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IIRC Pere M U S. NUCLE A A REGULATORY -
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On January 16, 1986, a reactor trip occurred immediately following the inadvertent de-energization of the 1A Vital Bus.
The initiating event was the actuation of the bus differential relay which, by design, caused the 1A Vital Bus to be de-energized.
Investigation revealed that the relay actuation was caused by a direct shock, resulting from the harder than normal closing of the 1A Diesel Generator output circuit breaker cabinet door by an operator who was tagging out the diesel for routine maintenance activities.
The loss of the bus'resulted in the loss of one of the two power supplies for the rod control power and logic cabinets.
Ilo w e v e r, the remaining power supply failed due to an internal fault, resulting in the loss of all power to the logic cards.
This, in turn, caused the control rods in shutdown banks C and D to drop into the core.
The Reactor Protection System then responded as designed to initiate a rsactor trip on high negative flux rate.
The failed power supply was replaced and satisfactorily tested.
Although the seismic qualification of the differential relays is not in question, their service qualification is being investigated; i.e.,
the relays contain " telephone contacts" which are vulnerable to actuation upon shock loading.
In the interim, operators were made aware of this incident and signs were placed on the cabinet doors instructing personnel to close the doors easily.
f 8602260069 060214 i
{DR ADOCK 05000272 a,,P- ~
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salen Generating Station DOCKET NUMBER LER NUMBER FAGE Unit 1 05000272 86-001-00 2 0F 4 FLANT AND SYSTEM IDENTIFICATIONl Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
IDENTIFICATION OF OCCURRENCE:
Reactor Trip From 100% on High Negative Flux Rate Event Date:
01/16/86 Report Date: 02/14/86 This report was initiated by Incident Report No.86-024 CONDITIONS FRIOR TO OCCUERENCE:
/ Mode 1 - Rx Power 100 % - Unit Load 1115 MWe DESCRIPTION OF OCCUERENCE:
- 0n January 16, 1986, during routine power operation, IA 4KV Vital Bus [EB] de-energized.
This was followed almost immediately, at 0640 hours0.00741 days <br />0.178 hours <br />0.00106 weeks <br />2.4352e-4 months <br />, by a reactor trip.
lA Emergency Diesel Generator [EK]
was being tagged out for routine relay maintenance activities, which was the only evolution in progress at the time of the trip.
The Unit was stabilized in Mode 3 (Hot Standby), and at 0748 hours0.00866 days <br />0.208 hours <br />0.00124 weeks <br />2.84614e-4 months <br />, in accordance with the requirements of the Code of Federal Regulations, 10CFR 50.7 2(b)( 2)(ii), the Commission was notified of the automatic actuation of the Reactor Protection System [JC].
AFPARENT CAUSE OF OCCUERENCE:
The initiating event was the actuation of the 1 A 4KV Vital Bus differential relay which, by design, caused the 1A Vital Bus to be de-energized.
Investigation revealed that the relay actuation was not caused by an actual electrical fault on the bus, but instead was the result of a direct shock to the relay.
This shock was the result of a harder than normal closing of the 1A Diesel Cenerator output circuit breaker cabinet door by the operator performing the diesel tagout.
The " normal" power supplies for the rod control power and logic cabinets are fed from the rod drive motor-generator sets, while 1A Vital Bus feeds the " backup" power supplies.
The outputs of these power supplies are auctioneered, with the highest being automatically selected to carry the load.
Troubleshooting revealed that the " normal" negative twenty-four (-24) volt power supply on Rod Control Power Cabinet SCD had failed in such a manner tha t, when loaded, its output was only minus 1.4 volts.
4 f
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salen Generating Station DOCKET NUMBER LER NUMBER FAGE Unit 1 05000272 86-001-00 3 0F 4 AFFARENT CAUSE OF OCCURRENCE:'(cont'd)
However, when not loaded (when the rod control power and logic circuits were being supplied by the " backup" power supply) the
" normal" power supply voltage was reading normal.
Therefore, at the time of occurrence, cabinet 'SCD was being supplied by the " backup" power supply.
When the 1A Vital Bus de-energized, the " backup" power supply f ailed to zero, and the " normal" supply, attempting to pick up the load, went to minus 1.4 volts.
This resulted in a loss of all negative twenty-four ( -24) volt supply to the logic cards, causing the control rods in i*nhutdown banks C and D to drop into the core.
As a result, all four'(4) power range negative flux rate trips were initiated resulting in a reactor trip.
ANALYSIS OF OCCURRENCE:
s e
The reactor trip, on negative flux r a t e',
ensures that the minimum Departure from Nucleate Boiling Ratio'(DNBR) is maintained above 1.30 for multiple control rod drop accidenta.
The loss of power to Rod Control Power Cabinet SCD resulted in the dropping of eight (8) rods, and the Reactor Protection System responded as designed to initiate a reactor trip on high negative flux rate.
The plant is designed for four-hundred (400) trips from full power; therefore, this transient was within the design of the plant.
t As stated, the operstion of the vital bus differential relay was caused by an impact or shock load due to a hard closure ck the cubicle door (the relay is mounted on the door).
An impact load is not considered as part of the seismic criteria for thesrelay.
Seismic loading is a result of ground motion which is a low frequency vibration, whereas an impact load results in a high frequency response.
Therefore, the seismic qualification of the relay is not in question.
Concerning the loss of the 1A Vital Bus, sufficient redundant equipment remained available from the IB and 1C Vital Busses to provide the minimum required safeguards equipment to mitigate the consequences of a design basis event.
Therefore, this event involved no undue risk to the health or safety of the public.
However, because of the automatic actuatl'on of the Reactor Protection System, the event. is reportable in accordance with the Code of Federal Regulations,J10CFR 50.73(a)(2)(iv)..
CORRECTIVE ACTION _;
The failed power supply in the SCD cabinet was replaced and satisfactorily tested.
Because of the peculiar way in which this power supply failed (supplying normal output voltage while unloaded), a "non-urgent" failure alarm was not received; therefore, the failure of this power supply went undetected until the loss of the backup power supply.
Following a similar event which occurred in August of 1983 (see Unit 2 LEH 83-041/03L), testing of the rod control cabinet power supplies'was instituted on a refueling outage basis.
During the last refueling outage, all power supplies were tested with satisfactory results.
s
e LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salen Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 05000272 86-001-00 4 0F 4
CORRECTIVE ACTION
(cont'd)
Because of this recent occurrence, PSE&G Engineering is now investigating possible methods of verifying the operability of the power supplies in the rod control cabinets during normal operation.
This item is being addressed by SORC Open Item number 86-003B-01.
Concerning the inadvertent actuation of the bus differential relay, testing of the relays associated with the remaining vital busses verified that they too were subject to similar actuations upon hard closure of the cabinet doors.
Although the seismic qualification of these relays is not in question, PSE&G Engineering is invertigating their service qualification; i.e.,
these relays contain " telephone contacts" which are vulnerable to actuation upon shock loading.
This item is being addressed by SORC Open Item number 86-0038-02.
In the interim, operators were made aware of this incident via the Operations Department Newsletter.
Additionally, signs were placed on the cabinet doors instructing personnel to close the doors easily.
FAILURE _DAT_Al Lambda Electronics D.
C.
Power Supply Type LM-262
/
4/
General Manager-Salem Operations JLR:tna SORC Mtg 86-008
O PSEG Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, N+w Jersey 08038 Salem Generating Station February 14, 1986 U. S.
Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Dear Sirs SALEN GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 86-001-00 This Licensee Event Report is being submitted pursuant to the requirements of 10CFR 50.73(a)(2)(iv).
This report is required within thirty (30) days of discovery.
Sincerely yours, J.
M.
Zupko', Jr.
General Manager-Salem Operations l
JLRaama C
Distribution l
l l
l I
The Energy People
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| 05000311/LER-1986-001-02, :on 860320,waste Gas Holdup Sys Not Continuously Sampled for Oxygen.Caused by Procedural Inadequacy Which Prevented Returning Sampling Selector Switch to Auto. Procedure Being Revised |
- on 860320,waste Gas Holdup Sys Not Continuously Sampled for Oxygen.Caused by Procedural Inadequacy Which Prevented Returning Sampling Selector Switch to Auto. Procedure Being Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1986-001, :on 860116,reactor Trip Occurred Following Inadvertent Deenergization of Vital Bus 1A.Caused by Direct Shock to Relay.Failed Power Supply Replaced.Svc Qualification of Relays Being Investigated |
- on 860116,reactor Trip Occurred Following Inadvertent Deenergization of Vital Bus 1A.Caused by Direct Shock to Relay.Failed Power Supply Replaced.Svc Qualification of Relays Being Investigated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1986-002, :on 860131,failure to Implement Portions of Inservice Testing Program Discovered.Caused by Inadequate Mgt Attention to Program Requirements.Required Testing of Valves in ASME Sections 1-10 Performed |
- on 860131,failure to Implement Portions of Inservice Testing Program Discovered.Caused by Inadequate Mgt Attention to Program Requirements.Required Testing of Valves in ASME Sections 1-10 Performed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1986-002-02, :on 860416,reactor Trip Occurred Due to Turbine Trip Caused by Steam Generator 23 Reaching hi-hi Level Setpoint.Caused by Excessive Moisture in Feedwater Pump Control Oil Sys.Lube Oil Separator Replaced |
- on 860416,reactor Trip Occurred Due to Turbine Trip Caused by Steam Generator 23 Reaching hi-hi Level Setpoint.Caused by Excessive Moisture in Feedwater Pump Control Oil Sys.Lube Oil Separator Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1986-003, :on 860131,reactor Trip Occurred on Steam Generator 11 Due to Valve Partially Closing & Failure to Respond to Manual Control.Caused by Leak on Valve 11BF40 Positioner.Valve Replaced |
- on 860131,reactor Trip Occurred on Steam Generator 11 Due to Valve Partially Closing & Failure to Respond to Manual Control.Caused by Leak on Valve 11BF40 Positioner.Valve Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1986-003-02, :on 860502,safety Injection Occurred,Resulting in Reactor Trip.Caused by High Steam Flow Coincident W/Low Average Reactor Coolant Temp (Tave).Operating Procedures Revised to Ensure Tave within Programmed Band |
- on 860502,safety Injection Occurred,Resulting in Reactor Trip.Caused by High Steam Flow Coincident W/Low Average Reactor Coolant Temp (Tave).Operating Procedures Revised to Ensure Tave within Programmed Band
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1986-004, :on 860209,required Plant Vent Sampling Not Performed.Caused by Inadequate Means of Scheduling Samples Required by Radiological Eis.Training Programs Updated |
- on 860209,required Plant Vent Sampling Not Performed.Caused by Inadequate Means of Scheduling Samples Required by Radiological Eis.Training Programs Updated
| | | 05000311/LER-1986-004-02, :on 860714,reactor Tripped Due to Loss of Vital Instrument Inverter 2B.Caused by Personnel Inadvertently Repositioning AC Output Deion Switch.Personnel Counseled.W/ |
- on 860714,reactor Tripped Due to Loss of Vital Instrument Inverter 2B.Caused by Personnel Inadvertently Repositioning AC Output Deion Switch.Personnel Counseled.W/
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1986-004, :on 860714,reactor Trip Occurred Due to Loss of Power on Vital Instrument Inverter 2B.Caused by Blown Ac Output Fuses & Open Ac Output Deion Switch.Fuses Replaced & Inverter Tested,Aligned & Returned to Svc |
- on 860714,reactor Trip Occurred Due to Loss of Power on Vital Instrument Inverter 2B.Caused by Blown Ac Output Fuses & Open Ac Output Deion Switch.Fuses Replaced & Inverter Tested,Aligned & Returned to Svc
| | | 05000311/LER-1986-005-02, :on 860715,during Reactor Startup,Voltage Spike Occurred on Vital Instrument Inverter 2B.Caused by Technician Connecting Leads Incorrectly.Technician Counseled.Procedure Revised |
- on 860715,during Reactor Startup,Voltage Spike Occurred on Vital Instrument Inverter 2B.Caused by Technician Connecting Leads Incorrectly.Technician Counseled.Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1986-005, :on 860218,Tech Spec 3.8.1.1.a Requiring Surveillance of Diesel Generators 13 & 1C While 1A Tagged for Maint,Violated.Caused by Personnel Error.Operability of Generators Verified.Personnel Counseled |
- on 860218,Tech Spec 3.8.1.1.a Requiring Surveillance of Diesel Generators 13 & 1C While 1A Tagged for Maint,Violated.Caused by Personnel Error.Operability of Generators Verified.Personnel Counseled
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1986-006, :on 860220,reactor Trip Occurred When Steam Generator Water Level Signal Drifted Closed.Caused by Broken Wire to Solenoid Valve Damaged During Installation. Connections on All Subj Valves Replaced |
- on 860220,reactor Trip Occurred When Steam Generator Water Level Signal Drifted Closed.Caused by Broken Wire to Solenoid Valve Damaged During Installation. Connections on All Subj Valves Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1986-006-02, :on 860716,reactor Trip Occurred Due to Steam Generator 23 hi-hi Level.Caused by Equipment Malfunction & Personnel Error.Governor Actuator & Linkages for Steam Generator Feed Pump 21 Disassembled & Cleaned |
- on 860716,reactor Trip Occurred Due to Steam Generator 23 hi-hi Level.Caused by Equipment Malfunction & Personnel Error.Governor Actuator & Linkages for Steam Generator Feed Pump 21 Disassembled & Cleaned
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1986-007, :on 860408,discovered That Several motor-operated Valves Inside Containment Not in Compliance w/10CFR50.49 Due to T-drains Not Being Installed.Caused by Design Change Package Omissions |
- on 860408,discovered That Several motor-operated Valves Inside Containment Not in Compliance w/10CFR50.49 Due to T-drains Not Being Installed.Caused by Design Change Package Omissions
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000311/LER-1986-007-02, :on 860826,reactor Trip & Safety Injection Initiated by Spurious Actuation of Bistables & Contacts, Resulting from Voltage Spike on Vital Instrument Bus 2C, Resulting in Loss of Offsite Power |
- on 860826,reactor Trip & Safety Injection Initiated by Spurious Actuation of Bistables & Contacts, Resulting from Voltage Spike on Vital Instrument Bus 2C, Resulting in Loss of Offsite Power
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000000/LER-1986-008-02, :on 860917,equipment Hatch Discovered Open.Fire Watch Not Posted as Required by Tech Spec 3.7.11.a.Caused by Personnel Error.Roving Fire Watch Established & Personnel Counseled |
- on 860917,equipment Hatch Discovered Open.Fire Watch Not Posted as Required by Tech Spec 3.7.11.a.Caused by Personnel Error.Roving Fire Watch Established & Personnel Counseled
| | | 05000000/LER-1986-008-01, :on 860414,not All Required Valves Listed in Valve Position Verification Surveillances.Caused by Difference of Opinion Re Valves.Discrepancies Corrected |
- on 860414,not All Required Valves Listed in Valve Position Verification Surveillances.Caused by Difference of Opinion Re Valves.Discrepancies Corrected
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(1) | | 05000000/LER-1986-008, Forwards LER 86-008-00 | Forwards LER 86-008-00 | 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1986-009, :on 860911,reactor Trip Occurred.Caused by Isolation of Station Power Transformer 12 Due to Phase a & B Differential Relay Protection Operation.Required Insps Clarified & Expanded |
- on 860911,reactor Trip Occurred.Caused by Isolation of Station Power Transformer 12 Due to Phase a & B Differential Relay Protection Operation.Required Insps Clarified & Expanded
| | | 05000272/LER-1986-009, :on 860425,oxygen Content of Waste Gas Decay Tanks Exceeded Allowable Limits.Caused by Procedural Inadequacy.Operating Instructions OI-II-8.3.4 & OI-II-11.3.4 Revised |
- on 860425,oxygen Content of Waste Gas Decay Tanks Exceeded Allowable Limits.Caused by Procedural Inadequacy.Operating Instructions OI-II-8.3.4 & OI-II-11.3.4 Revised
| 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1986-009-02, :on 860911,during Routine Power Operation, Reactor Trip Occurred.Caused by Electrical Fault in 4,160/ 230-volt Transformer 2F.Transformer Replaced.Investigation Continuing |
- on 860911,during Routine Power Operation, Reactor Trip Occurred.Caused by Electrical Fault in 4,160/ 230-volt Transformer 2F.Transformer Replaced.Investigation Continuing
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1986-010-02, :on 861016,cable Tray Penetration Located in Wall Between Auxiliary Bldg Elevation & Switchgear Room Discovered Impaired.Cause Under Investigation.Roving Fire Watch Established & Personnel Counseled |
- on 861016,cable Tray Penetration Located in Wall Between Auxiliary Bldg Elevation & Switchgear Room Discovered Impaired.Cause Under Investigation.Roving Fire Watch Established & Personnel Counseled
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1986-010-01, :on 860512,turbine/reactor Trip from Approx 95% Power Occurred.Caused by Loss of Both Steam Generator Feedwater Pumps & Failure of Manual Restraining Device.Leads Removed |
- on 860512,turbine/reactor Trip from Approx 95% Power Occurred.Caused by Loss of Both Steam Generator Feedwater Pumps & Failure of Manual Restraining Device.Leads Removed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1986-011-02, :on 861117,Tech Spec 4.9.7 Re Fuel Handling Crane Overload Cutoff Not Performed within Required Time Period.Caused by Personnel error.Seven-day Insp Order Will Be Initiated When Crane in Use |
- on 861117,Tech Spec 4.9.7 Re Fuel Handling Crane Overload Cutoff Not Performed within Required Time Period.Caused by Personnel error.Seven-day Insp Order Will Be Initiated When Crane in Use
| 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1986-011-01, :on 860627,continuous Fire Watch Not Maintained for Inoperable Fire Door,Contrary to Tech Specs.Caused by Personnel Error.Hourly Fire Watch Posted & Info Directive AP-25 Will Be Issued |
- on 860627,continuous Fire Watch Not Maintained for Inoperable Fire Door,Contrary to Tech Specs.Caused by Personnel Error.Hourly Fire Watch Posted & Info Directive AP-25 Will Be Issued
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1986-012-02, :on 861121,valve 2PR25 in as Found Condition Exhibited Leak Rate Greater than Acceptable.Caused by Buildup of Small Amount of Boron Crystals on Valve Seat. Valve Cleaned & Retested Satisfactorily |
- on 861121,valve 2PR25 in as Found Condition Exhibited Leak Rate Greater than Acceptable.Caused by Buildup of Small Amount of Boron Crystals on Valve Seat. Valve Cleaned & Retested Satisfactorily
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1986-012-01, :on 860606,reactor Trip Initiated by Turbine Trip Due to Main Generator Protection Circuitry.Caused by Internal Fault in Auxiliary Power Transformer (Apt).Apt Removed & Repaired by Mfg |
- on 860606,reactor Trip Initiated by Turbine Trip Due to Main Generator Protection Circuitry.Caused by Internal Fault in Auxiliary Power Transformer (Apt).Apt Removed & Repaired by Mfg
| | | 05000311/LER-1986-013, :on 861223,while Removing Turbine Generator from Grid for Overspeed Testing,Reactor Trip Occurred When Mechanical Overspeed Trip Device Actuated Turbine Trip. Caused by Personnel Error |
- on 861223,while Removing Turbine Generator from Grid for Overspeed Testing,Reactor Trip Occurred When Mechanical Overspeed Trip Device Actuated Turbine Trip. Caused by Personnel Error
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1986-013-01, :on 860612,feedwater Heater Control Valve 13C Closed,Resulting in Loss of Feedwater Heater Train & Subsequent Tripping of Steam Generator Feedwater Pump 1. Caused by Personnel Error |
- on 860612,feedwater Heater Control Valve 13C Closed,Resulting in Loss of Feedwater Heater Train & Subsequent Tripping of Steam Generator Feedwater Pump 1. Caused by Personnel Error
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1986-013-02, :on 861223,turbine Reactor Trip Occurred When Steam Reset Interlock P-7 Causing Turbine Overspeed.Caused by Failure of electro-hydraulic Control Sys Circuit Cards. Cards Replaced & Sys Tested Satisfactorily |
- on 861223,turbine Reactor Trip Occurred When Steam Reset Interlock P-7 Causing Turbine Overspeed.Caused by Failure of electro-hydraulic Control Sys Circuit Cards. Cards Replaced & Sys Tested Satisfactorily
| 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1986-014-01, :on 860613,turbine/reactor Trip Occurred Due to Problem W/Svc Water Valve on Inservice Cooler.Caused by Inadequate Indication of Completely Full & Vented Cooler. Pressure Gauges Will Be Installed on Coolers |
- on 860613,turbine/reactor Trip Occurred Due to Problem W/Svc Water Valve on Inservice Cooler.Caused by Inadequate Indication of Completely Full & Vented Cooler. Pressure Gauges Will Be Installed on Coolers
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000311/LER-1986-014-02, :on 861228,control Room Console Alarm Received Due to Closure of Feed Regulating Valve for Steam Generator 23.Caused by Failure of Steam/Feed Mismatch Signal Summator. Signal Summator Replaced |
- on 861228,control Room Console Alarm Received Due to Closure of Feed Regulating Valve for Steam Generator 23.Caused by Failure of Steam/Feed Mismatch Signal Summator. Signal Summator Replaced
| 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1986-015-01, :on 860708,discovered That Raychem Splices W/Heat Shrinkable Incorrectly Installed on Transmitters,Per IE Info Notice 86-053.Caused by Misunderstanding of Environ Qualification Requirement |
- on 860708,discovered That Raychem Splices W/Heat Shrinkable Incorrectly Installed on Transmitters,Per IE Info Notice 86-053.Caused by Misunderstanding of Environ Qualification Requirement
| | | 05000272/LER-1986-016, :on 860805,steam Generator Feed Pump Tripped on Overspeed Trip.Caused by Failed Diode.Diode Replaced.All Four Steam Generator Feed Pump Electrical Control Panels Completely Refurbished |
- on 860805,steam Generator Feed Pump Tripped on Overspeed Trip.Caused by Failed Diode.Diode Replaced.All Four Steam Generator Feed Pump Electrical Control Panels Completely Refurbished
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1986-016-01, :on 860805 & 06,steam Generator Feed Pump 11 Tripped & Feed Flow/Steam Flow Mismatch Alarm Occurred, Respectively.Caused by Diode Failure & Accidental Grounding of Circuit.Diode Replaced.Wiring Relocated |
- on 860805 & 06,steam Generator Feed Pump 11 Tripped & Feed Flow/Steam Flow Mismatch Alarm Occurred, Respectively.Caused by Diode Failure & Accidental Grounding of Circuit.Diode Replaced.Wiring Relocated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000272/LER-1986-017, :on 860729,Fire Door C-8-1 Blocked Open for Maint of Component Cooling HX 11.Action Statement Not Issued.Caused by Error in Judgement Re Proper Classification of Fire Doors.Doors Will Be Clearly Marked |
- on 860729,Fire Door C-8-1 Blocked Open for Maint of Component Cooling HX 11.Action Statement Not Issued.Caused by Error in Judgement Re Proper Classification of Fire Doors.Doors Will Be Clearly Marked
| 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1986-017-01, :on 860729,Fire Door C-8-1 Blocked Open to Allow Maint on Component Cooling HX 11.Caused by Error in Judgement Re Proper Classification of Fire Door.Fire Doors Will Be Clearly Marked |
- on 860729,Fire Door C-8-1 Blocked Open to Allow Maint on Component Cooling HX 11.Caused by Error in Judgement Re Proper Classification of Fire Door.Fire Doors Will Be Clearly Marked
| | | 05000272/LER-1986-018-01, :on 860806,Limitorque Motor Valve Operators W/O Environ Qualified Wires Discovered.Caused by Insufficient Control of Wiring During Operator Assembly. Wiring Replaced.Stored Wires Will Be Inspected |
- on 860806,Limitorque Motor Valve Operators W/O Environ Qualified Wires Discovered.Caused by Insufficient Control of Wiring During Operator Assembly. Wiring Replaced.Stored Wires Will Be Inspected
| 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000272/LER-1986-019-01, :on 861001,two 2-inch Conduit Penetrations in Svc Water Intake Structure Fire Barrier Wall Discovered Improperly Sealed Per Tech Spec 3.7.11.Cause Undetermined. Penetration Sealed.Investigation Continuing |
- on 861001,two 2-inch Conduit Penetrations in Svc Water Intake Structure Fire Barrier Wall Discovered Improperly Sealed Per Tech Spec 3.7.11.Cause Undetermined. Penetration Sealed.Investigation Continuing
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000272/LER-1986-020-01, :on 861108,Tech Spec Surveillance 4.7.7.1.A Not Completed within Required Time.Caused by Personnel Error. Shift Supervisors Counseled Re Failure to Take Necessary Steps to Allow Performance of Surveillance |
- on 861108,Tech Spec Surveillance 4.7.7.1.A Not Completed within Required Time.Caused by Personnel Error. Shift Supervisors Counseled Re Failure to Take Necessary Steps to Allow Performance of Surveillance
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1986-021-01, :on 861112,discovered That Tech Spec Surveillance 4.3.3.9 for Quarterly Functional Test of Noble Gas Activity Monitor Not Performed within Required Time Frame.Caused by Personnel Error |
- on 861112,discovered That Tech Spec Surveillance 4.3.3.9 for Quarterly Functional Test of Noble Gas Activity Monitor Not Performed within Required Time Frame.Caused by Personnel Error
| 10 CFR 50.73(a)(2)(1) |
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