05000311/LER-1982-009, Forwards LER 82-009/03L-0.Detailed Event Analysis Encl

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Forwards LER 82-009/03L-0.Detailed Event Analysis Encl
ML20041D851
Person / Time
Site: Salem PSEG icon.png
Issue date: 02/24/1982
From: Midura H
Public Service Enterprise Group
To: Haynes R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20041D852 List:
References
NUDOCS 8203090333
Download: ML20041D851 (3)


LER-1982-009, Forwards LER 82-009/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
3111982009R00 - NRC Website

text

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1 PSEG Pubhi, S"rvu e I lo<.tric arri Gn Cornpany P O. Box E Hancocks Br nJ e, New Jersey 08038 9

Salem Generating Station February 24, 1982 P

Mr.

R.

C.

Ilaynes g

Roc ional Administrator A

pgg,

'g MAR 08 ;g Region 1 u

631 Park Avenue

- a Nfgy.~

King of Prussia, Pennsylvania 19406

Dear Mr. Ilaynes :

LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 82-09/03L Pursuant to the requirements of Salem Generating Station Unit No.

2, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 82-09/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

//

> <f /wa II.

J.

Midura General Manager -

Salem Operations h FD:al CC:

Distribution The Eneray People gWg l

8203090333 820224 PDR ADOCK 05000311 5

S PDR

. ~. __

Report Number:

82-09/03L Report Date:

02-24-82 Occurrence Date:

01-29-82 Facility:

Salem Generating Station, Unit 2 Public Service Electric & Gas Company liancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Air Particulate Detector Pump - Low Flow Alarm.

This report was initiated by Incident Report 82-026.

CONDITIONS PRIOR TO OCCURRENCE:

Mode 1 - Rx Power 97% - Unit Load 1100 MWe DESCRIPTION OF OCCURRENCE:

On January 29, 1982 the Air Particulate Detector (APD) Pump Low j

Flow Alarm annunciated.

At 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> the APD was declared inoperable, rendering radiation monitors 2RllA, 2R12A, and 2R12B inoperable, and Action Statement 3.3.3.1 Actions 24 and 25 was entered.

This occurrence constituted operation in a degraded mode in accordance with Technical Specification 6.9.1.9.b.

f DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

The normal flow path valve line-up to the APD Pump was incorrect in that valve 2VC908 was shut when it should have been open.

ANALYSIS OF OCCURRENCE:

Technical Specification 3.3.3.1 requires:

Action 24 l

With the number of channels operable less than required by the minimum channels operable requirement, comply with the l

Action requirements of Specification 3.4.7.1.

Action 25 With the number of channels operable less than required by j

the minimum channels operable requirement, comply with the l

Action requirements of Specification 3.9.9.

i

I.Ep 82-09/03L,

l Technical Specification 3.4.7.1 requires:

i With only two of the required Leakage Detection Systems j

operabic, operation may continue for up to 30 days provided i

grab samples of the containment atmosphere are obtained and analyzed at least once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> when the required Gaseous i

and/or Particulate Radioactivity Monitoring System is in-operable.

i Technical Specification 3.9.9 requires:

With the Containment Purge and Pressure-Vacuum Relief Isolation System inoperable, close each of the purge and pressure-vacuum relief penetrations providing direct access from the containment atmosphere to the outside atmosphere.

The provisions of Specification 3.0.3 are not applicable.

CORRECTIVE ACTION

At 1435 hours0.0166 days <br />0.399 hours <br />0.00237 weeks <br />5.460175e-4 months <br /> the APD Pump was removed from the normal flow lineup and placed in the backup flow lineup.

Adequate flow was reestablished, returning the APD to operable status, and Action Statement 3.3.3.1 Actions 24 and 25 was terminated.

All requirements of Action Statements 3.4.7.1 and 3.9.9 were met.

Subsequently, it was discovered that valve 2VC908, which 4

should have been open in the normal lineup, was shut.

2VC908 was opened and the normal flow lineup was restored.

Personnel were counseled on proper valve lineups in order to prevent reoccurrence.

I I

FAILURE DATA:

Not Applicable i

i l

Prepared By F.

Dickey

/c kt[*

5" Geperal Manager -

Salem Operations i

SORC Meeting No.

82-22 i

f

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