ML20246P945

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Notice of Violation from Insp on 890327-31.Violation Noted: Containment Sump Recirculation Valve Backup Air Supply Accumulators Not Designed or Tested to Ensure Proper Sys Operation for All Postulated Conditions
ML20246P945
Person / Time
Site: Waterford Entergy icon.png
Issue date: 05/10/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20246P933 List:
References
50-382-89-11, NUDOCS 8905220315
Download: ML20246P945 (1)


Text

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APPENDIX A NOTICE OF VIOLATION Louisiana Power & Light Company (LP&L) Docket: 50-382 Waterford Steam Electric Station, Unit 3 (W-3) Operating License: NFF-38 During an NRC inspection conducted on March 27-31, 1989, a violation of NRC requirements was identified. The violation involved failure to provide adequate design controls. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1988),

the violation is listed below:

Inadequate Design Control Criterion III of Appendix B to 10 CFR Part 50 states, in part " Measures shall be established to assure that applicable regulatory requirements and

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the design basis, as defined in 10 CFR 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies are correctly translated into specifications, drawings, procedures, and instructions. . . . The design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. . . ." This is implemented by the licensee's approved Quality Assurance Plan.

l l Contrary to the above, the following examples of the failure to control l the facility design adequately were identified:

1. Containment sump recirculation valves' backup air supply accumulators were not designed or tested to ensure proper system operation for all conditions postulated by the design basis.
2. Static uninterruptible power Supply 3A-S was modified by the addition of a nonsafety-related load to the distribution panel without accounting for the effects of load faults on the inverter operation.

These examples are a Severity Level IV violation. (Supplements)(382/8911-01)

]

Pursuant to the provisions of 10 CFR 2.201, Louisiana Power & Light Company is hereby required to submit to this office, within 30 days of the date of the letter transmitting this Notice, a written statement or explanation in reply, including for each violation: (1) the reason for the violation if admitted,  ;

2) the corrective steps which have been taken and the results achieved,
3) the corrective steps which will be taken to avoid further violations, and
4) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending the response time.

l Dated at Arlington, Texas, this /0 & day of 1 72 1989 890522031G 890510 PDR ADOCK 0500038'2 Q PDC

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