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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARML20216H0781997-09-10010 September 1997 LER 97-S01-00:on 970816,security Sys Degradations Discovered Due to Inclement Weather.All Components Were Returned to Svc & Compensatory Posts Terminated After Completion of Repairs & Testing 05000425/LER-1993-0051993-08-30030 August 1993 LER 93-005-00:on 930809,B Train Chiller Tripped.Caused by High Condenser Pressure Due to Excess of non-condensable Gases in Sys.Solenoid Valve Replaced,Ecw Chiller Purged & Surveillance Test Reperformed successfully.W/930830 Ltr 05000424/LER-1993-0091993-08-23023 August 1993 LER 93-009-00:on 930728,reactor Tripped During Maint Due to Low Pressure Signal.Caused by Cognitive Personnel Error. Personnel Involved Disciplined & Reminded of Importance of Procedural compliance.W/930823 Ltr 05000424/LER-1993-0041993-05-0303 May 1993 LER 93-004-00:on 930410,ESFAS Sequencer Operation Initiated During Testing.Caused by Design Flaw in Circuit Card. Affected Cards in Both Train a & Train B Sequencers modified.W/930503 Ltr 05000425/LER-1990-0081990-07-27027 July 1990 LER 90-008-00:on 900628,indication Received in Control Room That MSIV 2HV-3026A Was Closing.Caused by Failure of O-ring Which Seals Connection of Nonpump Side Manifold Assembly to Boss on Actuator cylinder.O-ring replaced.W/900727 Ltr 05000424/LER-1990-0131990-06-29029 June 1990 LER 90-013-00:on 900601,discovered That Containment Air Lock Leakage Surveillance Exceeded 6-month Test Interval,Per Tech Spec 4.6.1.3.b.Caused by Personnel Error.Plant Surveillance Tracking Program revised.W/900629 Ltr 05000424/LER-1990-0121990-06-28028 June 1990 LER 90-012-00:on 900529,discovered That Sequencer Delay Times Not Taken Into Account During Summation Procedure for Control Room Emergency Filtration Sys.Caused by Inadequate Procedure Review.Procedures changed.W/900628 Ltr 05000424/LER-1990-0111990-05-21021 May 1990 LER 90-011-00:on 900425,reactor Manually Tripped Due to Inadvertent Closure of Main Feed Regulating Valve.Caused by Mispositioning of Local Control Levers.Local Control Levers removed.W/900521 Ltr 1997-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4591999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20217K8041999-09-30030 September 1999 Rev 1 to Vegp,Unit 2 Cycle 7 Colr ML20217K7741999-09-30030 September 1999 Rev 1 to Vegp,Unit 1 Cycle 9 Colr ML20216E5061999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Vegp,Units 1 & 2. with ML20210P9841999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H1211999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20196F9711999-05-31031 May 1999 Owner Rept for ISI for Vogtle Electric Generating Plant, Unit 1 Eighth Maint/Refueling Outage ML20195G1731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for VEGP Units 1 & 2. with ML20206N2141999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20206A6561999-04-21021 April 1999 Safety Evaluation Authorizing Licensee Re Rev 9 to First 10-year ISI Interval Program Plan & Associated Requests for Relief (RR) 65 from ASME Boiler & Pressure Vessel Code ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20206C2291999-03-31031 March 1999 Revised Monthly Operating Repts for Mar 1999 for Vogtle Electric Generating Plant,Units 1 & 2 ML20205Q8081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Vegp,Units 1 & 2. with ML20205A9581999-03-31031 March 1999 Rev 0 to VEGP Unit 1 Cycle 9 Colr ML20207K6051999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20209H3951999-02-15015 February 1999 Rev 2 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20209H4091999-02-15015 February 1999 Rev 1 to ISI Program Second 10-Year Interval Vogtle Electric Generating Plant Units 1 & 2 ML20202H9851999-01-29029 January 1999 Safety Evaluation Accepting Rev 8 to First 10-year Interval Inservice Insp Program & Associated Requests for Relief for Vogtle Electric Generating Plant,Unit 1 ML20199F8041999-01-13013 January 1999 Corrected Pages to VEGP-2 ISI Summary Rept for Spring 1998 Maint/Refueling Outage ML20199E7561998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20198S1781998-12-31031 December 1998 SER Re Second 10-year Interval Inservice Insp Program Plan & Associated Requests for Relief for Southern Nuclear Operating Co,Inc Units 1 & 2 ML20196E5221998-12-0101 December 1998 Rev 8 to ISI-P-014, ISI Program for VEGP-2 ML20198B8571998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Vogtle Electric Generating Plant,Units 1 & 2.With ML20195H2131998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Vogtle Electric Generating Station,Units 1 & 2.With ML20154L5681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Vegp,Units 1 & 2 ML20151W3681998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Vogtle Electric Generating Plant Units 1 & 2.With ML20154L5721998-08-31031 August 1998 Corrected Page from MOR for Aug 1998 for Vegp,Unit 2 ML20237D2051998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Vogtle Electric Generating Plant Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236P6991998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20236Q3051998-06-30030 June 1998 Owner'S Rept for ISI for Sixth Maint/Refueling Outage of Vogtle Electric Generating Plant,Unit 2 ML20249A3911998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Vogtle Electric Generating Plant ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20249A3931998-04-30030 April 1998 Revised MOR for Apr 1998 for Vogtle Electric Generating Plant Unit 1 ML20247F3841998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20154Q9721998-04-20020 April 1998 10CFR50.59(B) Rept of Facility Changes,Tests & Experiments for Vogtle Electric Generating Plant,Units 1 & 2 ML20217H7181998-04-0101 April 1998 Corrected Page 5 to 980324 SER Re Relief Requests Associated W/Second 10-year Interval Insp program.RR-21 in Error in That Component,Suction Damper Inadvertently Omitted. Corrected Page 7 of Technical Ltr Rept Also Encl ML20216D6141998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20217Q1301998-03-31031 March 1998 Rev 0 to Vepc Unit 2 Cycle 7,COLR ML20217B8831998-03-24024 March 1998 SER Accepting Relief Request RR-5,RR-19,RR-20,RR-21,RR-23 & RR-24 for Second 10-yr Interval ISI Program Plan ML20216E2421998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203H9551998-02-23023 February 1998 SER Denying Quality Assurance Program Description Change for Vogtle Electric Generating Plant,Units 1 & 2 ML20203E4831998-02-11011 February 1998 Rev 1 to Vogtle Electric Generating Plant,Units 1 & 2 Second Ten-Yr Interval Pump Inservice Test Program ML20198T1211998-01-31031 January 1998 Owners Rept for Inservice Inspection for Seventh Maintenance/Refueling Outage ML20202G5441998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Vogtle Electric Generating Plant,Units 1 & 2 ML20199E5431998-01-31031 January 1998 Rev 3 to WCAP-14720, Vogtle Units 1 & 2 Spent Fuel Rack Criticality Analysis W/Credit for Soluble Boron ML20198L6471997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Vogtle Electric Generating Plant,Units 1 & 2 ML20203C2811997-12-0909 December 1997 Safety Evaluation Authorizing Request for Relief of Second 10 Yr Interval Inservice Insp Program ML20202B7881997-12-0101 December 1997 Rev 8 to ISI-P-006, ISI Program for Gpc Vogtle Electric Generating Plant Unit 1 ML20203H0601997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Vegp,Units 1 & 2 1999-09-30
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text
Geo g>a Power Company
- f 40 invemess Center PMway a Post Oftce Bov 1295 Bmngham AiMuma 35201 Teiepnone 200 E77 7122 L
C.K facCoy Georgia Power vce Prese;unt NucW Yogite Pictect I?IF SCWM*n UllCIHC Sf;IO71 May 3, 1993 ELV-05421 Docket No. 50-424 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Gentlemen:
VOGTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT ENGINEERED SAFETY FEATURE ACTUATION SYSTEM SEOUENCER OPERATION IS INITIATED DURING TESTING In accordance with the requirements of 10 CFR 50.73, Georgia Power Company submits the enclosed report related to an event which occurred on April 10,1993.
Sincerely, of '
C. K. McCoy CKM/NJS
Enclosure:
LER 50-424/1993-004 xc: Georcia Power Company Mr. W. B. Shipman Mr. M. Sheibani NORMS U. S. Nuclear Reculatory Commission Mr. S. D. Ebneter, Regional Administrator Mr. D. S. Hood, Licensing Project Manager, NRR Mr. B. R. Bonser, Senior Resident Inspector, Vogtle 070000 9305110097 930503 '
{DR ADOCK 05000424 I>
PDR [,l
g m ass u.s. KutAR xtuuwu wmaswm u n g< a g g 3p o-a us LICENSEE EVENT REPORT (LER) [
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M IT hAML (1) Daau hsMbtR gj nu rs) l V0GTLE ELECIRIC CENERATDC PLA!TI - INIT 1 05000424 I lDrl3 -
TITLT (4) ';
DEINEERED SAFEIY FEARRE ACIUATION SYSTDi SEQUENCER OPERATION IS INITIATED DURING TESTI!C T AT DAi; (5) LER huMBER (6) kEP0RI DATE (7)' OTHER FACILITIES IhkOLbED (8) i GTn DAY VEAR TEAR SEQ huh REW N0hTH DAY VEAR FALILIIV hAMES DOCLET huMBER(5) 05000 i 04 10 93 93 004 00 05 03 93 05000 i OPERATING THI5 MRT 15 M M MN M M WRM5 W M UR U1) f QODE (9) 6 ^ 50.73(a)(2)(iv) '
20.402(b) 20.405(c) 73.71(b)
POUER -
20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c) .i LEVEL 0 20.405(a)(1)(ii) 20.405(a)(1)(iii)
[ 50.36(c)(2) _
50.73(a)(2)(vit) _
OTHER (Specify in
_ _ 50.73(a)(2)(1) _ 50.73(a)(2)(viii)(A) Abstract below) 20.405(a)(1)(iv) -
50.73(a)(2)(ii) -
50.73(a)(2)(v111)(B) f 20.405(a)(1)(v) 50.73(a)(2)(111) 50.73(a)(2)(x)
LICEh5E E C0hT ACT FOR THIS LER (11) ;
NAME TELEPn0hE huMbER f
4REA LODE MD!DI SHEIBANI, NUCIIAR SAFE 1Y AND COMPLIANCE 706 826-3209 COMFLETE OhE LIhE FOR EACH FAILORE DESCRIEED IN THIS kEP0kT (13)
CAUSE SYSTEN COMPONENT gP0RT CAUSE SYSTEN COMP 0hEhe MAhUFAC- R PD T l N(hhUFAC-ER pRDS TU ER SUFFLEMEhTAL REPDRI EXPECTED (14c MONIn DAY VEAR ,
SUBMISSION '
~'"]YES(Ifyes,completeEXPECTEDSUBMISSIONDATE) y h0 DATE (15)
Ab5 TRACT (16) ,
On April 10, 1993, personnel were testing the Train A engineered safety features .
actuation system (ESFAS) sequencer. New circuit cards had been installed as a followup corrective action to LER 50-424/1992-002. During the test, the !
sequencer caused the Train A 4160 volt bus to open the normal incoming feeder breaker (causing a loss of power to the bus), shed its loads, and initiat.e the undervoltage loading sequence. Components actuated as designed, and operators :
in the control room responded by stopping equipment started by this engineered ;
safety feature actuation.
The cause of this event was a design flaw in a circuit card not affected by the !
card replacements. Investigation found that a protective filter allowed a small j portion of a test signal to pass. This small portion of the test signal }
initiated the load shed. However, it was shown that this condition existed only during testing with a specific circuit board configuration and would not have j
~
affected sequencer operation during normal use. The affected circuit cards in both the Train A and Train B sequencers were modified to shorten the initiating I test pulse. Both cards were reinstalled, and testing was completed successfully. >
[
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g g rm m u.a. xxww awaum um>>m uggegpm 3 3 LICENSEE EVENT REPORT - (LER) -l TEXT CONTINUATION :l FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (5) PAGE (3) l YEAR SEQ huh REW i
05000424 93 004 00 2 0F 3 90GIII ELECIRIC GINERATING PIANT - UNIT 1 i T Lu I A. REQUIREMENT FOR REPORT .l This report is required per 10 CFR 50.73 (a)(2)(iv) because an unplanned ;
engineered safety features (ESF) actuation occurred when the ESF actuation 'l system sequencer initiated an undervoltage loading sequence during testing. j B. UNIT STATUS AT TIME OF EVENT t
At the time of this event Unit I was operating in Mode 6 (refueling) at !
O percent of rated thermal power. Other than that described herein, there l was no inoperable equipment that contributed to the occurrence of this event, j i
C. DESCRIPTION OF EVENT t l
On April 10, 1993, personnel were testing the Train A engineered safety j features actuation system (ESFAS) sequencer. New circuit cards had been [
installed as a followup corrective action to LER 50-424/1992-002. During the j test, the sequencer caused the Train A 4160-volt bus to open the normal incoming feeder breaker (causing a loss of power to the bus), shed its loads, ;
and initiate the undervoltage loading sequence. . Components actuated as ;
designed, and operators in the control room responded by stopping equipment started by this ESF actuation. ,
i D. CAUSE OF EVENT
{
The cause of this event was a design flaw in a circuit card not affected by !
the card replacements. Investigation found that a protective filter allowed ;
a small portion of a test signal to pass. This small portion of the test signal initiated the load shed. However, it was shown that this condition existed only during testing with a specific circuit board configuration and ;
would not have affected sequencer operation during normal use.
}
E. ANALYSIS OF EVENT l
When the ESFAS sequencer sensed a loss of voltage on the primary bus, it i commenced operation, starting the emergency diesel generator to energize the !
bus and loading'the necessary equipment,-as designed. Plant operators responded to shut down.this equipment, and there was no detrimental impact on ;
unit operations. Based on this' consideration, there was no adverse effect on ;
plant safety or on the health and safety of the public as a result of this !
event. i l
F. CORRECTIVE ACTIONS-
- 1. The affected circuit card'in both the Train A and Train B sequencers.was :
modified to shorten the initiating test pulse. Both cards were i reinstalled, and testing was. completed successfully. !
- 2. Other cards of this type will be modified and installed in the Unit 2 sequencers during the Fall 1993 refueling outage. j i
E-l': -
. .i 15 0 m U.5. IlhA,LLAR HLUdLAlWK1 wmlbblUN APFAUV W M ND 31 W-DID4 (6 . ,' EXPIRES: 4/30/92 LICENSEE-EVENT REPORT (LER) ,
't TEXT CONTINUATION ' !
p U
rACILITV NAME (1) DOCKET NUMBER (2) LER NUMBER (5) PAGE (3) !
TEAR SEQ hum REV
.}
l V0GIII ELECIRIC GENERATING FURI - INIT 1 05000424- 93 004 00 3 0F 3- -[
ItxI l G. ADDITIONAL'INFORMATION f
- 1. Failed Components None :
- 2. Previous Similar Events l
.None
- 3. Energy Industry Identification System Code l Engineered Safety Features Actuation System - JE I
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05000424/LER-1993-004 | LER 93-004-00:on 930410,ESFAS Sequencer Operation Initiated During Testing.Caused by Design Flaw in Circuit Card. Affected Cards in Both Train a & Train B Sequencers modified.W/930503 Ltr | | 05000425/LER-1993-005 | LER 93-005-00:on 930809,B Train Chiller Tripped.Caused by High Condenser Pressure Due to Excess of non-condensable Gases in Sys.Solenoid Valve Replaced,Ecw Chiller Purged & Surveillance Test Reperformed successfully.W/930830 Ltr | | 05000424/LER-1993-009 | LER 93-009-00:on 930728,reactor Tripped During Maint Due to Low Pressure Signal.Caused by Cognitive Personnel Error. Personnel Involved Disciplined & Reminded of Importance of Procedural compliance.W/930823 Ltr | |
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