ML20058E625

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Notice of Violation from Insp on 930919-1030.Violation Noted:On 930817,Valve CMU-1131 Was Opened & Left in Open Position Until 931019
ML20058E625
Person / Time
Site: Waterford Entergy icon.png
Issue date: 11/29/1993
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20058E621 List:
References
50-382-93-32, NUDOCS 9312070082
Download: ML20058E625 (2)


Text

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APPENDIX A NOTICE OF VIOLATION i

i Entergy Operations, Incorporated Docket No.:

50-382 i

Waterford Steam Electric Station, Unit 3 Operating License No.: NPF-38 l

l During an NRC inspection nducted on September 19 through October 30, 1993, l

one violation of NRC requi ements was identified.

In accordance with the i

" General Statement of Policy and Procedure for NRC Enforcement Actions,"

10 CFR Part 2, Appendix C, the violation is listed below.

l A.

Technical Specification 6.8.1 requires, in part, that written procedures be established, implemented, and maintained covering the activities j

i referenced in Appendix A of Regulatory Guide 1.33, Revision 2, j

February 1978.

j Section 1 of Appendix A of Regulatory Guide 1.33 requires safety-related activities to be covered by written procedures, which includes maintenance of the ultimate heat sink.

j System Operation Procedure OP-003-004, Revision 6, " Condensate Makeup,"-

i requires that the recirculation header isolation valve, CMU-1131, be l

closed after transferring water from the demineralized water storage i

tank to the condensate storage tank.

l Contrary to the above, on August 17, 1993, Valve CMU-1131 was opened and I

left in the open position until October 19, 1993. As a result of this j

misalignment, the automatic makeup system for the safety-related wet cooling tower basins did not function as designed, allowing the level of the basins to decrease to a point below the Technical Specification required minimum level.

i i

This is a Severity Level IV violation.

(Supplement I) (382/93-32-01)

Pursuant to the provisions of 10 CFR 2.201, Entergy Operations, Inc. is hereby l

required to submit a written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555 with a copy to the Regional Administrator, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011, and a copy to the NRC Resident Inspector, within 30 days of the date of the letter transmitting this Notice of Violation l

(Notice). This reply should be clearly marked as a " Reply to a Notice of Violation" and should include for each violation:

(1) the reason for the violation, or, if contested, the basis for disputing the violation, (2) the l

corrective steps that have been taken and the results achieved, (3) the

(

corrective steps that will be taken to avoid further violations, and (4) the date when full compliance will be achieved.

If an adequate reply is not 1

received within the time specified in this Notice, an order may be issued to l

show cause why the license should not be modified, suspended, or revoked, or l

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9312070082 931129 PDR ADOCK 050003B2 O

PDR_

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l 1 l why such other action as may be proper should not be taken. Where good cause is shown, consideration will be given to extending the response time.

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Dated at Arl'ngton, Texas, dayoff 1993 l

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