Similar Documents at Salem |
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PS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 90-001-00 January 31, 1990 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a} (2) (iv).
This report is required within thirty (30) days of discovery.
MJP:pc Distribution Q00?090~1~ 900131
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PDC Sincerely yours, L. K. Miller General Manager -
Salem Operations 95-2189 (SM) 12-88
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On 1/6/90 at 0204 hours0.00236 days <br />0.0567 hours <br />3.373016e-4 weeks <br />7.7622e-5 months <br />, a Containment Purge/Pressure-Vacuum Relief System (CP/P-VRS) isolation signal actuated as a result of a channel spike on the Radiation Monitoring System (RMS) Containment Particutate Radiation Monitor, lRllA.
Subsequently, Technical Specification 3.4.6.1 Action Statement was entered.
A second spike and subsequent CP/P-VRS isolation signal occurred the same day at 1011 hours0.0117 days <br />0.281 hours <br />0.00167 weeks <br />3.846855e-4 months <br />.
The root cause of the channel spikes has been attributed to an equipment failure.
The channel drawer PC cards were found dirty.
The lRllA RMS is a NaI scintillation type detector, model LFE MDSB.
The lRllA channel drawer PC cards were cleaned and the channel connectors were checked and found satisfactory.
A channel functional test was successfully completed and, at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on January 9, 1990, the channel was declared operable and Technical Specification 3.4.6.1 Action Statement was exited.
The preventive maintenance program for the lRllA RMS channel will be reviewed and revised as applicable to prevent recurrence of this event.
NllCF.--
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER 5000272
PLANT AND SYSTEM IDENTIFICATION
Westinghouse Pressurized Water Reactor LER NUMBER 90-001-00 PAGE 2 of 4 Energy Industry Identification System (EIIS} codes are identified in the text as {xxJ IDENTIFICATION OF OCCURRENCE:
Engineered Safety Feature Actuation -
Containment Ventilation Isolation Due To Equipment Concerns Event Date:
1/06/90 Report Date:
1/31/90 This report was initiated by Incident Report Nos.90-014, and 90-016.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 Reactor Power 100% - Unit Load 1155 MWe DESCRIPTION OF OCCURRENCE:
On January 6, 1990 at 0204 hours0.00236 days <br />0.0567 hours <br />3.373016e-4 weeks <br />7.7622e-5 months <br />, a Containment Purge/Pressure-Vacuum Relief System (CP/P-VRS) isolation signal actuated as a result of a channel spike on the Radiation Monitoring System (RMS) {ILi Containment Particulate Radiation Monitor, lRllA.
Subsequently, Technical Specification 3.4.6.1 Action Statement was entered.
A second spike and subsequent CP/P-VRS isolation signal occurred the same_ day at 1011 hours0.0117 days <br />0.281 hours <br />0.00167 weeks <br />3.846855e-4 months <br />.
Technical Specification 3.4.6.1 states:
"The following Reactor Coolant System leakage detection systems shall be OPERABLE:
a.
The containment atmosphere particulate radioactivity monitoring system, b.
The containment pocket sump level monitoring system, and c.
Either the containment fan cooler condensate flow rate or the containment atmosphere gaseous radioactivity monitoring system."
Technical Specification 3.4.6.1 Action Statement states:
"With only two of the above required leakage detection systems OPERABLE, operation may continue for up to 30 days provided grab samples of the containment atmosphere are obtained and analyzed at least once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> when the required gaseous and/or particulate radioactivity monitoring system is inoperable;
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER 5000272 DESCRIPTION OF OCCURRENCE:
(cont'd)
LER NUMBER 90-001-00 PAGE 3 of 4 otherwise, be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />."
The CP/P-VRS is considered an Engineered Safety System (ESF).
Subsequently, on January 6, 1990 at 0315 hours0.00365 days <br />0.0875 hours <br />5.208333e-4 weeks <br />1.198575e-4 months <br />, and again at 1151 hours0.0133 days <br />0.32 hours <br />0.0019 weeks <br />4.379555e-4 months <br />, the Nuclear Regulatory Commission was notified of the*
automatic actuation signal for CP/P-VRS isolation in accordance with Code of Federal Regulations 10CFR 50.72(b) (2) (ii).
APPARENT CAUSE OF OCCURRENCE:
The cause of the lRllA channel spikes has been attributed to an equipment failure.
The channel drawer PC cards were found dirty.
The lRllA RMS is a NaI scintillation type detector, model LFE MD5B.
ANALYSIS OF OCCURRENCE:
The lRllA, Containment Particulate Monitor, monitor's the air particulate gamma radioactivity in the Containment atmosphere.
It is used identification of Reactor Coolant System {ABJ leakage in conjunction with the containment pocket sump level monitoring system, the containment fan cooler condensate flow rate monitors, and the containment atmosphere gaseous radioactivity ( 1R12A) RMS.channel.
An alarm signal will cause the automatic isolation of the CP/P-VRS.
Air samples are pulled directly from the Containment atmosphere through a filter paper which continuously moves past the lRllA scintillation detector.
After the air sample passes through the filter paper, it passes through a charcoal cartridge (monitored by the 1R12B monitor) and is then mixed into a fixed shielded volume where it is viewed by the 1Rl2A noble gas monitor.
The air sample is then returned to the Containment.
Several area radiation monitors, in addition to the 1R12A monitor*,
are used to corroborate the lRllA channel's indications.
The corroborating area radiation monitors do not have isolation capabilities.
They only have alarm capability.
The 1R41A Plant Vent Particulate monitor also corroborates the lRllA channel indications during Containment purge or pressure-vacuum relief operations.
It also has the capability of automatic isolation of the CP/P-VRS.
During the inoperable period for the lRllA channel, Containment pressure relief was conducted.
The 1R41A channel remained operable during the pressure relief.
During this event, RCS leakage within Containment did not increase.
Additionally, a Containment purge or pressure-vacuum relief was not performed.
Therefore, this event did not affect the health or safety of the public.
However, due to the automatic actuation signal of an ESF system, this event is reportable in accordance with Code of Federal Regulations 10CFR 50.73(a) (2) (iv).
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1
CORRECTIVE ACTION
DOCKET NUMBER 5000272 LER NUMBER 90-001-00 PAGE 4 of 4 The lRllA channel drawer PC cards were cleaned and the channel connectors were checked and found satisfactory.
A channel functional test was successfully completed and, at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on January 9, 1990, the channel was declared operable and Technical Specification 3.4.6.1 Action Statement was exited.
The preventive maintenance program for the lRllA RMS channel will be reviewed and revised as applicable to prevent recurrence of this event.
MJP:pc SORC Mtg.90-008
- ft~~
General Manager -
Salem Operations
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| 05000272/LER-1990-001, :on 900106,containment purge/pressure-vacuum Relief Sys Isolation Signal Actuated as Result of Channel Spike on Particulate Radiation Monitor 1R11A.Caused by Dirty Pc Cards.Cards Cleaned & Connectors Checked |
- on 900106,containment purge/pressure-vacuum Relief Sys Isolation Signal Actuated as Result of Channel Spike on Particulate Radiation Monitor 1R11A.Caused by Dirty Pc Cards.Cards Cleaned & Connectors Checked
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-001-01, :on 900101,general Area Radiation Monitoring Sys Monitor Spiked Into Alarm Resulting in Second Automatic Switching of Control Room Ventilation.Caused by Design/ Equipment Concerns.Channel Reset |
- on 900101,general Area Radiation Monitoring Sys Monitor Spiked Into Alarm Resulting in Second Automatic Switching of Control Room Ventilation.Caused by Design/ Equipment Concerns.Channel Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-002-01, :on 900117 & 0201,containment Purge/Pressure Vacuum Relief Sys Isolation Signals Initiated Due to Failures of Radiation Monitor Channel 1R41.Caused by Design/ Equipment Problem.Control Modules Reseated |
- on 900117 & 0201,containment Purge/Pressure Vacuum Relief Sys Isolation Signals Initiated Due to Failures of Radiation Monitor Channel 1R41.Caused by Design/ Equipment Problem.Control Modules Reseated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-002, :on 900104,determined That ECCS Flow Balance Verification Surveillance Not Correctly Calculated After Last Refueling Outage on 881023.Caused by Personnel Error. Discretionary Enforcement Granted by NRC |
- on 900104,determined That ECCS Flow Balance Verification Surveillance Not Correctly Calculated After Last Refueling Outage on 881023.Caused by Personnel Error. Discretionary Enforcement Granted by NRC
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1990-003-01, :on 900122,plant Vent Radioactive Noble Gas Monitor 1R41C Spiked High,Causing Containment Purge/Pressure Vaccum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Detector.Channel Relay Repaired |
- on 900122,plant Vent Radioactive Noble Gas Monitor 1R41C Spiked High,Causing Containment Purge/Pressure Vaccum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Detector.Channel Relay Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-003, :on 900105,steam Generator 22 Blowdown Radiation Monitoring Sys Channel 2R19B Failed.Caused by Design/Equipment Concerns.Radiation Monitoring Sys Monitors & Modules Reseated |
- on 900105,steam Generator 22 Blowdown Radiation Monitoring Sys Channel 2R19B Failed.Caused by Design/Equipment Concerns.Radiation Monitoring Sys Monitors & Modules Reseated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-004-01, :on 900124,spurious Actuation Signal for Containment Purge/Pressure Vacuum Relief Sys Isolation Received.Probably Caused by Failed Radiation Monitoring Sys Channel.Sys Design Mods Underway |
- on 900124,spurious Actuation Signal for Containment Purge/Pressure Vacuum Relief Sys Isolation Received.Probably Caused by Failed Radiation Monitoring Sys Channel.Sys Design Mods Underway
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-004, :on 900112,plant Vent Noble Gas Monitor 2R41A Channel Failed Low,Resulting in Containment Purge/Pressure Vacuum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Monitor.Channel Module Adjusted |
- on 900112,plant Vent Noble Gas Monitor 2R41A Channel Failed Low,Resulting in Containment Purge/Pressure Vacuum Relief Sys Isolation Signal.Caused by Problems W/ Victoreen Monitor.Channel Module Adjusted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-005-01, :on 900220,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor Channel Began Intermittently Spiking High Resulting in Containment Purge.Caused by Design /Equipment Problem.Equipment Replaced |
- on 900220,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor Channel Began Intermittently Spiking High Resulting in Containment Purge.Caused by Design /Equipment Problem.Equipment Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-005, :on 900117,Tech Spec Action Statement 3.0.3 Entered Due to Inoperability of Two High Head ECCS Subsys. Caused by Leak from Welded Pipe Cap on Boron Injection Tank. Pipe-to-cap Socket Welded Joint Repaired |
- on 900117,Tech Spec Action Statement 3.0.3 Entered Due to Inoperability of Two High Head ECCS Subsys. Caused by Leak from Welded Pipe Cap on Boron Injection Tank. Pipe-to-cap Socket Welded Joint Repaired
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1990-006-01, :on 900302,ESF Actuation & Containment Ventilation Isolation Occurred.Caused by Design/Equipment Problem.Channel Backplane Replaced & Functional Test Completed |
- on 900302,ESF Actuation & Containment Ventilation Isolation Occurred.Caused by Design/Equipment Problem.Channel Backplane Replaced & Functional Test Completed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-006, :on 900117,control Room General Area Radiation Monitor Spiked High,Resulting in Switching Ventilation Sys to Emergency Mode of Operation.Caused by Damaged Pins on Channel Backplate & Modules.Pins Repaired |
- on 900117,control Room General Area Radiation Monitor Spiked High,Resulting in Switching Ventilation Sys to Emergency Mode of Operation.Caused by Damaged Pins on Channel Backplate & Modules.Pins Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-007-01, :on 900321,found Tech Spec Surveillance for Containment Spray Not Performed Historically.Root Cause of Event Attributed to Past Inadequate Administrative Controls. Administrative Procedure Revised |
- on 900321,found Tech Spec Surveillance for Containment Spray Not Performed Historically.Root Cause of Event Attributed to Past Inadequate Administrative Controls. Administrative Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-007, :on 900117,main Steam Line Isolation Signal Actuated During Surveillance for Pressure Transmitter, Causing Isolation Signal & ESF Actuations.Caused by Inadequate Procedure.Panel Labeling Corrected |
- on 900117,main Steam Line Isolation Signal Actuated During Surveillance for Pressure Transmitter, Causing Isolation Signal & ESF Actuations.Caused by Inadequate Procedure.Panel Labeling Corrected
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-008, :on 900120,plant Vent Noble Gas Monitor 2R41C Failed Low,Resulting in Closure Signal for Waste Gas Decay Tank Vent Control Valve 2WG41.Caused by Personnel Error. Operator Aid Will Be Posted on Panel |
- on 900120,plant Vent Noble Gas Monitor 2R41C Failed Low,Resulting in Closure Signal for Waste Gas Decay Tank Vent Control Valve 2WG41.Caused by Personnel Error. Operator Aid Will Be Posted on Panel
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-008-01, :on 900327,controlled Shutdown Commenced,Per Tech Spec Action Statement Due to Inoperability of Safeguards Equipment Controls Cabinet 1A.Caused by Equipment Failure.Spare Chassis Installed |
- on 900327,controlled Shutdown Commenced,Per Tech Spec Action Statement Due to Inoperability of Safeguards Equipment Controls Cabinet 1A.Caused by Equipment Failure.Spare Chassis Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | | 05000311/LER-1990-009, :on 900123,plant Vent Radioactive Iodine Monitor Channel Spiked High Resulting in Containment Purge/ pressure-vacuum Relief Sys Isolation Signal.Caused by Design & Equipment Problems.Scaler Test Jack Replaced |
- on 900123,plant Vent Radioactive Iodine Monitor Channel Spiked High Resulting in Containment Purge/ pressure-vacuum Relief Sys Isolation Signal.Caused by Design & Equipment Problems.Scaler Test Jack Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-009-01, :on 900328,main Steamline Isolation Signal Actuated During Performance of Channel I Main Steamline Flow Calibr.Caused by Inadequate Procedure.Main Steamline Flow Detector Calibr Procedure Revised |
- on 900328,main Steamline Isolation Signal Actuated During Performance of Channel I Main Steamline Flow Calibr.Caused by Inadequate Procedure.Main Steamline Flow Detector Calibr Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-010, :on 900216,containment Radioactive Iodine Monitor Radiation Monitoring Sys Channel Failed Low.Caused by Design/Equipment Concerns.Sys Design Mods Will Be Implemented to Eliminate ESF Actuation Signals |
- on 900216,containment Radioactive Iodine Monitor Radiation Monitoring Sys Channel Failed Low.Caused by Design/Equipment Concerns.Sys Design Mods Will Be Implemented to Eliminate ESF Actuation Signals
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-010-01, :on 900403,reactor Trip Signal Initiated Due to lo-lo Level in Steam Generator 12.Caused by Personnel Error. Event Reviewed by Operations Dept Mgt & Personnel Involved Held Accountable |
- on 900403,reactor Trip Signal Initiated Due to lo-lo Level in Steam Generator 12.Caused by Personnel Error. Event Reviewed by Operations Dept Mgt & Personnel Involved Held Accountable
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-011, :on 900301,containment Ventilation Isolation Signal (ESF) Occurred.Caused by Equipment Failure.Frayed Wire Repaired & Functional Surveillance Requirement Modified to Include Insp of Wire |
- on 900301,containment Ventilation Isolation Signal (ESF) Occurred.Caused by Equipment Failure.Frayed Wire Repaired & Functional Surveillance Requirement Modified to Include Insp of Wire
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-011-01, :on 900406,turbine Trip & Feedwater Isolation Actuation Occurred on Steam Generator 14 hi-hi Level. Caused by Equipment Failure.Valve Stem on Valve 12TB10 Polished & Adjusted |
- on 900406,turbine Trip & Feedwater Isolation Actuation Occurred on Steam Generator 14 hi-hi Level. Caused by Equipment Failure.Valve Stem on Valve 12TB10 Polished & Adjusted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-012, :on 900403,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor 2R41C Lost Power Resulting in Isolation in Containment purge/pressure-vacuum Relief Sys. Cause Not Determined |
- on 900403,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor 2R41C Lost Power Resulting in Isolation in Containment purge/pressure-vacuum Relief Sys. Cause Not Determined
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-012-01, :on 900409,reactor Trip on Steam Generator 12 lo-lo Level Occurred.Caused by Equipment Failure.Steam Generator 12 Governor Valve Linkage Repaired |
- on 900409,reactor Trip on Steam Generator 12 lo-lo Level Occurred.Caused by Equipment Failure.Steam Generator 12 Governor Valve Linkage Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-013, :on 900410,radiation Monitoring Sys Channel 1R12A Spiked Into Alarm,Resulting in ESF Actuation Signal. Caused by Failure of Electrical Signal Connectors &/Or Electronic Circuit Connections.Repairs Made |
- on 900410,radiation Monitoring Sys Channel 1R12A Spiked Into Alarm,Resulting in ESF Actuation Signal. Caused by Failure of Electrical Signal Connectors &/Or Electronic Circuit Connections.Repairs Made
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-013-01, :on 900416,discovered That Setpoint for 2R11A & 2R12A Monitors for Radiation Monitoring Sys Channels Not Changed During Last Refueling Outage.Caused by Inadequate Administrative Control.Procedure Revised |
- on 900416,discovered That Setpoint for 2R11A & 2R12A Monitors for Radiation Monitoring Sys Channels Not Changed During Last Refueling Outage.Caused by Inadequate Administrative Control.Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1990-014, :on 900419,ESF Actuation Signal for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40 |
- on 900419,ESF Actuation Signal for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(b)(2)(ii) | | 05000272/LER-1990-014-01, :on 900409,determined That Last Calculated Safety Injection Pump Flow Rate for Pumps 12 & 21 Greater than 650 Gpm.Caused by Personnel Error & Procedural Deficiencies.New Orifice Plates Installed |
- on 900409,determined That Last Calculated Safety Injection Pump Flow Rate for Pumps 12 & 21 Greater than 650 Gpm.Caused by Personnel Error & Procedural Deficiencies.New Orifice Plates Installed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-015, :on 900415,ESF Signal Actuation for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40 |
- on 900415,ESF Signal Actuation for Containment Ventilation Isolation Occurred.Caused by Procedural Inadequacy.Setpoint Setting Modified & Detector Time Constant Extended from 20 to 40
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-015-01, :on 900430,control Room Intake Radiation Monitor 1R1B Alarm Circuitry Failed,Resulting in Switching Control Room Ventilation from Normal to Accident Mode. Caused by Short in Bulb.Bulbs Replaced |
- on 900430,control Room Intake Radiation Monitor 1R1B Alarm Circuitry Failed,Resulting in Switching Control Room Ventilation from Normal to Accident Mode. Caused by Short in Bulb.Bulbs Replaced
| | | 05000272/LER-1990-016-01, :on 900419,determined That Six Fast Closure Turbine Bldg Svc Water Sys Isolation Valves Could Not Be Counted on to Function During Design Base Event.Caused by Inadequate Design |
- on 900419,determined That Six Fast Closure Turbine Bldg Svc Water Sys Isolation Valves Could Not Be Counted on to Function During Design Base Event.Caused by Inadequate Design
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000311/LER-1990-016, :on 900420,discovered That Containment Pressure Relief Conducted W/Associated Radiation Monitoring Sys Channels Inoperable.Caused by Inoperability of Control Room Pump Low Flow Alarm.Procedures Revised |
- on 900420,discovered That Containment Pressure Relief Conducted W/Associated Radiation Monitoring Sys Channels Inoperable.Caused by Inoperability of Control Room Pump Low Flow Alarm.Procedures Revised
| 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1990-017-01, :on 900507,high Head Safety Injection Pumps Failed to Meet Seismic Criteria.Caused by Equipment Mfg Failure to Complete Required Welding.Intermediate Head Safety Injection Pumps Design Reviewed |
- on 900507,high Head Safety Injection Pumps Failed to Meet Seismic Criteria.Caused by Equipment Mfg Failure to Complete Required Welding.Intermediate Head Safety Injection Pumps Design Reviewed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000311/LER-1990-017, :on 900501,inadvertent Manual Safety Injection Occurred Due to Personnel Error.Technician Made Assumption Re Wiring Changes Performed.Train B Wiring Corrected & Deficiency Rept Initiated |
- on 900501,inadvertent Manual Safety Injection Occurred Due to Personnel Error.Technician Made Assumption Re Wiring Changes Performed.Train B Wiring Corrected & Deficiency Rept Initiated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-018, :on 900528,control Room Air Intake Radiation Monitoring Sys Monitor Alarm Circuitry Failed & on 900701, Channel 1R1B Failed Resulting in Actuation of ESF Function. Caused by Spurious High Channel Spike |
- on 900528,control Room Air Intake Radiation Monitoring Sys Monitor Alarm Circuitry Failed & on 900701, Channel 1R1B Failed Resulting in Actuation of ESF Function. Caused by Spurious High Channel Spike
| | | 05000272/LER-1990-018-01, :on 900528,ESF Actuation Involving Control Room Ventilation Switch Occurred.Caused by Spurious High Channel Spike.Channel Functional Test Successfully Completed on 900611 |
- on 900528,ESF Actuation Involving Control Room Ventilation Switch Occurred.Caused by Spurious High Channel Spike.Channel Functional Test Successfully Completed on 900611
| 10 CFR 50.73(a)(2) | | 05000311/LER-1990-018, :on 900511,containment Purge/Pressure Vacuum Relief Sys Actuated.Caused by Design/Equipment Failures. Lighting Transformer 2HL Replaced |
- on 900511,containment Purge/Pressure Vacuum Relief Sys Actuated.Caused by Design/Equipment Failures. Lighting Transformer 2HL Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-019-01, :on 900603,main Steam Line Isolation Actuation Occurred & Bistables for Low Steam Line Pressure Logic Tripped.Caused by Equipment/Design Concerns W/Sensing Lines. Design Mods Re Flow Instrumentation Underway |
- on 900603,main Steam Line Isolation Actuation Occurred & Bistables for Low Steam Line Pressure Logic Tripped.Caused by Equipment/Design Concerns W/Sensing Lines. Design Mods Re Flow Instrumentation Underway
| 10 CFR 50.73(a)(2) | | 05000311/LER-1990-019, :on 900511,ESF Actuation Occurred When Radioactive Noble Gas Monitor 2R12A RMS Channel Spiked High. Caused by Equipment/Design Failures.Several Sys Design Mods Will Eliminate Spurious Actuation |
- on 900511,ESF Actuation Occurred When Radioactive Noble Gas Monitor 2R12A RMS Channel Spiked High. Caused by Equipment/Design Failures.Several Sys Design Mods Will Eliminate Spurious Actuation
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-020-01, :on 900608,identified That maint-I&C Procedures for Setting Intermediate Range Excore Nuclear Instrumentation Sys Permissive P-6 Not Correct.Caused by Inadequate Procedure Control |
- on 900608,identified That maint-I&C Procedures for Setting Intermediate Range Excore Nuclear Instrumentation Sys Permissive P-6 Not Correct.Caused by Inadequate Procedure Control
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-020, :on 900512,containment purge/pressure-vacuum Relief Sys Isolation Signal Received from Radiation Monitoring Sys.Caused by Equipment Design Concerns. Uninterruptible Power Supply Installed |
- on 900512,containment purge/pressure-vacuum Relief Sys Isolation Signal Received from Radiation Monitoring Sys.Caused by Equipment Design Concerns. Uninterruptible Power Supply Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-021, :on 900515,radiation Monitoring Sys Channel 2R12A Failed Resulting in ESF Signal Actuation for Containment Purge/Pressure Vacuum Relief Sys Isolation. Caused by Equipment/Design Concerns |
- on 900515,radiation Monitoring Sys Channel 2R12A Failed Resulting in ESF Signal Actuation for Containment Purge/Pressure Vacuum Relief Sys Isolation. Caused by Equipment/Design Concerns
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-021-01, :on 900717,discovered That Work Order Not Issued to Perform Revised Procedure 1IC-16.1.008.Caused by Personnel Error.Event Reviewed by Technical Department Mgt Appropriate Personnel |
- on 900717,discovered That Work Order Not Issued to Perform Revised Procedure 1IC-16.1.008.Caused by Personnel Error.Event Reviewed by Technical Department Mgt Appropriate Personnel
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1990-022-01, :on 900717,observed That Relief Valve 1SJ167 Was Leaking Past Seat as Result of Investigation to Determine Cause of Decreasing Level in Accumulators.Caused by Equipment Failure.Valve Repaired on 900722 |
- on 900717,observed That Relief Valve 1SJ167 Was Leaking Past Seat as Result of Investigation to Determine Cause of Decreasing Level in Accumulators.Caused by Equipment Failure.Valve Repaired on 900722
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1990-022, :on 900522,radiation Monitoring Sys Channel 2R12A Failed Low.Probably Caused by Equipment/Design Concerns.Anticipates That Several Sys Design Mods Will Eliminate Spurious ESF Actuation Signals |
- on 900522,radiation Monitoring Sys Channel 2R12A Failed Low.Probably Caused by Equipment/Design Concerns.Anticipates That Several Sys Design Mods Will Eliminate Spurious ESF Actuation Signals
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1990-023, :on 900516,4 Kv Vital Bus Deenergized During 2A Safeguard Equipment Control 18-month Surveillance.Caused by Personnel Error.Personnel Reprimanded & Procedure M3U Revised |
- on 900516,4 Kv Vital Bus Deenergized During 2A Safeguard Equipment Control 18-month Surveillance.Caused by Personnel Error.Personnel Reprimanded & Procedure M3U Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1990-023-01, :on 900725,discovered That Surveillance of Svc Water Sys Check Valves Not Completed Per Inservice Testing Program Manual Requirements.Caused by Inadequate Administrative Controls.Program Modified |
- on 900725,discovered That Surveillance of Svc Water Sys Check Valves Not Completed Per Inservice Testing Program Manual Requirements.Caused by Inadequate Administrative Controls.Program Modified
| 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1990-024, :on 900521,T-handle Instrument Isolation Valve Discovered Closed,Resulting in Isolation of Liquid Radwaste Effluent Line Monitor 2R18.Caused by Personnel Error.Valve Added to Tagging Request Info Sys Data Base |
- on 900521,T-handle Instrument Isolation Valve Discovered Closed,Resulting in Isolation of Liquid Radwaste Effluent Line Monitor 2R18.Caused by Personnel Error.Valve Added to Tagging Request Info Sys Data Base
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000272/LER-1990-024-01, :on 900728,discovered That Interlock Functions for P-10 & P-12 Permissives Not Fully Tested Per Tech Spec Surveillance 4.3.1.1.2.Caused by Inadequate Administrative Controls.Procedures Revised to Address Testing |
- on 900728,discovered That Interlock Functions for P-10 & P-12 Permissives Not Fully Tested Per Tech Spec Surveillance 4.3.1.1.2.Caused by Inadequate Administrative Controls.Procedures Revised to Address Testing
| | | 05000272/LER-1990-025-01, :on 900806,control Room Air Intake Radiation Sys Monitor Alarm Circuitry Spiked High Resulting in Automatic Switching of Ventilation to Accident Mode of Operation.Addl Spikes Occurred on 900807 & 08 |
- on 900806,control Room Air Intake Radiation Sys Monitor Alarm Circuitry Spiked High Resulting in Automatic Switching of Ventilation to Accident Mode of Operation.Addl Spikes Occurred on 900807 & 08
| 10 CFR 50.73(a)(2)(iv), System Actuation |
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