L-2011-042, Inservice Inspection Program Fourth Interval-Second Period-Third Refueling Outage Owner'S Activity Report (OAR-1)

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Inservice Inspection Program Fourth Interval-Second Period-Third Refueling Outage Owner'S Activity Report (OAR-1)
ML110480047
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 02/07/2011
From: Kiley M
Florida Power & Light Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
L-2011-042, OAR-1 ISI-PTN-3-2010
Download: ML110480047 (4)


Text

FEB 7 2011 POWERING TODAY.

EMPOWERING TOMORROW. L-2011-042 10 CFR 50.55a U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555-00001 Re: Turkey Point Unit 3 Docket No. 50-250 Inservice Inspection Program Fourth Interval-Second Period-Third Refueling Outage Owner's Activity Report (OAR-1)

Attached find the Owner's Activity Report (Form OAR-i), for Turkey Point Unit 3 Fourth Inservice Inspection Interval, Second Period, Third Refueling Outage (PTN 3-25). The Form OAR-i, Owner's Activity Report, implements Code Case N-532-4.

Should there be any questions concerning this report, please contact Robert J. Tomonto at 305-246-7327.

Very truly yours, Michael Kiley Vice President Turkey Point Nuclear Plant SM Attachment k--o/-y(

P"L an FPL Group company

Attachment I Page 1 of 3 FORM OAR-I OWNER'S ACTIVITY REPORT Report Number: ISI-PTN-3-2010 Plant: Turkey Point Nuclear Power Plant Unit 3 P.O. Box 4332 Florida City. Florida 33032 Commercial Service Date: December 14, 1972 Refueling Outage No.: PTN 3-25 Current Inspection Interval: ISI-Fourth IWE-Second Current Inspection Period: ISI-Second IWE-First Edition and Addenda of Section XI applicable to the inspection plans: ISI-1998 Edition with Addenda through 2000 and IWE-2001 with Addenda through 2003.

Date and Revision of inspection plans: ISI-July 23. 2010. Rev .3 IWE-March 3, 2009, Rev. 0 Edition and Addenda of Section Xl applicable to repairs and replacements, if different than the inspection plan:

Same Code Cases Used: N-460. N-532-4. N-533-1. N-566-1. N-624. N-686. N-513-2 CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection plan as required by the ASME Code, Section Xl; and (c) the repair/replacement activities and evaluations supporting the c9. 9pletion of PTN 3-25 conform to the requirements of Section XI.

wer Sig*ne w, s-ne F, ,- ,i - 04. Paot.4MS Date /3 Owner or Owner's Designee, Title MANG6-CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and the State or Province of Florida and employed by HSBCT of Hartford Connecticut have inspected the items described in this Owner's Activity Report, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.

By signing this certificat6, neither the Inspector nor his employer makes any warranty, expressed or Implied, concerning the repair/replacement activities and evaluation described In this report. Furthermore, neither the Inspector nor his employer shall be liable In any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.

A .S z Commissions FZ 4 1'(,' U.,e Ilnspector's Signatur National Board, State, Province, and Endorsemeants Date  ? Oo/I

Attachment 1 Page 2 of 3 FORM OAR-1 OWNER'S ACTIVITY REPORT TABLE I ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Category and Item Description Evaluation Description Item Number Evaluate for continued service with D-B/D2.10 8" Pipe Upstream of Valve 3-910 thru-wall leak until leak is addressed.

See Table 2 for Repair Evaluate for continued service with D-B/D2.10 4" Pipe Upstream of 3-12-028 thru-wall leak until leak is addressed.

See Table 2 for Repair Evaluate for continued service with D-B/D2.10 4" Pipe Upstream of 3-12-028 thru-wall leak until leak is addressed.

See Table 2 for Replacement Evaluate for continued service with D-B/D2.1 0 4" Pipe Downstream of 3-12-029 thru-wall leak until leak is addressed.

See Table 2 for Repalcement

Attachment 1 Page 3 of 3 FORM OAR-1 OWNER'S ACTIVITY REPORT TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Item Description Date Repair/Replacement Description Of Work Completed Plan Number 2 Reactor Sump Replace Corroded 11/1/10 RR40049244-05 Containment Liner section of Liner plate 2 Pipe down steam of Replace section of Valve 3-20-132 pipe due to external 11/4/10 RR40035857-09 corrosion 2Support 7883-H-013 Repair corroded 2 trunion (Integral 10/29/10 RR400461 00-01 Attachment)

Pipe upstream of Repair pipe with Valve 3-12-028 thru-wall leak due to 4/17/10 RR40002240-06 external corrosion.

Pipe upstream of Repair pipe with thru-wall leak due to 2/15/10 RR39016861-01 external corrosion.

Valves 3-12-028 Replace pipe with 3and 3-12-029 thru-wall leaks due 12/30/10 RR40002240-04 to external corrosion 3 Condensate Storage Weld Buildup on 1/26/10 RR39016774-01 Tank corroded tank