ML20134K778

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Notice of Violation from Insp on 961021-25.Violations Noted:Licensee Failed to Verify Operational Readiness of Valves Whose Function Required for Safety IAW Section 11 of ASME Boiler & Pressure Vessel Code
ML20134K778
Person / Time
Site: Waterford Entergy icon.png
Issue date: 11/13/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20134K762 List:
References
50-382-96-24, NUDOCS 9611200025
Download: ML20134K778 (2)


Text

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I ENCLOSURE 1 NOTICE OF VIOLATION Entergy Operations, Inc. Docket No.: 50-382 Waterford Steam Electric Station, Unit 3 License No.: NPF-38 l During an NRC inspection conducted on October 21-25,1996, two violations of NRC requirements were identified in accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," NUREG-1600, the violations are listed below:

A. 10 CFR Part 50, Appendix 8, Criterion XVI, requires, in part, that conditions adverse to quality be promptly identified and corrected.

Procedure OP-901-511," Instrument Air Malfunction," Attachment 5, Note 1, required that accumulators for Valves CC-135A(B), Dry Cooling Tower A(B) inlet isolation valve, have pre-staged motive cylinders (nitrogen bottle) to allow a backup air source to be connected to the accumulators on a loss of instrument air.

Contrary to the above, conditions adverse to quality were not promptly identified and corrected in that:

1. As of October 22,1996, the licensee failed to determine all of the potential water usage sources from the condensate storage pool following a design basis tornado event, as required by Condition Report 96-0086, dated l January 22,1996.
2. From October 14-21,1996, the licensee did not implement immediate corrective actions specified in Condition Report 96-1630 by prestaging a nitrogen cylinder for Valve CC-135B, as required in Procedure OP-901-511.

This is a Severity Level IV violation (Supplement 1) (50-382/9624-01).

! i B. 10 CFR 50.55a(g) requires, in part, that inservice testing to verify operational readiness of pumps and valves whose function is required for safety be accomplished in accordance with Section XI of the ASME Boiler and Pressure i Vessel Code.

l Section XI, " Rules for Inservice inspection of Nuclear Power Plant Components," i Subsection IWV-1100, includes within the scope of inservice testing, Class 1,2,  ;

and 3 valves (and their actuating and position indicating systems), that are required to perform a specific function in shutting down the reactor or in mitigating the consequences of an accident.

Contrary to the above, as of October 22,1996, the licensee failed to verify the operational readiness of valves whose function is required for safety in accordance with Section XI of the ASME Boiler and Pressure Vessel Code. Specifically, the

! licensee failed to perform testing that ensured operational readiness of the j safety-related air accumulators of ASME Class 3 valves.

This is a Severity Level IV violation (Supplement I) (50-382/9624-02).

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9611200025 961113 PDR ADOCK 05000382 l, G PDR

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' Pursuant to the provisions of 10 CFR 2.201, Entergy Operations, Inc. is hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory Commission, i ATTN: Document Control Desk, Washington, D.C. 20555 with a cor y to the Regional i Administrator, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011, and a i copy to the NRC Resident inspector at the facility that is the subject of this Notice, within ,

30 days of the date of the letter transmitting this Notice of Violation (Notice). This reply  ;

should be clearly marked as a " Reply to a Notice of Violation" and should include for each  !

violation: (1) the reason for the violation, or, if contested, the basis for disputing the  !

violation, (2) the corrective steps that have been taken and the results achieved, (3) the  !

corrective steps that will be taken to avoid further violations, and (4) the date when full {

compliance will be achieved. Your response may reference or include previous docketed  ;

correspondence, if the correspondence adequately addresses the required response. If an +

adequate reply is not received within the time specified in this Notice, an order or a  !

Demand for information may be issued as to why the license should not be modified,  ;

suspended, or revoked, or why such other action as may be proper should not be taken.

Where good cause is shown, consideration will be given to extending the response time, i Because your response will be placed in the NRC Pubhc Dacument Room (PDR), to the y extent possible, it should not include any personal privacy, proprietary, or safeguards  ;

information so that it can be placed in the PDR without redaction. However, if you find it j necessary to include such information, you should clearly indicate the specific information )

that you desire not to be placed in the PDR, and provide the legal basis to support your l request for withholding the information from the public.

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l Dated at Arlington, Texas this 13th day of November 1996

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