ML20065R331

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Monthly Operating Rept for Nov 1990 for Callaway Unit 1.W/
ML20065R331
Person / Time
Site: Callaway Ameren icon.png
Issue date: 11/30/1990
From: Blosser J, Mccann R
UNION ELECTRIC CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
ULNRC-2336, NUDOCS 9012190018
Download: ML20065R331 (6)


Text

.. UNION ELECTRIC COMPANY Calicway Plant December 6, 1990 Nuclear Regulatory Commission Document Control Dent Washington, DC 20555 ULNRC- 2 336

Dear Sir:

DOCKET NUMBER 50-483 CALLAPAY PLANT UNIT 1 FACILITY OPERATING LICENSE NPF-30

!!ONTHLY OPERATING REPORT

. NOVD!PER 1990 The enclosed Monthly Operating Report for November, 1990 is submitted pursuant to ocction 6.9.1.8 of the Callaway Unit 1 Technical Specifications, wLe J. D. B]oeser 4 Manager, Callaway Plant hI, \M '/h @

JDB/DEYTRDA/ 'AM/RJM/ crc Enclosure ec: Distribution attached 9012190018 901130 PDR ADOCK 05000483 R PDR f/

Mohng Address RO. Box 620 Fulton.MO65251 18:;02 a J li

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cc distribution for.ULNRC-2336 with enclosurec Mr. Richard Hague, Chief Project Section 1A U. S. Nuclear-Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Mr. Anthony Gody, Jr. (?. coples) 7 Office of Nuclear Reactor Regulation U.-S. Nuclear Regulatory Connieofon Mail Stop P-316 7920 Norfolk Avenue Bethesda, MD 20014 NRC Renident Inspector Manager, Elcetric Department Missouri Public Service Commission  ;

P. O. Box'360.

Jefferson City,-MO 65102 V , . -. . ,. . . - , - . . . . . -- .- - . - - .

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DOCKET NO. 50-483 UNIT NAIJ. . CAllAWAY UNIT 1 f DATE 12*6 90 00FfPLETED PY. - R, J. McCant TELEPIIONT. . -314/676 0243 PART A OPERATIONS SUbNARY h plant returned to.approxinately 100% power following Refuel 4 The followler events took' place On 11/15/90 refuelinr, outage nalntenance activities pr<d startup pny.'ics testing were conpleted.

On'11/15/90 while warmire the' main. turbine prior to synchrontration, main tut?ine bearing e3 failed. A stator cooling coil leak on the generetor output bushing was subsequently identitled as needing repair also. The rain generotcr won synchrontred to the grid on 11/19/90.  !

'On 11/20/90 a main turbine-overspeed test was conducted at 10% power.

On 11/24/90 a turbine trip /recctor trip occurred while performing a plant shutdown due to high sulfatos in the reactor coolant system. '1he turbine trip was caused by a falso HSR high level trip logic

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circuit which subseqently. caused the reactor to trip on low-low S/C level. The unit was returned to

' service on~11/25/90.- 7 PART B uPORY AND SAFETY. VALVE S11 NARY o

.During the. turbine /rcactor trip _ transient on 11/24/90, pressurizer PORY - BBFCV0455A + momentarily itfted and then rescated.-

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$ 4 Port C AVERACE DATLY UNIT POER 1.EVEL DOCDT NO. 50-483 UNIT NAME CALLAWAY UNIT 1 DATE 32-(-90 COMPLETED BY R. J. McCane TELEPHohE 314/676-8243 Mot'lli t l'0VDCER 1990 AVERACE DAILY POVER LEVEL AVERACE DAILY POWER LEVEL DAY (MWe-Net) DAY OMe Net) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 185 5 0 21 281 6 0 22 457 7 0 23 570 8 0 24 0 9 0 25 9 10 0 26 438 11 0 27 647 12 0 28 1099 23 0 29 1166 14 0 30 1170 15 0 16 0 Page 2 of 4

  • , 6 Part D
  • OPERATJ C DATA LEPORT DOCKET NO. 50-483 UNIT NAME CALLAk'AY l'!!IT 1 DATE 12 6-90 COMPLETED BY R. J. McConn TELEPil0NE 314/676 6243 OPEkATING STA'ITS MI) CI'P )

1 REPORTINC PERIOD: NOVEt1LL 1990 GROSS HOURS IN REPORTING FERIOD: 720 B,016 f2,117.5 2 CITJ1L*nY AU'I110RIZED POWER LEVEL OtWt): 35f5 PAX, DEPEND. CAPACITY U Ue !et): 1125 DESIGN ELECTP.ICAL RATING (FMe-Net): 1171

3. Pok'ER LEV 1170 WICII hESTRICTED (IF ANY) ONe-het):

4 REASONS FOR RESTRICTION (IF ANY):

T1115 MONTil YR TO DATE CUMULATIVE

5. hu1EER OF 1100RS RFACTOR k'AS CRITICAL . . . . . . . . . . . . . . . 400.6 6,630.6 44,611.0
6. REACTOR RESERVE SIIUTDOW llCl'RF . . . . . . . . . . . . . . . . . . . . . 0 0 0
7. IlCURS CE!ERATOR ON LINE . . . . . . . . . . . . . . . . . . . . . . . . . . . . 223.4 6,438.5 43,392.9
8. UNIT RESERVL SilUTDOW ll01'RS . . . . . . . . . . . . . . . . . . . . . . . . 0 0 0 9 CROSS TiiERHAL ENERGY CENERATED (MWH) ............... 481,701 21,895,924 343,330,347 10 GROSS l'LECTRICAI FNERCY GENERATED ONil) . . . . . . . . . . . . 157,500 7,529,693 48,734,549
11. NET ELECTRICAL ENEPCY CENERATED O Nil) .............. 130,339 7,158,393 46,253,514 12 REACTOR SERVICE FACIOR ............................. 55.6 82.7 85.6
23. REACTOR AVAILABILITY FACTOR . . . . . . . . . . . . . . . . . . . . . . . . 55.6 62.7 85.6
14. UNU SERVICE FACTOR ................................ 31.0 80.3 83.3
15. UNIT AVAILABILITY FACTOR ........................... 31.0 80.3 83.3
16. UNIT CAPACITY FACTOR (UsirE MDC) ................... 10.1 79.4 78.9 17 ' UNIT CAPACITY FACTOR (Using Design FNe) ............ 15.5 76.3 75.8
18. UNIT FORCED OUTAGE RATE ..................... ...... 39.4 3.67 3.48 19 SilUIDOWNS SCllEDULED OVER NEXT 6 MONTHS (TYPE, DATE, ANT DLRATION OF EACll):
20. IF SimT DOW AT FND OF REPORTING PERIOD, E5TIttATED DATE OF STARTUP l l' age 3 of 4 l

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ETH SHL"IIG;NS AND POkIR REDUCIIOf;S IWTTT NO. 50-483 ,

Utill IME Call >VAY iTIT I DATE 12-6-90 COMPLETFP ET R. J. Sccann i

TELEPHCtNE 314/674-6242 REIv]RT MONTH: NOVDSER 1%O METHOD OF TITE SIRTIING DO'.;N F: FORCED DURATION TEE REACTf R CR DATE S: SOiDULED G!OURS) TFASCO REDUCING PObTR Cr??FCTIVE ACTIONS /CO'^'BTS

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12 9/21/90 S 350.0 C 1 On 11/15/90 refueling cutage maintenance activitics cr<' rtartup physics testing were co pleted.

13 11/15/90 F 104.1 A 4 On 11/15/90 dile vareing the main turb!re prior to synchronization, rein tutire tearing e3 failed. A stater cooling coil leak on the generator output 1-ush!ng vss subsaquently identified as needing repair also. H e esfr generator was synchrenized to the grid on 11/19/90.

14 13-10/90 S 1.2 B 4 Cn 11/20/00, a main turtire overspeed test was conducted at IfA pcuer.

15 11/24/90 F 41.3 A 3 On 11/2!.!90 a turbine trip / reactor trip eccurred stile performing a plant shuttec due to high sulfates in the reactor cociant system.

The turbine trJp was caused ty false MSR high level trip Irgic circuit which rutsequently caused the reacter to trip en Icv-Icv S/G 1evel.

The unit was retur-ed te service en 11/25/90 SD M.RY:

REASOf: FETHOD A: Erf!IPMENT FAILURE (EXFLAIN) 1: MANUAL B: MAlf.T. CR TFST 2: "ANUAL SCRJLv  !

C: REFUELING 3: AGl*'ATIC SCRAM D: REGULATORY TESTT3CTION 4: OTHER (EXPLAIf)

E: OPERATOR TRAINIEG /13 LICENSE EXAMIf:ATTF F: AD"INISTRATIVE G: OPERATIMAL ERRCR (EXPLAIN)

H- OUTR (EMAIN)

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