ML20027B273

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LER 82-089/03L-0:on 820815,reactor Core Isolation Cooling Turbine Tripped on Overspeed During STP 14,Step 10.2.F Vessel Injection Cold Quick Start Test.Caused by Turbine Governor Valve Binding Due to Problem in Mechanical Section
ML20027B273
Person / Time
Site: LaSalle Constellation icon.png
Issue date: 09/13/1982
From: Houston R
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20027B252 List:
References
1-1-82-186, LER-82-089-03L, LER-82-89-3L, NUDOCS 8209160599
Download: ML20027B273 (2)


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1. LER NUMBER: 1-82-089/03L-0
11. LASALLE. COUNTY STATION: UNIT 1 111. DOCKET NUMBER: 050-373 IV. EVENT DESCRIPTION:

On August 15, 1982 at 5:37 p.m. the Reactor Core isolation Cooling turbine tripped on overspeed during the performance of Start-Up Test 14 step 10.2.F, Vessel Injection Cold Quick Start Test. This was a level I acceptance criteria.

V. PROBABLE CONSEQUENCES OF THE OCCURRENCE:

At the time of the occurrence Unit I was in the run mode at approximately 300 MWT., rated pressure and temperature. All ECCS Systems were operable. Had a high pressure injection system been needed for emergency core cooling, the High Pressure Core Spray would have ini tiated. Safe plant operation was main-tained at all times. The RCIC Turbine was manufactured by Terry Steam Turbine Co.

VI. CAUSE:

Analysis of General Electric Startrec. Traces monitoring the RCIC System indicated that the turbine governor valve was binding while traveling to the closed position in its unsuccessful attempt to control turbine speed.

The startree traces indicated that the problem originated in the mechanical section of the governor system and that the electronic governor section had operated properly.

Vll. CORRECTIVE ACTION:

A work request was ini tiated to inspect the mechanical linkages of the RCIC governor valve. These linkages were disassambled to check for abnormal wear and binding. Slight indication of binding and wear were found and the linkages were reassembled and adjusted to vendor recommended tolerances.

The RCIC system was subsequently manually ini tiated to pump to and from the condensate storage tank. Governor valve response proved to be satisfactory during this test loop run.

Prepared by: R. W. Houston m----~ -e a- w mi -- -M