IR 05000244/2010006

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IR 05000244-10-006; 05/24/10 - 06/11/2010; R.E. Ginna Nuclear Power Plant; Biennial Baseline Inspection of the Identification and Resolution of Problems
ML101900511
Person / Time
Site: Ginna Constellation icon.png
Issue date: 07/09/2010
From: Glenn Dentel
Reactor Projects Branch 1
To: John Carlin
Constellation Energy Nuclear Group
Dentel, G RGN-I/DRP/BR1/610-337-5233
References
IR-10-006
Download: ML101900511 (23)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406-1415 July 9. 2010 Mr. John T. Carlin, Vice President R.E. Ginna Nuclear Power Plant, LLC Constellation Energy Nuclear Group, LLC 1503 Lake Road Ontario, New York 14519 SUBJECT; R.E. GINNA NUCLEAR POWER PLANT NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000244/2010006

Dear Mr. Carlin:

On June 1'1, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your R.E. Ginna Nuclear Power Plant. The enclosed report documents the inspection results, which were discussed on June 11, 2010. with you and other members of your staff.

This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, and compliance with the Commission's rules and regulations and the conditions of your operating license. Within these areas, the inspection involved e~:amination of selected procedures and representative records, observations of activities, and interviews with personnel.

Based on the samples selected for review, the inspection team concluded that Constellation was generally effective in identifying, evaluating and resolving problems. Ginna personnel identified problems at a low threshold and entered them into the Corrective Action Program (CAP). Ginna screened issues appropriately for operability and reportability, and prioritized issues commensurate with the safety significance of the problems. Causal analyses appropriately considered extent of condition, generic issues, and previous occurrences.

Corrective actions addressed the identified causes and were typically implemented in a timely manner. However, the team noted several examples of less than adequate evaluation or documentation of evaluations, and examples where corrective actions were not timely and effective.

This report documents one NRC-identified finding of very low safety significance (Green). The finding was determined to involve a violation of NRC requirements. However, because of its very low safety significance and because it has been entered into your corrective action program, the NRC is treating this finding as a non-cited violation (NCV), in accordance with Section VI.A 1 of the NRC's Enforcement Policy. If you deny the non*cited violation, you should provide a response with the basis for your denial, within 30 days of the date of this inspection report, to the U.S. Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001, with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at the R.E. Ginna Nuclear Power Plant. In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report, you should provide a response withfn 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Senior Resident Inspector at the R.E. Ginna Nuclear Power Plant.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this Jetter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading~rm/adams.html(the Public Electronic Reading Room).

Sincerely,

~'l.J.d:i Glenn T. Dentel, Chief Projects Branch 1 Division of Reactor Projects Docket No. 50-244 license No. DPR-18 Enclosure: Inspection Report No. 05000244/2010006 wI Attachment: Supplemental Information cc wIener: Distribution via listServ

SUMMARY OF FINDINGS

IR 05000244/2010006; 05/24/2010 - 06/11/2010; R.E. Ginna Nuclear Power Plant; Biennial

Baseline Inspection of the Identification and Resolution of Problems. One finding was identified in the area of effectiveness of corrective actions.

This team inspection was performed by three NRC regional inspectors and one resident inspector. One finding of very low safety significance (Green) was identified during this inspection and was classified as a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). The cross-cutting aspect was*

determined using IMC 0310, "Components Within The Cross-Cutting Areas." Findings for which the SOP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4,

Decem bar 2006.

Identification and Resolution of Problems The team concluded that Constellation was generally effective in identifying, evaluating, and resolving problems. Ginna personnel identified problems at a low threshold and entered them into the Corrective Action Program (CAP). The team determined that Ginna screened issues appropriateily for operability and reportability, and prioritized issues commensurate with the safety significance of the problems. Causal analyses appropriately considered extent of condition, generic issues, and previous occurrences. The team determined that corrective actions addressed the identified causes and were typically implemented in a timely manner.

However, the team noted one example of very low safety significance involving less than adequate corrective actions .resulting in an NRC-identified finding. The issue was entered into Constellation's CAP during the inspection.

Constellation's audits and self~assessments reviewed by the team were thorough and probing.

Additionally, the team concluded that Constellation adequately identified, reviewed, and applied relevant industry operating experience (OE) to the RE. Ginna Nuclear Power Plant Based on interviews, c>bservations of plant activities, and reviews of the CAP and the Employee Concerns Program (ECP), the team did not identify any concerns with site personnel willingness to raise safety issues nor did the team identify conditions that could have had a negative impact on the site's safety conscious work environment

Cornerstone: Mitigating Systems

Green.

The team identified an NRC-identified finding of very low safety significance associated with a non-cited violation (NCV) of 10 CFR Part 50, Appendix B. Criterion XVI, "Corrective Action," in that measures were not established to assure that a condition adverse to quality was promptly identified and corrected. Specifically, after

Ginna identified that monthly samples of the emergency diesel generator (EDG) jacket water system were not being taken and analyzed for chlorides and fluorides, a sample was not taken and anal}'7..ed for approximately five months. Additionally, after the analysis indicated that the chlorides were over twice the procedural limit, Ginna did not increase the chloride sampling frequency, did not take action to return the chlorides to within specifications, and did not complete an analysis for long term effects on the EDG as nsquired by chemistry procedure CH-138, "Closed Cooling Water Systems Chemistry Optimization Plan," Revision 1. Ginna's corrective actions included evaluating the degradation of* the A*EDG jacket water due to the elevated chloride level in the A EDG jacket water heat exchanger exceeding 90 days and developing a plan to reduce the chloride level to within speCification.

This finding is more than minor because if left uncorrected, elevated chloride levels in the A EDG jacket water system could lead to a more significant safety concern.

Specifically, elevated chlorides in the A EDG jacket water heat exchanger could lead to degradation of the jacket water heat exchanger through stress corrosion cracking and impact the reliability of the A EDG. This finding is associated with the Mitigating Systems Cornerstone and affects the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undeSirable consequences (Le., core damage). The team determined that the finding was of very low safety significance (Green), because it was not a design or qualification deficiency confirmed not to result in loss of operability; did not result in a loss of safety function; and did not screen as potentially risk significant due to a seismic, flooding, or a severe weather initiating event. This finding has a cross-cutting aspect in the area of problem identification and resolution because Ginna did not take appropriate actions to address the elevated chloride level in the A EDG jacket water system (P.1(d) per IMC 0310).

Other Findings

None

REPORT DETAILS

OTHER ACTIVITIES

{OA} 40A2 Problem Identification and Resolution (PI&R) (711528)

.1 Assessment of the Corrective Action Program (CAP) Effectiveness

a. Inspection Scope

The team reviewed Constellation's procedures that describe the CAP at the R.E. Ginna Nuclear Power Plant (Ginna). Constellation personnel identified problems by initiating condition reports (CRs) for conditions adverse to quality, plant equipment deficiencies.

industrial or radiological safety concerns, and other significant issues. Condition reports were subsequently screened for operability and reportability, categorized by significance level (1, most significant, through 4, least significant), and assigned to personnel for evaluation and resolution or trending.

The team evaluated the process for assigning and tracking issues to ensure that issues were screened for operability and reportability, prioritized for evaluation and resolution in a timely manner commensurate with their safety significance, and tracked to identify adverse trends and repetitive issues. In addition, the team interviewed plant staff and management to determine their understanding of, and involvement with, the CAP.

The team reviewed CRs selected across the seven cornerstones of safety in the NRC's Reactor Oversight Process (ROP) to determine if site personnel properly identified, characterized. and entered problems into the CAP for evaluation and resolution. The team selected items from functional areas that included chemistry, emergency preparedness, engineering, maintenance, operations, physical security, radiation safety, and oversight programs to ensure that Constellation appropriately addressed problems identified in these functional areas. The team selected a risk-informed sample of CRs that had been issued since the last NRC PI&R inspection conducted in September 2008.

Insights from the station's risk analyses were considered to focus the sample selection and plant walkdowns on risk-significant systems and components. The corrective action review was expanded to five years for evaluation of identified concerns within CRs relative to overdue preventive maintenance (PM) and surveillance activities, and the charging pumps.

.

The team selected items from various processes at Ginna to verify that they were appropriately considered for entry into the CAP. Specifically, the team reviewed a sample of engineering requests, operator workarounds, operability determinations, system health reports. equipment problem lists, work orders (WOs), and issues entered into the Employee Concerns Program (ECP). Plant areas walked down included the:

control room, intake structure, emergency diesel generators (EDGs), and auxiliary and intermediate buildings.

The team reviewed CRs to assess whether Constellation personnel adequately evaluated and prioritized identified issues. The CRs reviewed encompassed the full range of evaluations, including root cause analyses, apparent cause evaluations, and common cause analyses. A sample of CRs that were assigned lower levels ot" significance which did not include formal cause evaluations were also reviewed by the team to ensure they were appropriately classified. The team's review included the appropriateness of the assigned significance, the scope and depth of the causal analysis, and the timeliness of resolution. The team assessed whether the evaluations identified likely causes for the issues and identified appropriate corrective actions to address the identified causes. As part of this review, the team interviewed various station personnel to fully understand details within the evaluations, and the proposed and completed corrective actions. The team observed CR screening meetings and management review committee (MRC) meetings in which Constellation personnel reviewed new CRs for prioritization and assignment. Further, the team reviewed eqUipment operability determinations, reportabilityassessments, and extent-of-condition reviews for selected CRs to verify these specific reviews adequately addressed equipment operability, reporting of issues to the NRC, and the extent of problems.

The team's review of CRs also focused on the associated corrective actions in order to determine whether the actions addressed the identified causes of the problems. The team reviewed CRs for adverse trends and repetitive problems to determine whether corrective actions were effective in addressing the broader issues. The team reviewed Constellation's timeliness in implementing corrective actions and effectiveness in prec:luding recurrence for significant conditions adverse to quality. Lastly, the team reviewed CRs associated with NRC non-cited violations (NCVs) and findings since the last PI&R inspection to determine whether Constellation personnel properly evaluated and resolved the issues. Specific documents reviewed during the inspection are listed in the Attachment to this report.

.

b. Assl3ssment Effectiveness of Problem Identification Based on the selected samples reviewed, plant walkdowns, and interviews of site personnel, the team determined that Constellation personnel identified problems at a low threshold and entered them into the CAP. For the issues reviewed, the team noted that problems or concerns had been appropriately documented in enough detail to understand the issues. The team observed managers and supervisors at MRC meetings appropriately questioning and challenging CRs to ensure clarification of the issues. The team determined that Constellation trended equipment and programmatic issues, and CR descriptions appropriately included references to repeat occurrences of issues. The ieam concluded that personnel were identifying trends at low levels. In general, the team did not identify any significant issues or concerns that had not been appropriately entered into the CAP for evaluation and resolution. In response to several minor issues identified by the team, Constellation personnel promptly initiated CRs and/or took immediate action to address the issue.

Effectiveness of Prioritization and Evaluation of Issues The team determined that, in general, Constellation personnel appropriately prioritized and evaluated issues commensurate with their safety significance. CRs were screened for operability and reportability, categorized by significance, and assigned to a department for evaluation and resolution. The CR screening process considered human performance issues, radiological safety concerns, repetitiveness and adverse trends.

The team observed managers and supervisors at MRC meetings appropriately questioning and challenging CRs to ensure appropriate prioritization.

CRs were categorized for evaluation and resolution commensurate with the significance of the issues. Based on the sample of CRs reviewed, the guidance provided by the Constellation implementing procedures appeared sufficient to ensure consistency in categorization of the issues. Operability and reportability determinations were performed when conditions warranted and the evaluations supported the conclusions.

Causal analyses appropriately considered extent of condition, generic issues, and previous occurrences. During this inspection, the team noted that Constellation's root cause analyses were generally thorough, and corrective and preventive actions addressed the identified causes. Additionally, the identified causes were well supported.

However, there were several instances of less than adequate evaluation or documentation of evaluations within the CRs reviewed, for example:

., The team reviewed a number of Category 2 CRs with apparent cause evaluations that were evaluated by non-certified individuals, Ginna procedure CNG-CA-1.01-1005. "Apparent Cause Evaluation (ACE)," section 5.8 requires ACE evaluators to be certified by the Director of Performance Improvement.

Ginna initiated several eRs indentifying the use of non-certified ACE evaluators.

The inspectors reviewed CR-2009-8235, where eight Category 2 CRs had been completed by operations since May 1, 2009 that had a non-certified ACE evaluator contrary to the requirements of CNG-CA-1.01-1005. The inspectors questioned whether the eight identified ACEs had been re-evaluated by certified ACE evaluators for quality and completeness. Constellation had addressed the procedural adherence and training verification aspects of the issue; however, there was no corrective action to verify the quality of the ACEs performed by the non-certified individuals. Ginna initiated CR-2010-003350 and concluded that the ACEs had all been adequately evaluated based on the review completed by the MRC.

  • On March 9, 2009, a Ginna radiation worker entered a high radiation area (HRA)on a radiation work permit (RWP) that did not allow HRA entry. This condition was documented in CR-2009-001575. Ginna implemented several corrective actions to prevent a worker from entering the radiologically controlled area (RCA)on the incorrect RWP. To ensure that their corrective actions were adequate, Ginna conducted an effectiveness review of all CRs from May 1, 2009, to December 31, 2009, to verify that there were no repeat occurrences. Ginna's effectiveness review concluded that were no repeat occurrences. During the team's CR review the team identified CR-2009-006417. which documented that a Ginna employee entered the RCA on the wrong RWP task number on September 14,2009. Specifically, the employee entered containment on a task number that did not allow containment entries. Ginna failed to include CR-2009 006417 in their effectiveness review for CR-2009-001575. CR-2010-003664 documented this instance of an inadequate effectiveness review performed by Ginna.
  • On October 9, 2008, the resident inspectors identified a potential unmonitored release path to the environment with door 28 open inside of the auxiliary building and positive auxiliary building pressure. Ginna documented this condition in CR 2008-008520. Ginna implemented several corrective actions to prevent unmonitored release paths from the RCA. To ensure that their corrective actions were adequate, Ginna conducted an effectiveness review of all CRs from January 23, 2009. to January 22, 2010, to verify that there were no repeat occurrences. During the team's CR review however, the team identified CR 2009-006376, which documented potential unmonitored release paths from doors 40 and 45 on September 14, 2009. Ginna failed to include CR-2009 006376 in their effectiveness review for CR-2008-008520. CR-2010-003664 documented this instance of an inadequate effectiveness review performed by Ginna.

t, The team reviewed operability determination documentation associated with CRs, and noted several which did not adequately give a basis for the determination that the equipment was operable. No instances were identified by the team where the equipment was incorrectly determined to be operable. Ginna entered this issue into the CAP as CR-201 0~003663.

.. On November 25,2009, during STP-O-2.7.1B, "Loop B Service Water Pump Test," Revision 0, Ginna operators noted that the service wa1er loop B inlet isolation valve to the EDG heat exchangers, 46688, had meta! shavings on the threads and hand wheel bushing of the valve. This condition was documented in CR-2009-008835 and WO C90714049 was completed to clean and lubricate the valve. During the next quarterly surveillance test on February 22, 2010, Ginna operators noted that when attempting to close valve 46688, the hand wheel spun freely and the valve remained in the open position as documented in CR-2010 001207. Subsequent investigation revealed that the valve failed to close due to deterioration of the stem bushing threads as a result of improper lubrication.

Ginna failed to identify that the metal shavings noted on the threads and hand wheel bushing of valve 46688 indicated significant bushing deterioration on November 25, 2009. This resulted in valve 46688 failing to close on February 22, 2010, during subsequent surveillance testing. The inspectors determined that valve 46686 was not required to be closed between November 25,2009, and February 22,2010, and therefore EDG operability was not impacted. The I valve's safety function is to remain open.

The team independently evaluated the deficiencies noted above for potential significance in accordance with the guidance in IMC 0612, Appendix B, "Issue I.i' i

Scngening," and Appendix E, "Examples of Minor Issues." The team determined that the issues were not findings of more than minor significance.

Effectiveness of Corrective Actions The team concluded that corrective actions for identified deficiencies were generally timely and adequately implemented. For significant conditions adverse to quality, corrective actions were identified to prevent recurrence. The team concluded that corrective actions to address NRC NCVs and findings since the last PI&R inspection were timely and effective. There were, however, a few examples where corrective actions were not timely and effective, for example:

" The team reviewed a test performed past its due date on an EDG fuel oil booster pump relief valve. The relief valve lift setpoint was found lower that the acceptable range. Ginna therefore removed the other EDG's relief valve in November 2009 for testing as required by the in-service test (1ST) program.

When the team, on June 9, 2010, asked for the results of the testing on the second valve. Ginna personnel discovered that the valve had not yet been sent out for testing. The valve was then sent out, and results were received on June 21,2010; results indicated that the valve passed the pressure lift test. Ginna entered the issue of not sending the valve out for testing in a timely manner into the CAP as CR-2010-003640. Ginna entered the issue of the impact of the delayed testing on the valve into the CAP as CR-2010-003685.

  • Corrective actions recommended for the motor driven auxiliary feedwater (MDAFW) check valve (4000C) failure in 2006 were not implemented or adequately dispositioned in 2006. The team reviewed two ACE reports (CR 2006-000721, CR 2008-008345) associated with valve 4000C failing to close after completion of performance of the A MDAFW pump quarterly surveillance test in 2006 and 2008. It was determined that the apparent cause of the valve failure in 2006 was corrosion and wear. The recommended corrective actions for this apparent cause were: 1) shorter actuation and maintenance cycles to prevent sticking due to periods with no use; 2) smoother valve surfaces to prevent adhesion of corrosion product; and 3} an alternate valve design or relocating the valve farther away from the elbow. None of the recommended corrective actions, after the 2006 failure, were implemented; however, the valve was replaced with a like-far-like valve. The replacement valve did not pass the acceptance criteria for the next prompt closure test in 2008; however, the valve did pass the operability test for closure. The apparent cause of valve 4000C failing the prompt closure test in 2008 was the location and design of the valve.

Valve chatter during operation caused the disc to wear, which created a leakage path. The valve chatter in combination with the reduced margin due to the valve repair caused the valve to fail the prompt closure test after only two years of service. The team concluded that the failure to implement the recommended corrective actions in 2006 resulted in the valve failing the prompt closure acceptance criteria in 2008. Appropriate corrective actions were initiated in 2008. Although the valve failed the prompt closure test in 2008, A MDAFW operability was not impacted.

  • After Ginna identified in 2008 that a number of surveillances and PM activities were missed and performed late, actions were ineffective in correcting the conditions throughout 2009 and into 2010. Three surveillances were missed in 2008 (A MDAFW pump comprehensive [full flowl pump surveillance, EDG fuel oil booster pump relief valve test, and plant vent mass air flow check surveillance);two PMs were missed in 2009 (ultrasonic noise analysis for lightning arrester monitoring and thermography PM for battery charger A1); and one PM was missed in 2010 (auxiliary and intermediate building fuseable link dampers).

Corrective actions were taken by Ginna during this time period, but were not completely effective in resolving the issues that resulted in PMs or surveillances being performed past the late end date. Additionally, on March 22, 2010, Ginna completed an effectiveness review of all CRs for missed PMs and surveillances from May 20, 2009, to February 18, 2010, and identified one missed PM (CR 2010-000273). During the inspector's review, the team identified one additional missed PM (CR-2010-003279) for thermography on battery charger A1 which passed its late end date on October 29,2009, which was not identified in the effectiveness review as the scope of the effectiveness review only included a CR search. In 2010, Ginna initiated more comprehensive corrective actions, including organizational changes and program tracking changes which were designed to replace the interim corrective actions taken in 2008 and 2009.

These changes took effect after the missed PM in 2010, and no other missed PMs or surveillances were identified. In all cases, system functionality was not impacted.

The team independently evaluated the deficiencies noted above for potential significance in accordance with the guidance in IMC 0612, Appendix B, "Issue Screening," and Appendix E, "Examples of Minor Issues." The team determined that the issues were not findings of more than minor significance.

The team identified one additional example where corrective actions were not effective in addressing the issue. The team determined that Constellation did not implement timely and appropriate corrective actions with respect to verifying proper EDG jacket water chemistry as described below.

c. Findings

EDG Jacket Water Chemistry

Introduction.

The team identified an NRC-identified finding of very low safety significance (Green) associated with a NCVof 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," in that measures were not established to assure that a condition adverse to quality was promptly identified and corrected. Specifically, after Ginna identified that monthly samples of the EDG jacket water system were not being taken and analyzed for chlorides and fluorides, a sample was not taken and analyzed for approximately five months. Additionally, after the analysis indicated that the chlorides were over twice the procedural limit, Ginna did not increase the chloride sampling frequency, did not take action to return the Chlorides to within specifications, and did not complete an analysis for long term effects on the EDG as required by chemistry procedure CH-138, "Closed Cooling Water Systems Chemistry Optimization Plan," Revision 1.

Description.

On October 28, 2009, Ginna identified that they were not in compliance with chemistry procedure CH-138, "Closed Cooling Water Systems Chemistry Optimization Plan," Revision 1. Specifically, Ginna was not performing chloride and fluoride analysis as required by procedure CH-138 on the EDG jacket water cooling system and on the component cooling water (CCW) system. Ginna wrote CR-2009 008213 to document this condition. Approximately five months later in March of 2010, Ginna sampled the diesel jacket water for both the A and B EDGs and both trains of CCW and analyzed the samples for chloride and fluoride levels. Sample results were received on April 15, 2010, and revealed that the A EDG jacket water chloride value was out of specification at 23 parts per million (ppm), more than twice the procedural limit.

Procedure CH-138 specifies a chloride target level of less than 10 ppm. If this value is exceeded, CH-138 requires increased monitoring as appropriate, and that chlorides be reduced to less than 10 ppm within 90 days. A limit of 10 ppm is established to prevent stress corrosion cracking (SCC) of the stainless steel tubes within the EDG jacket water cooling heat exchangers. Ginna documented the elevated chloride level in the A EDG jacket water heat exchanger in CR-2010-002480. However, contrary to procedure CH 138, Ginna did not increase the sampling frequency and did not take action to reduce the Chloride level to less than 10 ppm within 90 days, or perform an engineering evaluation showing that the elevated chloride level did not adversely affect the long term reliability of the A EDG. Ginna continued to sample and trend the chloride level of the A EDG jacket water on a monthly frequency. Chloride results for April and May continued to exceed action level criteria of greater than 10 ppm at 33 ppm and 30 ppm, respectively.

After the team questioned the corrective actions, Ginna evaluated the degradation of the A EDG jacket water due to the elevated chloride level in the A EDG jacket water heat exchanger exceeding 90 days and developed a plan to reduce the chloride level to

. within specification as documented in CR-2010-003648. Ginnars evaluation determined that there was no immediate impact to the jacket water heat exchanger due to the elevated chlorides based on the system pH, the type of stainless steel tubes used in the heat exchanger, the vertical orientation of the heat exchanger, the fact that the tubes were replaced in 2009, and the water temperature of the system.

Analysis.

The performance deficiency associated with this finding was that Ginna did not take timely and appropriate corrective actions to address the elevated chloride level in the A EDG jacket water heat exchanger as required by CH-138, "Closed Cooling Water Systems Chemistry Optimization Plan," Revision 1. The finding was more than minor because if left uncorrected, elevated chloride levels in the A EDG jacket water system could lead to a more significant safety concern. Specifically. elevated chlorides in the A EDG jacket water heat exchanger could lead to degradation of the jacket water heat exchanger through SCC and impact the reliability of the A EDG. This finding is associated with the Mitigating Systems Cornerstone and affects the cornerstone objective of ensuring the availability, reliability. and capability of systems that respond to initiating events to prevent undesirable consequences (Le., core damage). The team reviewed this finding using the Phase 1 significance determination process (SDP) Table 4a worksheet in Manual Chapter 0609 for Mitigating Systems and determined that the finding was of very low safety significance (Green), because it was not a design or qualification deficiency confirmed not to result in loss of operability; did not result in a loss of safety function; and did not screen as potentially risk significant due to a seismic, flooding, or a severe weather initiating event.

This finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Corrective Action Program Component, because Ginna did not take appropriate actions to address the elevated chloride level of the A EDG jacket water system, as documented in CR-2010-002480 (P.1(d) per IMC 0310).

Enforcement 10 CFR 50, Appendix 8, Criterion XVI, "Corrective Action," requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, defiCiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. Contrary to the above, after Ginna identified that monthly samples of the A EDG jacket water system were not being taken and analyzed for chlorides and fluorides, a sample was not taken and analyzed for approximately five months. Additionally, after the analYSis indicated that the jacket water .chlorides were over twice the procedural limit, action was not taken to increase the chloride sampling frequency or to get the chlorides to within specification within 90 days as required by chemistry procedure CH-138, "Closed Cooling Water Systems Chemistry Optimization Plan," Revision 1. when it was identified on April 15.

2010, and an analysis was not completed to evaluate the long term effects on the EDG.

Since this finding was determined to be of very low safety significance (Green) and has been entered into Constellation's CAP (CR-2010-002480) it is being treated as a non cited violation, consistent with Section VI.A.1 of the NRC Enforcement Policy. (NCV 0500024412010006-01, Failure to Take Adequate Corrective Actions for Elevated Chlorides in the A EDG Jacket Water Heat Exchanger)

Enc'osure

.2 Assessment of the Use of Operating Experience

a. Inspection Scope

The team selected a sample of CRs associated with the review of industry operating experience (OE) to determine whether Constellation personnel appropriately evaluated the OE information for applicability to Ginna and had taken appropriate actions, when warranted. The team reviewed CR evaluations of OE documents associated with a

~ample of NRC generic letters and information notices to ensure that Constellation adequately considered the underlying problems associated with the issues for resolution via their CAP. The team also observed plant activities to determine if industry OE was considered during the performance of routine activities. A list of the documents reviewed is included in the Attachment to this report.

b.

Assessment The team determined that, in general, Constellation appropriately considered industry OE information for applicability, and used the information for corrective and preventive actions to identify and prevent similar issues when appropriate. The team determined that OE was appropriately applied and lessons learned were generally communicated and incorporated into plant operations.

c. Findings

No findings of significance were identified .

.3 Assessment of Self-Assessments and Audits

a. Inspection Scope

The team reviewed a sample of Quality Assurance (QA) audits, including a review of several of the findings from the most recent audit of the CAP, and a variety of self~

assessments focused on various plant programs. These reviews were performed to determine if problems identified through these assessments were entered into the CAP, when appropriate, and whether corrective actions were initiated to address identified deficiencies. The effectiveness of the audits and assessments was evaluated by comparing audit and assessment results against self-revealing and NRC-identified observations made during the inspection. A list of documents reviewed is included in the Attachment to this report.

b. Assessment The team concluded that QA audits and self-assessments were critical, thorough, and effective in identifying issues. The team observed that these audits and self asses.sments were completed by personnel knowledgeable in the subject areas and were completed to a sufficient depth to identify issues that were then entered into the CAP for evaluation. COrrective actions associated with the issues were implemented commensurate with their safety significance. Constellation managers evaluated the results and initiated appropriate actions to focus on areas identified for improvement.

c. Findings

No findings of significance were identified .

.4 Asse,ssment of Safety Conscious Work Environment

a.

Insl;!9ction Scope During interviews with station personnel, the team assessed the safety conscious work environment (SCWE) at Ginna. Specifically, the team interviewed personnel to determine whether they were hesitant to raise safety concerns to their management and/or the NRC. The team also interviewed the station ECP coordinator to determine what actions were implemented to ensure employees were aware of the program and its availability with regard to raiSing concerns. The team reviewed the ECP files to ensure that issues were entered into the CAP when appropriate.

b. Assessment During interviews, plant staff expressed a willingness to use the CAP to identify plant issues and deficiencies and stated that they were willing to raise safety issues. The team noted that no one interviewed stated that they personally experienced or were aware of a situation in which an individual had been retaliated against for raising a safety issue. All persons interviewed demonstrated an adequate knowledge of the CAP and ECP. Based on these limited interviews, the team concluded that there was no evidence of an unacceptable SCWE and no significant challenges to the free flow of information.

c. Findings

No findings of significance were identified.

40A6 Meetings. Including Exit On June 11, 2010, the team presented the inspection results to Mr. John Carlin, Site Vice President, and to other members of the Ginna staff. The team verified that no proprietary information was documented in the report.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

J. Carlin Vice PreSident, Ginna
J. Bowers Acting General Supervisor, Radiation Protection

E. Palmer Jr Director Security

M.lves Supervisor Security Access & FFD

J. Scalzo Supervisor Security Operations

D. Dean Assistant Operations Manager (Shift)

T.Hedges Emergency Preparedness Manager

E. Larson Plant General Manager

T. Paglia Scheduling Manager

S. Snowden Chemistry Supervisor

J. Sullivan Manager of Operations

P. Swift Manager, Nuclear Engineering Services

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000244/2010006-01 NCV Failure to Take Adequate Corrective Actions for Elevated Chlorides in the A EDG Jacket Water Heat Exchanger

LIST OF DOCUMENTS REVIEWED