaluations (71114.06)

September 27, 2004, Emergency Preparedness Performance Indicator Drill

a. Inspection Scope

The inspectors observed station personnel during a licensee only participation

emergency preparedness drill exercise on September 27, 2004, to determine the

effectiveness of drill participants and the adequacy of the licensees critique in

identifying weaknesses and failures. The drill scenario involved failure of the master

recirculation flow controller, trip of the 2A reactor building closed cooling water pump, a

break in an instrument line in the drywell, and failure of the core spray pump.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Public Radiation Safety

2PS3 Radiological Environmental Monitoring Program (REMP) And Radioactive Material

Control Program (71122.03)

.1 Inspection Planning - Reviews of Radiological Environmental Monitoring Reports and

Data

a. Inspection Scope

The inspectors reviewed the 2002 and 2003 Annual Radiological Environmental

Operating Reports, the results of monthly radiological environmental monitoring

analyses for January through May 2004, and the most recent licensee assessment

results to verify that the REMP was implemented as required by TSs and the Offsite

Dose Calculation Manual (ODCM). The inspectors reviewed the radiological

environmental reports for changes to the ODCM with respect to environmental

monitoring, commitments in terms of sampling locations, monitoring and measurement

frequencies, land use census, the sample analysis vendors inter-laboratory comparison

program, and analysis of radiological environmental sample data. The inspectors

reviewed the ODCM to identify the environmental monitoring stations and evaluated the

locations of these stations and the types of samples collected from each to determine if

they were consistent with the ODCM and NRC guidance in Regulatory Guide 1.21,

Measuring, Evaluating, and Reporting Radioactivity in Solid Wastes and Releases of

Radioactive Materials in Liquid and Gaseous Effluents from Light Water Cooled Nuclear

Power Plants, and in Regulatory Guide 4.8, Environmental TSs for Nuclear Power

Plants. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) for

information regarding the monitoring program and the Emergency Response Plan for

information regarding meteorological monitoring instrumentation to determine whether

the environmental monitoring program was developed consistent with its design basis.

23 Enclosure

The inspectors reviewed the scope of the licensees audit program to verify that it met

the requirements of 10 CFR 20.1101(c).

These reviews represented one inspection sample.

b. Findings

No findings of significance were identified.

.2 Onsite Inspection Activities

a. Inspection Scope

The inspectors walked-down all eight indicator environmental air sampling stations, the

sole control station, both operable special air sampling stations, and approximately

25 percent of the thermoluminescence dosimeter (TLD) monitoring stations. The

walkdowns were performed to determine whether these environmental stations were

located as described in the ODCM, to assess equipment material condition and

operability, and to verify that environmental station orientation relative to plant effluent

release points, vegetation growth control, and equipment configuration allowed for the

collection of representative samples.

The inspectors accompanied the REMP contract technician and observed the collection

and change-out of air particulate and charcoal cartridges at each air sampling station

and observed the collection of surface water samples to determine whether appropriate

practices were used to ensure sample integrity and to verify that sampling techniques

were in accordance with the licensees procedures.

The meteorological tower was walked down by the inspectors to verify it was adequately

sited and that instrumentation was installed consistent with Regulatory Guide 1.23,

Meteorological Programs in Support of Nuclear Power Plants. The inspectors verified

that the meteorological instruments were operable, calibrated, and maintained in

accordance with the Emergency Response Plan, the guidance provided in NRC Safety

Guide 23, and applicable licensee procedures. The inspectors compared real-time data

collected at the meteorological tower versus the time-averaged data transmitted to the

control room to verify data integrity.

The inspectors reviewed each event documented in the Annual Environmental

Monitoring Reports which involved a missed sample, inoperable sampler, lost TLD, or

anomalous measurement for the cause and corrective actions and conducted a review

of the licensees assessment of any positive sample results (i.e., licensed radioactive

material detected above the lower limits of detection (LLDs)).

The inspectors reviewed sampler station modifications since the last inspection and/or

significant changes made by the licensee to the ODCM as dictated by the 2002 or

2003 land use census. The inspectors reviewed technical justifications for changed

sampling locations. The inspectors verified that the licensee performed the reviews

required to ensure that the changes did not affect its ability to monitor the impacts of

radioactive effluent releases on the environment.

24 Enclosure

The inspectors reviewed the calibration and maintenance records for all indicator,

control and special environmental air samplers, focusing on the air flow meter and

particulate filter/charcoal cartridge components. Additionally, records of the most recent

full calibration for each of the two field rotameters and for the master rotameter used by

the licensee to measure and validate air sample pump flow rates was reviewed to

ensure traceability to the National Institute of Standards and Technology. As the

licensee does not conduct analyses of REMP samples on-site and utilizes a vendor

laboratory to provide analytical services, the inspectors did not review licensee

calibration records for environmental sample radiation measurement instrumentation

(i.e., count room equipment) or quality control charts.

The inspectors reviewed the results of the REMP sample vendors quality control

program including the inter-laboratory comparison program to verify the adequacy of the

vendors program and the corrective actions for any identified deficiencies. The

inspectors reviewed the LLD values achieved by the vendor laboratory for all REMP

required sample media to verify that analytical detection capabilities met ODCM

requirements for each environmentally monitored pathway. The inspectors reviewed the

report of the last quality assurance audit of the radiological environmental monitoring

program to determine whether the licensee met its TS/ODCM requirements.

These reviews represented six inspection samples.

b. Findings

No findings of significance were identified.

.3 Unrestricted Release of Material from the Radiologically Controlled Area (RCA)

a. Inspection Scope

The inspectors observed locations where the licensee typically monitors potentially

contaminated material and individuals leaving the RCA, and evaluated the procedures

and practices used for control, survey, and release of materials and workers from these

areas. The inspectors questioned several radiation protection staff responsible for the

performance of personnel surveying and releasing material for unrestricted use to

assess their knowledge of procedures and protocols and to verify that release surveys

are performed appropriately.

The inspectors assessed the radiation monitoring instrumentation used for both the

unrestricted release of workers and material/equipment from the RCA, to determine if it

was appropriate for the radiation types present and was calibrated with radiation

sources consistent with the plants nuclide mix. The inspectors reviewed the licensees

criteria for the survey and release of potentially contaminated material and workers to

verify that there was guidance on how to respond to an alarm which indicates the

potential presence of licensed radioactive material. The inspectors reviewed the

licensees radiation survey equipment to ensure the radiation detection sensitivities were

consistent with the NRC guidance for surface contamination contained in Circular 81-07,

Control of Radioactively Contaminated Material, and Information Notice 85-92, Survey

of Wastes Before Disposal from Nuclear Reactor Facilities, and with Health Physics

25 Enclosure

Positions (position-221) in NUREG/CR-5569 for volumetrically contaminated material.

The inspectors reviewed the licensees program to determine if it adequately identified

and evaluated the impact of difficult-to-detect radionuclides (i.e., those that decay via

electron capture) and accounted for those nuclides during routine unrestricted release

surveys. The inspectors reviewed the licensees procedures and records to verify that

the radiation detection instrumentation was used at its typical sensitivity level based on

appropriate counting parameters (i.e., counting times and background radiation levels).

The inspectors verified that the licensee had not established a release limit by altering

the instruments typical sensitivity through such methods as raising the energy

discriminator level or locating the instrument in a high radiation background area.

Additionally, the inspectors reviewed the circumstances associated with the

unconditional release of a workers contaminated boot in September/October 2002, that

was subsequently identified when the worker attempted to leave the Braidwood Nuclear

Station approximately 1 year later wearing those boots. Specifically, the inspectors

reviewed the licensees condition evaluation of the incident, reviewed radiation

protection (RP) procedures governing the unconditional release program, and discussed

the incident with RP staff. The inspectors also independently performed a dose

assessment to verify the adequacy of the occupational dose assigned to the worker that

wore the contaminated boot.

These reviews represented two inspection samples.

b. Findings

Introduction: A self-revealed finding of very low safety significance which involved a

Non-Cited Violation was identified for the failure to conduct an adequate radiological

survey of a workers footwear following a contamination monitor alarm, prior to its

unconditional release from the RCA. As a result, the licensee failed to detect a discrete

radioactive particle (DRP) embedded in a boot worn by a worker which allowed the

contaminated boot to be released unconditionally without any radiological restrictions.

Description: On October 16, 2003, a contract worker alarmed the portal radiation

monitor at the gatehouse upon attempting to depart the Braidwood Nuclear Station. The

cause of the alarm was later determined to be a DRP comprised primarily of cobalt-60

that was embedded (fixed) on the upper exterior portion of the individuals work boot.

The individual had not entered any RCAs since starting work at Braidwood 3 days

earlier and had not worked at a nuclear plant since October 2002. In September and

October 2002, the individual worked at the Dresden Station during their refueling outage

and was involved in reactor assembly/disassembly. The boots were worn exclusively for

work at nuclear plants and remained at the individuals residence when not being used.

An investigation by Dresden RP staff revealed that the individual had contaminated his

boots twice while at Dresden Station (September 18 and October 25, 2002) but was

allowed to leave the site with the boots after they were decontaminated and hand

surveyed by RP staff, and the worker subsequently cleared the personal contamination

monitor (PCM) at the RCA egress. The boots had remained at the station during the

individuals employment tenure at Dresden and were hand carried through the

gatehouse portal monitors on the workers final day onsite on October 25, 2002. Due to

26 Enclosure

the location and the quantity (90 nanocurie maximum) of radioactive material on the

workers boot and the type of radiation monitors used at Dresdens RCA and plant

egress locations, the DRP was probably not detected by these automated monitors.

Based on the licensees evaluation and the inspectors independent assessment of the

problem, the contaminated boot escaped detection by the licensee primarily because

the RP staff failed to conduct a thorough survey (hand-held instrument frisk) on one or

both of those occasions when the worker alarmed the automated PCM at the RCA

egress. Following a survey (frisk) of the worker and decontamination of the workers

boots by the RP staff, the worker was allowed to leave after successfully clearing a

PCM. The embedded DRP probably escaped detection by the PCM due to the type of

detectors used at the RCA egress and the location of the particle relative to the detector

geometry. The PCMs located at the contractor RCA egress used by the worker were

sensitive to beta-emitting radioactive material only and lacked gamma-sensitivity. The

DRP likely escaped gatehouse portal monitor detection because the worker hand-

carried the boots through the monitor in a less than optimal detection configuration.

Analysis: The inspectors determined that the licensee failed to conduct an adequate

survey following PCM alarms. As a result, the licensee did not detect a DRP that was

embedded on the workers boot. This failure represents a performance deficiency. The

inspectors determined that the issue was associated with the Program and Process

and Human Performance attributes of the Public Radiation Safety Cornerstone and

affected the cornerstone objective to ensure adequate protection of the public health

and safety from exposure to radioactive materials released into the public domain. Also,

the issue involved an occurrence in the licensees radioactive material control program

that was contrary to NRC regulations. Therefore, the occurrence represents a more

than minor issue which was evaluated using the significance determination process

(SDP) for the Public Radiation Safety Cornerstone.

The inspectors determined that the licensee failed to prevent the inadvertent release

and loss of control of licensed material outside the protected area that could have

potentially caused radiation dose to the public. Utilizing Manual Chapter (MC) 0609,

Appendix D, Public Radiation Safety SDP, the finding involved radioactive material

control but did not involve transportation, public radiation exposure was not greater than

0.005 rem total effective dose equivalent (TEDE) and the licensee did not have more

than five radioactive material control occurrences in the previous eight quarters. Based

on both the licensees and the inspectors independent dose assessments, the DRP did

not result in a TEDE dose (as defined in 10 CFR Part 20) to either the worker or a

member of the public greater than one mrem. Therefore, consistent with Section VI of

Appendix D to MC 0609, the finding is not suitable for SDP evaluation. The extremity

(foot) dose determined for the worker was conservatively calculated at 500 mrem or one

percent of the occupational dose limits of 10 CFR 20.1201. Based on the lack of public

dose consequence and the magnitude of the occupational dose to the worker, the

finding is determined to be of very low safety significance.

Enforcement: Title 10 CFR 20.1501 requires, in part, that surveys be made as

necessary to comply with the requirements of 10 CFR Part 20 to evaluate the quantities

of radioactive material, the magnitude of radiation levels, and the potential radiological

hazards. Subpart I of 10 CFR Part 20, Storage and Control of Licensed Material, and

27 Enclosure

specifically 10 CFR 20.1802 require that licensed material in an unrestricted area that is

not in storage be controlled. However, between September 18 and October 25, 2002,

the licensee failed to conduct adequate followup surveys of a worker that alarmed PCMs

upon attempting to leave the RCA. As a result, a DRP was released into the public

domain where it remained uncontrolled until detected at the Braidwood Station

approximately 1 year later. The failure to conduct adequate surveys following PCM

alarms is a violation of 10 CFR 20.1501 which led to a violation of 10 CFR 20.1802. The

finding is not suitable for SDP evaluation, but has been reviewed by NRC management

and is determined to be a Green finding of very low safety significance.

The licensee performed an apparent cause evaluation of this event, assessed the dose

to the worker and implemented adequate corrective action. These corrective actions

included tailgate training to radiation protection staff that respond to contamination

monitor alarms, improvements to RCA automated radiation monitors used at the main

RCA egress location via the installation of new gamma-sensitive monitors, and actions

to enhance gamma-sensitivity of those radiation monitors located at alternate RCA

egresses and at the gatehouse. Since the licensee documented this issue in its

corrective action program (condition report (CR) 181692) and because the violation is of

very low safety significance, its is being treated as a Non-Cited Violation.

(NCV 05000237/2004010-05; 05000249/2004010-05).

.4 Identification and Resolution of Problems

a. Inspection Scope

The inspectors reviewed the licensees self-assessments, audits and Special Reports,

as applicable, related to the radiological environmental monitoring and radioactive

material control programs since the last inspection to determine if identified problems

were entered into the corrective action program for resolution. The inspectors also

verified that the licensee's self-assessment and/or audit program was capable of

identifying repetitive deficiencies or significant individual deficiencies in problem

identification and resolution.

The inspectors also reviewed CRs related to the REMP and the radioactive material

control program since the previous inspection, interviewed staff and reviewed

documents to determine if the following activities were being conducted in an effective

and timely manner commensurate with their importance to safety and risk:

  • Initial problem identification, characterization, and tracking;
  • Disposition of operability/reportability issues;
  • Evaluation of safety significance/risk and priority for resolution;
  • Identification of repetitive problems;
  • Identification of contributing causes;
  • Identification and implementation of effective corrective actions; and
  • Implementation/consideration of risk significant operational experience feedback.

These reviews represented one inspection sample.

28 Enclosure

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES (OA)

4OA1 Performance Indicator Verification (71151)

.1 Initiating Events and Mitigating Systems

a. Inspection Scope

The inspectors reviewed a sample of plant records and data against the reported

Performance Indicators in order to determine the accuracy of the indicators:

Unit 2:

  • Heat Removal (Low Pressure Coolant injection/Containment Cooling Service

Water), July 2003 - 2004

  • Emergency AC Power System, April 2003 - September 2004
  • Safety System Functional Failure, July 2003 - September 2004

Unit 3:

  • Heat Removal (Low Pressure Coolant injection/Containment Cooling Service

Water), July 2003 - 2004

  • Emergency AC Power System, April 2003 - September 2004
  • Safety System Functional Failure, July 2003 - September 2004

b. Findings

No findings of significance were identified.

Cornerstone: Public Radiation Safety

.2 Radiation Safety Strategic Area

a. Inspection Scope

The inspectors sampled licensee submittals for the performance indicator (PI) listed

below for the period indicated. To verify the accuracy of the PI data reported during that

period, PI definitions and guidance contained in Revision 2 of Nuclear Energy Institute

Document 99-02, Regulatory Assessment Performance Indicator Guideline, were

used. The following PI was reviewed:

29 Enclosure

  • Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent

Occurrence PI

The inspectors reviewed the licensees assessment of this PI by reviewing CRs

generated during approximately the 18 months preceding the inspection to identify any

potential occurrences such as unmonitored or improperly calculated effluent releases

that could have impacted offsite dose. Also, the inspectors evaluated the licensees

methods for determining offsite dose from radiological effluents and reviewed monthly

PI data elements for the April 2003 through June 2004 period to verify that data was

recorded and verified as required by the licensees PI procedure.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues

during baseline inspection activities and plant status reviews to verify that they were

being entered into the licensees corrective action system at an appropriate threshold,

that adequate attention was being given to timely corrective actions, and that adverse

trends were identified and addressed. Minor issues entered into the licensees

corrective action system as a result of inspectors observations are generally denoted in

the report. In addition, in order to help identify repetitive equipment failures or specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. This review was

accomplished by reviewing daily condition reports and attending daily condition report

review meetings.

b. Findings

No findings of significance were identified.

4OA3 Event Follow-up (71153)

a. Inspection Scope

The inspectors reviewed licensee event reports (LERs) to ensure that issues

documented in these reports were adequately addressed in the licensees corrective

action program. The inspectors also interviewed plant personnel and reviewed

operating procedures to ensure that generic issues were captured appropriately.

The inspectors reviewed the Updated Final Safety Analysis Report and other documents

to verify the statements contained in the LERs.

30 Enclosure

a. Findings

.1 (Closed) LER 50-237;249/2004-003-00: Unit 2 and 3 Control Room Emergency

Ventilation System Inoperable Due To Damper Failure to Close

Introduction: Two Green findings were identified during the review of

LER 50-237;249/2004-003. The first was a Green self-revealing finding involving the

failure to restore the control room emergency ventilation (CREV) system to operable

status following maintenance. This resulted in a NCV of TS 3.7.4 , CREV System,

Action Statement A.1. This finding was considered to be self-revealing because it was

discovered when the system did not operate properly during routine realignment from

train A to train B.

The second was a Green NRC identified finding involving failure to control parts and

equipment necessary for the performance of a post accident procedure to maintain

control room habitability in the event of a failure of train B of control room ventilation.

This finding was considered to be NRC identified because, when the inspector was

doing an in-plant walk-down of an operating procedure that had been modified as a

corrective action for this LER, the inspector found that necessary parts were not being

controlled as called for in the procedure.

Discussion: The Unit 2 and 3 control room heating ventilation and air conditioning

(HVAC) system has two trains, A and B. Normally, control room ventilation is supplied

by train A. The CREV system is used to protect control room personnel in the event of

high outside airborne radioactive contaminants, outside toxic gases, and to purge

smoke from the control room in the event of an internal fire. Following a loss of coolant

accident (LOCA), the normal outside air intake is isolated and outside air is supplied

thought an air filtration unit (AFU) containing high efficiency particulate filters and

charcoal adsorbers. Analysis has shown that as long as the control room outside air

supply is switched to the AFU within 40 minutes of a LOCA, control room operator doses

will remain within limits.

On April 19, 2004, a temporary modification was installed on the CREV system to allow

operation of train A HVAC while preventive maintenance (PM) was being performed on

a 480 Volt breaker. While the PM was being performed, control power to solenoid

valves that supply pneumatic air to position CREV isolation dampers would be lost.

Without control power the CREV dampers would fail closed and control room ventilation

would be unavailable. The temporary modification provided pneumatic jumpers, (plugs

for the solenoid valve exhaust ports and temporary tubing that bypassed the solenoid

valves) to maintain the CREV isolation dampers open. With the temporary modification

in place the CREV system was declared inoperable on a 7 day time clock.

On April 22, 2004, with the breaker PM completed, a work order to remove the

temporary modification was completed, and the CREV system was tested and declared

operable. On April 28, 2004, a routine realignment of the control room HVAC from

train A to B was attempted. During this realignment the HVAC damper for the unfiltered

air supply should have closed but remained open. With the unfiltered air supply damper

failed open, protection from external airborne radioactivity and toxic gas was

unavailable. The CREV system was again declared inoperable and troubleshooting was

31 Enclosure

initiated. It was found that the temporary modification that had been installed on

April 19, 2004, had only been partially removed on April 22, 2004. The temporary tubing

that bypassed the solenoid valves had been removed but the plugs in the solenoid valve

exhaust ports had been left installed. Therefore, the CREV system had been inoperable

for greater than 7 days from April 19 until April 28, 2004, in violation of TS 3.7.4.

On August 3, 2004, the inspectors conducted an in-plant walkdown of procedure

DOA 5750-01, VENTILATION SYSTEM FAILURE, Revision 37. This procedure

contained instructions for the installation of the temporary modification for placement of

the pneumatic jumpers to maintain the CREV isolation dampers open. This procedure

was revised as a corrective action resulting from this LER. The inspectors walked down

this procedure because it called for installation of the temporary modification, following a

LOCA and failure of the train B air handling unit, to restore control room ventilation.

Procedure DOA 5750-01 called for this to be completed within 40 minutes of the LOCA

in order to maintain control room radiation dose within limits. The complexity of the

procedure made the inspector question if it could be completed in the required time.

The procedure is written assuming jumpers, pipe plugs, fittings, and wrenches are pre-

staged in the control room Dresden Emergency Operating Procedures (DEOP) Cabinet.

When asked, neither of the two control room Unit Supervisors were able to locate the

pre-staged equipment for inspection. With the help of the NRC inspector the equipment

was located in a miscellaneous equipment drawer of the DEOP Cabinet, the jumper

tubes were lying loose and unmarked, the fittings were in two plastic bags labeled with

black felt tip marker Temp Alt 5-10-99," and no hexagonal-end wrench was available to

install the required pipe plugs. The inspector concluded that had it been necessary to

install the temporary modification and restore control room ventilation following a LOCA

it may have taken more than the allotted 40 minutes.

Analysis: For the self-revealing finding involving the violation of TS 3.7.4, Action

Statement A.1, the licensee determined that the root cause of the failure to completely

remove the temporary modification from the CREV system was inadequate instructions

in procedure DOA 5750-01, Ventilation System Failure, in that guidance for removal

was not included in the procedure. Using IMC 0612, Appendix B, Issue Screening, the

inspector determined that the failure to return the CREV system to operable status

within its TS allowed outage time was a performance deficiency. The inspectors

concluded that this issue was more than minor because it affected the Reactor Safety

Barrier Integrity Cornerstone design control and configuration control attributes, and the

objective of protecting persons in the control room from radionuclide releases caused by

accidents or events.

Using IMC 0609, Appendix A, Significance Determination of Reactor Inspection

Findings for At-Power Situations, dated September 10, 2004, the inspector answered

No to question one in the Containment Barriers column of the Phase 1 worksheet of

the SDP worksheet in that not only was the radiological barrier function for the control

room effected but also the barrier against toxic atmosphere. For the same reason

question number one was answered No, question two was answered Yes which

required a Phase 3 SDP analysis.

The finding was referred to the SRA for a Phase 3 analysis. The analyst consulted with

licensee risk specialists to gain an understanding of the potential sources for toxic gas

32 Enclosure

intrusion into the control room. These sources included onsite sources, especially those

that might be deployed on the roof areas near the outside air intake and chemical plants

or refineries in the vicinity of the plant. The principal risk to core damage would be

debilitation of the control room operators or a forced evacuation requiring alternate

means to achieve a safe shutdown. Based on a qualitative judgement of the

unlikelihood of toxic gas reaching the outside air intake in sufficient concentrations to

affect operators in combination with the short exposure period of the finding (6 days),

the analyst concluded that the finding was of very low risk significance (Green).

The second finding, that the licensee had failed to control parts and equipment

necessary for the performance of a post accident procedure to maintain control room

habitability, was also evaluated using IMC 0612, Appendix B, Issue Screening. The

inspectors concluded that this issue was more than minor because it also affected the

Reactor Safety Barrier Integrity Cornerstone design control and configuration control

attributes, and the objective of protecting persons in the control room from radionuclide

releases caused by accidents or events. Using IMC 0609, Appendix A, Significance

Determination of Reactor Inspection Findings for At-Power Situations, the finding

screened as very low safety significance (Green). This was due to the inspector

answering Yes to question number one in the Containment Barriers column of the

Phase 1 worksheet of the SDP worksheet, because the uncontrolled equipment would

have only been used to provide the radiological barrier function for the control room

following an accident.

Enforcement: The failure to restore the CREV system to operable status following

maintenance, resulted in a violation of TS 3.7.4. Action Statements B.1 and B.2 require

that if restoration of the CREV system to operable status is not complete in 7 days, the

plant is to be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in Mode 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Contrary to the

above, the licensee failed to properly remove a temporary modification to the CREV

isolation dampers, which resulted in the CREV system being inoperable for 9 days from

April 19, 2004, to April 28, 2004. Believing the system had been restored to an operable

status on April 22, 2004, the licensee failed to take the appropriate actions dictated by

T.S. 3.7.4, Action Statements B.1 and B.2. The licensee revised the procedure to give

better guidance on how to remove the temporary modification. Because this issue is of

very low safety significance and has been entered into the licensees corrective action

program as Condition Report 217741, this violation is being treated as a Non-Cited

Violation, consistent with Section VI.A., of the NRC Enforcement Policy.

(NCV 05000237/2004010-06; 05000249/2004010-06)

The failure to control parts and equipment needed for the performance of a post

accident procedure to maintain control room habitability in the event of the failure of

train B of control room ventilation was not considered a violation of regulatory

requirements. This was because, although procedures call for the use of CREV train A

in the event of a train B failure, the finding involved non-safety related equipment. The

licensee entered this issue into the stations corrective action program as CR 242461.

The licensee identified a number of corrective actions including properly packaging the

necessary parts and tools, revising procedures DOA 5750-01 and 5750-04, and initiating

a training request to ensure operations personnel are properly trained in the use of the

33 Enclosure

DOA air jumpers. This issue was considered a finding of very low significance.

(FIN 05000237/2004010-07; 05000249/2004010-07)

.2 (Closed) LER 50-237/2004-004-00 and LER 50-237/2004-004-01: Unit 2 Manual Scram

Due To The Trip Of A Reactor Recirculation Pump

Introduction: A Green self-revealed finding was identified involving several performance

issues which resulted in the initiation of a manual scram. The performance issues

included an inadequate process for rewinding the 2A recirculation pump motor when it

was installed in 1999, an inadequate evaluation of the testing of the motor before

installation, and the failure to perform post maintenance testing of the reactor building

closed cooling water (RBCCW) system piping to identify leakage. This failure resulted

in the deposit of a conductive substance inside the motor.

Description: On April 24, 2004, with Unit 2 at 66 percent power, the 2A reactor

recirculation pump tripped when a short between phases A and B of the motor winding

occurred. Operators initiated a manual scram in accordance with Dresden Abnormal

Procedure DOA 202-01, Recirculation (RECIRC) Pump Trip - One Or Both Pumps,

Revision 25. The plant was in a region of the reactors power to flow map that required

an immediate manual scram. All plant systems responded normally to the scram.

The licensee initiated a root cause investigation which identified that on

October 10, 1999, during the Unit 2 refueling outage, the 2A reactor recirculation pump

motor was replaced. This motor was originally sent to the vendor for rewind and testing

in March of 1997.

In June 1999, during the testing of the rewound spare motor, inadequately sealed spots

at the series connections location at the lower end of the motor were identified. A repair

was initiated and the test was completed satisfactorily. However, the licensee did not

evaluate or determined the cause at that time of the deficiency. The licensees root

cause report stated that this condition may have indicated a potential weak spot that

would have required a full repair.

During the replacement of the motor, the RBCCW piping was reconnected to the

rewound motor. However, post maintenance testing was not performed to ensure the

piping and fittings did not leak. Following the refuel outage, in October 2001, the

licensee identified a RBCCW water leak in an elbow in a lower air intake of the 2A

recirculation pump motor. The leak was from a loose pipefitting. This condition had

resulted in the presence of electrically conductive surface deposits and moisture

intrusion onto the motor winding. Subsequently, this deficiency contributed to the failure

of the connection points insulation and the motor failure.

A failure analysis was conducted by the vendor which concluded that the motor failure

was attributed to the presence of moisture, conductive surface contamination, and weak

spots in the insulation of the series connections due to a voltage and mechanical stress

concentration point at the end of the conductor.

34 Enclosure

Based on the licensees determination of the root cause and contributing causes, one

Green finding was identified involving performance issues which resulted in the initiation

of a manual scram. The performance issues included an inadequate process for

rewinding the 2A recirculation pump motor when it was installed in 1999, an inadequate

evaluation of the testing of the motor before installation, and the failure to perform post

maintenance testing of the RBCCW system piping to identify leakage. This failure

resulted in the deposit of conductive substance inside the motor.

Analysis: Using IMC 0612, Appendix B, Issue Screening, the inspectors determined

that this finding was more than minor because it affected the initiating events

cornerstone objective to limit the likelihood of an initiating event. The inspectors

completed a significance determination of this issue using IMC 0609, Appendix A,

Significance Determination of Reactor Inspection Findings for At-Power Situations.

The inspectors answered No to all questions in the initiating event column of the

Phase 1 Screening Worksheet; and therefore, concluded that the issue was of very low

safety significance (Green). (FIN 05000237/2004010-08)

Enforcement: No violation of NRC requirements occurred because the finding involved

non-safety related equipment. The licensee entered this issue into the stations

corrective action program as CR 217570. The licensee identified a number of corrective

actions including replacing the failed reactor recirculation pump motor and revising

Exelon Nuclear Engineering Standard NES-EIC-40.01, Revision 1, Large Motor (>2kv)

Repair Requirements, to include enhanced testing requirements

.3 (Closed) LER 50-237;249/2004-003-00: Unit 3 Scram Due to Loss of Offsite Power and

Subsequent Inoperability of the Standby Gas Treatment System for Units 2 and 3

On May 5, 2004, at 1327 hours0.0154 days <br />0.369 hours <br />0.00219 weeks <br />5.049235e-4 months <br />, with Unit 3 at 100 percent power, an automatic scram

occurred due to a main generator load reject when a loss of offsite power occurred. All

systems initially responded to the scram as expected except the standby gas treatment

system was unable to maintain the secondary containment at the TS surveillance

requirement limit of greater than or equal to 0.25 inches of vacuum water gauge. An

Unusual Event for the loss of offsite power was declared at 1342 hours0.0155 days <br />0.373 hours <br />0.00222 weeks <br />5.10631e-4 months <br /> and terminated

at 1601 hours0.0185 days <br />0.445 hours <br />0.00265 weeks <br />6.091805e-4 months <br /> on May 5, 2004. Additionally, during restoration of offsite electrical power

to Bus 33, the emergency diesel generator 2/3 output breaker tripped.

This event was reviewed during an NRC Special Inspection conducted on May 6 through

May 14, 2004, and documented in Special Inspection Report 05000249/2004009 issued

on June 21, 2004. The report documents three self-revealed findings of very low safety

significance (Green). Two of the findings were determined to be violations of NRC

requirements. The first finding, not associated with a violation of NRC requirements,

was related to inadequate preventive and corrective maintenance performed on

switchyard circuit breaker 8-15 which caused the C phase of the breaker to not open

when operated on May 5, 2004. The second finding, associated with a violation of NRC

requirements, dealt with inadequate procedures for restoration of offsite power to safety

related busses. The third finding, associated with a violation of NRC requirements dealt

with an inoperable secondary containment when the opposite units drywell purge fans

were in operation.

35 Enclosure

Since the Special Inspection, the licensee completed W.O. 698088 on August 18, 2004,

which implemented the ABB Product Advisory for the remaining gas SF6 circuit

breaker 6-7. In August 2004, the system engineer verified that ABB has provided

Exelon Energy Distribution all applicable product advisories. Dresden Operations issued

Standing Order 04-06 for switchyard activity control which discusses the proper

management of work occurring in the Dresden switchyards.

Exelon Nuclear has established an executive committee, which includes representatives

from Exelon Energy Delivery, to enhance the reliability of its nuclear station switchyards.

A significant outcome of this initiative will be the development of preventative

maintenance templates for the various switchyard components. The licensee expects

full implementation of the templates at Dresden by June 30, 2005. In addition, an

Exelon liaison position has been established for industry switchyard issues.

The cause of the emergency diesel generator output breaker trip was still under

investigation at the time of the LER submittal. The final corrective actions for the

breaker trip will be described in a supplemental report scheduled to be submitted no

later than October 30, 2004.

.4 (Closed) LER 50-249/2004-004-00: Unit 3 Shutdown due to Inoperable Source Range

Monitor

On May 8, 2004, at 0229 hours0.00265 days <br />0.0636 hours <br />3.786376e-4 weeks <br />8.71345e-5 months <br />, with Unit 3 subcritical during startup in Mode 2, source

range monitor (SRM) 24 was declared inoperable due to erratic indications. SRM 22

was already inoperable due to the inability to fully insert the detector into the core

region. This resulted in the plant being unable to meet the TS 3.3.1.2, SRM

Instrumentation, requirement of three operable SRMs in Mode 2. A reactor shutdown

was commenced at 0450 hours0.00521 days <br />0.125 hours <br />7.440476e-4 weeks <br />1.71225e-4 months <br />. All control rods were fully inserted in the reverse order

in which they had been withdrawn, and the plant entered Mode 3 at 0535 hours0.00619 days <br />0.149 hours <br />8.845899e-4 weeks <br />2.035675e-4 months <br />.

The licencee determined that SRM 22 had a faulty full-in limit switch. The limit switch

was replaced. SRM 24 was inoperable due to an oxide buildup on the connectors. The

connectors were disconnected and reconnected numerous times, stopping the erratic

indication during troubleshooting. A work request was written to thoroughly clean all the

connectors during the next refueling outage. Engineering will evaluate the need for a

preventive maintenance item to periodically clean the SRM connectors and evaluate the

potential of refurbishing the limit switch and a replacement frequency. No findings were

identified.

.5 (Closed) LER 50-237/2004-002-00: Unit 2 SCRAM Due to Main Steam Isolation Valve

Closure and Subsequent Inoperability of the Isolation Condenser

Introduction: A violation of 10 CFR 50, Appendix B, Criterion V, of very low safety

significance (Green) was self-revealed during the recovery from a reactor scram on

April 24, 2004. Licensee maintenance personnel failed to correctly set the open torque

switch bypass setting for motor operated Valve (MOV) 2-1301-3, Isolation Condenser

Outboard Condensate Return Valve, on October 8, 1999. This resulted in the failure of

Valve 2-1301-3 to open when an operator tried to manually operate the valve from the

control room.

36 Enclosure

Description: On October 8, 1999, two electrical maintenance personnel performed

procedure DEP 0040-10, MOV Votes Test Procedure, Revision 13, in accordance with

Work Order 97071725-01. Procedure DEP 0040-10, Attachment C, Step 30, stated,

Verify limit switch settings are correct and that on four rotor models the Open Torque

Switch Bypass opens at 50 percent to 70 percent of the full open stroke. Valve 2-1301-

3 was a gate valve with a 12 inch full mechanical stroke. Because of the valves

function, the licensee determined that the full electrical stroke should only be

1.65 inches. The electrical maintenance personnel set the open torque switch bypass

at .975 inches per the procedure. However, Step E.6 stated, Verify the limits are set

per the MOV Set Point Binder using the VOTES trace and to adjust as necessary, and

Step G.5.F, stated, Verify limit switch settings comply with the Set Point Binder, if

adjustments have to be made refer to DEP 040-09, Limitorque Valve Operator

Maintenance. Both of these steps were signed off as complete. The MOV Set Point

Binder had the correct open torque switch bypass setting of 4.5 inches which was

beyond the valves electrical open stroke. The licensee concluded that the procedure

was inadequate since it contradicted itself and that human performance was a

contributing cause. The inspectors agreed with the licensees conclusions. The

procedure was misleading; however, had the technicians read the MOV Set Point Binder

and saw the discrepancy the problem could have been resolved.

Analysis: The inspectors determined that the failure to adequately set the open torque

switch bypass setting for Valve 2-1301-3 was a performance deficiency warranting a

significance evaluation. The inspectors concluded that the finding was more than minor

in accordance with IMC 0612, Appendix B, Issue Screening, dated June 20, 2003.

The inspectors determined this was more than minor because it affected the

configuration control, equipment performance, and procedure quality attributes of the

mitigating systems cornerstone and the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences.

The inspectors completed a significance determination of this issue using IMC 0609,

Appendix A, Significance Determination of Reactor Inspection Findings for At-Power

Situations, dated September 10, 2003. For the Phase 1 analysis the inspectors

answered questions 1 and 2, Yes under the mitigating systems cornerstone column.

This resulted in the required performance of a Phase 2 analysis. The inspectors

reviewed worksheet tables for the following: Transients, Transients without Primary Heat

Sink, Loss of Service Water, Loss of Instrument Air, Loss of An AC [alternating current]

Bus, and Loss of Offsite Power. The inspectors assumed that 1) the isolation

condenser was unavailable from the beginning of each transient, and 2) that the

isolation condenser valve could not be recovered. Base on these two assumptions,

using the counting rule, worksheet step 13 was greater than zero which initially had a

risk significance of Yellow. The inspectors realized that the assumptions made to

perform the Phase 2 were inaccurate. The evaluation was sent to the Regional Office in

order to perform a Phase 3 analysis. The Phase 3 analysis performed by the Senior

Reactor Analyst (SRA) concluded that the safety significance of this finding based on

the change in core damage frequency was Green. The Phase 3 analysis reviewed the

potential failure probabilities based on the procedure and equipment inadequacies.

37 Enclosure

Enforcement: The failure to have adequate instructions for work involving a safety-

related valve resulted in a violation of 10 CFR 50, Appendix B, Criterion V. Code of

Federal Regulations Title 10, Part 50, Appendix B, states in part, Activities affecting

quality shall be prescribed by documented instructions, procedures, or drawings, of a

type appropriate to the circumstances... The setting of the open torque switch bypass

on Valve 2-1301-3 was an activity affecting quality. Contrary to the above, on

October 8, 1999, the open torque switch bypass was set improperly on Valve 2-1301-3

due to inadequate procedural guidance. Because this issue is of very low safety

significance and has been entered into licensees corrective action program

(IR 216787), this violation is being treated as a Non-Cited Violation, consistent with

Section VI.A., of the NRC Enforcement Policy. (NCV 05000237/2004010-09)

.6 (Closed) LER 50-237;249/2004-005-00: Units 2 and 3 Inoperable Turbine Condenser

Vacuum - Low Switches

Introduction: The inspectors identified a NCV of TS 3.3.1.1 having a very low safety

significance (Green) for failing to properly enter a required TS LCO when the 3C and 2A

turbine main condenser low vacuum Reactor Protection System (RPS) scram channels

were inoperable. This issue was considered to be NRC-identified because the licensee

had failed to identify this deficiency without the inspectors questions on July 1, 2004.

The licensee looked into the issue further and identified that these switches had been

inoperable outside their TS outage time multiple times in the past 2 years. Had it not

been for the inspectors questioning, the licensee would not have found the problem at

this particular time. Therefore, the finding is considered inspector identified.

Description: On April 5, and May 3, 2004, vacuum indication taken from the 3C main

condenser hood was not indicating accurate values after circulating water flow was

reversed. Subsequent trending activities by the system engineer revealed that the

vacuum indication from the 2A condenser hood was also exhibiting bad vacuum

indication on some occasions after flow reversals.

The low condenser vacuum pressure switches provided reactor scram signals to protect

the reactor from loss of the main heat sink. Protection for the condenser itself was

assured by closure of the turbine stop and bypass valves as vacuum decreases below a

preset low level. Condition Report (CR) 218325 dated May 1, 2004, Condenser

Vacuum Indication Error Caused by Condensation, stated that the 3C condenser low

vacuum reading was inaccurate. The error caused a measured vacuum that was higher

than the actual value; and therefore, farther away from the trip setpoint. The cause of

the inaccurate vacuum indication was attributed to improperly sloped sensing lines and

water accumulation. The sensing lines connected vacuum instrumentation to the

condenser hoods. The RPS trip switches utilized the same sensing lines as the control

room indication and plant process computer points.

Operations personnel failed to recognize that the 3C switch was inoperable. At the time

of discovery, the switch had already been inoperable for a time greater than the TS

allowed completion time. At the time of discovery operations personnel took appropriate

actions and restored the channel to an operable status within the TS LCO.

38 Enclosure

The inspectors discussed the Unit 3 main condenser vacuum sensing line operability

evaluation with system engineering personnel and were able to obtain historical data

that demonstrated that the 3C and 2A pressure switches were inoperable for greater

than their allowable outage time at least four times in the past 2 years. The licensee

agreed that periods of longer than the TS LCO allowed completion time were exceeded.

The licensees root cause report stated that on some occasions, initial interaction

between plant engineering and the operations personnel failed to identify vacuum

indication instrumentation as inoperable. The licensee attributed these failures to

weaknesses in the operations training materials with regard to the inter-relations

between the RPS pressure switches and the control room recorder. The licensee also

identified weaknesses in the operator rounds appendices and procedures. Specifically,

the operations flow reversal procedure, DOP 4400-08, Revision 33, Circulating Water

System Flow Reversal, did not include information to tell operators what to observe

relative to hood vacuum following a circulating water flow reversal. Finally, the root

cause report identified a weakness in the corrective action program, in that previous

corrective actions from Licensee Event Report (LER) 249/98006 for a similar issue were

too narrowly focused and did not correct the problem.

Analysis: The inspectors determined that the failure to take adequate corrective actions

to prevent recurrence of inoperable low vacuum RPS switches, failure to recognize the

switches were inoperable, and failure to enter the appropriate TS LCO were

performance deficiencies warranting a significance evaluation. The inspectors

concluded that the finding was more than minor in accordance with IMC 0612, Appendix

B, Issue Screening, dated June 20, 2003. The inspectors determined that this finding

was more than minor because it affected the mitigating systems cornerstone design

control and equipment performance attributes, and the objective of ensuring the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. The inspectors completed a significance

determination of this issue using IMC 0609, Appendix A, Significance Determination of

Reactor Inspection Findings for At-Power Situations, dated September 10, 2004. The

inspectors answered No to all questions in the mitigating systems column of the

Phase 1 Screening Worksheet; and therefore, concluded that the issue was of very low

safety significance (Green). This finding was associated with the reactor safety

cross-cutting attribute of Problem Identification and Resolution.

Enforcement: Technical Specification 3.3.1.1, Reactor Protection System (RPS)

Instrumentation, Condition A, stated that if one or more required channels were

inoperable, place the channel in trip within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Contrary to the above, the licensee

failed to enter the TS required action within the 12-hour allowable outage time when the

3C and 2A turbine main condenser low vacuum RPS scram channels were inoperable,

which caused an indicated vacuum value that was greater than the actual value; and

therefore, farther away from the trip limit. This occurred on four separate occasions

between 2002 and 2004. The licensees corrective actions, as described in the root

cause report, included installing temporary vent valves on the 3C and 2A sensing lines

to continuously purge and clear condensation from the lines, enhancing operations

training materials to include adequate level of detail on main condenser vacuum

indications, revising the operations procedure DOP 4400-08, Revision 33, Circulating

Water System Flow Reversal, and performing internal and external condenser

39 Enclosure

walkdowns during the next outage on Unit 2 and Unit 3 to determine the sensing line

slope and to repair the sensing line slope, if necessary. Because this issue is of very

low safety significance and has been entered into the licensees corrective action

program as Condition Report 234361, this violation is being treated as a Non-Cited

Violation, consistent with Section VI.A., of the NRC Enforcement Policy.

(NCV 05000237/2004010-10; 05000249/2004010-10)

4OA4 Cross-Cutting Findings

.1 A finding described in 1R06 of this report had, as its primary cause, a Problem

Identification and Resolution deficiency, in that weaknesses had been previously

identified by the NRC with the external flooding surveillance and operating procedures.

.2 A finding described in Section 1R12 of this report had, as its primary cause, a Problem

Identification and Resolution deficiency, in that two functional failures of the reactor

building ventilation system occurred and were not properly entered into the corrective

action program which resulted in the failure to move the reactor building ventilation

system from 10 CFR 50.65 a(2) to a(1).

.3 A finding described in Section 1R20 of this report had, as its primary cause, a Human

Performance deficiency, in that operators failed to perform a return to service clearance

checklist as written. The operators failed to lock open the 2-220-57B main feedwater

isolation valve when it was returned to service.

.4 A finding described in 40A3 of this report had, as its primary cause, a Problem

Identification and Resolution deficiency, in that 1) the licensee failed to correct

equipment deficiencies which resulted in one channel of main condenser low vacuum

reactor trip signals being inoperable on both units after it had been identified as a

problem in 1998; and 2) operations personnel failed to identify that the main condenser

vacuum low pressure switches were inoperable on multiple occasions from 2002 to

2004.

4OA5 Other Activities

(Closed) Unresolved Item 50-237-97021-01 (DRS); 50-249-97021-01 (DRS): The

inspector had 4 concerns: 1) licensee had inadequate analysis to support UFSAR

statements that the Dresden station could be safely shutdown following a Dresden Dam

failure coincident with a loss of coolant accident (LOCA) in one of the units; 2) licensee

had inadequate analysis to support UFSAR statements that station could be safely

shutdown following a Dresden Dam failure during normal operations using only Class I

systems; 3) ultimate heat sink (UHS) inventory was less than assumed in the Systematic

Evaluation Program (SEP) Safety Evaluation Report (SER); and 4) licensee had

inadequate analysis supporting the assumed Service Water Pump (SWP) performance.

These items were referred by Task Interface Agreement (TIA) for Office of Nuclear

Reactor Regulation (NRR) review. The TIA response stated that the accident scenario

of Concern 1 was beyond design basis and no supporting analysis was needed. Also,

the Current Licensing Basis was codified in the Power Uprate SER of license

amendment 191 to Unit 2 and license amendment 185 to Unit 3. The license

40 Enclosure

amendments and SER were issued December 21, 2001. The Power Uprate SER is

located in ADAMS at accession number ML0135401870. The Power Uprate SER did

not require the Dresden Station to safely shutdown following a Dresden Dam failure

coincident with a LOCA in one of the units. Therefore, Concern 1 is closed. For

Concern 2, the Power Uprate SER stated that the licensee did not need to use only

class I systems to shut down. Therefore Concern 2 is closed. For Concern 3, the TIA

response stated that the licensees planned action of using portable engine-driven

pumps to pump water from the intake and discharge canals was acceptable to

compensate for the reduced UHS inventory assumption since the planned actions were

in the emergency procedure. The Power Uprate SER also stated this was acceptable.

Therefore, Concern 3 is closed. For Concern 4, the TIA response stated that the SWPs

could not be assumed to perform without a supporting analysis. The licensee informed

the inspector that the SWPs would no longer be relied on to function after a dam failure

and changed the UFSAR accordingly. Also, the Power Uprate SER stated that the

licensee did not need to credit the SWP pumps for shutdown; therefore, Concern 4 is

closed. This item is considered closed.

40A6 Meetings

Interim Exit Meetings

Interim exit meetings were conducted for:

radioactive material control with Messrs. D. Bost and D. Wozniak on

July 22, 2004. On July 28, 2004, the inspection results were further discussed in

a telephone conversation with Mr. S. Taylor.

4OA7 Licensee Identified Violation

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which met the criteria of Section VI of

the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a Non-Cited

Violation.

Cornerstone: Public Radiation Safety

Technical Specification 5.4.1 requires that written procedures be established,

implemented and maintained covering the applicable procedures in Regulatory

Guide 1.33, Revision 2, Appendix A, February 1978. Procedures specified in

Regulatory Guide 1.33 include those for radiation surveys and for contamination control,

which are provided, in part, by licensee procedure RP-AA-503, Unconditional Release

Survey Method. The licensees procedure requires that material or equipment not be

released for unrestricted use unless it has no detectable licensed radioactive material.

Contrary to this procedure, two separate incidents occurred in October 2003, when low

level but detectable quantities of licensed radioactive material (contaminated materials)

were identified by radiation protection (RP) staff outside the Radiologically Controlled

Area (RCA) (but inside the protected area). These problems occurred because workers

41 Enclosure

failed to understand requirements for the unconditional release of personal items and

other materials from the RCA, exacerbated by inattentive radiation protection staff. The

occurrences are documented in the licensees corrective action program as

CR 00181367 and CR 00184544. Corrective actions included tailgate training with RP

staff, counseling of involved workers and plans to enhance plant and contractor staff

training along with procedural revisions. These problems are of very low safety

significance because the contamination levels on the items inadvertently released

outside the RCA were very low and consequently of little to no dose consequence. The

contaminated items remained within the licensees protected area; and therefore, are

not counted as occurrences as provided in NRC Manual Chapter 0609, Appendix D,

Public Radiation Safety Significance Determination Process.

ATTACHMENT: SUPPLEMENTAL INFORMATION

42 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

D. Bost, Site Vice President

D. Wozniak, Plant Manager

H. Bush, Radiological Engineering Manager

R. Conklin, Radiation Protection Supervisor

J. Fox, Design Engineer

R. Gadbois, Operations Director

D. Galanis, Design Engineering Manager

V. Gengler, Dresden Site Security Director

J. Griffin, Regulatory Assurance - NRC Coordinator

J. Hansen, Regulatory Assurance Manager

R. Kalb, Chemistry ODCM Coordinator

T. Loch, Supervisor, Design Engineering

M. McGivern, System Engineer

D. Nestle, Radiation Protection Technical Manager

M. Overstreet, Radiation Protection Supervisor

R. Quick, Security Manager

N. Spooner, Site Maintenance Rule Coordinator

B. Surges, Operations Requalification Training Supervisor

B. Svaleson, Maintenance Director

S. Taylor, Radiation Protection Director

NRC

M. Ring, Chief, Division of Reactor Projects, Branch 1

IEMA

R. Schulz, Illinois Emergency Management Agency

Contractor

A. Lewis, REMP Technician, Environmental Inc., Midwest Laboratory

1 Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000237/2004010-01 URI USFAR change 50.59 (1R06)05000249/2004010-01

Opened and Closed

05000237/2004010-02 NCV Source of Make-up Water (1R06)05000249/2004010-02

05000237/2004010-03 NCV The Licensee Did Not Move the Reactor

05000249/2004010-03 Building Ventilation System Into the Maintenance Rule

(a)(1) Category (1R12)05000237/2004010-04 NCV Operators Failed to Lock Valve in Unit 2 Drywell (1R20)05000237/2004010-05 NCV Failure to Perform an Adequate Radiological

05000249/2004010-05 Survey Prior to the Unconditional Release of Material

Outside the RCA (Section 2PS3)05000237/2004010-06 NCV The Licensee Failed to Correctly Restore the Control

05000249/2004010-06 Room Emergency Ventilation System to Operable Status

Following Maintenance (4OA3)05000237/2004010-07 FIN The Licensee Did Not Control Tools and Equipment

05000249/2004010-07 Staged to Install a Temporary Modification to Keep the

Control Room Emergency Ventilation System Dampers

Open in the Event of an Accident (4OA3)05000237/2004010-08 FIN Performance Issues Which Resulted in the Initiation of a

Manual Scram on Unit 2 Due to Failure of the 2A

Recirculation Pump Motor (4OA3)05000237/2004010-09 NCV Improperly Set Open Torque Switch Bypass of the

Isolation Condenser Outboard Condensate Return Valve

(4OA3)05000237/2004010-10 NCV Failure to Prevent Recurrence of Inoperable Condenser

05000249/2004010-10 Low Vacuum Reactor Protection System Switches (4OA3)

Closed

50-237;249/2004-003-00 LER Unit 2 and 3 Control Room Emergency Ventilation System

Inoperable Due to Damper Failure to Close

2 Attachment

50-237/2004-004-00 and LER Unit 2 Manual Scram Due to the Trip of a Reactor

50-237/2004-004-01 Recirculation Pump

50-237;249/2004-003-00 LER Unit 3 Scram Due to Loss of Offsite Power and

Subsequent Inoperability of the Standby Gas Treatment

System for Units 2 and 3

50-249/2004-004-00 LER Unit 3 Shutdown Due to Inoperable Source Range Monitor

50-237/2004-002-00 LER Unit 2 Scram Due to Main Steam Isolation Valve Closure

and Subsequent Inoperability of the Isolation Condenser

50-237;249/2004-005-00 LER Units 2 and 3 Inoperable Turbine Condenser Vacuum -

Low Switches

50-237/97021-01 (DRS); URI UFSAR Dam Failure Discrepancies

50-249/97021-01 (DRS)

Discussed

None.

3 Attachment

LIST OF ACRONYMS USED

ABB Asea, Brown, and Boveri

AFU air filtration unit

CFR Code of Federal Regulations

CR Condition Report

CREV control room emergency ventilation

DEOP Dresden Emergency Operating Procedure

DIS Dresden Instrument Surveillance

DOA Dresden Abnormal Operating Procedure

DOP Dresden Operating Procedure

DOS Dresden Operating Surveillance

DRP Division of Reactor Projects

DRP discrete radioactive particle

DRS Division of Reactor Safety

HPCI high pressure coolant injection

HVA heating, ventilation, and air conditioning

IEMA Illinois Emergency Management Agency

IMC Inspection Manual Chapter

IR Issue Report

LCO limiting condition for operation

LER Licensee Event Report

LLD lower limit of detection

LOCA loss of coolant accident

MC Manual Chapter

MOV motor operated valve

MWe megawatts electrical

NCV Non-Cited Violation

NRC Nuclear Regulatory Commission

NRR Office of Nuclear Reactor Regulation

OA Other Activities

ODCM Offsite Dose Calculation Manual

PCM personnel contamination monitor

PM preventive maintenance

PMF probable maximum flood

PI Performance Indicator

RBCCW reactor building closed cooling water

REMP Radiological Environmental Monitoring Program

RCA radiologically controlled area

RP radiation protection

RPS reactor protection system

SDP Significance Determination Process

SEP Systematic Evaluation Program

SER Safety Evaluation Report

SRA Senior Reactor Analyst

SRM source range monitor

SWP service water pump

TEDE total effective dose equivalent

Attachment

TER Technical Evaluation Report

TIA Task Interface Agreement

TLD thermoluminescence dosimeter

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

UHS ultimate heat sink

URI Unresolved Item

WO Work Order

5 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety but rather that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R04 Equipment Alignment

DOP 2300-01, High Pressure Coolant Injection (HPCI) System Standby Operation,

Rev. 28

Unit 2/3, DOP 7500-M1/E1, Unit 2/3 Standby Gas Treatment Valve Checklist, Rev. 05

DOP 1500-M1, Unit 2 Unit 2 LPCI and Containment Cooling Valve Checklist, Rev. 36

M-26, Low Pressure Coolant Injection (LPCI) System Diagram

DOP 0300-M1/E1, Unit 3 Control Rod Drive Hydraulic System Checklist, Rev. 32

DOP 0300-M4, Unit 3 Hydraulic Control Units East (Bank 3) Row 3 and 4, Rev. 03

DOP 0300-M2, Hydraulic Control Units West (Bank 1) Row 7 and 8, Rev. 03

M-365, Diagram of Control Rod Drive Hydraulic Piping

DOP 1400-M1/E1, Unit 3 Core Spray System, Revision 17

CR 214447; ASCO solenoid valves 2(3)-399-548A(B) and 548A(B); April 12, 2004

CR 231734; Unplanned LCO entry for CRD M-14 coupling check; June 25, 2004

CR 229869; Unplanned LCO entries for HCU K-6; June 19, 2004

DOP 1400-M1/E1; Unit 3 Core Spray System; Revision 17

M-358; Diagram of Core Spray Piping; Revision CC

1R05 Fire Protection

IR# 169275; 2/3 EDG interlock door malfunctioned; July 28, 2004

Dresden Unit 2 Fire Pre-Plan U2TB-43

Dresden Unit 2 Fire Pre-Plan U2TB-37

Dresden Unit 2 Fire Pre-Plan U2TB-36

Dresden Unit 3 Fire Pre-Plan U3TB-68

Dresden Unit 3 Fire Pre-Plan U3TB-69

OP-AA-201-001, Fire Marshall Tours, Revision 2

1R11 Operator Requalification

LT017, Simulator Exercise Guide, Revision 01, dated September 2004

CR 0255880; Target rock valve degradation found during valve rebuild,

September 22, 2004

1R06 Flood Protection

Document Based Instruction Guide; 12NL04; Operation of the Isocondenser External

Flood Emergency Make-up Pump; Revision 00

AR 111005; NRC Identifies Weakness in External Flood Procedure; June 5, 2002

Attachment

NRC Inspection Report 50-010/85013; 50-237/85030; 50-249/85026; dated

November 15, 1985

AD-AA-101; Floods; Revision 7

LS05-82-06-069; Safety Evaluation of Hydrology SEP Topics II-3.A; II-3.B; II-3.B.1;

and II-3.C; June 21, 1982

SA-1334; Input for NRC Contingent Dresden Phase 3 SDP Analysis - External Flooding

Frequency for Elevation 517'; Revision 0

CR 246038; DOA 0010-04 Flooding Procedure potentially inadequate; July 27, 2004

DOA 0010-04; Floods; Revision 16

DOA 0040-02; Localized Flooding in Plant; Revision 15

DOP 1300-03; Manual Operation of the Isolation Condenser; Revision 20

WO 668549; D2/3 QRT PM Emergency Diesel Pump (Flood pump) Operation;

July 9, 2004

CC-AA-309-1001; Capacity and Discharge Head for Portable Isolation Condenser

Make-up Pump to be used During Flood Conditions; Revision 0

UFSAR 2.4; Hydrologic Engineering; Revision 01A

UFSAR 3.4; Water Level (Flood) Design; Revision 4

1R13 Maintenance Risk Assessments and Emergent Work Control

Final Clear checklist # 30458

IR# 248839; B SBGT heater current relay out of tolerance; August 31, 2004

IR# 248991; Incorrect grid location for the 2/3-7506B in DOP 7500-M1/E1;

August 31, 2004

WO# 679078-01; Replace/regrease CR105X contacts; September 2, 2004

WO# 679077-01; Replace/regrease CR105X contacts; September 2, 2004

WO# 679080-01;Replace/regrease CR105X contacts; September 2, 2004

WO# 731568-03; Acoustic monitoring of piping to determine leaks outside, between

B CST and west side of trackway interlock, and 2/3 diesel generator room

OP-MW-109-101, Clearance Preparation and Approval Checklist, Rev. 2

WO# 724335; U3 250V Station Battery Cell #113

MA-DR-EM-6-83001; Battery Cell Jumpering, Rev. 0

EC 343009; Evaluation of Units 2&3 125V and 250V Battery Capacity with One (1) Cell

Jumpered as a 2003 Summer Contingency

EC 366236; Evaluation For Jumpering Of One Cell On The Unit 3 250VDC Safety

Related Battery

EC 350740; Evaluation Of Battery Cell Jumper Cart Molded Case Ckt Bkr (Unit 3)

250 Battery

CR 243971; NRC Identified Slight Corrosion On Two U3 125V Battery Posts;

August 12, 2004

1R12 Maintenance Effectiveness (71111.12)

CR 221610; Reactor Bldg dP low due to Degraded Purge Filter Housing; May 17, 2005

CR 219346; Following U3 scram, inadequate secondary containment dP; May 5, 2004

CR 208282; Loss of Rx Bldg DP during fan swap; March 14, 2004

CR 206777; Reactor building dP lost while stopping/starting RB Vent; March 7, 2004

7 Attachment

CR 197643; Reactor Building Differential Pressure >.25"; January 26, 2004

CR 173440; Rx bldg dP <.25" H2O due to starting unit 3 RB ventilation; August 28, 2003

1R15 Operability Evaluations

NED-I-EIC-0303; Reactor Water Level ATWS RPT/ARI Logic and ECCS Initiation

Setpoint Analysis and Reactor Pressure ATWS RPT/ARI Logic and Setpoint Analysis,

Rev. 5

DIS 0263-07, Unit 2 ATWS RPT/ARI and ECCS Level Transmitters Channel Calibration

Test and EQ Maintenance Inspection, Rev. 12

SIL No. 470S2; Non-Condensable Gas Buildup in RPV Water Level Instrumentation;

August 28, 1992

IR 245395; NRC Concern with Reactor Level Density Error; August 18, 2004

IR 245856; ERV discharge piping break flange does not meet USAS B31.1;

August 19, 2004

CR 229550; Unit 3 reactor Bldg Vent intake plenum collapsing; June 18, 2004

EC Eval 350806; U3 Reactor Building Ventilation Duct Collapsing

EC No. 334998; U3 Reactor Building Ventilation Duct Collapsing; June 27, 2004

CR 2411737; U3 RX Building HVAC duct work found collapsed in three areas;

August 4, 2004

CR 223169; U2 RX HVAC duct has split creating in-leakage path for SBGT;

May 24, 2004

OE 03-013, Electromatic Relief Valve Discharge Flanges, Revision 1

CR 204690: HPCI Steamline Water Carryover during Design Basis Events;

February 27, 2004

CR 194722; Previously Identified Problem Lead to a Smoked Component;

January 12, 2004

CR 208093; CR 105X Auxiliary Contactor Failure Analysis Results; March 12, 2004

CR 215956; Unit 3 Containment Cooling Service Water Keep Fill Line Does not Meet

Design Span Requirements; April 20, 2004

Control Room Logs August 23, and September 14, 2004

DOA 6500-12, Low Switchyard Voltage, Revisions 5 and 6

Technical Specifications 3.8.1, AC Sources -Operating

1R17 Permanent Plant Modification

EC 340303;Replacement of SBGT Solenoid Valves 2/3-7541-43A and B; Rev. 000

WO# 600451-01; Replace solenoid valve 2/3-7541-43B on AO-7510-B OPER;

September 14, 2004

MA-AA-726-620, Installation instructions for 0-600 Volt EQ Related Splices, Rev. 0

50.59 Screening Form

1R19 Post Maintenance Testing

WO# 99054268-01; D2/3 72M Eq Limitorque Vlv Oper Surv 2/3-7507-B

MA-AA-723-301, Periodic Inspection of Limitorque Model SMB/SB/SBD-000 Through

5 Motor Operated Valves, Rev. 1

WO# 565269-07; D3 2Y EQ GE 3B CS Pump Motor Surv

DOS 0040-32, LPCI and Core Spray Motor EQ Surveillance, Rev. 06

8 Attachment

DOS 1400-05; Core Spray System Pump Operability And Quarterly IST [Inservice Test]

Test With Torus Available

WO 344213-01; Disassemble & Inspect CS Min Flow Stop Check Valve

WO 724335-01; U3 250V Station Battery Cell #113, Revision 0 and Revision 1

MA-DR-EM-6-83001; Battery Cell Jumpering, Revision 0

WO# 00736967, Inspect/Repair Unit 2 HPCI Discharge Testable Check

Valve 2-2301-7"

DOS 7100-06, Seat Leakage Testing of Valve 2-2301-7," Revision 02

1R20 Refueling and Outage Activities

IR 240083; Outage vulnerability to crane issues; July 29, 2004

IR 240341; Supply identifies pre-outage milestone not met; July 29, 2004

IR 245395; NRC concern with reactor level density error; August 18, 2004

Operator Aid # 8, Rev. 0

DGP 01-01, Unit Startup, Revision 116

DGP 01-S1, Startup Checklist, Revision 63

DGP 01-S3, Unit 2 Mater Outage Checklist, Revision 18

DGP 02-01, Attachment B, Reactor Cooldown Monitoring, Revision 88

1R22 Surveillance Testing

WO# 9905344-01; D2/3 72M EG Limitorque Vlv Oper Surv 2/3 7504-B

MA-AA-723-301, Periodic Inspection of Limitorque Model SMB/SB/SBD-000 Through

5 Motor Operated Valves, Revision 1

Unit 2/3 DEP 40-09, Limitorque Valve Operator Maintenance, Revision 12

1R23 Temporary Modifications

Exelon Procedure CC-MW-112-1001, Temporary Configuration Change Packages,

Revision 3

DAN 902(3)-4 G-13, Steam Dryer Parameter Alarmed, Revision 02

CR 254954; TCCP 347984, Steam Dryer Parameter Temporary Recorder; dated

September 20, 2004

2PS3 Radiological Environmental Monitoring and Radioactive Material Control Programs

Offsite Dose Calculation Manual; Chapters 5 - 6 and Appendices A - C (Revision 2),

Chapter 10 (Revision 4), Chapter 11 (Revision 2), Chapter 12 (Revision 5) and

Appendix F (Revision 2)

Environmental Inc. Midwest Laboratory, Sampling Procedures Manual; Revision 7

Dresden Nuclear Power Station Annual Radiological Environmental Operating Report

for 2002 (dated May 2003) and for 2003 (dated May 2004)

CY-AA-170-100; Radiological Environmental Monitoring Program; Revision 1

RP-AA-503; Unconditional Release Survey Method; Revision 0

TID-2004-003; Unconditional Release Detection Thresholds and Dose Consequences;

Revision 0

9 Attachment

Focus Area Self-Assessment Report; Radioactive Material Control and Radiological

Environmental Monitoring Program; dated June 14, 2004

Nuclear Oversight Health Physics/Radiation Protection Audit Report; Audit No. NOSA-

DRE-03-06; dated May 16, 2003

REMP, ODCM, Non-Radiological Effluent Monitoring Audit Report

Audit No. NOSA-DRE-03-08; dated November 19, 2003

Field Rotameter (serial numbers 95W012433 & 91W506166) Quarterly Flow

Verifications for January 2003 - July 2004

Field Rotameter (serial numbers 95W012433 & 91W506166) Calibration Certificates;

dated May 6, 2003 and July 17, 2003, respectively

Master Rotameter (serial number 91W513308) Calibration Certificate; dated August 12,

2002 and August 8, 2003

Annual Maintenance and Monthly Flow Checks for Environmental Air Sample

Pumps; Pump #s 445,455,486,457,454,458,446,443,452,431,453,451,429 and 462;

January 2003 - June 2004

Murray and Trettel, Inc. Monthly Reports on the Meteorological Monitoring Program at

the Dresden Station; January 2003 - May 2004

CR 00147626; Magenta Tools Found Outside RCA; dated March 5, 2003

CR 00116137; High Tritium Concentration in Non-REMP Well; dated July 18, 2002 and

Associated Apparent Cause Evaluation; dated January 21, 2003

CR 00157499; Excessive Off-Site Sampler Shutdowns for 2002; dated May 6, 2003

CR 00181131; Yellow Velcro Strap Found in Venture Break Area; dated

October 14, 2003

CR 00181367; Infra-Red Camera Released While Isotopic Showed Cobalt and

Manganese; dated October 16, 2003

CR 00181692; Individual Alarms Portal Monitor at Braidwood Station; dated

October 16, 2003

CR 00183938; PM-7 Gatehouse Alarm - Found Particle on Boot Lace; dated

October 30, 2003

CR 00184544; Low-Level Radioactive Clothing Found Outside the RCA; dated

November 2, 2003

4OA1 Performance Indicator Verification

LS-AA-2150; Attachment 1; Monthly PI Data Elements for RETS/ODCM Radiological

Effluent Occurrences; April 2003 - June 2004

Quarterly Summary Data of Dresden Station Units 2/3 Maximum Doses Resulting from

Airborne Releases and from Aquatic Effluents; 2nd Quarter 2003 - 2nd Quarter 2004

4OA3 Event Follow-up

Operability Evaluation No.04-008, Main Condenser Hood/Bay, Revision 0

Operability Evaluation No.04-008, Unit 2 & 3 2A and 3C Condenser Bay Vacuum

Indication/Switch Sometimes Indicates a Non-conservative Value after a Flow Reversal

to East-to-West Flow, Revision 1

CR 218325; Condenser Vacuum Indication Error Caused by Condensation; May 1, 2004

CR 221099; Bad vacuum indication taken from the 3C main condenser hood was

previously reported in CR 218325;

10 Attachment

CR 213244; Apparent Error in Condenser Turbine Hood Vacuum Indication;

April 5, 2004

CR 234361; NRC Questions Potentially Exceeding Tech Spec Comp Time; July 1, 2004

DOA 200-01, Recirculation (Recirc) Pump Trip - One or Both Pumps, Revision 25

DOS 0500-18, Verification of Flow Control Line and Average Core Thermal Power,

Revision 27

NES-EIC-40.01, Large Motor (>2kV) Repair Requirements, Revision 1

CR 217533; Unit 2 TADS trigger manually disabled; April 28, 2004

CR 217570; Unit 2 scram due to 2A Recirc pump trip; April 28, 2004

LER 50-237/249/2004-003-00, Unit 3 Scram Due to Loss of Offsite Power and

Subsequent Inoperability of the Standby Gas Treatment System for Units 2 and 3,

dated July 6, 2004

CR 219063; Switching Fault Causes LOOP and Reactor Scram; May 5, 2004

WO 0069088-01, Rebuild Operating Mechanism All Phases BT 6-7 CB

Exelon Energy Delivery Maintenance Template, Circuit Breaker 2 Pressure SF6, 2004

Revision 2

CR 219062, Unit 3 Startup Aborted due to Insufficient SRMs, dated 05/08/2004

Technical Specification 3.3.1.2, SRM Instrumentation

Control Room Logs May 8, 2004

11 Attachment