Similar Documents at Salem |
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LER-1982-054, Forwards LER 82-054/03L-0.Detailed Event Analysis Encl |
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O PSEG i
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l Public Service Electric and Gas Cornpany P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station August 18, 1982 i
t i
l Mr.
R. C.
Ilaynes i
Regional Administrator USNRC Region 1 631 Park Avenue 1
King of Prussia, Pennsylvania 19406
Dear Mr. Ilaynes:
LICENSE NO. DPR-70 DOCKET NO. 50-272
' REPORTABLE OCCURRENCE 82-054/03L Pursuant to the requirements of Salem Generating Station j
Unit No.
1, Technical Specifications, Section 6.9.1.9.b,
)
we are submitting Licensee Event Report for Reportable Occurrence 82-054/03L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours, f. D I
i H.
J.
Midura General Manager -
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Salem Operations RF:ks /J[
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Distribution i
3 8209020487 820818 PDR ADOCK 05000272 S
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The Energy People p#
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Report Number:
82-054/03L Report Date:
08-18-82 Occurrence Date:
07-31-82 Facility:
Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Reactor Coolant System Unidentified Leakage - Out-of-Specification.
This report was initiated by Incident Reports82-204 and 82-208.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 - Rx Power 98% - Unit Load 1040 MWe.
DESCRIPTION OF OCCURRENCE:
At 0811 hours0.00939 days <br />0.225 hours <br />0.00134 weeks <br />3.085855e-4 months <br />, July 31, 1982, during performance of Surveillance Procedure SP (O) 4. 4. 6. 2, Reactor Coolant System (RCS) unidentified leakage was found to be 1.8 GPM.
This is greater than the 1.0 GPM allowed by the Technical Specifications, and Action Statement 3.4.6.2.b was entered.
An operator was immediately sent into containment to determine the source of the additional leakage.
At 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />, the operator reported that 1 GPM was leaking from the packing of Pressurizer Auxiliary Spray Isolation Valve 1CV75.
The surveillance was satisfactorily completed and indicated a new unidentified leak rate of 0.4 GPM.
This is below the 1 GPM limit, and Action Statement 3.4.6.2.b was terminated.
i At 1040 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.9572e-4 months <br />, August 2, 1982, the Control Operator noticed an l
increasing indication on the containment air particulate monitor.
l The leak rate, as determined by the Containment Sump Monitoring System, was found to have increased from 0.55 GPM to 2.9 GPM, and at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />, Action Statement 3.4.6.2.b was re-entered.
The 3eakage was again identified as being from Valve 1CV75, and unidentified leakage was calculated to be 0.5 GPM.
With leakage in specification, at 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br />, August 2, 1982, Action Statement 3.4.6.2.b was terminated.
In both cases, identified leakage was less than the Technical Specification limit of 10 GPM and no l
Reactor Coolant Pressure boundary leakage was observed.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The additional RCS leakage in both instances was due to the failure of the packing on Valve 1CV75.
l l
l
i LER 82-054/03L.
ANALYSIS OF OCCURRENCE:
The RCS leakage limits are based on insuring the ability of detecting. leakt ge from the Reactor Coolant Pressure boundary.
The boundary is one of several design features which prevent the release of radioactive fission products to the environment (the others are the fuel cladding and primary containment).
Since the redundant barriers were maintained, and leakage was subsequently identified as not being from the pressure boundary, no risk to the public or environment was involved.
As such, the occurrence constituted operation in a degraded mode permitted by a limiting condition for operation and is reportable in accordance with Technical Specification 6.9.1.9.b.
Action Statement 3.4.6.2.b requires:
With any pressure boundary leakage, be in at least hot standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />; with any RCS leakage greater than any one of the Technical Specification limits, excluding pressure boundary leakage, reduce the leakage rate to within limits within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, or be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
CORRECTIVE ACTION
As noted, no Reactor Coolant Pressure boundary leakage was observed.
In both instances, unidentified leakage was brought within the 1 GPM limit, and the action statement was terminated.
Due to the increase in leakage past the packing of Valve 1CV75, on August 2, 1982, the packing gland was injected with Furmanite and leakage was stopped.
Permanent repair of the valve will be performed during the next refueling outage.
FAILURE DATA:
Copes-Vulcan Inc.
2" Control Valve Type D-100-100 Prepared By R.
Frahm I
S MkI%
Genefal Ma' nager -
Salem Operations SORC Meeting No.
82-77
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| 05000311/LER-1982-001, Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed | Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed | | | 05000272/LER-1982-001-03, Pressurizer Overprotection Sys Valve 1PR1 Was Isolated Due to Leakage. on 820107,while Draining Rcs,Valve 1RP2 Would Not Open. Caused by Generic Problem.Reactor Vessel Head Removed | Pressurizer Overprotection Sys Valve 1PR1 Was Isolated Due to Leakage. on 820107,while Draining Rcs,Valve 1RP2 Would Not Open. Caused by Generic Problem.Reactor Vessel Head Removed | | | 05000311/LER-1982-001-03, /03L-0:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Sticking Open,Freezing Pressure Sensing Line.Damper Freed & Closed. Line Thawed | /03L-0:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Sticking Open,Freezing Pressure Sensing Line.Damper Freed & Closed. Line Thawed | | | 05000272/LER-1982-001, Forwards Revised LER 82-001/03X-1.Detailed Event Analysis Encl | Forwards Revised LER 82-001/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-002-01, /01T-0:on 820119,indications of Tube Thinning Were Detected by Eddy Current Exam.Steam Generators 12 & 14 Required Two & Three Sample Insp,Respectively.All Defective Tubes & Tubes Degraded Above 30& Plugged | /01T-0:on 820119,indications of Tube Thinning Were Detected by Eddy Current Exam.Steam Generators 12 & 14 Required Two & Three Sample Insp,Respectively.All Defective Tubes & Tubes Degraded Above 30& Plugged | | | 05000311/LER-1982-002-03, /03L-0:on 820111,2A1 Battery Charger Tripped, Was Reset & Tripped Again.No Problem Found.Subsequent Trip Caused by Difference Between Battery Voltage & Battery Charger Voltage Setting.Personnel Instructed | /03L-0:on 820111,2A1 Battery Charger Tripped, Was Reset & Tripped Again.No Problem Found.Subsequent Trip Caused by Difference Between Battery Voltage & Battery Charger Voltage Setting.Personnel Instructed | | | 05000272/LER-1982-002, Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing | Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing | | | 05000311/LER-1982-002, Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Vo | Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Voltage | | | 05000311/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-003-03, /03L-0:on 820106,1B & 1C Diesels Locked Out, Rendering Diesels Inoperable at Same Time.On 820106,diesel Generator 1C Declared Inoperable While Diesel 1B Out of Svc for Maint.Caused by Misinterpretation of Lockout Switch Tag | /03L-0:on 820106,1B & 1C Diesels Locked Out, Rendering Diesels Inoperable at Same Time.On 820106,diesel Generator 1C Declared Inoperable While Diesel 1B Out of Svc for Maint.Caused by Misinterpretation of Lockout Switch Tag | | | 05000311/LER-1982-003-03, /03L-0:on 820112,during Routine Calibr Testing, Radiation Monitor 2R11A Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Tested Satisfactorily | /03L-0:on 820112,during Routine Calibr Testing, Radiation Monitor 2R11A Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Tested Satisfactorily | | | 05000272/LER-1982-004-03, /03L-0:on 820109,primary Coolant Water Sample Results Indicated Excessive Boron Concentration,Constituting Positive Reactivity Change.Caused by Water Draining Out of Steam Generator Tubes.Rcs Rapid Boration Initiated | /03L-0:on 820109,primary Coolant Water Sample Results Indicated Excessive Boron Concentration,Constituting Positive Reactivity Change.Caused by Water Draining Out of Steam Generator Tubes.Rcs Rapid Boration Initiated | | | 05000272/LER-1982-004, Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration | Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration | | | 05000311/LER-1982-004, Forwards LER 82-004/03X-1.Detailed Event Analysis Encl | Forwards LER 82-004/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-005-01, /01X-1:on 820131,degradation of Fuel Cladding on Fuel Assembly C-04 Discovered.Caused by Fuel Lockup Due to Wedged Fuel Pellet.Fuel Assembly Placed in Spent Fuel Pit. 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All C Assemblies Scheduled for Reuse in Core | | | 05000272/LER-1982-005, Forwards LER 82-005/01X-1.Detailed Event Analysis Encl | Forwards LER 82-005/01X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-005-03, /03L-0:on 820121,during Performance of M3T Maint Surveillance Test Undervoltage Relay on 2C Vital Bus Actuated at 5.5 Volts Instead of 77.3 Volt Trip Setpoint Value.No Defects Found.Relay Recalibr | /03L-0:on 820121,during Performance of M3T Maint Surveillance Test Undervoltage Relay on 2C Vital Bus Actuated at 5.5 Volts Instead of 77.3 Volt Trip Setpoint Value.No Defects Found.Relay Recalibr | | | 05000272/LER-1982-006-03, /03L-0:on 820113,air Particulate Detector Failed. Cause Not Stated.All Required Containment Purge & Pressure Vacuum Relief Penetrations Isolated.High & Low Speed Filter Paper Drives Replaced | /03L-0:on 820113,air Particulate Detector Failed. Cause Not Stated.All Required Containment Purge & Pressure Vacuum Relief Penetrations Isolated.High & Low Speed Filter Paper Drives Replaced | | | 05000272/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-006-03, /03L-0:on 820128,svc Water Flow Indicator Indicated No Flow Condition.Caused by Svc Water Discharge Valve 22SW223 Being Stuck Shut.Valve Opened,Locally Tested & Returned to Svc | /03L-0:on 820128,svc Water Flow Indicator Indicated No Flow Condition.Caused by Svc Water Discharge Valve 22SW223 Being Stuck Shut.Valve Opened,Locally Tested & Returned to Svc | | | 05000272/LER-1982-007-01, /01X-2:on 820211,during Design Review,Discovered That Check Valves 1AF71 & 1AF72 & Associated Piping Not Seismically Analyzed & Protected.Protective Steel Structures Provided Off Seismic Wall | /01X-2:on 820211,during Design Review,Discovered That Check Valves 1AF71 & 1AF72 & Associated Piping Not Seismically Analyzed & Protected.Protective Steel Structures Provided Off Seismic Wall | | | 05000272/LER-1982-007, Forwards LER 82-007/01X-2 | Forwards LER 82-007/01X-2 | | | 05000272/LER-1982-008, Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added | Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added | | | 05000272/LER-1982-008-03, /03L-0:on 820126,sample Results from Boric Acid Tanks Indicated Boric Acid Concentration Below Tech Specs. Refueling Water Storage Tank Low.Core Alterations & Positive Reactivity Changes Suspended.Level Adjusted | /03L-0:on 820126,sample Results from Boric Acid Tanks Indicated Boric Acid Concentration Below Tech Specs. Refueling Water Storage Tank Low.Core Alterations & Positive Reactivity Changes Suspended.Level Adjusted | | | 05000311/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-008-03, /03L-0:on 820128,overpower Delta T Indication for Channel 21 Failed High.Caused by Signal Summator 2T-M412E Having No Output Due to Failed Capacitors. Five Capacitors Replaced | /03L-0:on 820128,overpower Delta T Indication for Channel 21 Failed High.Caused by Signal Summator 2T-M412E Having No Output Due to Failed Capacitors. Five Capacitors Replaced | | | 05000311/LER-1982-009, Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-009, Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage | Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage | | | 05000272/LER-1982-009-03, /03L-0:on 820118 & 25,switches for Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Tank Area 12 Had Been in Manual Position for Greater than 14 Days Due to Maint Outage | /03L-0:on 820118 & 25,switches for Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Tank Area 12 Had Been in Manual Position for Greater than 14 Days Due to Maint Outage | | | 05000311/LER-1982-009-03, /03L-0:on 820129,air Particulate Detector Pump Low Flow Alarm Annuniciated.Caused by Incorrect Normal Flow Valve Lineup to Pump.Pump Removed from Normal Flow & Placed in Backup Flow Lineup | /03L-0:on 820129,air Particulate Detector Pump Low Flow Alarm Annuniciated.Caused by Incorrect Normal Flow Valve Lineup to Pump.Pump Removed from Normal Flow & Placed in Backup Flow Lineup | | | 05000311/LER-1982-010-03, /03L-0:on 820201,discrepancy Between Individual Rod Position Indicator (Irpi) & Control Rod Bank Demand Indicator for Rod 2C2 Exceeded 12 Steps in Either Direction. Caused by Incorrect Calibr of Irpi.Irpi Calibr | /03L-0:on 820201,discrepancy Between Individual Rod Position Indicator (Irpi) & Control Rod Bank Demand Indicator for Rod 2C2 Exceeded 12 Steps in Either Direction. Caused by Incorrect Calibr of Irpi.Irpi Calibr | | | 05000272/LER-1982-010-03, /03X-1:on 820201,temporary Hose Connection from Unit 1 Spent Fuel Pool to Unit 2 Exchanger Found Leaking on Auxiliary Bldg 84-ft Elevation.Caused by Improper Clamp Installation.Hose Disconnected | /03X-1:on 820201,temporary Hose Connection from Unit 1 Spent Fuel Pool to Unit 2 Exchanger Found Leaking on Auxiliary Bldg 84-ft Elevation.Caused by Improper Clamp Installation.Hose Disconnected | | | 05000311/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-010, Forwards LER 82-010/03X-1.Detailed Event Analysis Encl | Forwards LER 82-010/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-011-03, /03L-0:on 820205,during Radiological Survey of Hot Laundry Trailer Area,Technician Discovered Lint from Dryer Exhaust of Trailer B Revealing Traces of Cs-137,Co-60 & Co-58.New Trailer & Lint Collector Installed | /03L-0:on 820205,during Radiological Survey of Hot Laundry Trailer Area,Technician Discovered Lint from Dryer Exhaust of Trailer B Revealing Traces of Cs-137,Co-60 & Co-58.New Trailer & Lint Collector Installed | | | 05000272/LER-1982-011, Forwards LER 82-011/03X-1.Detailed Event Analysis Encl | Forwards LER 82-011/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-012, Forwards LER 82-012/03X-1.Detailed Event Analysis Encl | Forwards LER 82-012/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-012-03, /03X-1:on 820209,steam Generator Level Channel 2 Displayed Erratic Behavior,Indicating Drift.Apparently Caused by Intermittent Ground on Signal Lead.Ground Eliminated by Lifting Leads While Troubleshooting Problem | /03X-1:on 820209,steam Generator Level Channel 2 Displayed Erratic Behavior,Indicating Drift.Apparently Caused by Intermittent Ground on Signal Lead.Ground Eliminated by Lifting Leads While Troubleshooting Problem | | | 05000272/LER-1982-012-03, /03L-0:on 820223,operator Found Significant Amount of Chromated Water on Floor in Diesel Generator 1B Cubicle. Caused by Leakage on Right Side Jacket Water Heater.Jacket Water Heaters Replaced | /03L-0:on 820223,operator Found Significant Amount of Chromated Water on Floor in Diesel Generator 1B Cubicle. Caused by Leakage on Right Side Jacket Water Heater.Jacket Water Heaters Replaced | | | 05000272/LER-1982-013-03, /03L-0:on 820301,control Room Operator Closed Pressurizer Relief Valve 1PR1 When Valve 1PR2 Was Still Closed.Caused by Operator Error.Operator Counseled by Senior Shift Supervisor | /03L-0:on 820301,control Room Operator Closed Pressurizer Relief Valve 1PR1 When Valve 1PR2 Was Still Closed.Caused by Operator Error.Operator Counseled by Senior Shift Supervisor | | | 05000311/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-013-03, L-0:on 820215,shift Supervisor Informed That Two 4-inch Core Bores Opened on 78-ft Elevation Between Mechanical & Electrical Penetration Areas.No Fire Watch Posted.Caused by Inadvertently Posting Watch on Wrong Unit | L-0:on 820215,shift Supervisor Informed That Two 4-inch Core Bores Opened on 78-ft Elevation Between Mechanical & Electrical Penetration Areas.No Fire Watch Posted.Caused by Inadvertently Posting Watch on Wrong Unit | | | 05000272/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-014-03, /03L-0:on 820219,steam Generator 21 Level Channel 2 Read 20% Higher than Channels 3 & 4.Channel 2 Declared Inoperable.Cause Unknown.Transmitter Tested & Found Satisfactory.Sensing Lines Blown Down to Remove Solids | /03L-0:on 820219,steam Generator 21 Level Channel 2 Read 20% Higher than Channels 3 & 4.Channel 2 Declared Inoperable.Cause Unknown.Transmitter Tested & Found Satisfactory.Sensing Lines Blown Down to Remove Solids | | | 05000272/LER-1982-014-03, /03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable | /03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable | | | 05000311/LER-1982-014, Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | |
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