IR 05000272/1987006

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Insp Repts 50-272/87-06 & 50-311/87-11 on 870324-0420. Violation Noted:Fuel Handling Crane Surveillance Test Not Performed within Required Time
ML18092B551
Person / Time
Site: Salem  PSEG icon.png
Issue date: 04/28/1987
From: Norrholm L, Roxanne Summers
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18092B549 List:
References
50-272-87-06, 50-272-87-6, 50-311-87-11, NUDOCS 8705060337
Download: ML18092B551 (12)


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U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-272/87-06 Report Nos. *

50-311/87-11 50-272.

Docket No DPR-70 License No DPR-75 Licensee:

Public Service Electric and Gas Company 80 Park Plaza Newark, New Jersey 07101 DCS Nos. 050272-870130 050272-870312 050311-861223 050311-870226 050311-870312 Facility Name: Salem Nuclear Generating Station - Units 1 and 2 Inspection At: Hancocks Bridge, New Jersey

  • Inspection Conducted:

March 24, 1987 - April 20, 1987 Inspectors:

Reviewed Approved by:

Inspection Summary:

Engineer, Projects Section 28 Reactor Projects Secti-0n 28 Inspections on March 24 - April 20, 1987 (tombined Report Numbers 50'"'.272/87-06 and 50-311/87-11)

Areas Inspected: Routine inspections of plant operations including: follow-up on outstanding inspection items, operational safety verification, maintenance, sur-veillance, review of special reports, licensee event followup, and allegation follow-u The inspection involved 89 inspector hours, including 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> of back-shift inspection by the resident NRC inspector Results: One violation was identified involving two occasions in which a fuel handling crane surveillance test was not performed within the required tim The violation is discussed in Section 7 of this repor PDR ADOCK 05000272 G

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DETAILS Persons Contacted Within this report period, interviews and discussions were conducted with members of licensee management and staff as necessary to support inspection activit.

Follow-up on Outstanding Inspection Items (Closed) Unresolved Item (50-272/86-32-02)~ Failure to conduct a unit specific procedure which resulted in a missed technical specification surveil 1 ance te.st. The work order and survei 11 ance test procedure are. now both printed on color coded paper to ensure surveillance tests will be performed on the intended unit. The inspector has n6 further questions at this tim.

Operational Safety Verification*

3.1 Documents Reviewed Selected Operators' Logs Senior Shift Supervisor's (SSS) Log Jumper Log Radioactive Waste Release Permits (liquid & gaseous)

Selected Radiation Work Permits (RWP)

Se 1 ected Chemistry Lo.gs Selected Tagouts Health Physics Watch Log 3.2 The inspector conducted routine entries into the protected areas of the plants, including the control rooms, Auxiliary Building, fuel buildings, and containments (when access is possible). During the inspection acti-vities, discussions were held with operators, 'technicians (HP & I&C),

mechanics, supervisors, and plant managemen The purpose of the in-spection was to affirm the licensee's commitments and compliance with 10 CFR, Technical Specifications, and Administrative Proced~. On a daily basis, particular attention was directed to th~

following areas:

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Instrumentation and recorder traces for abnormalities; Adherence to LCO's directly observable from the control room; Proper control room shift manning and access control; Verification of the status of control room annunciators that are in alarm;

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Proper use of procedures; Review of logs to obtain plant conditions; and, Verification of surveillance testing for timely completio On a weekly basis, the inspector confirmed the operability of selected ESF trains by:

Verifying that accessible valves in the flow path were in the correct positions; Verifying that power supplies and breakers were in the correct positions; Verifying that de-ene,rgi zed portions of these systems were de-energized as identified by Technical ~pecifications; Visually inspecting major components for leakage, lubri-cation, vibration, cooling water supply, and general operating conditions; and, Visually inspecting instrumentation, where possible, for proper operability.

On a biweekly basis, the in~pector:

Verified the correct application of a tagout to a safety-

  • related system; Observed a shift turnover; Reviewed the sampling program including the liquid and gaseous effluents; Verified that radiation protection and controls were properly established; Verified that the physical security plan was being implemented; Reviewed licensee-identified problem areas; and, Verified selected portions of containment isolation lineup.

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      • Inspector Comments/Findings:

The inspector selected phases of the units' operation to determine com-pliance with the NRC's regulations.. The inspector determined that the areas inspected and the licensee's actions did not constitute a health and safety hazard to the public or plant personne The following are noteworthy areas the inspector researched in depth:

3.3. Un-it 1 Unit 1 began the report period operating at the reduced power level of approximately 70% (790 MWe) due to electrical grid system stability limits as a result of the loss of the No. 5015 Hope Creek~ Keeney 500KV lin The licensee completed the installation of the design change and the 10 CFR 50.59 Safety Evaluation for the Unit 1 trip scheme on the loss of the No. 5021 Salem - Deans 500KV line as discussed in Combined Inspection 87-07/87-0 The NRC re-viewed the completed design change package and safety evalu-ation during an NRC-licensee meeting in NRC headquarters on March 27, 1987 (See Attachment A).

The resident inspectors

.verified that procedures and controls were in *place prior to the 11trip-a-unit" (TAU) scheme being enable Discussions were held with Unit 1 and 2 licensed operators and supervisors and the following documents were reviewed:

Integrated Operating Procedure-4, Power Operation Operating Instruction III, Appendix 2, Generator Operating Guide Operating Instruction III, Appendix 3, Generator Cap-ability Curves Console Reading Sheets At 1:20 p.m. on March 28, 1987, TAU was enabled and Unit 1 power was increased to 100%.

The unit operated at 100% power for the remainder of the report period with the exception of several short term load reductions for turbine valve testing, secondary plant repairs and elec-trical system stability requirement No ~iolations were identified.

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Unit 2 Unit 2 began the report period operating at the reduced power level of approximately 70% (790 MWe) due to electrical grid system stability limits as a result of the loss of the No. 5015 Hope Creek - Keeney SOOKV lin On March 28, 1987, the Unit 1 TAU scheme was enabled and Unit 2 power level was increased to approximately 90% (1000 MWe).

At 9:37 p.m. on April 7, 1987, while troubleshooting the tur-bine electro-hydraulic control (EHC) system, a faulty replace-ment circuit card resulted in a Unit 2 turbine trip and reactor trip from 88% powe On April 8, 1987, the licensee restored the EHC system to operable status and was preparing for start~p of the uni During a Mode 3 containment inspection, the licensee identified a bonnet leak on valve No. 2CV27 The valve is the first in a series of two check valves on the normal charging line from the regenerative heat exchanger to No. 23 Reactor Coolant System (RCS) cold leg.* Upon further investigation the licensee discov~red that the valve studs were severely corrode The unit was cooled down to Mode 5 and the RCS water level lowered to facilitate repairs. (See Section 4.1 of this report for details on the repair of the valve.. )

The Unit was returned to service on April 17, 1987 at 12:12 p.m., and operated at approximately 90% power (1000 MWe) for the remainder of the the report perio nn April 10, 1987, a radiation protection technician, upon exiting from the auxiliary building control point after count-ing Unit 2 pressurizer area swipe samples, alarmed the Betamax whole body personnel radiation monito Further monitoring with an RM14-HP210 frisker, which registered offscale on the XlOO scale, identified a small area of skin contamination on the right forear Counting of the contaminated skin area with a Nuclear Data multichannel analyzer/Geli crystal identified the contamination as a miniscule fuel particl The indivi-dual 1 s arm was decontaminated by washing with soap and wate The calculated absorbed dose to one square centimeter of the skin resulted in a skin dose of between 222 - 332 mR (20-30 minute exposure time estimated).

Licensee follow-up actions and results included:

The individual had made one other entry into the auxiliary building earlier in the day, but had subsequently success-fully passed through the Betamax.

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The individual who performed the swipe surveys of the pressurizer had no contamination dete~ted on his person or anti-C clothin Surveys of the count room and path to the control point where the individual had bee No abnormal results were identifie Increased monitoring of personnel, anti-C clothin~ and material leaving the Unit 2 auxiliary buildin No fur-ther problems were identifie Swipe surveys and large area masslin surveys of the pres-surizer are No abnormal results or particles were identifie A step off pad was placed at the base of the pressurizer..

The licensee concluded that the particle may have been present on one of the pressurizer swipe sample Isotope ratios indi-cate that the particle is approximately 225 days old which traces back to around the time of the.Unit 2 refueling outag Three fuel particles were identified in the fuel handling area during the refueling; the licensee surmises that this particle may have been tracked into the pressurizer area during the refuelin The inspector discussed this occurrence with lic-ensee management and reviewed licensee documentation, calcula-tions, and data concernin~ the contamination and follow-u The inspector has no further questions at this tim No violations were identifie.

Matntenance Observations The inspector reviewed the following safety related maintenance activities to verify that repairs were made in accordance with approved procedures and in compliance-with NRC regulations and recognized codes and standards. The-inspector also verified that the replacement parts and Quality Control uti-lized on the repairs were in compliance with the licensee's QA progra.1 On April 8, 1987 during a Unit 2 Mode 3 containment inspection in pre-paration for startup, the licensee identified a bonnet leak on valve N CV27 The valve is the first in a series of two check valves on the normal reactor coolant system (RCS) charging line between the regenera-tive heat exchanger and No. 23 RCS cold le The check valve w~s wrapped in insulation and the leak was identified by boron crystallization on the insulation and on the floor under the valv Upon removal of the insulation, the licensee observed that the valve body to bonnet nuts and

. studs were severely corrode The materials involved are as follows:

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body - No. 316 stainless steel nuts - Grade 2H carbon steel studs - Grade 87 chrome-moly carbon steel The unit was cooled down to Mode 5 and the RCS drained to the 98 foot elevation to facilitate valve repai The nuts, studs, and gasket were replace In addition, the li-censee inspected the downstream check valve (No. 2CV78), and the two check valves (Nos. 2CV275 and 2CV80) on the

alternate charging line to No. 24 RCS cold le No problems were ob-served with these valve The lagging on the covers of 2CV274 and 2CV78 was not replaced following valve maintenance to facilitate inspections to identify degradation prior to leakag The covers of 2CV275 and 2CV80 were already expose The inspector reviewed the following documents relative to the valve repair:

Work Order No. 870408006 Code Job Package 587-079 Deficiency Reports Nos. SSP-87-121 and SSP-87-131 10 CFR 50.59 Safety Evaluation (to use 3 1/2 11 b*olts instead of studs since a seismic support near the valve does not allow enough clear-ance to replace with studs)

Inspection*Point Checklist Form NR-1 Report of Repair to Nuclear Components and Systems in Nuclear Power Plants Code Job Package Approval Cover Sheet Procedure No. M14A-3 General Instructions for Check Valve Mainten-ance Procedure M9-IIP-2 ISI Visual Examination of Bolting and Component Internal Surfaces, Nuclear Class 1, 2, and 3 Visual Examination Data Sheet Storeroom Material Issue Records Quality Release Tags Public Service Blue Print No. 106251

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Radiation Work Permit Nos. 87-25-203 and 87-25-205 No violations were identified, however an error in the identification of material type classifications on the Visual Exami.nation Data Sheet was brought to the licensee's attention by the inspecto.2 The inspector followed the disassembly, inspection, repair and retest of a body to bonnet leak on valve 22AF22 (downstream isolation valve for 22AF21, steam generator No. 22 inlet control valve).

The inspector re-viewed the following documents relative to. this maintenance activity:

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Work Order No. 870304042 Code Job Package S-87-084 Deficiency Reports SMD-M87-069, SMD-M87-069A, and SMD-M87-070 10 CFR 50.59 Safety Evaluation (to reuse pressure seal gaskets and weld repair the bonnet)

10 CFR 50.59 Safety Evaluation (to use Furmanite sheet packing to seal body to bonnet leak until new parts are ordered and installed)

Code Job Package Approval Cover Sheet Welding Procedure Specification NDWP-13 Weld History Record Inspection Point Checklist Nondestructive Examination Reports

Magnetic Particle Exam of Bonnet Prior to Weldi~g

Liquid Penetrant Exam of Welds on Bonnet Procedure M14A-1 General Instruction for Bolted Bonnet Gate Valve Maintenance Procedure MllD Pressure Test Storeroom and Pre-stage Materiat Issue Records A hydrostatic test was attempted in accordance with MllD, however since valve 22AF23 (stopcheck valve downstream of 22AF22) does not provide isolation in the direction of normal flow, the test pressure could not

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be attaine The licensee requested the Authorized Nuclear Inspector (ASME Code Inspector) to waive the requirement.. An inservice leak test was substituted for the hydrotest and was successfully complete No violations were identifie.

Surveillance Observations During this inspection period, the inspector reviewed in-progress surveillance testing as well as completed surveillance package The inspector verified that* the surveillance tests were performed in accordance with licensee ap-proved procedures and NRC regulations. The inspector also verified that the instruments used were within calibration tolerances and that qualified tech-nicians performed the surveillance test The following surveillance tests were reviewed:

Unit 1 Procedure lPD-4. 5. 011 1 PD-4. 1. 025 Reactor Engineering Part 2, Section Unit 2 Procedure SP(0)4.1.2.1A SP(0)4.6. IC-2.6.027 SP(0)4.4.7.2d SP(0)4.7. '-

Manual, No violations were identified.

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Description Radiation Monitoring System 1Rl6 Plant Vent Effluent Channel Calibration Chec Low results were obtained so a full calibration was performed in accordance with the following procedure.*

Radiation Monitoring System 1R16 Plant Vent Effluent Channel Calibration Calorimetric Calculation Description Reactivity Control Systems - Boration Flow Path Containment Systems - Purge Supply and Exhaust Isolation Valves Reactor Protection System - 2FT-511, No. 21 Steam Generator Feedwater Flow Protection Chan-nel II - Functional Test Reactor Coolant System - Water Inventory Balance Main Steam Isolation Valve Emergency Close Time Response

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10 Review of Periodic and Special Reports Upon receipt, the inspector reviewed periodic and special report The review included the following: inclusion of information required by the NRC; test results and/or supporting information consistent with de.sign predictions and performance specifications; planned corrective action for resolution of prob-lems, and reportability and validity of report informatio The following periodic reports were reviewed:

Unit 1 Monthly Operatirig Report - March 1987 Unit 2 Monthly Operating Report - March 1987 No violations were identifie Licensee Event Report Followup The inspector reviewed the following LERs to determine that reportability requirements were fulfilled, immediate corrective action was taken, and cor-rective action to prevent recurrence had been accomplished in accordance with Technical Specification Unit 1 86-001 87-002 Refueling Water Storage Tank (RWST) Boron Concentration Out of Specification Due to Personnel Error On March 9, 1987 during a review of chemistry logs, the licensee discovered that the boron concentration for the RWST on January 30, 1987 was 5 ppm greater than the 2200 ppm Technical Specification limit. A sample taken on February 4, 1987 was within specificatio The out of specification boron result was not initially recognized because the Technical Specification limit listed ori the chemistry data sheet as 2000 ppm had not been updated following~ Technical Specification amendment changing the limit to 2000 - 2200 pp The chemistry log book data sheets have been proceduralized and revised to reflect the correct limit The inspector*discussed this occur-rence and corrective actions taken with the licensee and has no further question Loss of Control of a High Radiation Area Locked Door Due to Per-sonnel Error This event was discussed in Inspection Report 50-272/87-0 The inspector reviewed the LER and has no further questions.

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  • Unit 2 87-003 87-004 86-013-

11 Fuel Handling Crane Missed Surveillance Due to Personnel Error On February 26, 1987, fuel handling crane manipulations were done by a licensee vendor prior to performing the crane overload cutoff surveillance test-within the specified time as required by Technical Specification 4.9.7 and FP-PNJ-FE-1, "Fuel Inspection Procedure."

The surveillance was subsequently performed satisfactorily on the same da A previous similar occurrence, involving the same vendor, took place on November 17, 1986 and was discussed in Inspection Report 50-311/

86-3 Failure to perform the overload cutoff surveillance test within 7 days (plus 25% extension) prior to use is a violation of Technical Specification 4. In accordance with 10 CFR 2, Appen-dix C, a notice of violation was not issued for the November 17, 1986 missed surveillance tes However, it appears that the licensee's corrective actions for the first occurrence were not effective in preventing the violation from recurring. This is a violation (50-311/87-11-01).

Generator-Turbine/Reactor Trip Due to Loss of Field on the Main Generator This event was discussed in Inspection Report 50-311/87-0 The

  • root. cause of the loss of generator field is under investigation by the license The inspector will review the licensee's supple-mental report when issue Turbine/Reactor Trip from 8% Power on P-7 Interlock Due to Personnel Error While Controlling Speed Using Governor Valve Position Limit This event was discussed in Inspec~ion Reports 50-311/86-36 and 50-311/87-01." This supplemental LER changes the root cause of the occurrence to personnel error, rather than equipment malfunction as reported in LER 86-01 The inspector has no further question One violation was identifie.

Allegation Followup The resident inspectors conducted an investigation into allegations made in a letter to Senator Bradley by a concerned citizen. The letter states that a listener to a news station called in and discussed her visit to Salem, New Jersey where she observed workers from the nuclear power plant using.drugs.

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The results of the inspector's investigation are as follows:

The licensee has a drug testing program that tests all new employees, both contractor and permanent, prior to allowing access to the facilit The licensee has an ongoing system of unannounced physical examinations which includes drug testing for all employee Several personnel have been dismissed as a result of the drug testing. This program also in-cludes a rehabilitation program for personnel who need and apply for hel In accordance with the drug program on site, supervisors are trained in the assessment of employees through the observation of impaired perform-ance or aberrant-behavio The resident inspectors deal with many employees on a daily basis and are also alert for impaired performance or aberrant behavio The inspectors conclude that programs have been implemented and appear to be effective in restricting site access to personnel who are free from drug and alcohol abus.

Exit Interview At periodic intervals during the course of the inspection, meetings were held with senior facility management to discuss the inspection scope and finding An exit interview was held with licensee management at the end of the report-ing perio The licensee did not identify 10 CFR 2.790 material.

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