IR 05000352/2018004

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Integrated Inspection Report 05000352/2018004 and 05000353/2018004
ML19044A637
Person / Time
Site: Limerick  Constellation icon.png
Issue date: 02/13/2019
From: Jon Greives
Reactor Projects Region 1 Branch 4
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
Greives J
References
IR 2018004
Download: ML19044A637 (18)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION ary 13, 2019

SUBJECT:

LIMERICK GENERATING STATION - INTEGRATED INSPECTION REPORT 05000352/2018004 AND 05000353/2018004

Dear Mr. Hanson:

On December 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Limerick Generating Station, Units 1 and 2. On January 11, 2019, the NRC inspectors discussed the results of this inspection with Mr. Rick Libra, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented one finding of very low safety significance (Green) in this report.

This finding involved a violation of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance of the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Limerick Generating Station. In addition, if you disagree with the cross-cutting aspect assignment you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at Limerick Generating Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos. 50-352 and 50-353 License Nos. NPF-39 and NPF-85

Enclosure:

Inspection Report 05000352/2018004 and 05000353/2018004

Inspection Report

Docket Numbers: 50-352 and 50-353 License Numbers: NPF-39 and NPF-85 Report Numbers: 05000352/2018004 and 05000353/2018004 Enterprise Identifier: I-2018-004-0073 Licensee: Exelon Generation Company, LLC Facility: Limerick Generating Station, Units 1 & 2 Location: Sanatoga, PA 19464 Inspection Dates: October 1, 2018 to December 31, 2018 Inspectors: S. Rutenkroger, PhD, Senior Resident Inspector M. Fannon, Resident Inspector H. Anagnostopoulos, Senior Health Physicist J. DeBoer, Emergency Preparedness Inspector P. Ott, Operations Engineer C. Hobbs, Reactor Inspector M. Rossi, Project Engineer Approved By: Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Exelons performance at

Limerick Generating Station (LGS), Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC-identified and self-revealed findings, violations, and additional items are summarized in the table below.

List of Findings and Violations Failure to Maintain the Design Control of the D23 Emergency Diesel Generator Cornerstone Significance Cross-cutting Report Aspect Section Mitigating Green H.11 - Human 71152 Systems NCV 05000353/2018004-01 Performance -

Opened/Closed Challenge the Unknown A self-revealing Green non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion III was identified when Exelon replaced the D23 emergency diesel generator lube oil heater temperature switch with a new style switch on December 6, 2018. The new style switch subsequently failed on December 7, 2018, due to overheating and charring of the switch wiring when coming in contact with the cover.

Additional Tracking Items Type Issue number Title Report Status Section LER 05000353/2018-001-00 HPCI Inoperability due to 71153 Closed Discharge Check Valve Failure to Close

TABLE OF CONTENTS

PLANT STATUS

INSPECTION SCOPES

................................................................................................................

REACTOR SAFETY

..................................................................................................................

RADIATION SAFETY

................................................................................................................

OTHER ACTIVITIES - BASELINE

............................................................................................

INSPECTION RESULTS

..............................................................................................................

EXIT MEETINGS AND DEBRIEFS

............................................................................................ 13 THIRD PARTY REVIEWS .......................................................................................................... 13

DOCUMENTS REVIEWED

......................................................................................................... 14

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On December 16, 2018, operators

reduced power to 57 percent for power suppression testing. The unit was returned to rated

thermal power on December 20, 2018, and remained at or near rated thermal power for the

remainder of the inspection period.

Unit 2 began the inspection period at rated thermal power. On December 29, 2018, operators

reduced power to 70 percent for repairs on the main turbine control valve #4. The unit was

returned to rated thermal power on December 30, 2018, and remained at or near rated thermal

power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors also performed plant status activities described

in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152,

Problem Identification and Resolution. The inspectors reviewed selected procedures and

records, observed activities, and interviewed personnel to assess licensee performance and

compliance with Commission rules and regulations, license conditions, site procedures, and

standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather (1 Sample)

The inspectors evaluated readiness for seasonal extreme weather conditions prior to

seasonal cold temperatures.

71111.04 - Equipment Alignment

Partial Walkdown (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) Unit common A control room fresh air system on October 11, 2018

(2) Unit common emergency service water system on October 19, 2018

(3) Unit common residual heat removal service water system on October 22, 2018

Complete Walkdown (1 Sample)

The inspectors evaluated system configurations during a complete walkdown of the Unit 2

high pressure coolant injection system.

71111.05AQ - Fire Protection Annual/Quarterly

Quarterly Inspection (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected

areas:

(1) Fire areas 122 and 123, Unit common spray pond pump structure, on October 19, 2018

(2) Fire area 56, Unit 2 reactor core isolation cooling pump room, on November 15, 2018

(3) Fire area 80, Unit 1 D13 emergency diesel generator and fuel oil-lube oil tank room, on

November 16, 2018

(4) Fire areas 31 and 32, Unit 1 residual heat removal heat exchanger and pump rooms 203

and 204, elevation 201, on November 19, 2018

(5) Fire areas 54 and 55, Unit 2 residual heat removal heat exchanger and pump rooms 280

and 281, elevation 201, on November 19, 2018

71111.06 - Flood Protection Measures

Internal Flooding (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the Unit 2 A and C

residual heat removal pump room on December 27, 2018.

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (1 Sample)

The inspectors observed and evaluated licensed operator requalification training on

October 23, 2018.

Operator Performance (1 Sample)

The inspectors observed Unit common A loop residual heat removal service water pump

testing, Unit common emergency service water throttle valve flushing, and Unit 1 redundant

reactivity control system restoration on December 1, 2018. The inspectors also observed

Unit 1 power suppression testing on December 17, 2018.

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

(Annual)

Operator Requalification Exam Results (Annual) (1 Sample)

The inspectors reviewed and evaluated requalification examination results on December 10,

2018.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness (1 Sample)

The inspectors evaluated the effectiveness of routine maintenance activities associated with

the following equipment and/or safety significant functions:

(1) Unit 2 high pressure coolant injection system

71111.13 - Maintenance Risk Assessments and Emergent Work Control (4 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work

activities:

(1) Unit 2 D23 emergency diesel generator fuel oil storage tank cleaning and inspection on

October 15, 2018

(2) Unit 2 A division 1 nuclear steam supply shutoff system logic test on November 2, 2018

(3) Unit 1 high pressure coolant injection testing on November 6, 2018

(4) Unit 2 reactor core isolation cooling flow controller replacement on November 13, 2018

71111.15 - Operability Determinations and Functionality Assessments (6 Samples)

The inspectors evaluated the following operability determinations and functionality

assessments:

(1) Issue Report (IR) 4178994, Unit 1 D11 emergency diesel generator speed meter

fluctuations on October 1, 2018

(2) IR 4185363, Unit 2 standby liquid control tank foreign material on October 24, 2018

(3) IR 4183163, Unit 2 D22 emergency diesel generator discharge coupling lube oil leak on

October 25, 2018

(4) IR 4166174, Unit 2 emergency diesel generator keepwarm system issues on

October 26, 2018

(5) IR 4192575, Unit 1 division 2 battery room low temperature on November 7, 2018

(6) IR 4195383, Unit 1 reactor core isolation cooling pump suction valve from the

condensate storage tank had a torque switch trip that was outside the allowable value

during diagnostic testing on November 15, 2018

71111.19 - Post Maintenance Testing (4 Samples)

The inspectors evaluated post maintenance testing for the following maintenance/repair

activities:

(1) Unit 2 reactor core isolation cooling flow transmitter venting, filling, and alignment on

October 29, 2018

(2) Unit 2 reactor core isolation cooling maintenance outage on November 14, 2018

(3) Unit common D residual heat removal service water pump replacement on

November 16, 2018

(4) Unit 1 D11 emergency diesel generator speed switch replacement on November 29,

2018

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine (1 Sample)

(1) ST-6-092-311-1, Unit 1 D11 emergency diesel generator instrumented run on

October 30, 2018

In-service (1 Sample)

(1) ST-6-049-230-2, Unit 2 reactor core isolation cooling pump, valve, and flow test on

November 15, 2018

71114.02 - Alert and Notification System Evaluation (1 Sample)

The inspectors evaluated the maintenance and testing of the alert and notification system

from December 2016 to November 2018.

71114.03 - Emergency Response Organization Staffing and Augmentation System (1 Sample)

The inspectors conducted a review of Exelons Emergency Response Organization (ERO)

augmentation staffing requirements and the process for notifying and augmenting the ERO.

71114.04 - Emergency Action Level and Emergency Plan Changes (1 Sample)

The inspectors verified that the changes made to the emergency plan were done in

accordance with 10 CFR 50.54(q)(3), and any change made to the Emergency Action

Levels, Emergency Plan, and its lower-tier implementing procedures, had not resulted in any

reduction in effectiveness of the Plan. This evaluation does not constitute NRC approval.

71114.05 - Maintaining Emergency Preparedness (1 Sample)

The inspectors reviewed a number of activities to evaluate the efficacy of Exelons efforts to

maintain LGSs emergency preparedness programs.

RADIATION SAFETY

71124.04 - Occupational Dose Assessment

Source Term Characterization (1 Sample)

The inspectors evaluated Exelons source term characterization.

External Dosimetry (1 Sample)

The inspectors evaluated Exelons external dosimetry program.

Internal Dosimetry (1 Sample)

The inspectors evaluated Exelons internal dosimetry program.

Special Dosimetric Situations (1 Sample)

The inspectors evaluated Exelons performance for special dosimetric situations.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified Exelons performance indicator submittals listed below for the period

October 1, 2017 through September 30, 2018. (9 samples)

(1) Unit 1 and Unit 2 cooling water

(2) Unit 1 and Unit 2 reactor coolant system leak rate

(3) Unit 1 and Unit 2 reactor coolant system specific activity

(4) Alert and Notification Reliability

(5) Drill and Exercise Performance

(6) ERO Drill Participation

The inspectors verified Exelons performance indicators submittals listed below for the

period from December 6, 2017 through November 16, 2018. (2 Samples)

(1) Occupational Exposure Control Effectiveness

(2) Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences

71152 - Problem Identification and Resolution

Semiannual Trend Review (1 Sample)

The inspectors reviewed Exelons corrective action program for trends that might be

indicative of a more significant safety issue.

Annual Follow-up of Selected Issues (2 Samples)

The inspectors reviewed Exelons implementation of its corrective action program related to

the following issues:

(1) Emergent shutdown of the Unit 1 D12 emergency diesel generator due to high

scavenging air temperatures (IR 4081882)

(2) Unit 1 recirculation pump adjustable speed drive (ASD) failures (IR 4168043, 4145616,

4044408)

71153 - Follow-up of Events and Notices of Enforcement Discretion

Licensee Event Reports (1 Sample)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000353/2018-001-00, HPCI Inoperability due to Discharge Check Valve Failure

to Close (ADAMS Accession No. ML18037A914). The inspectors determined that it was

not reasonable for Exelon to foresee or correct the cause discussed in the LER, and

therefore no performance deficiency was identified. The inspectors also concluded that

no violation of NRC requirements occurred.

INSPECTION RESULTS

Failure to Maintain the Design Control of the D23 Emergency Diesel Generator

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green H.11 - Human 71152

Systems NCV 05000353/2018004-01 Performance -

Opened/Closed Challenge the

Unknown

A self-revealing Green NCV of 10 CFR Part 50, Appendix B, Criterion III was identified when

Exelon replaced the D23 emergency diesel generator lube oil heater temperature switch with

a new style switch on December 6, 2018. The new style switch subsequently failed on

December 7, 2018, due to overheating and charring of the switch wiring when coming in

contact with the cover.

Description: The emergency diesel generator systems are safety-related standby emergency

power systems for LGS Units 1 and 2 consisting of four diesel generator sets per unit. Each

diesel generator has a lube oil heater that is used to maintain lube oil temperatures above

105 degrees Fahrenheit to ensure system operability. On December 6, 2018, Exelon

replaced the lube oil heater temperature switch with a new style temperature switch under

Engineering Change 619379 for the D23 emergency diesel generator due to a failure of the

previous style switch and repeated reliability issues. After replacing the temperature switch,

the lube oil heater system operated normally until an alarm was received on December 7,

2018, after approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of operation (IR 4201280). The alarm was caused by low

lube oil temperature, subsequently measured at 103 degrees Fahrenheit, which rendered the

D23 emergency diesel generator inoperable.

At the time of the low lube oil temperature alarm for the D23 emergency diesel generator,

the D22 emergency diesel generator was inoperable and unavailable for a similar issue with

its lube oil heater temperature switch (IR 4200941). With two emergency diesel generators

inoperable, Technical Specification 3.8.1.1.b 72-hour limiting condition for operation action

statement was entered. The temperature switch was replaced with the new style switch, the

D22 emergency diesel generator was declared operable, and the 72-hour action statement

was exited. The unit remained in the 30 day action statement (Technical Specification 3.8.1.1.a) for one emergency diesel generator inoperable.

Exelon performed troubleshooting and identified an uninsulated wire lug with a raised arch at

the terminal block. This uninsulated wire came into contact with the cover gasket due to the

lower profile design of the new switch housing. The other two wires on adjacent terminals

were installed with insulated lugs that prevented electrical contact with the cover. While the

heaters were energized, current passing through the uninsulated wire resulted in heating and

decomposition of the gasket. The decomposition continued and allowed current to flow

through the cover to ground, which resulted in a blown fuse for the circuit. Exelon inspected

the D22 emergency diesel generator and identified similar decomposition of the gasket.

After completing troubleshooting, the D22 and D23 emergency diesel generator lube oil

heater temperature switches were sequentially replaced with the previous style switches.

The modification to replace these switches with the new style had not been performed on any

other emergency diesel generators.

The inspectors interviewed engineering personnel, reviewed the engineering change request,

and reviewed the prompt investigation. The inspectors determined that the modification

process (development through installation) reasonably should have identified the potential

impact from the wiring and cover clearance due to the lower profile design of the new style.

Walkdowns were performed in accordance with Exelon procedure CC-AA-106-1001,

Configuration Change Walkdowns, as a part of the configuration change process by

engineering and maintenance personnel that identified the preference to use a lower profile

terminal housing to limit interferences during installation, removal, and testing. The change to

the lower profile switch configuration was not fully evaluated, and the potential issues caused

by reduced clearance between the wiring and cover were not identified.

Corrective Actions: Following the failure on December 7, 2018, Exelon declared the D23

emergency diesel generator inoperable, performed a prompt investigation, and replaced the

new switch assembly with an old style switch. Since the D22 emergency diesel generator

also had the same switch installed for the lube oil heater system, an inspection was

performed and identified similar issues with the wiring and cover clearance resulting in

decomposition of the gasket. Exelon replaced the new D22 emergency diesel generator

switch with an old style switch.

Corrective Action Reference: IR 4201280

Performance Assessment:

Performance Deficiency: The inspectors determined that the failure to ensure the design

control of the emergency diesel generator lube oil heater system was maintained during the

modification process was reasonably within Exelons ability to foresee and correct and should

have been prevented.

Screening: The inspectors determined the performance deficiency was more than minor

because it adversely affected the Design Control attribute of the Mitigating Systems

cornerstone to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the

modification of the D23 emergency diesel generator lube oil heater temperature switch failed

and resulted in the inability to maintain lube oil temperatures above the 105 degrees

Fahrenheit operability limit for the emergency diesel generator to perform its technical

specification required function.

Significance: The inspectors assessed the significance of the finding using IMC 0609,

4, Initial Characterization of Findings, and IMC 0609, Appendix A, The

Significance Determination Process (SDP) for Findings at Power. The inspectors determined

that the finding was of very low safety significance (Green) because the D23 emergency

diesel generator maintained the ability to perform its probabilistic risk assessment function.

Cross-Cutting Aspect: The inspectors determined this finding has a cross-cutting aspect in

the area of Human Performance, Challenge the Unknown, because Exelon personnel did not

maintain a questioning attitude during the modification process up to, and including, the

installation in order to identify and resolve unexpected conditions. [H.11]

Enforcement:

Violation: 10 CFR Part 50, Appendix B, Criterion III states, in part, that design changes,

including field changes, shall be subject to design control measures commensurate with

those applied to the original design. Contrary to this, on December 6, 2018, Exelon did not

maintain the design control of the D23 emergency diesel generator such that a modification

to the lube oil heater temperature switch failed and resulted in the inoperability of the

emergency diesel generator. In addition, on December 7, 2018, Exelon performed the same

modification on the D22 emergency diesel generator. The D23 and D22 emergency diesel

generators were restored to operable status following replacement of the lube oil heater

temperature switches with the previous design on December 8, 2018.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy.

Observations 71152 Semiannual Trend Review

The inspectors performed a semi-annual review of site issues to identify trends that might

indicate the existence of more significant safety concerns. As part of this review, the

inspectors included repetitive or closely-related issues documented by Exelon in the

corrective action program database, trend reports, site performance indicators, major

equipment problem lists, system health reports, maintenance rule assessments, and

maintenance or corrective action program backlogs. The inspectors also reviewed how

Exelons corrective action program evaluated and responded to individual issues identified by

the NRC inspectors during routine plant walkdowns and daily condition report reviews. The

inspectors specifically reviewed and assessed one adverse trend in equipment reliability, last

discussed in the 2018 second quarter integrated inspection report (ADAMS Accession No.

ML18221A483).

Regarding equipment reliability, the inspectors noted two findings documented in inspection

reports during the period related to equipment reliability that were identified during reviews of

LERs (ADAMS Accession No. ML18317A116 and ML18347A403). The inspectors also noted

additional examples evaluated during the period that impacted operations. However, the

inspectors determined the issues substantially consisted of trends in systems with appropriate

actions planned by Exelon, such as the Unit 1 ASD system, emergency diesel generator

keepwarm systems, and the control enclosure chiller system. The inspectors reviewed these

trends and determined Exelon implemented mitigating actions and initiated planned

permanent modifications to restore the systems to reliable operation. The inspectors noted

Exelons actions to improve interdepartmental communication, heighten personnels sensitivity

to recognizing degraded conditions, and increase the sites response to more proactively

resolve degraded conditions. Notwithstandign this, the inspectors identified a finding

associated with the modification to the emergency diesel generator keepwarm systems that is

documented in this report. However, though associated with actions being taken to address

reliability challenges, it was not determined to be indicative of ineffective corrective actions to

address the adverse trend.

Based on the overall results of the semi-annual trend review, the inspectors did not identify

additional trends not being resolved by Exelon and determined that Exelon was appropriately

identifying and entering issues into the corrective action program, adequately evaluating the

issues, and properly resolving adverse trends before they became more safety significant

problems.

Observations 71152 Annual Follow-Up of Selected Issues

Emergent shutdown of the Unit 1 D12 emergency diesel generator due to high scavenging

air temperatures (IR 4081882)

The inspectors reviewed Exelons subsequent actions after the Unit 1 D12 emergency diesel

generator was declared inoperable due to high scavenging air temperatures. The inspectors

reviewed Exelons cause evaluation, operability determination, problem analysis, extent-of-

condition reviews, operating experience reviews, and corrective actions to determine whether

Exelon was appropriately identifying, characterizing, and correcting problems associated with

this issue and whether the planned corrective actions were appropriate. The inspectors

evaluated the actions taken to the requirements of Exelons corrective action program and 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action.

The inspectors determined that Exelon identified and implemented corrective actions for each

identified deficiency commensurate with their safety significance. In addition, Exelon has

implemented revised procedures and communications to site personnel, engaged industry

with operating experience, and has performed an effectiveness review to ensure the

timeliness and adequacy of corrective measures. Exelon is also continuing additional

monitoring of the system for subsequent issues and evaluating potential changes to training

requirements based on events.

Observations 71152 Annual Follow-up of Selected Issues

Unit 1 recirculation pump adjustable speed drive (ASD) failures (IR 4168043, 4145616,

4044408)

The ASD provides variable speed control for a reactor recirculation pump. The ASD is a solid

state, digital based system that replaced a mechanical, analog based motor-generator set

that previously provided the same function. There is one ASD for each reactor recirculation

pump for a total of two ASDs on Unit 1 and two ASDs on Unit 2. Failure of one ASD results in

a loss of a reactor recirculation pump and a power reduction for the unit. Failure of two ASDs

results in loss of both reactor recirculation pumps, and a reactor shutdown. The reactor

recirculation system is a non-safety-related system on both LGS units. ASDs were first

installed at LGS on Unit 1 in the 2012 refueling outage and on Unit 2 in the 2013 refueling

outage. Since that time, there have been no significant failures on the Unit 2 ASDs and 3

significant failures on the Unit 1 ASDs as follows.

In August 2017, the Unit 1 A recirculation pump tripped due to an arc fault in the b4 power

cell. This resulted in single loop operation and reactor power reduction to 36%. The cause of

the arc fault was determined to be tin whiskering in the internal metal bus plane of the power

cell. As a result of this event, LGS replaced all 24 power cells for the Unit 1 ASDs with power

cells containing nickel plated buses in the 2018 refueling outage. Replacement power cells

with nickel plated buses have been procured and staged for installation for the Unit 2 ASDs,

and Exelon has work orders prepared for installation of the power cells at the next available

forced outage or refueling outage.

In June 2018, a leak developed in the supply coolant hose for the a1 power cell on Unit 1 B

AS

D. The Unit 1 B recirculation pump was secured in order to repair the leak, resulting in

single loop operation and a manual reactor power reduction to 31%. The coolant hose was

sent to Exelon power labs for failure analysis. The failure mechanism was determined to be

stress corrosion cracking of a brass fitting on the end of the hose. As a result of this event,

corrective actions are planned for the next Unit 1 and Unit 2 refueling outages as follows. A

sampling of power cell and heat exchanger hoses will be selected for disassembly and

inspection for evidence of cracking, and containment devices will be installed over the power

cell and heat exchanger coolant hoses to direct any leaks away from electrical components.

In August 2018, an uninterruptable power supply (UPS) failure occurred on the Unit 1 A ASD

and caused the recirculation pump to automatically runback to 28% speed. This resulted in a

manual reactor power reduction to 32%. As a result of this event, failure analysis was

performed by the supply vendor of the UPS which determined two circuit cards had failed in a

manner that was not deemed plausible by the vendor. As a result, Exelon continues to

evaluate solutions to this failure.

The inspectors noted that the ASD system has been scoped into the maintenance rule since

original installation, and that the Unit 1 ASDs were appropriately moved into a(1) status in

September 2018, following the three significant failures described above. The reliability

performance criteria for the system to return to a(2) status is no unplanned reactor power

changes greater than 20% in the 12 month period following completion of planned corrective

actions. The inspectors determined that corrective actions taken and planned are

reasonable, timely, and commensurate with the safety significance of the issue.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On January 11, 2019, the inspectors presented the quarterly integrated inspection results to

Mr. Rick Libra, Site Vice President, and other members of the Exelon staff.

THIRD PARTY REVIEWS

Inspectors reviewed Institute of Nuclear Power Operations reports that were issued during the

inspection period.

DOCUMENTS REVIEWED

71114.04

Miscellaneous

Evaluation 17-68, EP-AA-1000, Exelon Nuclear Standardized Radiological Emergency Plan,

Revision 29

71114.05

Procedures

EP-AA-1000, Exelon Nuclear Standardized Radiological Emergency Plan, Revision 29

EP-AA-1008, Exelon Nuclear Radiological Emergency Plan Annex for Limerick Generating

Station, Revision 30

71152

Procedures

OT-104, Unexpected / Unexplained Positive or Negative Reactivity Insertion, Revision 56

OT-112, Unexpected / Unexplained Change in Core Flow, Revision 59

PI-AA-125, Corrective Action Program (CAP) Procedure, Revision 6

PI-AA-125-1003, Corrective Action Program Evaluation Manual, Revision 4

S.43.1.F, Responding to Alarms at ASD HMI, Revision 4

S.43.8.F, Unit 1 Adjustable Speed Drive, Runback UPS Operation, Revision 0

S.43.8.F, Unit 2 Adjustable Speed Drive, Runback UPS Operation, Revision 0

S92.9.N, Routine Inspection of the Diesel Geenrators, Revision 73

ST-6-092-112-1, D12 Diesel Generator 24 Hour Endurance Test, Revision 39

ST-6-092-322-1, D12 Diesel Generator LOCA/Load Reject Testing and Fast Start Operability

Test Run, Revision 30

Temporary Procedure Change 17-0305-1

Temporary Procedure Change 17-0323-1

Condition Reports

20972 4133876 4148177 4160975 4166177 4183163

21268 4134063 4150473 4160976 4166690 4180366

4044408 4135378 4150687 4163928 4166263 4184570

4044613 4138517 4151972 4164099 4167604 4184725

4081882 4140885 4154318 4164464 4168136 4188572

4081907 4141042 4154379 4166740 4166738 4190560

4082335 4141257 4154414 4166743 4170168 4189992

4083987 4141279 4155154 4166744 4173191 4190614

4084040 4141283 4155315 4166745 4173171 4191872

4084043 4143573 4155343 4168043 4177545 4193458

4084045 4143776 4155545 4168892 4178994 4193541

4092404 4144866 4157093 4181540 4179096 4196956

4099289 4145616 4157170 4184778 4178980 4196957

4100187 4145776 4157772 4195250 4178984 4196958

24183 4147127 4158171 4164597 4178987 4198316

24674 4147134 4159137 4165589 4178989 4198633

25208 4147137 4160972 4166119 4178998 4200177

25416 4147140 4160974 4166174 4181413 4199902

200941 4201280 4201364

Maintenance Orders/Work Orders

4665744 4777106 4780170 4794531

Miscellaneous

Adjustable Speed Drive PCM Template, dated 7/16/18

Limerick Generating Station Unit 1 Technical Requirements Manual, Revision 64

Limerick Generating Station Unit 1 Technical Specifications, revised through Amendment 231

Limerick Generating Station Unit 2 Technical Requirements Manual, Revision 63

Limerick Generating Station Unit 2 Technical Specifications, revised through Amendment 194

Limerick Generating Station Updated Final Safety Analysis Report, Revision 19

L-S-19, Design Basis Document for Recirculation System, Limerick Generating System

Units 1 & 2, Revision 11

Root Cause Investigation Report RCR 04081882-15

71153

Condition Reports

2496668 4082181

Work Orders

22137