L-2009-167, Inservice Inspection Program Fourth Interval-Second Period-Second Refueling Outage Owner'S Activity Report (OAR-1)

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Inservice Inspection Program Fourth Interval-Second Period-Second Refueling Outage Owner'S Activity Report (OAR-1)
ML092300112
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 08/06/2009
From: Kiley M
Florida Power & Light Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
L-2009-167
Download: ML092300112 (4)


Text

0 FPL.

POWERING TODAY.

AUG o 6-2009 EMPOWERING TOMORROW L-2009-167 10 CFR 50.55a U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555-00001 Re: Turkey Point Unit 3 Docket No. 50-250 Inservice Inspection Program Fourth Interval-Second Period-Second Refueling Outage Owner's Activity Report (OAR-1)

Attached find the Owner's Activity Report (Form OAR-i), for Turkey Point Unit 3 Fourth Inservice Inspection Interval, Second Period, Second Refueling Outage (PTN 3-24). The Form OAR-i, Owner's Activity Report, implements Code Case N-532-4.

Should there be any questions concerning this report, please contact Robert J. Tomonto at 305-246-7327.

Very truly yours, Michael Kiley Vice President Turkey Point Nuclear Plant SM Attachment cc: Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant AC-)(1-7 an FPL Group company

Attachment 1 Page 1 of 3 FORM OAR-1 OWNER'S ACTIVITY REPORT Report Number: ISI-PTN-3-2009 Plant: Turkey Point Nuclear Power Plant Unit 3 P.O. Box 4332 Florida City, Florida 33032 Commercial Service Date: December 14, 1972 Refueling Outage No.: PTN 3-24 Current Inspection Interval: ISI-Fourth IWE-Second Current Inspection Period: ISI-Second IWE-First Edition and Addenda of Section XI applicable to the inspection plans: IS1-1998 Edition with Addenda through 2000 and IWE-2001 with Addenda through 2000.

Date and Revision of inspection plans: ISI-February 10, 2006, Rev .2 IWE-March 3, 2009, Rev. 0 Edition and Addenda of Section Xl applicable to repairs and replacements, if different than the inspection plan:

Same Code Cases Used: N-460. N-532-4. N-533-1. N-566-1. N-624. N-686, N-722. N 729-1 CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluatio upporting t)e completion of PTN 3-24 conform to the requirements of Section X-.

Signed 'wnCr 4 i.-wn er' Tl " Date 7 Ownor~k wnerq Designee, Title CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and the State or Province of Florida and employed by HSBCT of Hartford Connecticut have inspected the items described in this Owner's Activity Report, and state that, to the best of my knowledge .and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.

By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report. Furthermore, neither the inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.

Commissions A2 477/A,- *,r X..-)

" Inspector's Signature National Board, State, Province, and Enidorsements Date 7-31-09

Attachment 1 Page 2 of 3 FORM OAR-1 OWNER'S ACTIVITY REPORT TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE

.Examination Category and Item Description Evaluation Description Item Number Evaluate for continued service with D-B/D2.10 4" Pipe upstream of 3-710A thru-wall leak until pipe is replaced.

See Table 2 for replacement Evaluate for continued service with D-B1D2.10 4" Pipe upstream of 3-710B thru-wall leak until pipe is replaced.

See Table 2 for replacement

Attachment 1 Page 3 of 3 FORM OAR-1 OWNER'S ACTIVITY REPORT TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Item Description Date Repair/Replacement Description Of Work Completed Plan Number 1 CRDM D-6 Replace Control Rod 5/3/09 RR39008256-02 Drive Mechanism 1 Seal Table D-3 Repair weld on low 4/4/09 RR37022558-02 pressure seal weld 1 Seal Table L-8 Replace High .5/3/09 RR39008217-03 Pressure fitting Replaced snubber 2 3-1040 due to Functional 3/28/09 RR38012179-01 Test failure Replaced due to 2 3-1042 worn parts found 3/27/09 RR38012179-01 during hand stroke Replace pipe with 3 3-710A thru-wall leak due to 1/15/09 RR38018953-01 external corrosion.

Replace pipe with 3 3-710B thru-wall leak due to 1/13/09 RR38018953-03 external corrosion