IR 05000255/1989009

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Forwards Safety Insp Rept 50-255/89-09 on 890314-0410 & Notice of Violation.Record Copy
ML20245K690
Person / Time
Site: Palisades Entergy icon.png
Issue date: 04/21/1989
From: Axelson W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Hoffman D
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
References
NUDOCS 8905050133
Download: ML20245K690 (1)


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Docket No. 50-255 APR 211989

l Consumers Power Company ATTN:

David P. Hoffman Vice President Nuclear Operations

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1945 West Parnall Road Jackson, MI 49201 Gentlemen:

This refers to the routine safety inspection conducted by Messrs. E. R. Swanson, J. K. Heller, and M. A. Kunowski during the period of March 14 through April 10, 1989, of activities at the Palisades Nuclear Generating Plant authorized by NRC Provisional Operating License No. DPR-20, and to the discussion of our findings with Mr. G. B. Slade and others of your staff and at the conclusion of the inspection.

The enclosed copy of our inspection report identifies areas examined during the inspection. Within these areas, the inspection consisted of a selective examination of procedures and representative records, observations, and interviews with personnel.

During this inspection, certain of your activities appeared to be in violation i

of NRC requirements, as specified in the enclosed Notice. A written response is required.

The responses directed by this letter and the accompanying Notice are not subject to the clearance procedures of the Office of Management and Budget as required by the Paperwork Reduction Act of 1980, PL 96-511.

In accordance with 10 CFR 2.790 of the Commission's regulations, a copy of this letter, your response and the enclosed inspection report will be placed in the NRC Public Document Room.

We will gladly discuss any questions you have concerning this inspection.

Sincerely, W.

. AR i s il t Projects Branch 2

Enclosures:

1.

Notice of Violation 2.

Inspection Report

No. 50-255/89009(DRP)

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See Attached Distribution

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NOTICE OF VIOLATION

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Consumers Power Company

Docket No. 50-255

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As a result of the inspection conducted on March 14 through April 10, 1989,.

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and in a

REGION III==

Report No. 50-255/89009(DRP)

Docket No. 50-255

License No. DPR-20

Licensee: Consumers Power Company

212 West Michigan Avenue

Jackson, MI 49201

Facility Name:

Palisades Nuclear Generating Plant

Inspection At:

Palisades Site, Covert, Michigan

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Inspection Conducted: March 14 through April 10, 1989

Inspectors:

E. R. Swanson

J. K. Heller

M. A. Kunowski

Approved By:

.L.

urggts, Chief

f/ 2//'77

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Reactor Projects Section 2A

Da'te

Inspection Summary

Inspection on March 14 through April 10,1989 (Report No. 50-255/89009(DRP)

Areas Inspected:

Routine unannounced inspection by the resident inspectors

of: actions on previously identified items; operational safety verification;

radiological controls; maintenance; surveillance; security; safety assessment /

quality verification; reportable events; Engineered Safety System walkdown;

and allegation followup.

Several SEP open items (Safety Issues Management

System (SIMS) items) were reviewed.

Results: Of the areas inspected, one violation was identified (leak testing

of the containment escape lock - Paragraph 6.f).

The inspection did not

disclose any notable weaknesses in the licensee's programs. The inspection

noted strengths in the areas of operator turnovers and the licensee's ability

to maintain black board conditions during most of the period.

No new Open

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Items and/or Unresolved Items were identified.

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DETAILS

1.

Persons Contacted

Consumers Power Company

G. B. Slade, Plant General Manager

+J.

G. Lewis, Technical Director

R. D. Orosz,-Engineering and Maintenance Manager

R. M. Rice, Operations Manager

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+W. L. Beckman, Radiological Services Manager

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+R. E. McCaleb, Planning and Administrative Director

+R. A. Fenech, Operations Superintendent

+K. E. Osborne, Projects Superintendent

+K. M. Hass, Reactor Engineering Superintendent

+R. P. Margol, QA Administrator

R. M. Brzezinski, I&C Superintendent

L. J. Kenaga, Staff HP

+C. S. Kozup, Licensing Engineer

+J. R. Brunet, Licensing Analyst

D. J. Malone, Licensing Analyst

R. J. Frigo, Operations Staff Support Sur,ervisor

U.S. Nuclear Regulatory Commission (USNT.CJ

+E. R. Swanson, Senior Resident Inspector

+J. K. Heller, Resident Inspector

+ Denotes those present at the Management Interview on April 12, 1989.

Others members of the plant staff, and several members of the Contract

Security Force, were also contacted during the inspection period.

2,

Actions on Previously Identified Items (92701, 92702)

a.

(Closed) Open Item 255/04S09-00(DRP): Effects of charging line and

letdown system pipe breaks. The NRC documented acceptance of the

licensee's analysis, submitted May 31, 1985, which demonstrated that

the subject pipe breaks need not be postulated in a Safety Evaluation

dated February 4,1987.

b.

(0 pen) Open Item 255/04S10-00(DRP):

Completion of evaluation of

specific components for seismic design.

Consumers Power responded

to the NRC's questions on April 30, 1987.

The NRC's review of

this issue is tracked under SEP Topic III-6 and Unresolved Safety

Issue A-46.

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c.

.(0 pen) Open Item 255/04S12-00(DRP):

Evaluation of specific

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structural loads referenced in SEP Topic III-7.B and IPSAR 4.12.

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The NRC is reviewing the licensee submittals.

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d.

(0 pen) Open Item 255/04S15-02(DRP): Consumers Power committed

to submit revised Technical Specifications for primary coolant

leakage detection systems inside containment as documented in the

IPSAR 4.15.2 (NUREG-0820). As committed in their January 24, 1989

letter, the licensee will submit revised Technical Specifications

as part of their restructured Technical Specification effort.

e.

(Closed) Open Item 255/04S28-02(DRP):

Install forced coeling

for inverter and charging cabinets and AFW junction boxes. The

inspector verified that fans had been installed in the inverter

cabinets.

The NRC is preparing a Safety Evaluation of this topic

(SEP IX-5, IPSAR 4.28.2).

f.

(Closed) Open Item 255/86035-08(DRP): Develop a long term solution

to the freezing of the stack gas flow recorder sensing lines. A

monthly periodic activity control (PAC) has been generated to

periodically blow down the sensing lines.

PAC RIA-002 has been

performed on a monthly basis (+/- 25 percent) since May 1988.

In

a letter to File PR12/01/86A-258 the system engineer stated that

this is an acceptable alternative to modifying the sensing lines

or revising the piping.

g.

(Closed) Open Item 255/86035-10(DRPj: The licensee will evaluate

the flow characteristic of Auxiliary Feedwater (AFW) flow control

Valves FCV-0736A, FCV-0737A, FCV-0727 and FCV-0749 to determine the

methodology to improve flow control below 100 gpm.

The licensee

chose to install per FC-789 a 1 and 1/2" bypass flow control valve

for the

"C" AFW pump.

The inspector reviewed the control room

prints and confirmed that the prints reflected the Facility Change.

Also, the inspector discussed the modification with control room

operators and confirmed that they had been trained on the

modifications. An Engineering review team has selected FC-789

for additional reviews.

Items identified by that review are

discussed in Inspection Report No. 255/89007.

h.

(0 pen) Open Item 255/86035-12(DRP):

Replace AFW Valve CV-0521

because internal valve leakage is causing a slow rotation of the

Turbine Driven Auxiliary Feedwater (TDAFW) pump, The valve was

repaired by the vendor per Work Order 24706677.

Internal

Correspondence DAB 89*002 stated the valve was repaired satisfactory

and is leak tight. A tour of the AFW pump room on March 22, revealed

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that the TDAFW still has a slow rotation. The inspector discussed

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this with control room operators and found that at the start of

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operations subsequent to the 88 refueling outage that the pump was

not rotating. The inspector has asked the licensee to revisit this

item and determine if additioral actions are required.

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1.

(Closed) Open Items 255/86035-18, -19 and -20(DRP):

Resolve the

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component cooling water pumps mechanical seal leakage problems.

During the 88 refueling, the

"C" pump was modified at the vendor

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facilities per SC 86-269 to accept a different mechanical seal.

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In addition, modified sleeves and nuts were installed on the pump.

Internal Correspondence GJS 89*002 stated that the repairs appear

successful in eliminating the seal leakage problem.

The licensee

plans to modify'the "A" and "B"' pump during an upcoming refueling

outage.

J.

(Closed) Open Item 255/88020-05(DRP):

The thermal overload on one

phase of the Emergency Diesel Generator starting air. compressor

motor was tripping.

It was found that the overloads were recently

replaced with a new style and one phase required a minor calibration.

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No similar problems have recurred.

No violations, deviations, unresobed or open items were identified.

3.

Operational Safety Verification (71707, 71710, 42700)

Routine facility operating activities were observed as conducted in

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the plant and from the main control rooms.

Plant startup, steady

power operation, plant shutdown, and system (s) lir.eup and operation

were observed as applicable.

The performance of licensed Reactor Operators and Senior Reactor Operators,

of Shift Technical: Advisors,.and of auxiliary' equipment operators was

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observed and evaluated including procedure use and adherence, records

and logs, communications, shift / duty turnover, and the degree of

professionalism of control room activities.

Evaluation, corrective action, and response for off normal conditions or

events, if'any, were examined. This included compliance to any reporting

requirements.

Two events (D-PAL-89-012 and 036) identified and. implemented

corrective action for late, and ' failure to implement, fire watch

requirements.

Observations of the control room monitors, indicators, and recorders were

made to verify the operability of emergency systems, radiation monitoring -

systems and nuclear reactor protection systems, as applicable. A strength

noted was the " black board" conditions maintained during most of the

period except during testing and repair activities. Operators were

well informed as to the reasons'for any alarms which indicates that

good turnovers are being conducted.

Reviews of surveillance, equipment

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condition, and tagout logs were conducted.

Proper return to service

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of selected components was verified. Activities' reviewed are discussed

below,

a.

Steam Generator Tube Leakage

The unit began the reporting period at a reduced power level of

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approximately 60 percent to maintain primary to secondary leakage

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at an acceptable level, while plans for a steam generator tube

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inspection outage were formalized. On April 3, during a licensee

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initiated conference call, the plant manager informed NRC personnel

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consisting of the resident inspection staff, the NRR project manager,

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section chiefs from Region III Divisions of Reactor Safety and

Reactor Projects, and NRR staam generator specialists, of six

options that were being considered by senior Consumers Power

corporate managers pertaining to operation of Palisades until

the upcoming outage.

The option that was implemented on April 4,

consisted of a power increase in three distinct steps to 90 percent

power with a specified holding period between steps.

Limitations

pertaining to the leakrate and off gas were imposed and

contingencies established if the limits were exceeded. A

90 percent power limit was a previously established administrative

limit to resolve NRC concerns pertaining to tube leakage.

Prior the

power increase, the resident inspection staff was informed of the

option selected. At the close of this inspection period, the power

level had been increased to 80 percent power with no changes in

primary to secondary leakrate.

b.

Post Accident Operation of the Component Cooling Water System

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On March 27, the licensee became aware of a potentially significant

design deficiency in the Component Cooling Water (CCW) system relating

to the lack of a qualified (safety grade) air system-to support the

operation of the CCW containment isolation valves.

The CCW piping

inside containment is not seismically qualified and has not been

reviewed for high energy line break (HELB) concerns.

Containment

isolation valve CV-0910 does not have an air accumulator and would

fail open on loss of air. Therefore, a HELB could result in a

complete loss of CCW and a containment integrity violation.

Postulating a single failure of the 1-2 diesel generator, all

containment cooling would be lost.

This concern should have been

evaluated under the NRC's Systematic Evaluation Program, but

apparently was not because the system portion inside containn.ent

is not considered safety related.

The issue was identified under

the licensee's Configuration Control Project design basis

reconstitution effort, a part of a continuing corrective action.

It is expected that a LER will be submitted discussing this

discovery.

c.

Off Gas Monitoring

(1) The licensee has installed an additional off gas flow meter

that is calibrated in the 0-3 cfm range.

The other flow meter

was not calibrated in this range and would not provide repeatable

readings in this range.

Primary to secondary leakrate

calculation results dropped by a factor of 10, as result

of the more accurate readings from the new meter.

(2) The inspector observed an auxiliary operator take an off

gas flow reading and implement the procedural requirements of

Paragraph 7.8.1 to S0P 13, " Air Ejector, Gland Steam Condenser

and Condenser Vacuum pump."

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(3) During a Turbine'Buiiding. tour on April 5, the inspector

observed the needle of the.5 to 3 cfm off gas flow meter

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rapidly bouncing from off scale. low to approximately.75 CFM.

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The inspector found that the. instrument root isolation valves

had not been closed subsequent to the last off gas measurerr. ant.

An Auxiliary Operator closed the root isolation valve and the

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reading. returned to zero.

This was discussed with-the Shift

Supervisor and Operation Superintendent.

A review of S0P 13 reveals that this configuration was contrary-

to the restoration steps of paragraph 7.8.1. This was discussed

at the management interview.

d.

During a. tour of the Auxiliary Building on April 10, the inspector

identified. leakage (a small spray) from a main feedwater vent line-

near the containment penetration.

The. leakage was at the cap on the

line. The inspector verified that the line and manual Valve FW-746

were not considered part of the containment integrity boundary and

that a work request was subsequently initiated.

No violations, deviations, unresolved or open items were identified.

4.

Radiological Controls (71707)

During routine tours of radiologically controlled plant facilities or

areas, the inspector observed occupational radiation safety practices

by the radiation protection staff and other workers.

Effluent relea~ses were routinely checked, including examination of

on-line recorder traces and proper operation of automatic monitoring

equipment.

. Independent surveys.were performed in various radiologically controlled

areas. The' inspector witnessed the conduct of a survey being performed

in'the West Safeguards Room.

5.

Maintenance (62703, 42700)

Maintenance activities in the-plant were routinely inspected, including

both corrective maintenance (repairs) and preventive maintenance.

Mechanical, electrical, and instrument and control group maintenance

activities were included as available.

The focus of the inspection was to assure the maintenance activities

reviewed were conducted in accordance with approved procedures,

regulatory guides and industry codes or standards and in conformance

with Technical Specifications.

The following items were considered

during this review: the Limiting Conditions for Operation were met while

components or systems were removed from service; approvals were obtained

prior to initiating the work; activities were accomplished using approved

procedures; and post maintenance testing was performed as applicable.

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The following activities were inspected:

a.

Repair of Sigma Indicator TIC-0111H (W,0. 24901095)

b.

Rebuild of Relief Valve RV-0527 (W.0. 24901031)

c.

Auxiliary Feedwater Pump Governor packing adjustment

(W.O. 24901446)

d.

Blowdown flow meter cleaning and repair (W.0. 24901304)

e.

Pump (P-60) alignment and coupling (W.0. 24901341, RWP P890240)

f.

Remove, calibrate and reinstall the 0-3 cfm flow meter

(W.O. 24901663)

g.

Install mechanical tube plugs in "B" steam generator (W.O. 24900478).

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The inspector confirmed the plugs were receipt inspected by review

of Purchase Order CP11-7012Q.

No violations, deviations, unresolved or open items were identified.

6.

Surveillance (61720, 61726, 42700)

The inspector reviewed Technical Specifications required surveillance

testing as described below and verified that testing was performed in

accordance with adequate procedures, that test instrumentation was

calibrated, that Limiting Conditions for Operation were met, that removal

and restoration of the affected components were properly accomplished,

that test results conformed with Technical Specifications and procedure

requirements and were reviewed by personnel other than the individual

directing the test, and that deficiencies identified during the testing

were properly reviewed and resolved by appropriate management personnel.

The following activities were inspected:

a.

00-21

Auxiliary Feedwater System Valve Test (CV-0521)

This test demonstrated the operability of the steam admission

valve and also the turbine control after adjustment of the governor

packing.

The test was successful but also revealed that the steam

pressure control was still not optimum in that the relief valve

lifted several times before steady state operation was achieved.

The inspector verified that long range plans exist to resolve this

issue which include the installation of new air supplies to the

steam valves which will modulate their operation and, if that is

not successful, system design changes.

b.

DWO-1

Daily Control Room Surveillance.

c.

SHO-1

Operators Shift Surveillance.

d.

S0-4b

Escape Air Lock Penetration Leak Test.

e.

DWO-13

Local Leak Rate Test for Inner and Outer Personnel

Air Lock Door Seals"

f.

S0-4a

Personnel Air Lock Penetration Leak Test

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The inspector performed a technical review of S0-4b and DWO-13 using

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10 CFR 50 Appendix J, Standard Technical Specifications and the

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vendor manuals (Licensee Files C-53) as references and referred

the following items to the site licensing engineer.

(1) The inspector found that a between the seal test of the

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escape lock door was not performed after the escape air

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lock penetration test was completed on March 2, 1989.

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Interviews with personnel involved with the test indicated

that the air lock doors were opened a number of times to

restore the air lock to service following the test.

Restoration includes removal of the strong backs and

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fluffing of the seals to remove the seal set induced

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by the strong backs.

10 CFR 50, Appendix J, III.D.2.(b) (iii) requires that air

locks opened during periods when containment integrity is

required shall be tested within three days after being

opened.

For air lock doors that have testable seals, testing

the seals fulfills the three-day test requirements.

In the

event that the testing for the three-day interval cannot be

done at Pa, the test pressure shall be stated in the Technical

Specification.

The current Technical Specifications do not address 10 CFR 50,

Appendix J, III.D.2.(b) (iii) but the licensee does have a

Technical Specification change request that is pending with

NRR. The proposed Technical Specification does require a

reduced pressure between the seal test after use of air locks.

The licensee is implementing this requirement after each use of

the personnel air lock but not for the escape air lock. The

escape air lock vendor's manual does not recommend a between

the seals test be performed at Pa but does state the seal

should be capable of a reduced test pressure.

Failure to do a between the seals test of the escape air lock

after each use of the air lock is a violation of 10 CFR 50,

Appendix J, III.D.2.(b) (iii) (255/P9009-01(DRP)).

(2) The inspector noted that the licensee Technical Specification

change request is for a reduced pressure between the seals

test.

However, the proposed Technical Specification does not

provide an acceptance criteria. A review of Standard Technical

Specification reveals that a general acceptance criteria for

reduced pressure testing appears to be.01 La. The acceptance

criteria implemented in DWO-13 is approximately.025 La. The

inspector asked the licensing engineer to review the information

and assure the appropriate acceptance criteria is used.

In

addition, the inspector discussed this item with the NRR

Project Manager on March 16 for consideration during review

of the Technical Specification change request.

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MO-7A

Emergency Diesel Generator Test.

One violation and no deviations, unresolved or open items were

identified.

7.

Security (71707)

Routine facility security measures, including control of access for

vehicles, packages and personnel, were observed.

Performance of

dedicated physical security equipment was verified during inspections

in various plant areas.

The activities of the professional security

force in maintaining facility security protection were occasionally

examined or reviewed, and interviews were occasionally conducted with

security force members. Tours of the central and secondary alarm

station were routinely conducted.

No violations, deviations, unresolved or open items were identified.

8.

Safety Assessment / Quality Verification (35502, 40500)

The effectiveness of management controls, verification and oversight

activities, in the conduct of jobs observed during this inspection,

was evaluated.

The inspector frequently attended management and supervisory meetings

involving plant status and plans and focusing on proper coordination

among Departments.

The results of licensee auditing and corrective action programs were

routinely monitored by attendance at Corrective Action Review Board

(CARB) meetings and by review of Deviation Reports, Event Reports,

Radiological Incident Reports, and security incident reports. As

applicable, corrective action program documents were forwarded to

NRC Region III technical specialists for information and possible

followup evaluation.

No violations, deviations, unresolved or open items were identified.

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9.

Reportable Events (92700, 93720)

The inspector reviewed the following Licensee Event Reports (LERs) by

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means of direct observation, discussions with licensee personnel, and

review of records. The review addressed compliance to reporting

requirements and, as applicable, that immediate corrective action

and appropriate action to prevent recurrence had been accomplished.

(Closed) LER 255/84001:

Loss of offsite power and communications.

Appropriate modifications, training, and procedure changes were made,

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which resolved the myriad of issues involved in the event.

Licensee

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Reports D-PAL-84-003, D-PAL-84-007, D-PAL-87-004, NAPO Report P85-36,

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and PRC minutes 85-37 were reviewed.

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(Closed) LER 255/840022-02:

Containment temperature exceeded the

analyzed value. The licensee revised their surveillance procedures

to require a plant shutdown if the containment temperature exceeds the

currently analyzed 145 degrees Fahrenheit. A Technical Specification

limit is planned to be submitted as part of the Restructured Technical

Specifications. The licensee is continuing to evaluate methodology for

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determining air temperature and the adequacy of installed

instrumentation.

(Closed) LER 255/86004-02:

Main Steam Relief valves failed to meet

the "as found" acceptance criteria. A Technical Specification change

was submitted and approved relaxing the tolerance requirements from

+/- 1 percent to +/- 3 percent, which bounded the tolerances identified

during this testing.

(Closed) LER 255/86017-01:

Primary Coolant System (PCS) leakage was

greater than one gpm requiring a plant shutdown.

Two sources were found.

Relief Valve RV-2006 which protects the letdown system piping had not

reseated and was discharging the PCS to the quench tank.

Disassembly

of the valve determined that the bellows were distorted.

Evaluation

of the valve determined that it was suitable for its service and it was

repaired and reinstalled. The secondary cause of the leakrate, was the

failure of three valves in the reactor head vent system to reseat.

These

valves, PRV-1067, PRV-1068, PRV-1072, were found to contain metal shavings

which were left in the system during fabrication. This conclusion was

reached'after the shavings were analyzed by Battelle (Columbus) to

determine their source.

The valves were replaced, the head vent system

was flushed and corrective action was taken to improve cleanliness

controls during modification work (refer to D-PAL-86-154).

No violations, deviations, unresolved or open items were identified.

10.

Engineered Safeguards System Walkdown (71710)

The inspector performed a walkdown of the Chemical Spray Additive System

and verified that each accessible valve in the flow path was in its

required position and operable, that power was aligned for components

that actuate on an initiation signal, that essential instrumentation

was operable; and that no conditions existed which could adversely

affect system operation.

The licensee was provided the identification

of a valve which was missing a label, and questions about changes to

the valve lineup for their resolution.

No violations, deviations, unresolved or open items were identified.

11. Allegation Followup (99024)

(Closed) Allegation (AMS No. RIII-88-A-0163): The following discussion

relates to an allegation concerning the radiation protection program,

which was evaluated during this inspection. The evaluation consisted of

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a review of licensee records and NRC Inspection Reports, and discussions

with licensee personnel.

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Concern No. 1: A dose of 1800 mrem assigned to an individual for steam

generator work in February 1978 was too low.

Discussion:

The alleged stated that during each of three separate

entries (" jumps") into a steam generators, his dosimeter went off

scale. He stated that he was assigned a dose of 1800 mrem total for

the three jumps, but he contends that this assigned dose was too low.

No documentation was provided by the alleger to support his contention

that his dose should have been higher. A review of licensee's dosimetry

records maintained for the individual indicated that the individual was

provided with three separate dosimetry devices to monitor his radiation

dose. According to the records, on January 23, 1978, the ir;dividual's

self-reading dosimeter (SRD) went off scale and his TLD badge read

670 mrem (the inspecto 5 could not establish the range of the dosimeter

worn by the allegerb

, January 24, 1978, the dosimeter again went

offscale and the TLD adp read 999 mrem; and on January 26, 1978, the

dosimeter again went M M ale and the TLD badge read 413 mrem, for a

total exposure by TLD badge of 2082 mrem. The record also indicated

that on January 30, 1978, the dosimeter read 0 and the TLD badge read

4 mrem, and on January 31, 1978, the dosimeter read 0 and the TLD badge

read 2 mrem, for additional total exposure by TLD of 6 mrem.

In total,

for the month of January 1978, the record lists the individual's final

exposure according to his TLD badges as 2088, while his monthly film

badge reading was 1800 mrem.

(There was no indication that the individual

received any radiation dose in February 1978.) At the time, Palisade's

practice was to use the film badge as the official record of worker

exposure, to satisfy the requirements of 10 CFR 20, and use the less

accurate TLD badge and the SRD as secondary or back-up dosimeters to

quickly provide exposure information. The TLDs and SRDs were read onsite

after each entry, whereas the film badges had to be sent to an independent

contractor offsite for a monthly readout. The 14% difference between the

TLD dose and the film badge dose is consistent with the accuracy of the

two methods and is not a health and safety concern nor a regulatory

concern.

An inspection conducted at Palisades by NRC radiation specialists in

,

January 1978, reviewed the licensee's control over outage activities,

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specifically steam generator work (Inspection Report No. 50-255/78-02).

)

The inspectors noted that during the work, the licensee experienced a

shortage of low-range (0-200 mrem) and high-range (0-1 rem and 0-5 rem)

SRDs; however, the inspectors verified that workers were sent into areas

only after surveys had been performed, wore film and TLD badges, and were

limited on their stay times so that an over-exposure was unlikely.

From

a health and safety perspective, the limitation on stay time imposed by

the licensee was an acceptable substitute for the lack of SRDs.

Findings: The allegation is not substantiated. Although the alleger's

SRD went off scale during three steam generator jumps, the individual's

dose was adequately monitored by a film badge and a backup TLD dosimeter.

The 1800-mrem dose assigned to the alleger was based on the film badge,

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which was the licensee's officially designated dosimeter at the time.

'

The allegation is closed.

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.

Concern No. 2: The licensee did not evaluate an uptake received by the

alleger when his airline became disconnected during a steam generator

jump.

Discussion: The inspectors were not able to retrieve any licensee

records that specifically dealt with the alleged airline disconnect.

However, the inspectors did review records that indicated that the

alleger received a whole body count on February 1,1978, shortly after

his steam generator entries. Whole body counting is an acceptable method

for evaluating possible uptakes of radioactive material, including that

found in steam generator channel heads during maintenance. The results

of this whole body count indicated the presence of approximately four

nanocuries of Cs-137 in the individual, a value which indicates exposure

to airborne radioactivity of no more than about 0.1% of the NRC limit

during the individual's steam generator jumps. NRC review in 1978 of

the licensee's whole body counting system and results of many counts

conducted during the outage determined that the licensee whole body

counting system was adequate and no exposures to airborne radioactive

material in excess of regulatory limits occurred during the outage

<

(Inspection Reports No. 50-255/78-02; 50-255/78-11).

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Findings: The allegation is not substantiated. The licensee conducted

a whole body count of the alleger shortly after the steam generator work.

Although this whole body count may not have been specifically given to

evaluate any uptake resulting from the alleged airline disconnect, it

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served that purpose. The amount of radioactive material detected by

the whole oody count indicated that the individual was not exposed to

airborne radioactivity in excess of regulatory limits during his steam

generator work.

NRC review during the period of concern determined that

the licensee was providing adequate internal exposure control and

assessment. The allegation is closed.

No violations, deviations, unresolved or open items were identified.

12. Management Interview (30703)

The inspectors met with licensee representatives (denoted in Paragraph 1)

on April 12, 1989, to discuss the scope and findings of the inspection.

In addition, the inspector also discussed the likely informational content

of the inspection report with regard to documents or processes reviewed by

the inspector during the inspectidn.

The licensee did not identify any

such documents / processes as proprietary.

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