Similar Documents at Salem |
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Public Service Electric and Gas Company. P~O. Box 236 * -Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit FEB 14 1998 LR-N980081 u. 's.***:Nucle~r *Regulatory Commission Document Control Desk
, Was_hin.g~on, DC,2055.5 Geri t 1 ern'.en :.. * *
- LER 212/98~601-oo SALEM GENERATING STATION -
UNIT 1 FACILITY OPERATING LICENSE NO. DPR-70 DOCKET NO. 50-272
- submitted pursuant to the requirements of the Code of.Federal Regulations 10CFR50. 73 (a) (2) (i) (B).
Distribution LER File 3.7 9802250022 980216 PDR ADOCK 05000272 S
PDR
- The power is in your hands.
A. C. Bakken III General Manager -
Salem Operations I If 1111 lllll lllll f 1111[1111 Jlll/{11/ If II 95-2168 REV. 6/94
NRCFORM 366 U.S. NUCL REGULATORY COMMISSION APP OVED BY OMB NO. 3150-0104 EXPIRES 04/30/98.
(4-95). *.
ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS
~ \\ MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
LICENSEE EVENT REPORT (LER)..
REPORTED.LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY.
FORWARD
. COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 F3~,.U.S. NUCLEAR (See reverse for required number of REGULATORY COMMISSION, WASHINGTON, DC 2 55-0001, AND TO digits/characters for each block)
THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAllE (1)
DOCKET NUllBER (2)
PAGE (3)
SALEM GENERATING STATION UNIT 1 05000272 1 OF 5 TITLE (4)
Auxiliary Feedwate:i::- Pump Internal Flooding. Protection Installed Incorrectly.
EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
YEAR..I MONTH DAY FACILITY NAME.
DOCKET NUMBER MONTH DAY YEAR.
SEQUENTIAL I REVISION YEAR NUMBER NUMBER
.98 01 16 98
.001 00 02 16 98 FACILITY NAME DOCKET NUMBER OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Checkoneormore) (11)
MODE(9) 5 20.2201(b) 20.2203(a)(2)(v) x 50. 73( a)(2)(i)
- 50. 73(a)(2)(viii)
POWER 20.2203(a)(1) 20.2203(a)(3)(i)
- 50. 73(a)(2)(ii)
- 50. 73(a)(2)(x)
LEVEL (10) 0 20.2203(a)(2)(i) 20.2203(a)(3)(ii)
- 50. 73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)(4)
- 50. 73(a)(2)(iv)
OTHER 20.2203(a)(2)(iii) 50.36(c)(1)
- 50. 73(a)(2)(v)
Spec!iin Abstract below or in C Form 366A 20.2203(a)(2)(iv) 50.36(c)(2)
- 50. 73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (Include Area Code)
E. H. Villar (Station Licensing Engineer) 609 339 5456 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REP.ORT (13)
CAUSE
SYSTEM COMPONENT.
MANUFACTURER REPORTABLE I TONPRDS II
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR IYES x1NO SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE).
DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
During a System Readiness Review walkdown by the assigned System Manager, it was noted that the flood gate counter-weight in the pipe alley on elevation 84 foot of the Salem Unit 1 Auxiliary Building was not functioning properly.
At this time, an action request was written to correct this condition.
During the maintenance activity that followed from this request, it was discovered that the failure to function properly was the result of improper installation. The flood gate is a part of the protection against the postulated effects of pipe ruptures. In the event of a line break inside the pipe alley and flooding of the alley, the flood gate must function properly to protect the turbine-driven auxiliary feedwater pump from internal flooding. The exact cause of this occurrence cannot be determined.
The apparent cause of this condition was an installation error during initial construction.
The condition was corrected, and an action request was written to address this condition adverse to quality.
This Licensee Event Report (LER) is being made in accordance with 10 CFR 50.73 as a condition prohibited by Technical Specifications.
NRC FORM 366 (4-95)
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'\\. :i. U.S. NUCLEAR REGULATORY COMMISSION (4-95)
FACILITY NAME (1)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUMBER (2)
LER NUMBER (6) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM GENERATING STATION UNIT 1 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
PLANT. IDENTIFICATION:.. _;
Salem Generating Station-: Unit.1.
Public Service Electric and Gas*compariy Hancocks Bridge,*New Jersey* 08038 IDENTIFICATION OF OCCURRE.NCE:
98 001 00 "Auxiliary Feedwater Pump*Internal Flooding Protection Installed Incorrectly" Date of Occurrence:
Date of Identification Report Date:
.January 16, 1998 January 16, 1998 February 16,~1998 CONDITIONS PRIOR TO OCCURRENCE:
Salem Unit 1 - Mode 5 DESCRIPTION OF OCCURRENCE:
PAGE (3) 2 OF 5
During*a System Readiness Review walkdown by the assigned System Manager, it wai noted that the flood gate counter-weight in the pipe alley on elevation 84 foot of the Salem Unit 1 Auxiliary Building was not functioning properly.
At this time, an action request (AR) 971204233 was written to correct this condition~ During the maintenance activity that followed from this request, it was discovered that the failure to function properly was the result of improper installation.
AR 980116245 was written address this condition.
The flood g*ate counter-weight was oriented 180 degrees out of alignment (upside-down).
The flood gate is a part of the protection'against the postulated effects of pipe ruptures.
The pipe alley contains portions of both the high energy Chemical and Volume Control System (CVCS) letdown lines and the steam line to the auxiliary feedwater pump turbine.
The pipe alley is connected with the.turbine-driven auxiliary feedwater pump room.
In the event of a line break inside the pipe alley and flooding of the alley; the flood gate must function properly to protect the turbine-driven auxiliary feedwater pump from internal flooding.
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U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUMBER (2)
LER NUMBER (6) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM GENERATING STATION UNIT 1 98 001 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
DESCRIPTION OF OCCURRENCE (cont'd):
PAGE (3) 3 OF Technical Specification 3.7.1.2 requires that three auxiliary feedwater pumps be OPERABLE in Modes 1-3.
The "as found" physical configuration of the flood gate counter-weight indicated that this flood gate was unable to perform it5'iritended function, and the exact period of time that this*
condition existed cannot be determined.
Therefore, PSE&G concluded that Salem Unit 1 was operated in Modes 1 through 3 with the flood gate inoperable.
Based:on the above, this condition is reportable as a condition prohib~.ted by the Planes Technical Specifications per 10 CFR so.73 (a) (2) (i) (bl.
CAUSE OF OCCURRENCE:
The exact cause of this occurrence cannot be determined.
The apparent cause of this condition is believed to be an installation error during initial construction.
Because the flood gate does not have a component
. identifier, it.is not possible to develop a maintenance history or determine how it occurred.
PRIOR SIMILAR OCCURRENCES:
A search of the LER database using the phrases "flood gate" and "counter-weight" did not identify any LERs within the past two years related to mispositioned flood gate counter-weight.
SAFETY CONSEQUENCES AND IMPLICATIONS
5 Although the flood gate counter-weight was oriented 180 degrees out of alignment (upside-down), the turbine-driven auxiliary feedwater pump was never chailenged from a line break and flooding of the pipe alley during this period.
Therefore, there were no safety consequences associated with this event.
Technical Specification allows only 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> of power operations with one inoperable pump and allows no power operation with two pumps inoperable.
The discussion below will show that within reasonable engineering judgment one motor driven pump would have been available to meet the Salem design basis, and demonstrate that the safety consequences and implications associated with this event were minimal.
- ::.~
)' (4-95)
U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUMBER (2)
LER NUMBER (6) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM GENERATING STATION UNIT 1 98 001 00 TEXT (If more space is required, use additional copies of NRC Form ~66A) (17)
SAFETY CONSEQUENCES AND IMPLICATIONS (cont'd):
PAGE (3) 4 OF. 5 Salem has a desi~n complement of one turbine-driven auxiliary feedwater pump (located in its own enclosure) and two motor driven pumps.
The two motor driven pumps are located in an adjacent open area on pedestals*.
approximately 6 inches above the floor.
The Salem design bas.i:s requires one motor driven pump to be available to supply two steam generators.
Drains installed in this area, as well as the openness of the area, further reduces the possibility of flooding.
Overpressurization of the pipe alley is prevented by venting the compartment through the mechanical penetration through a vent penthouse to the atmosphere.
Drains are also installed to minimize the potential for flooding.
Features designed to minimize (if not eliminate) a high energy pipe break in the alley are described in the Salem UFSAR.
Specifically, Sections 3.6.5.4 and 3.5.5.6 describe the results of postulated break of the letdown line of the eves (300psig/300 deg F) and the steam supply to the turbine driven auxiliary feedwater pump (790psig saturated steam).
The letdown line portion of the eves is constructed of Nuclear Class 2, Seismic II standards from ASTM-A312 TP-304 steel pipe.
Postulated break locations have been sl~eved and restrained to minimize the mass flow rate and preclude damage from pipe whip events.
These design features in conjunction with the venting of the pipe alley show that a postulated break would not affect any safety related equipment.
Similarly, the steam lines to the turbine-driven pump have been sleeved and restrained.
The design criteria associated with these sleeves is also described in the.Salem UFSAR, and is based on ASME Section III, Nuclear Power Plant* Components Code, for Class 2 Components, and the applicable revision of the ANSI Standard Code for Pressure Piping, ANSI B31.l.
The analysis concluded that the only anticipated consequence of the rupture of the steam supply to the turbine driven pump (larger pipe) is the loss of the turbine driven pump.
Note that this brea*k is assumed in the pump enclosure area itself, where the flood gate counter-weight mispositioning would not be a factor.
Therefore, as a result of the physical location of the pumps, as well as the design features associated with these high energy lines, it is within reasonable engineering judgment to expect that the motor driven pumps would have been unaffected by a high energy pipe break and flooding of the pipe alley, and at least one pump would have been available (assuming one motor driven* pump inoperable).
\\,\\.
- U.S. NUCLEAR REGULATORY COMMISSION (4-95)
FACILITY NAME (1)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION DOCKET NUMBER (2)
LER NUMBER (6) 05000272 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER SALEM GENERATING STATION UNIT 1 98 001 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
SAFETY CONSEQUENCES AND IMPLICATIONS (cont'd):
PAGE (3) 5 OF 5
However, notwithstanding the above discussion, the limiting case scenario of this condition is the*total loss of auxiliary feedwater to the steam generators.*.,Al though a* highly. unlikely event, as described above, control room licensed operators are trained and written instructions are provided (in the_ fo*:rm of_ Em.ergency Operating procedures) to mitigate the consequences of this event.
The Emergency Operating Procedures provide direction for identification and isolation of the break, as well as restoration of heat sink.
CORRECTIVE ACTIONS TAKEN:
- 1. The pipe alley flood gate counter-weight was properly positioned on January 24, 1998 via work-order *9712b4233.
- 2. The Salem Unit 2 flood gate counter-weight was verified to be in the proper position.
- 3. A preventive maintenance recurring.task for these flood gates will be evaluated.
This evaluation will be completed by March 31, 1998.
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| 05000272/LER-1998-001, :on 980116,AFP Internal Flooding Protection Was Installed Incorrectly.Caused by Installation Error During Construction.Pipe Alley Flood Gate counter-weight Was Properly Positioned on 980124 |
- on 980116,AFP Internal Flooding Protection Was Installed Incorrectly.Caused by Installation Error During Construction.Pipe Alley Flood Gate counter-weight Was Properly Positioned on 980124
| | | 05000311/LER-1998-001-01, :on 970705,failed to Meet TS 3.3.3.7 Table 3.3-11 Item 19 -RVLIS.Caused by Test Equipment Had Not Been Evaluated for Effect on Sys Operability.Installation of Isolators Has Been Included in Rev 5 |
- on 970705,failed to Meet TS 3.3.3.7 Table 3.3-11 Item 19 -RVLIS.Caused by Test Equipment Had Not Been Evaluated for Effect on Sys Operability.Installation of Isolators Has Been Included in Rev 5
| | | 05000311/LER-1998-002-01, :on 980129,23 Overtemperature Delta Temperature Channel Found Inoperable.Cause of Event Being Attributed to Human Error.Lead & Lag Switches Were Restored to Correct Positions |
- on 980129,23 Overtemperature Delta Temperature Channel Found Inoperable.Cause of Event Being Attributed to Human Error.Lead & Lag Switches Were Restored to Correct Positions
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-002, :on 971217,auxiliary Building Ventilation (Abv) Excess Flow Damper Was Found Wired Open W/Spring Removed. Caused by Personnel Error.Repaired 1ABS8 Damper & Inspected Other Abv Excess Flow Dampers in Abv Sys |
- on 971217,auxiliary Building Ventilation (Abv) Excess Flow Damper Was Found Wired Open W/Spring Removed. Caused by Personnel Error.Repaired 1ABS8 Damper & Inspected Other Abv Excess Flow Dampers in Abv Sys
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-003-02, :on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged |
- on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-003, Forwards LER 98-003-00 Re Inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2,SG | Forwards LER 98-003-00 Re Inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2,SG | | | 05000272/LER-1998-003, :on 980216,inadequate Surveillance Testing of FW Isolation & P-10 SR Block Was Noted.Caused by Inadequate Development of Original Surveillance Tps for Ssps Logic Testing.Revised Ssps Logic Functional Tps |
- on 980216,inadequate Surveillance Testing of FW Isolation & P-10 SR Block Was Noted.Caused by Inadequate Development of Original Surveillance Tps for Ssps Logic Testing.Revised Ssps Logic Functional Tps
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1998-004, :on 980204,failure to Comply W/Ts SR 4.1.3.1.1 Was Noted.Caused by Human Error.Review of Both Units 1 & 2 P250 Computer Points Was Conducted |
- on 980204,failure to Comply W/Ts SR 4.1.3.1.1 Was Noted.Caused by Human Error.Review of Both Units 1 & 2 P250 Computer Points Was Conducted
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-004, Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences | Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences | | | 05000272/LER-1998-004-01, :on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety Factors |
- on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety Factors
| 10 CFR 50.73(a)(2) | | 05000272/LER-1998-005-01, :on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP |
- on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1998-005, :on 980211,failure of 2A EDG Turbocharger Was Noted.Caused by Failure of Blade on Turbochargers Rotating Turbine Disc.Damaged Turbocharger on 2A EDG Was Replaced W/ Refurbished Turbocharger |
- on 980211,failure of 2A EDG Turbocharger Was Noted.Caused by Failure of Blade on Turbochargers Rotating Turbine Disc.Damaged Turbocharger on 2A EDG Was Replaced W/ Refurbished Turbocharger
| 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-005, Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs | Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs | 10 CFR 50.73(a)(2) | | 05000311/LER-1998-006-01, :on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure Transmitters |
- on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure Transmitters
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-006, :on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water Levels |
- on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water Levels
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-006, :on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database Info |
- on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database Info
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000272/LER-1998-007, :on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves Identified |
- on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves Identified
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000311/LER-1998-007, :on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With |
- on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000311/LER-1998-007-01, :on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected Tubing |
- on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected Tubing
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-008, :on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected |
- on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected
| 10 CFR 50.73(a)(2) | | 05000311/LER-1998-008-01, :on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised Procedure |
- on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised Procedure
| 10 CFR 50.73(a)(2)(i) | | 05000272/LER-1998-009, :on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was Performed |
- on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was Performed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000311/LER-1998-009-01, :on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke Detectors |
- on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke Detectors
| | | 05000272/LER-1998-010, :on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2 |
- on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000311/LER-1998-010-01, :on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve Repaired |
- on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve Repaired
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-011, :on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative Hold |
- on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative Hold
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) | | 05000311/LER-1998-011-01, :on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised Procedure |
- on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised Procedure
| | | 05000272/LER-1998-012, :on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been Revised |
- on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been Revised
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000311/LER-1998-012, :on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With |
- on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With
| 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1998-012-01, :on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to Svc |
- on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to Svc
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2)(1) | | 05000311/LER-1998-013-01, :on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With |
- on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000272/LER-1998-013, :on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With |
- on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With
| 10 CFR 50.73(a)(2)(i) | | 05000311/LER-1998-014, :on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With |
- on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With
| | | 05000272/LER-1998-014-01, :on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With |
- on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000311/LER-1998-015-01, :on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With |
- on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000272/LER-1998-015, Responds to NRC Re Violations Noted in Insp Repts 50-272/98-12 & 50-311/98-12.Corrective Actions:Discussions with NRC Senior Resident Inspector for Salem Indicated Encl LER 98-015-00 Responsive to NOV | Responds to NRC Re Violations Noted in Insp Repts 50-272/98-12 & 50-311/98-12.Corrective Actions:Discussions with NRC Senior Resident Inspector for Salem Indicated Encl LER 98-015-00 Responsive to NOV | | | 05000311/LER-1998-016, :on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With |
- on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition |
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