LER-1999-001, Forwards LER 99-001-00, Some Electrical Contacts for RCS Pressure Relief Valves Were Not Included in Surveillance Testing Procedures. New Licensing Commitments Identified in Attachment 1 |
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10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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| 4451999001R00 - NRC Website |
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Log # TXX-99136 7UELECTRIC File # 10200 Ref. # 10CFR50.73(a)(2)(i)(B)
June 8,1999 c. Imc nrry Senior Vice President
& PrincipalNuclear Oficer U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 SU3 JECT:
COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)
DOCKET NOS. 50-445 AND 50-446 CONDITIONS PROHIBITED BY TECHNICAL SPECIFICATIONS LICENSEE EVENT REPORT 445/99-001-00
. Enclosed is Licensee Event Report (LER) 99-001-00 for Comanche Peak Steam Electric Station Unit 1 and Unit 2," Some Electrical Contacts for the Reactor Coolant System Pressure Relief Valves Were Not included in the Surveillance Testing Procedures."
There are new licensing based commitments in the communication, as identified in.
Sincerely,
$s * &g C. L. Terry
]@
~ M By:
Rogeft. Walker Regulatory Affairs Manager OBlob JU Attachment
' -.i Enclosure '
cc:
Mr. E. W. Merschoff, Region IV Mr. J. I. Tapia, Region IV
- - Resident inspectors, CPSES i
COM ANCHE PEAK Sil-AM ELECTRIC STATION p n uns inn? Glen Rose Texas 760 0-1002 9906150201 990608 PDR ADOCK 05000445 S
PDR,
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- Attachment 1 to TXX-99136 Page,1 of x1 l
This communication contains the following new commitment which will be completed as noted:
CDF Number Commitment [27178]-
[ Procedures pertaining to the circuit testing are being revised, testing will be performed consistent with the existing LCO as warranted. )
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| 05000446/LER-1999-001, :on 981226,identified That TS Surveillance for Containment Integrity Verification Was Not Performed.Caused by Personnel Error.Required Surveillance Was Performed & Applicable Procedures Were Revised.With |
- on 981226,identified That TS Surveillance for Containment Integrity Verification Was Not Performed.Caused by Personnel Error.Required Surveillance Was Performed & Applicable Procedures Were Revised.With
| 10 CFR 50.73(a)(2)(i) | | 05000445/LER-1999-001, Forwards LER 99-001-00, Some Electrical Contacts for RCS Pressure Relief Valves Were Not Included in Surveillance Testing Procedures. New Licensing Commitments Identified in Attachment 1 | Forwards LER 99-001-00, Some Electrical Contacts for RCS Pressure Relief Valves Were Not Included in Surveillance Testing Procedures. New Licensing Commitments Identified in Attachment 1 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000445/LER-1999-001-01, :on 990510,discovered That Some Electrical Contacts for RCS Pressure Relief Valves Were Not Included in Surveillance Testing Procedures.Caused by Less than Adequate Procedures.Revised Circuit Testing Procedures |
- on 990510,discovered That Some Electrical Contacts for RCS Pressure Relief Valves Were Not Included in Surveillance Testing Procedures.Caused by Less than Adequate Procedures.Revised Circuit Testing Procedures
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000446/LER-1999-002, :on 990103,main Turbine Generator Control Valves Suddenly & Unexpectedly Closed While at 100 Percent Rated Power.Cause of Event Could Not Be Determined.Ehc Sys Has Been Connected to Minidas.With |
- on 990103,main Turbine Generator Control Valves Suddenly & Unexpectedly Closed While at 100 Percent Rated Power.Cause of Event Could Not Be Determined.Ehc Sys Has Been Connected to Minidas.With
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(s)(2) | | 05000445/LER-1999-002-01, :on 990518,missed TS Surveillance for SG Gross Activity Composite Sampling Was Noted.Caused by Cognizant Personnel Being Distracted from Normal Duties.Sg Sample Was Taken IAW TS Appropriate TS Requirement.With |
- on 990518,missed TS Surveillance for SG Gross Activity Composite Sampling Was Noted.Caused by Cognizant Personnel Being Distracted from Normal Duties.Sg Sample Was Taken IAW TS Appropriate TS Requirement.With
| 10 CFR 50.73(a)(2)(1) | | 05000446/LER-1999-003, :on 990421,discovered That CR HVAC Train a Was Outside TS AOT Limits Due to Blown Fuse.Caused by Incorrect Landing of Wires That Provide Relay Control Power for CR Ventilation Circuitry.Fuse Was Replaced.With |
- on 990421,discovered That CR HVAC Train a Was Outside TS AOT Limits Due to Blown Fuse.Caused by Incorrect Landing of Wires That Provide Relay Control Power for CR Ventilation Circuitry.Fuse Was Replaced.With
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000445/LER-1999-003-01, :on 990519,discovered Battery Surveillances Were Not Performed with Proper Periodicity as Required by Ts.Caused by Misinterpretation of Sr.Resistance Readings Taken,Noed Requested & LAR Requested.With |
- on 990519,discovered Battery Surveillances Were Not Performed with Proper Periodicity as Required by Ts.Caused by Misinterpretation of Sr.Resistance Readings Taken,Noed Requested & LAR Requested.With
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000445/LER-1999-004-01, :on 990830,some Grated Surfaces Were Noted Outside Design Basis.Caused by Use of Friction Type Grating Fasteners.Mods to Enhance Platforms Are Being Implemented. with |
- on 990830,some Grated Surfaces Were Noted Outside Design Basis.Caused by Use of Friction Type Grating Fasteners.Mods to Enhance Platforms Are Being Implemented. with
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000446/LER-1999-004, :on 990522,train a EDG Start,Occurred.Caused by Lockout Relay Actuation.Developed Troubleshooting Plan to Help Identify Cause of Problem.With |
- on 990522,train a EDG Start,Occurred.Caused by Lockout Relay Actuation.Developed Troubleshooting Plan to Help Identify Cause of Problem.With
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000445/LER-1999-005, :on 990830,potential Common Cause Failure Identified in Jrak Relief Valves.Caused by Pressure Surges Sys.Pressure Surges Sys Have Been Implemented.With |
- on 990830,potential Common Cause Failure Identified in Jrak Relief Valves.Caused by Pressure Surges Sys.Pressure Surges Sys Have Been Implemented.With
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) |
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