05000445/LER-1997-008, Forwards LER 97-008-01 Re Min Gap for Cold Leg Injection ECCS Throttle Valves Not IAW Design.Suppl Issued to Revise Implementation of Cas.Commitment Made by Util,Provided

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Forwards LER 97-008-01 Re Min Gap for Cold Leg Injection ECCS Throttle Valves Not IAW Design.Suppl Issued to Revise Implementation of Cas.Commitment Made by Util,Provided
ML20203K818
Person / Time
Site: Comanche Peak Luminant icon.png
Issue date: 02/27/1998
From: Terry C, Walder R
TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20203K821 List:
References
TXX-98052, NUDOCS 9803050245
Download: ML20203K818 (2)


LER-2097-008, Forwards LER 97-008-01 Re Min Gap for Cold Leg Injection ECCS Throttle Valves Not IAW Design.Suppl Issued to Revise Implementation of Cas.Commitment Made by Util,Provided
Event date:
Report date:
4452097008R00 - NRC Website

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Log # TXX-98052 File # 10200 M1ELECTR/C Ref. # 10CFR50.73(a)(2)(ii)(B)

February 27. 1998

c. te nmy Senior Mce PresMent

& PrincipalNuclear Oficer U.-S. Nuclear Regulatory Commission Attn : Document Control Desk Washin9 ton, D.C. 20555

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)

DOCKET NOS. 50-445 AND 50 446 CONDITION OUTSIDE OF DESIGN BASIS LICENSEE EVENT REPORT 445/97-008 01 Enclosed is supplement 1 to Licensee Event Report (LER) 97-008-00 for Comanche Peak Steam Electric Station Units 1 and 2. " Minimum gap for cold leg injection ECCS throttle valves not in accordance with design,"

Supplement 1 is being issued to revise the implementation dates for the corrective actions, which were previously submitted via LER 97-008-00.

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$$8 185$E oI8$$IEs IllElElE!EllllElllll 8 . v v v .a a COMANCl(E PEAK STEAM El.ECTRIC STATION P.O. Box 1002 Glen Rose, Texas 76043-1002

O , o TXX-98052 Page 2 of 2 This communication contains the following revised commitment which will be completed af, noted:

CDF Number Commitment 27126 The design modification for Unit 1 is expected to be completed during its seventh refueling outage (1RF07). and fourth refueling outage (2RF04) for Unit 2.

Sincerely,

.c or u . A Aug C.1 Terry l

0 By: Ol 0710A g- d O Rogef'D Walker Regulatory Affairs Manager OB:ob Enclosure cc: E. W. Merschoff. Region IV J. I. Tapia, Region IV Resident Inspectors, CPSES