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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D0201994-04-25025 April 1994 LER 94-007-01:on 931014,high Head Safety Injection Flow Balance Testing Found to Be Below TS Requirement.Caused by Unaccounted for Uncertainties.Cold Leg Safety Injection Leg Throttle Valve adjusted.W/940425 Ltr ML20045G9391993-07-0808 July 1993 Lr 93-017-00:on 930616,containment Hydrogen Analyzer Heat Trace Channel Calibration Not Performed on Staggered Test Basis Due to Inadequate Implementation of TS Amend.Test Procedure Satisfactorily performed.W/930708 Ltr ML20044H1591993-05-27027 May 1993 LER 93-016-00:on 930509,discovered That Containment Hydrogen Analyzer Pressure Switch PS-3 Sensing Line Disconnected in Local Panel.Caused by Personnel Error. Pressure Switch Calibr & Line reconnected.W/930527 Ltr ML20044D5711993-05-14014 May 1993 LER 93-002-00:on 930416,automatic Reactor Trip Initiated from Turbine Trip Due to Over Excitation of Main Generator. Emergency Procedure 2-E-0 Entered & Individuals Involved in Event Received Remediated training.W/930514 Ltr ML20044D2281993-05-12012 May 1993 LER 93-003-00:on 930424,manual Reactor Trip Initiated Due to Erratic Feedwater Flow Indications to SG C & Excessive Main Feedwater Regulating Valve Oscillations.Caused by Design Instabilities.Secondary Sys secured.W/930512 Ltr ML20044C9541993-05-0707 May 1993 LER 93-015-00:on 930427,discovered That Portions of Containment Pressure Channels That Input to Containment Spray hi-hi Pressure Not Tested Monthly.Caused by Personnel Error.Test Procedures changed.W/930507 Ltr ML20044C9811993-05-0606 May 1993 LER 93-014-00:on 930411,as-found Speed Setting of Steam Driven AFW Pump 1-FW-P-2 Found Below Required TS Limit. Caused by Incorrect Speed Control Setting.Pump Speed Adjusted & Maint Personnel counseled.W/930506 Ltr ML20024G6841991-04-18018 April 1991 LER 91-006-00:on 910403,discovered That Ac Offsite Power Source Surveillance Not Performed Due to Personnel Error. Surveillance Initiated Immediately & Positive Discipline Administered to supervisor.W/910418 Ltr ML20029B5601991-03-0606 March 1991 LER 91-005-00:on 910209,containment Building Penetrations Breached.Caused by Inadequate Procedural Controls.Core Mapping & Cavity Pump Down Activities Secured,Air Hose Removed & Hydrolase Hose capped.W/910306 Ltr ML20029A6471991-02-22022 February 1991 LER 91-004-00:on 910206,sealed Radioactive Source in Storage Not Leak Tested Prior to Use.Caused by Inadequate Procedures for Verifying Leak Testing of Sources.Procedures Revised.W/ 910222 Ltr ML20028H6681991-01-18018 January 1991 LER 90-009-01:on 900719,discovered That Response Time Testing of Pressurizer High Level Reactor Trip Function Not Performed in Accordance W/Tech Spec 3.3.1.1,Table 3.3-2. Caused by Personnel Error.Procedures revised.W/910118 Ltr ML20043H8321990-06-22022 June 1990 LER 90-007-00:on 900523,discovered That Two Sets of Concrete Roof Blocks on Svc Water Pump House Not in Required Safety Position.Caused by Lack of Administrative Controls.Blocks Restored to Required locations.W/900622 Ltr ML20043D5801990-06-0404 June 1990 LER 90-006-00:on 900504,casing Cooling Pump Not Put Into Alert Status & Surveillance Missed.Caused by Personnel Error.Pump 1-RS-P-3B Placed in Alert status.W/900604 Ltr ML20012E3301990-03-27027 March 1990 LER 90-003-00:on 900228,52 Valves Identified Not Included in Tech Spec Required Monthly Containment Integrity Verification Surveillance Program.Caused by Personnel Error & Inadequate Procedure.Procedure revised.W/900327 Ltr ML20012B6441990-03-0808 March 1990 LER 90-001-00:on 900215,inadvertent Partial Train a ESF Actuation of Containment Depressurization Sys Occurred. Caused by Human Error.Evaluation to Be Performed to Determine If Test Points Can Be moved.W/900308 Ltr ML20006E2371990-02-0808 February 1990 LER 90-001-00:on 900123,reactor Trip Occurred on Steam Feedwater Flow Mismatch.Caused by Failed Circuit Driver Card on Feedwater Regulating Valve.Feedwater Regulating Valve Driver Card replaced.W/900208 Ltr ML20006E3771990-02-0505 February 1990 LER 90-002-00:on 900127,fuel Bldg Ventilation Sys Not Aligned to Discharge Through Auxiliary Bldg HEPA Filter & Charcoal Adsorber Assembly During Fuel Movement.Caused by Personnel Error.Disciplinary Action taken.W/900205 Ltr ML20006A8531990-01-19019 January 1990 LER 89-019-00:on 891228,discovered That Outer Door of Containment Equipment Escape Air Lock Was Drawing in Air & Inner Door Noted as Not Being in Fully Closed Position.Cause Undetermined.Sys Enhancements Being evaluated.W/900119 Ltr ML20005F8781990-01-11011 January 1990 LER 89-018-00:on 891219,determined That Three Pressurizer Pressure Safety Injection Instrumentation Channels May Not Have Adequate Margin Between Actuation Setpoint & Bottom of Instrument span.W/900111 Ltr ML19332D5471989-11-22022 November 1989 LER 85-003-03:on 890907,determined That Situation Could Arise Where Water Level Would Rise to 264 Ft Before Next Required Surveillance Interval.Cause Not Determined.Dike to Be constructed.W/891122 Ltr ML20024B7821983-07-0606 July 1983 LER 83-048/03L-0:on 830606 & 17,intermediate Range Channels N35 & N36 High Neutron Flux Reactor Trip Setpoints Exceeded Tech Spec Requirements.Caused by Administrative Error. Setpoints reduced.W/830706 Ltr ML20024C1361983-06-30030 June 1983 LER 83-031/03L-0:on 830614,w/unit at 100% Power,Fire Door S54/5 from Emergency Switchgear Room to Cable Vault Would Not Latch.Fire Watch Posted Immediately.Caused by Misaligned Strike.Door Repaired within 1 h.W/830630 Ltr ML20024C3721983-06-30030 June 1983 LER 83-042/03L-0:on 830606,vital Bus 1-I Momentarily Deenergized While Trying to Clear Inverter Trouble Alarm. Caused by Operator Error.Bus energized.W/830630 Ltr ML20024B9891983-06-28028 June 1983 LER 83-047/03L-0:on 830530,emergency Diesel Generator 2J Tripped on High Crankcase Pressure During Surveillance Testing.Cause Not Determined.Diesel Tested Satisfactorily. W/830628 Ltr ML20024C2941983-06-23023 June 1983 LER 83-044/03L-0:on 830526,during Mode 3,one Recirculation Valve on Each of Two Casing Cooling Pumps Found Open.Caused by Procedure Inadequacy.Valves Closed Immediately.Maint Procedure Will Be revised.W/830623 Ltr ML20024C3071983-06-22022 June 1983 LER 83-034/03L-0:on 830525,during Mode 1,one Header of Control Room Bottled Air Pressurized Sys Had Lower than Required Pressure.Probably Caused by Leak from B Bank of Air Bottles.Header repressurized.W/830622 Ltr ML20024C0971983-06-22022 June 1983 LER 83-045/03L-0:on 830614,Fire Door S71-18,between Emergency Diesel Generator Room 2H & Turbine Bldg,Would Not Latch & Lock.Caused by Stuck Latch.Latch Adjusted & Lubricated.Door Designs modified.W/830622 Ltr ML20023E0951983-06-0101 June 1983 LER 83-027/03L-0:on 830505,one Header (42 Bottles) of Control Room Bottled Air Pressurized Sys Found to Have Lower than Required Pressure (2,290 Vs 2,300 Psig).Probably Caused by Leakage When Compressor malfunctioned.W/830601 Ltr ML20023E0721983-05-26026 May 1983 LER 83-029/03L-0:on 830509,following Rapid Rampdown from 100% to 4% power,I-131 Dose Equivalent Exceeded 1.0 Uci/G. Caused by Unidentified Fuel Element Defect Worsened by post-rampdown Conditions.Sampling increased.W/830526 Ltr ML20023D5371983-05-13013 May 1983 LER 83-022/03L-0:on 830412,review of ASME XI Iwv Program Identified 192 Valves Not Exercised &/Or Stroke Timed.Caused by Fragmented Implementation of Testing Program.Programs Upgraded ML20023D2491983-05-11011 May 1983 LER 83-032/03L-0:on 830412,during Mode 5,visual Insp of Hydraulic Snubber 2-WGCB-HSS-3B Revealed Damaged Reservoir W/O Fluid.Caused by Personnel Working in Area.Snubber Replaced ML20023C5371983-05-10010 May 1983 LER 83-021/03L-0:on 830411,Fire Door S-71-7 Between Svc Bldg Health Physics Area & Auxiliary Bldg Would Not Self Close.Caused by Removal of Reclosure Device for Maint of Closure Coupling.Reclosure Device Reinstalled ML20023B5931983-04-27027 April 1983 LER 83-029/03L-0:on 830402,during Mode 4,automatic Actuation of ECCS Occurred.Caused by Maint Personnel Standing on Conduit Resulting in Loss of lo-lo Pressurizer Pressure Safety Injection Block.Maint Personnel Reinstructed ML20023B5701983-04-27027 April 1983 LER 83-008/03L-0:on 830410,review Revealed That Procedure Used to Restore Boron Injection Tank Concentration Introduced Potential Unanalyzed Injection Flow Diversions. Caused by Oversight.Emergency Procedures Revised ML20028G6541983-02-0909 February 1983 LER 83-003/03L-0:on 830122,during Mode 5,RHR Flow Was Lost for 4 Minutes.Caused by Failure of 15 Kv a Inverter to Ac Vital Bus 1-III,de-energizing Auxiliary Relay for Pressure Channel P-1403.Vital Bus 1-III & RHR Flow Restored ML20028G6311983-02-0909 February 1983 LER 83-016/03L-0:on 830115 & 16,both Open & Closed Containment Isolation Valves TV-SI-200 & TV-CC-204C,train a Position Indication Lights Found Lit.Caused by Leaking Steam Generator Chemical Feed Line Vent Valve ML20028G0781983-01-31031 January 1983 LER 83-001/03L-0:on 830112,primary Grade Water Isolation Valve to Blender 1-CH-217 Remained Open Longer than Tech Spec Requirements.Caused by Personnel Error.Responsible Operator Reinstructed ML20028G0381983-01-28028 January 1983 LER 83-002/03L-0:on 830104,two of Four 2H Emergency Diesel Generator Surveillance Tests Required by Tech Spec Missed During Nov-Dec 1982.Caused by Scheduling Error.Test Frequency Increased to Meet Tech Spec Requirements ML20028G0131983-01-28028 January 1983 LER 83-011/03L-0:on 821119,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps.Caused by Instrument Drift.Indicator Channel for Rods B-09 & 02 & F-06 Recalibr ML20028F3501983-01-19019 January 1983 LER 83-008/03L-0:on 830107,during Mode 3,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps While Withdrawing Shutdown Bank B. Caused by Instrument Drift.Rods Recalibr ML20028E0391983-01-11011 January 1983 Updated LER 82-079/03X-1:on 821126,flow Path from Boric Acid Tanks to RCS Found Inoperable.Caused by Ruptured Diaphragm of Boric Acid Transfer Pump Suction Header Isolation Valve 1-CH-80.Valve Diaphragm Replaced ML20028E0441983-01-11011 January 1983 LER 82-085/03L-0:on 821215,w/unit at Full Power,Emergency Diesel Generator 2J Removed from Svc for 7 H to Adjust Voltage Regulator Response Time.Caused by Voltage Regulator Drift.Procedures Will Be Revised ML20028E0201983-01-11011 January 1983 LER 82-084/03L-0:on 821216,during Full Power,Input from Range Nuclear Instrument N-42 to Comparator Drawer N-50 Was in Defeat.Caused by Failure to Take N-42 Out of Defeat After Deviation Alarm Determination.Operators to Be Reinstructed ML20028E0781983-01-11011 January 1983 LER 82-078/03X-1:on 821125,w/unit in Mode 3,120-volt Ac Vital Bus 1-IV Lost Voltage.Caused by Failure of Normal Power Supply Inverter 1-VB-I-04,due to Failed Oscillator Board,Transformer & Fuse.Components Replaced ML20028D1311983-01-0505 January 1983 LER 82-083/03L-0:on 821213,emergency Diesel Generator 2J Removed from Svc.Caused by Failure of 40X Unexcitation Alarm Relay Coil.Carbon Deposits & Arcing Damage of 40/76 Relay Contact Prevented Good Contact ML20028D1571983-01-0505 January 1983 Updated LER 81-071/03X-2:on 810911,hydraulic Snubber on Main Steam Line Discovered Inoperable Due to Loss of Oil from Reservoir.Caused by Leak Due to Scored Brass Bushing on Piston Shaft.Snubber Purged & Refilled.Reach Rod Retorqued ML20028C5191982-12-31031 December 1982 LER 82-083/03L-0:on 821204,while Operating at 17% Rated Thermal Power,Turbine Control Sys Malfunctioned Causing Sudden Increase in Load,Resulting in Reactor Trip.Caused by Malfunction of Analog Converter ML20028A8651982-11-16016 November 1982 LER 82-067/03L-0:on 821019,suction to RHR Sys Pumps a & B Lost for 36 Minutes.On 821020,pump Suction Lost for 33 Minutes.Caused by Ambiguous RCS Level Indication While Water Drained to Centerline of Nozzles.Water Added ML20028A8821982-11-16016 November 1982 LER 82-060/03L-0:on 821019,station Battery I-IV Failed 18- Month Discharge Surveillance Test.Caused by Natural End of Life.Battery Replaced ML20028A9781982-11-16016 November 1982 LER 82-071/03L-0:on 821027,control Power for B Casing Cooling Pump Found de-energized.Caused by Opened Circuit Breaker Unintentionally Disturbed by Workers.Circuit Breaker Closed & Power Verified 1994-04-25
[Table view] Category:RO)
MONTHYEARML20029D0201994-04-25025 April 1994 LER 94-007-01:on 931014,high Head Safety Injection Flow Balance Testing Found to Be Below TS Requirement.Caused by Unaccounted for Uncertainties.Cold Leg Safety Injection Leg Throttle Valve adjusted.W/940425 Ltr ML20045G9391993-07-0808 July 1993 Lr 93-017-00:on 930616,containment Hydrogen Analyzer Heat Trace Channel Calibration Not Performed on Staggered Test Basis Due to Inadequate Implementation of TS Amend.Test Procedure Satisfactorily performed.W/930708 Ltr ML20044H1591993-05-27027 May 1993 LER 93-016-00:on 930509,discovered That Containment Hydrogen Analyzer Pressure Switch PS-3 Sensing Line Disconnected in Local Panel.Caused by Personnel Error. Pressure Switch Calibr & Line reconnected.W/930527 Ltr ML20044D5711993-05-14014 May 1993 LER 93-002-00:on 930416,automatic Reactor Trip Initiated from Turbine Trip Due to Over Excitation of Main Generator. Emergency Procedure 2-E-0 Entered & Individuals Involved in Event Received Remediated training.W/930514 Ltr ML20044D2281993-05-12012 May 1993 LER 93-003-00:on 930424,manual Reactor Trip Initiated Due to Erratic Feedwater Flow Indications to SG C & Excessive Main Feedwater Regulating Valve Oscillations.Caused by Design Instabilities.Secondary Sys secured.W/930512 Ltr ML20044C9541993-05-0707 May 1993 LER 93-015-00:on 930427,discovered That Portions of Containment Pressure Channels That Input to Containment Spray hi-hi Pressure Not Tested Monthly.Caused by Personnel Error.Test Procedures changed.W/930507 Ltr ML20044C9811993-05-0606 May 1993 LER 93-014-00:on 930411,as-found Speed Setting of Steam Driven AFW Pump 1-FW-P-2 Found Below Required TS Limit. Caused by Incorrect Speed Control Setting.Pump Speed Adjusted & Maint Personnel counseled.W/930506 Ltr ML20024G6841991-04-18018 April 1991 LER 91-006-00:on 910403,discovered That Ac Offsite Power Source Surveillance Not Performed Due to Personnel Error. Surveillance Initiated Immediately & Positive Discipline Administered to supervisor.W/910418 Ltr ML20029B5601991-03-0606 March 1991 LER 91-005-00:on 910209,containment Building Penetrations Breached.Caused by Inadequate Procedural Controls.Core Mapping & Cavity Pump Down Activities Secured,Air Hose Removed & Hydrolase Hose capped.W/910306 Ltr ML20029A6471991-02-22022 February 1991 LER 91-004-00:on 910206,sealed Radioactive Source in Storage Not Leak Tested Prior to Use.Caused by Inadequate Procedures for Verifying Leak Testing of Sources.Procedures Revised.W/ 910222 Ltr ML20028H6681991-01-18018 January 1991 LER 90-009-01:on 900719,discovered That Response Time Testing of Pressurizer High Level Reactor Trip Function Not Performed in Accordance W/Tech Spec 3.3.1.1,Table 3.3-2. Caused by Personnel Error.Procedures revised.W/910118 Ltr ML20043H8321990-06-22022 June 1990 LER 90-007-00:on 900523,discovered That Two Sets of Concrete Roof Blocks on Svc Water Pump House Not in Required Safety Position.Caused by Lack of Administrative Controls.Blocks Restored to Required locations.W/900622 Ltr ML20043D5801990-06-0404 June 1990 LER 90-006-00:on 900504,casing Cooling Pump Not Put Into Alert Status & Surveillance Missed.Caused by Personnel Error.Pump 1-RS-P-3B Placed in Alert status.W/900604 Ltr ML20012E3301990-03-27027 March 1990 LER 90-003-00:on 900228,52 Valves Identified Not Included in Tech Spec Required Monthly Containment Integrity Verification Surveillance Program.Caused by Personnel Error & Inadequate Procedure.Procedure revised.W/900327 Ltr ML20012B6441990-03-0808 March 1990 LER 90-001-00:on 900215,inadvertent Partial Train a ESF Actuation of Containment Depressurization Sys Occurred. Caused by Human Error.Evaluation to Be Performed to Determine If Test Points Can Be moved.W/900308 Ltr ML20006E2371990-02-0808 February 1990 LER 90-001-00:on 900123,reactor Trip Occurred on Steam Feedwater Flow Mismatch.Caused by Failed Circuit Driver Card on Feedwater Regulating Valve.Feedwater Regulating Valve Driver Card replaced.W/900208 Ltr ML20006E3771990-02-0505 February 1990 LER 90-002-00:on 900127,fuel Bldg Ventilation Sys Not Aligned to Discharge Through Auxiliary Bldg HEPA Filter & Charcoal Adsorber Assembly During Fuel Movement.Caused by Personnel Error.Disciplinary Action taken.W/900205 Ltr ML20006A8531990-01-19019 January 1990 LER 89-019-00:on 891228,discovered That Outer Door of Containment Equipment Escape Air Lock Was Drawing in Air & Inner Door Noted as Not Being in Fully Closed Position.Cause Undetermined.Sys Enhancements Being evaluated.W/900119 Ltr ML20005F8781990-01-11011 January 1990 LER 89-018-00:on 891219,determined That Three Pressurizer Pressure Safety Injection Instrumentation Channels May Not Have Adequate Margin Between Actuation Setpoint & Bottom of Instrument span.W/900111 Ltr ML19332D5471989-11-22022 November 1989 LER 85-003-03:on 890907,determined That Situation Could Arise Where Water Level Would Rise to 264 Ft Before Next Required Surveillance Interval.Cause Not Determined.Dike to Be constructed.W/891122 Ltr ML20024B7821983-07-0606 July 1983 LER 83-048/03L-0:on 830606 & 17,intermediate Range Channels N35 & N36 High Neutron Flux Reactor Trip Setpoints Exceeded Tech Spec Requirements.Caused by Administrative Error. Setpoints reduced.W/830706 Ltr ML20024C1361983-06-30030 June 1983 LER 83-031/03L-0:on 830614,w/unit at 100% Power,Fire Door S54/5 from Emergency Switchgear Room to Cable Vault Would Not Latch.Fire Watch Posted Immediately.Caused by Misaligned Strike.Door Repaired within 1 h.W/830630 Ltr ML20024C3721983-06-30030 June 1983 LER 83-042/03L-0:on 830606,vital Bus 1-I Momentarily Deenergized While Trying to Clear Inverter Trouble Alarm. Caused by Operator Error.Bus energized.W/830630 Ltr ML20024B9891983-06-28028 June 1983 LER 83-047/03L-0:on 830530,emergency Diesel Generator 2J Tripped on High Crankcase Pressure During Surveillance Testing.Cause Not Determined.Diesel Tested Satisfactorily. W/830628 Ltr ML20024C2941983-06-23023 June 1983 LER 83-044/03L-0:on 830526,during Mode 3,one Recirculation Valve on Each of Two Casing Cooling Pumps Found Open.Caused by Procedure Inadequacy.Valves Closed Immediately.Maint Procedure Will Be revised.W/830623 Ltr ML20024C3071983-06-22022 June 1983 LER 83-034/03L-0:on 830525,during Mode 1,one Header of Control Room Bottled Air Pressurized Sys Had Lower than Required Pressure.Probably Caused by Leak from B Bank of Air Bottles.Header repressurized.W/830622 Ltr ML20024C0971983-06-22022 June 1983 LER 83-045/03L-0:on 830614,Fire Door S71-18,between Emergency Diesel Generator Room 2H & Turbine Bldg,Would Not Latch & Lock.Caused by Stuck Latch.Latch Adjusted & Lubricated.Door Designs modified.W/830622 Ltr ML20023E0951983-06-0101 June 1983 LER 83-027/03L-0:on 830505,one Header (42 Bottles) of Control Room Bottled Air Pressurized Sys Found to Have Lower than Required Pressure (2,290 Vs 2,300 Psig).Probably Caused by Leakage When Compressor malfunctioned.W/830601 Ltr ML20023E0721983-05-26026 May 1983 LER 83-029/03L-0:on 830509,following Rapid Rampdown from 100% to 4% power,I-131 Dose Equivalent Exceeded 1.0 Uci/G. Caused by Unidentified Fuel Element Defect Worsened by post-rampdown Conditions.Sampling increased.W/830526 Ltr ML20023D5371983-05-13013 May 1983 LER 83-022/03L-0:on 830412,review of ASME XI Iwv Program Identified 192 Valves Not Exercised &/Or Stroke Timed.Caused by Fragmented Implementation of Testing Program.Programs Upgraded ML20023D2491983-05-11011 May 1983 LER 83-032/03L-0:on 830412,during Mode 5,visual Insp of Hydraulic Snubber 2-WGCB-HSS-3B Revealed Damaged Reservoir W/O Fluid.Caused by Personnel Working in Area.Snubber Replaced ML20023C5371983-05-10010 May 1983 LER 83-021/03L-0:on 830411,Fire Door S-71-7 Between Svc Bldg Health Physics Area & Auxiliary Bldg Would Not Self Close.Caused by Removal of Reclosure Device for Maint of Closure Coupling.Reclosure Device Reinstalled ML20023B5931983-04-27027 April 1983 LER 83-029/03L-0:on 830402,during Mode 4,automatic Actuation of ECCS Occurred.Caused by Maint Personnel Standing on Conduit Resulting in Loss of lo-lo Pressurizer Pressure Safety Injection Block.Maint Personnel Reinstructed ML20023B5701983-04-27027 April 1983 LER 83-008/03L-0:on 830410,review Revealed That Procedure Used to Restore Boron Injection Tank Concentration Introduced Potential Unanalyzed Injection Flow Diversions. Caused by Oversight.Emergency Procedures Revised ML20028G6541983-02-0909 February 1983 LER 83-003/03L-0:on 830122,during Mode 5,RHR Flow Was Lost for 4 Minutes.Caused by Failure of 15 Kv a Inverter to Ac Vital Bus 1-III,de-energizing Auxiliary Relay for Pressure Channel P-1403.Vital Bus 1-III & RHR Flow Restored ML20028G6311983-02-0909 February 1983 LER 83-016/03L-0:on 830115 & 16,both Open & Closed Containment Isolation Valves TV-SI-200 & TV-CC-204C,train a Position Indication Lights Found Lit.Caused by Leaking Steam Generator Chemical Feed Line Vent Valve ML20028G0781983-01-31031 January 1983 LER 83-001/03L-0:on 830112,primary Grade Water Isolation Valve to Blender 1-CH-217 Remained Open Longer than Tech Spec Requirements.Caused by Personnel Error.Responsible Operator Reinstructed ML20028G0381983-01-28028 January 1983 LER 83-002/03L-0:on 830104,two of Four 2H Emergency Diesel Generator Surveillance Tests Required by Tech Spec Missed During Nov-Dec 1982.Caused by Scheduling Error.Test Frequency Increased to Meet Tech Spec Requirements ML20028G0131983-01-28028 January 1983 LER 83-011/03L-0:on 821119,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps.Caused by Instrument Drift.Indicator Channel for Rods B-09 & 02 & F-06 Recalibr ML20028F3501983-01-19019 January 1983 LER 83-008/03L-0:on 830107,during Mode 3,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps While Withdrawing Shutdown Bank B. Caused by Instrument Drift.Rods Recalibr ML20028E0391983-01-11011 January 1983 Updated LER 82-079/03X-1:on 821126,flow Path from Boric Acid Tanks to RCS Found Inoperable.Caused by Ruptured Diaphragm of Boric Acid Transfer Pump Suction Header Isolation Valve 1-CH-80.Valve Diaphragm Replaced ML20028E0441983-01-11011 January 1983 LER 82-085/03L-0:on 821215,w/unit at Full Power,Emergency Diesel Generator 2J Removed from Svc for 7 H to Adjust Voltage Regulator Response Time.Caused by Voltage Regulator Drift.Procedures Will Be Revised ML20028E0201983-01-11011 January 1983 LER 82-084/03L-0:on 821216,during Full Power,Input from Range Nuclear Instrument N-42 to Comparator Drawer N-50 Was in Defeat.Caused by Failure to Take N-42 Out of Defeat After Deviation Alarm Determination.Operators to Be Reinstructed ML20028E0781983-01-11011 January 1983 LER 82-078/03X-1:on 821125,w/unit in Mode 3,120-volt Ac Vital Bus 1-IV Lost Voltage.Caused by Failure of Normal Power Supply Inverter 1-VB-I-04,due to Failed Oscillator Board,Transformer & Fuse.Components Replaced ML20028D1311983-01-0505 January 1983 LER 82-083/03L-0:on 821213,emergency Diesel Generator 2J Removed from Svc.Caused by Failure of 40X Unexcitation Alarm Relay Coil.Carbon Deposits & Arcing Damage of 40/76 Relay Contact Prevented Good Contact ML20028D1571983-01-0505 January 1983 Updated LER 81-071/03X-2:on 810911,hydraulic Snubber on Main Steam Line Discovered Inoperable Due to Loss of Oil from Reservoir.Caused by Leak Due to Scored Brass Bushing on Piston Shaft.Snubber Purged & Refilled.Reach Rod Retorqued ML20028C5191982-12-31031 December 1982 LER 82-083/03L-0:on 821204,while Operating at 17% Rated Thermal Power,Turbine Control Sys Malfunctioned Causing Sudden Increase in Load,Resulting in Reactor Trip.Caused by Malfunction of Analog Converter ML20028A8651982-11-16016 November 1982 LER 82-067/03L-0:on 821019,suction to RHR Sys Pumps a & B Lost for 36 Minutes.On 821020,pump Suction Lost for 33 Minutes.Caused by Ambiguous RCS Level Indication While Water Drained to Centerline of Nozzles.Water Added ML20028A8821982-11-16016 November 1982 LER 82-060/03L-0:on 821019,station Battery I-IV Failed 18- Month Discharge Surveillance Test.Caused by Natural End of Life.Battery Replaced ML20028A9781982-11-16016 November 1982 LER 82-071/03L-0:on 821027,control Power for B Casing Cooling Pump Found de-energized.Caused by Opened Circuit Breaker Unintentionally Disturbed by Workers.Circuit Breaker Closed & Power Verified 1994-04-25
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N9281999-10-20020 October 1999 Special Rept:On 991003,PZR PORV Actuation Mitigated RCS low- Temp Overpressure Transient.Caused by a RCP Facilitating Sweeping of Entrained Air Out of RCS Loops.Operating Procedure 2-OP-5.1 Will Be Revised ML20217H3631999-10-14014 October 1999 Rev 0 to COLR for North Anna 2 Cycle 14 Pattern Su ML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML20212J9251999-10-0101 October 1999 Safety Evaluation Accepting Licensee Relief Request IWE-3 for Second 10-year ISI for Plant ML20217D6851999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for North Anna Power Station,Units 1 & 2.With ML20211N2611999-09-0808 September 1999 Safety Evaluation Concluding That Proposed Irradiation of Fuel Rods Beyond Current Lead Rod Burnup Limit & Clarification of Terminology with Respect to Reconstituted Fuel Assemblies Acceptable ML20211J2561999-08-31031 August 1999 Safety Evaluation Accepting Elimination of Augmented ISI Program for Pressurizer Spray Lines at North Anna Unit 2 ML20216E5011999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Naps,Units 1 & 2. with ML20211J2421999-08-31031 August 1999 Safety Evaluation Supporting Removal of Augmented Insp Program on RCS Bypass Lines from Licensing Basis of North Anna,Units 1 & 2 ML20210T0791999-08-13013 August 1999 Safety Evaluation Concluding That Revised Withdrawal Schedules for North Anna Units 1 & 2 Satisfy Requirements of App H to 10CFR50 & Therefore Acceptable ML20210S1411999-07-31031 July 1999 Monthly Operating Repts for July 1999 for North Anna Power Station.With ML20210Q9931999-07-31031 July 1999 Rev 1 to COLR for North Anna Power Station,Unit 2 Cycle 13 Pattern Ud ML20209E5641999-06-30030 June 1999 Monthly Operating Repts for June 1999 for North Anna Power Stations,Units 1 & 2.With ML20195G1901999-05-31031 May 1999 Monthly Operating Rept for May 1999 for NAPS Units 1 & 2. with ML20206L4831999-05-10010 May 1999 SER Accepting Request to Delay Submitting Plant,Unit 1 Class 1 Piping ISI Program for Third Insp Interval Until 010430, to Permit Development of Risk Informed ISI Program for Class 1 Piping ML20206Q6671999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for North Anna Power Station,Units 1 & 2.With ML20205S0391999-04-21021 April 1999 SER Accepting Request for Relief IWE5,per 10CFR50.55a(a)(3) & Proposed Alternatives for IWE2,IWE4,IWE6 & IWL2 Authorized Per 10CFR50.55a(a)(3)(ii) ML20205K3041999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for North Anna Power Station,Units 1 & 2.With ML20207K5921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for North Anna Power Station,Units 1 & 2.With ML20207E1731999-02-18018 February 1999 Informs Commission of Status of Preparations of IAEA Osart Mission to North Anna Nuclear Power Plant Early Next Year ML20205A0241998-12-31031 December 1998 Summary of Facility Changes,Tests & Experiments,Including Summary of SEs Implemented at Plant During 1998,per 10CFR50.59(b)(2).With ML20199C8781998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for North Anna Power Station,Units 1 & 2.With ML20198H9541998-12-0303 December 1998 Safety Evaluation Authorizing Proposed Alternative for Remainder of Second 10-yr Insp Interval for Plant ML20198J5561998-12-0303 December 1998 ISI Summary Rept for North Anna Power Station,Unit 1 1998 Refueling Outage Owner Rept for Inservice Insps ML20197G8551998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for North Anna Power Station,Units 1 & 2.With ML20196G1381998-11-0303 November 1998 Safety Evaluation Authorizing Rev to Relief Request NDE-32 for Remainder of Second 10-yr Insp Interval for Each Unit ML20195D0571998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for North Anna Power Station,Units 1 & 2.With ML20154L0691998-10-14014 October 1998 COLR for North Anna Power Station Unit 1 Cycle 14 Pattern Xy ML20155J6911998-10-0909 October 1998 Staff Response to Tasking Memorandum & Stakeholder Concerns ML20154H4001998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for North Anna Power Station,Units 1 & 2.With ML20151X8011998-09-10010 September 1998 Special Rept:On 980622,groundwater Level at Piezometer P-22 Was Again Noted to Be Above Max Water Level by 0.71 Feet. Increased Frequency of Piezometer Monitoring & Installed Addl Piezometers at Toe of Slope Along Southwest Section ML20151W4711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for North Anna Power Station Units 1 & 2.With ML20237A4341998-07-31031 July 1998 Monthly Operating Repts for July 1998 for North Anna Power Station,Units 1 & 2 ML20236V1251998-07-14014 July 1998 ISI Summary Rept for Naps,Unit 2,1998 Refueling Outage Owners Rept of Isis ML20236K5531998-07-0707 July 1998 SER Accepting Request for Change in ISI Commitment on Protection Against Pipe Breaks Outside Containment ML20236M3381998-06-30030 June 1998 Monthly Operating Repts for June 1998 for North Anna Power Station,Units 1 & 2 ML20248M1011998-05-31031 May 1998 Monthly Operating Repts for May 1998 for North Anna Power Station,Units 1 & 2 ML20248C8831998-05-29029 May 1998 SER Accepting Alternatives Proposed by Licensee for Use of Code Case N-535,pursuant to 10CFRa(a)(3)(i) in ASME Section XI Inservice Insp Program ML20247K9281998-05-15015 May 1998 Special Rept:On 980428,letdown PCV Exhibited Slow Response When C RCP Was Started.Cause to Be Determined.Review of Operating Procedure Will Be Performed to Determine If Enhancements Are Necessary ML20216A8971998-05-0606 May 1998 Rev 0 to Cycle 13 Pattern Ud COLR for North Anna Unit 2 ML20247F4441998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for North Anna Power Station,Units 1 & 2 ML20217B5321998-04-20020 April 1998 Safety Evaluation Supporting Proposed Alternative to ASME Code for Surface Exam of Seal Welds on Threaded Caps for Plant Reactor Vessel Head Penetrations for part-length CRDMs ML20217H9611998-04-0707 April 1998 Special Rept:On 980216,groundwater Level at Piezometer P-22, Again Noted to Be Above Max Water Level by 0.41 Feet.Design Package for Installation of Addl Standpipe Piezometers at Toe of Slope Southeast Section,Developed ML20216B1891998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for North Anna Power Station,Units 1 & 2 ML20216E8801998-03-0606 March 1998 Safety Evaluation Authorizing Licensee Request for Relief from ASME Code Requirements,Paragraph IWA-2400(c) (Summer Edition W/Summer 1983 Addenda),For Upcoming Naps,Unit 1 Outage,Per 10CFR50.55a(a)(3)(ii) ML20216E2561998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for North Anna Power Station,Units 1 & 2 ML20199J6431998-02-0202 February 1998 Safety Evaluation Approving Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Code Class 3 SW Piping for North Anna,Unit 1,as Submitted in ISI Relief Request NDE-46 on 971218 ML20202D5811998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for North Anna Power Station,Units 1 & 2 ML20198S7571998-01-15015 January 1998 Safety Evaluation Accepting Licensee Request for Approval to Repair Flaws IAW GL-90-05 for ASME Code Class 3 Svc Water Piping ML20198P1351997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for North Anna Power Station,Units 1 & 2 1999-09-08
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NRC FORM 366- -(7-77)LICENSEE EVENT REPORT
- CONTROL 3 LOCK: l lllllh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATioN)
I bl Vl Al Nl Al Sl 1 l@l 0 l 0 l- l 0 l 0 l 0 l 0 l 0 l- l0 l 0 !@l 4 l1 l1 li l1 l@l l@O 1 F 8 9 LICENSEE CODL 14 15 LICEN$E NyVdER 23 26 LICENSE TYPE JJ 57 CA T bd CON'T$RC[ l L j@l 015 l 0 l 010 l 3 l 3 8 @l01912l5l7 lo @l il nl nl ol 71 ol@
0 1 i B tJ 61 DOCKET NUV8E R tA 69 EVENT DATE 14 15 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h 1 o 2l At 0514 a Safety Injectics occurred dua to a inv procever4+ar imm1nninn W t Il with low pressurizer pressure. This event is a 24 hcur recortabir nceurronca nc nor 0 3 Il req. guide 1.16 nnd as pe r T.S. 6.9.1. 8.i .
Followirm the evene n r,A ,e4nn val o e y fo 4 o 5 Ioccurred which was less than 0.05% of the instantaneous release rare nor tT.s-1 1 IOlsl l 2.2.3.a.
Boundary radiation detectors showed onl y h,ckornuna r,A i n,n+ 4v4 y ,na 0 7i l therefore at no time was the health and safety of the ce n p r ,1 mihl i c nFfocenA ll0 8]80 7 8 3 SY STEM CAUSE CAUSE COMP.VALVE CODE CODE SUSCODE COMPON ENT CODE SU8 CODE SUSCODE I S l v l @ l e @ l a l @ I v l A l L l T l E l X l@ W @ [3_j h O 9 7 8 9 to 11 12 13 18 19 20_SE QUE N TI AL OCCURRENCE REPORT REVISION LER EVENT YE AR REPORT NO.
CODE TYPE N O.@,ag.RO I 719 I l--J l1121si[/_jl011 ll TIl-l10 1 g u 21 22 23 24 26 27 28 29 30 31 32 TAK N ACT CN ON PLANT MET HOURS S 8 I O FO B.SU PP LI E R MAN FACTURER I XI@l XI@
L^J@Ic @l0 D 10 l0 l lYl@[N_j@Al@lC 6 l3 5l@33 34 35 36 3/40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h a ro,ctnr I j'Ihe cause of the SI was steam dump valve TCV-1408G stuck open followine i O g i g i g l trip, which depressurized the reactor coolant systen.
Correc tive nc+ 4 nna uarn en I g return the plant to stable conditions by the control room operators and later I , ,l initiate a plant cooldown to the cold shutdown mode of operation.
I , 3 1 4l80 7 8 0 ST S% POWER OTHER STATUS DISCO RY DISCOVERY DESCRIPTION 11 l5l lX @ l 0l 7 l 8 l@l Coastdown llAl@lAutomatic Actuation l'"*7 8 AETIVITY CO TENT RELEASEL OF RELEASE AMOUNT OF ACTtVtTY LOCATION OF RELE ASE lG l@ U@l7.5 Curies Total llVentilation and Process Vents to Atm.
!i c 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION NAll 0 l 0 l 0 l@l Z l@l 1 7 'PERSONNE L INJURIES oeSCRiPriOsh NuvsER l1lall0l0l0l@l NA 80 7 8 9 11 12- _)LOSS OF OR DAMAGE TO FACILITY
}li. -TYPE DESCRIPilON NAlZl@li 9 80 7 8 9 10 PUBLICITY.NRC USE ONLY
- b IST E D@ DESCRIPTION y 910110_a i i iiiiiiiiiiI;
[YjlPublic News Release
-2 O 68 69 80 ;;7 8 9 10 o Ca r t- r 1- t PHONE: ' g 33 g ;31
", NAME OF PREPARER ".
8 D
..Virginia Electric and Power Company North A na Power Station, Unit #1
Attachment:
Page 1 of 5 Pocket No. 50-338 Report No. LER 79-123/01T-0 Description of Event:
At 0544 on 9/25/79 with reactor power at 78%, the fif th point heater drain cooler dump valve LCV-SD-182B began to cycle. This cycling was believed to be due to a tube ruptere inside the 5B drain cooler. The leakage was more than the capability of the drain valves causing extraction steam condensate to back up into the 5th point heater to the turbine trip setpoint.
At 0609, a turbine trip occurred and resulted in a reactor trip. At this time the main steam dump valves opened to reduce RCS temperature to 547"F.
When the RCS temperature decreased below the steam dump setpoint, steam dump valve TCV-140BG failed to close. The steam dump valve was then isolated by closing the main steam trip valves.
Excessive cooldown caused by the open steam dump valve resulted in an RCS depressurization and a resultant Pressurizer Lo Pressure signal. This signal, combined with the administrative 1y tripped Pressurizer to Level signal, ini-tiated a safety injection of the Emergency Core Cooling System. Ttis event occurred at 0614.
The RCP's were immediately manually tripped as required. As a result of the safety injection and the termination of the cooldown, the RCS pressure began to increase.
One of two SI charging pumps was secured at 0619. At 0620, the pressurizer power operated relief valve began to cycle and main-tained pressure at 2335 psig until normal letdown and charging were estab-lished.When normal letdown was established, the remaining charging pump was still drawing suction from the RWST.
This resulted in an increasing level within the Volume Control Tank (VCT) such that the VCT level control valve (LCV-1115A) began to modulate to divert reactor coolant letdown to the Boron Recovery System via the gas stripper.
The high flow to the stripper resulted in the inlet trip valve to the stripper closing due to high stripper level.
At this time, LCV-1115A was fully diverted to the gas stripper; however, the inlet control valve to the stripper (TV-BR111A) was closed.
The pressure in the letdown line increased to the low pressure letdown line relief valve (RV-1209) (setpoint of 200 psig.
This valve discharged directly to the VCT.
The VCT pressure increased to the VCT relief valve (RV-1257) setpoint of 75 psig. This valve discharged letdown water and gases directly to the High Level Liquid Waste Tank (HLLWT).
The normal action at this point would be the relessa of noble gases from the HLLWT through a vent line and through the plar.: process vents.
In a point in the vent line a flange had been disconnected and the noble gases were released into the auxiliary building.
The gases were then vented through the plant charcoal and HEPA filters and out of the plant ventilation vents.
Had the flange not been disconnected, a release of noble gases to the auxiliary building may have occurred.
The discharge rate of VCT reactor coolant to the HLLWT may have been too much to pass through the normal vent line, therefore the reactor coolant gases would have vented to the Low Level Liquid Waste Tanks and out into the auxiliary building via the Low Level Liquid Waste Tank overflow line.
113i 201.
.Attachment Page 2 of 5 The f ollowing is submitted as additional information.
The release was well within the Environmental Technical Specifications limit.
AUXILIARY BUILDING AIRBORNE ACTIVITIES 09 /2 5/79 TIME ELEVATION EXPLANATION 0700 274'100.9 6* Times MPC.
Principle Nuclei involved were Xe 133 & 135 with some Kr 85 and Rb 88.
259'155.68* Times MPC.
Principle Nuclei involved were Xe 133 & 135 with some Kr 85 and Rb 88.
0800 274'1.12* Times MPC.
Principle Nuclei involved were Xe 133 & 135 with traces of Rb 88.
0900 259 '6.01* Times MPC, Principle Nuclei involved were Xe 133 & 135 with traces of Rb 88.
1000 259 'O.68* Times MPC.
Principle Nuclei involved were Xe 133 & 135 with traces of Rb 88.
1030 259 'Less than 0.1 times MPC.
Principle Nuclei involved was Rb 88.
All readings af ter 1030 were less than 0.1 times MPC.
- This value represents the total submersion hazard involved with the total of all Nuclei.
Perimeter TLD's were pulled and evaluated.
No radiation exposures above background were observed in the 14 TLD's in the downwind direction on the perimeter fence.
Total Noble gas releases from ventilation vents A and B and the process vent amounted to 4.7E-02% of the release rate limit of noble gases.
During this event, several other events occurred which are contrary to Technical Specifications.
Af ter the turbine trip, a turbine reheat valve failed to close which is contrary to T.S. 3.7.1.8.
The action statement was entered and the turbine was isolated from the main steam supply.
When the main steam dump valve failed to close, an RCS cooldown of 110*F in 30 minutes occurred.
This event is contrary to T.S. 3.4.9.1.b.
The RCS temperature was restored to within the T.S. limits by closing the main steam trip valves.
113i 202 Attachment Page 3 of 5 Upon receiving +he SI signal, the control room bottled air system failed to initiate as required by T.S. 3.7.7.1.
The Action Statement requirements were cet by cooling down to the cold shutdown mode.
As a result of the safety injection, the Boron Injection Tank was lef t containing 2000 ppa borated water instead of 20,000 ppa borated water as required by T. S. 3.5.4.1 and the Emergency Condensate Tank was de-pleted less than 110,000 gallons by the Auxiliary Feedwater Pumps which is contrary to T.S. 3.7.1.3.
The appropriate Action Statements of these events were entered.
Although not reportable, a Hi Hi air particulate alarm in the Contain-ment occurred. This is believed to be due to leakage by the #3 seals from the secured RCP's.
The ECCS actuation is reportable as per T.S. 3.5.2 which requires a 90 day report, Reg. Guide 1.16 requires a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> notice and written follow up as pe r T. S. 6.9.1. 8.f .
This is the third ECCS actuation reportable as per T.S. 6.9.1.b.
This event is generic to Unit #2 since it uses the same type of steam dump valves.Probable Consequences of Occurrences:
The purpose of the Emergency Core Cooling System is to ensure adequate cooling of the reactor in the event of a loss of coolant accident.
Since the ECCS actuated as required and at no time was the reactor in danger of being undercooled, the safe operation of the plant was not affected.Also, since the radiation release was well within the limits of the Tech-nical Specifications at no time was the health and safety of the general public affected.
Cause of Occurrence:
The cause of the intial reactor trip was a turbine trip due to a Hi Level in the 5B feedwater heater.
The resulting RCS cooldown of 110*F and depressurization was due to a steam dump valve f ailing to close. The reason for the valve failure is currently being investigated by Vepco, Westinghouse and Copes-Vulcan.
The cause of the Reheat Stop valve f ailing to close is unknown at this time and will be investigated by Vepco and Westinghouse during a turbine inspection.
The low level of the ECST and the underboration of the BIT are results of the safety injection.
The safety injection pumps draw suction from the RWST and pump through the BIT leaving 2000 ppm borated water in the BIT.The ECST level was lowered by the Auxiliary feedwater pumps feeding water to the steam generators.
-)
Attachment page 4 of 5 The failure of the control room bottled air system was the result of an apparent pressure shock to the Bourdon tubes in the discharge of pressure controller of the system. This pressure shock deformed the tubes leaving them inoperable.
The release of radioactive noble gases was due to the automatic shutdown of the gas stripper and the continued letdown of the reactor coolant while the VCT was not supplying makeup to the reactor coolant system. The overfilling of the VCT occurred during the time operations personnel were regaining RCS pressure control while still maintaining the required high head safety injection flow to the RCS.
The transition from the safety injection mode to the normal charging .aode of operation was made in a slow and cautious manner so as not to overpressurize the RCS.
This evolution resulted in overfilling the VOT and the resultant release of radioactive gases.
Immediate Corrective Actions:
Upon actuation of the automatic reactor trip, the operators performed the required immediate corrective actions of the emergency procedures.
Af ter the main steam dump valve failed in the open position. the operators attempted to isolate the valve by manually closing a steam dump isolation valve.It was determined that closing the large valve would consume too much time, therefore, the dump valve was isolated by closing the main steam trip valves.
Af ter the automatic initiation of safety injection from low RCS pressure, the operators manually tripped the RCP's as required by procedures and began monitoring RCS parameters to ensure adequate core cooling.
approximately 0619 the operators secured one of two High Head Safety
" injection pumps and at. approximately 0627 began to establish normal le td own.
Af ter 20 minutes of cold leg injection, at approximately 0633, safety injection was secured. At this time a RCP and a feedwater pump were in operation and the plant was determined to be stable.
When a high Icvel and pressure were noted in the VCT, operationc personnel re-established the RCS letdown to the Boron Recovery System via the gas stripper. This alleviated the high pressure and level condition in the VCT and the relief valve closed ending the release of reactor coolant to the liquid waste tank. The disconnected flange in the HLLWT vent line was reconnected.
The operators refilled the ECST as required by the appropriate action statements and began to cooldown the plant to the cold shutdown mode by following normal procedures.
Following the 110*F cooldown of the RCS, Westinghouse was notified and they determined that there was no ef fect on the RCS fracture toughness properties.
Scheduled Corrective Actions:
During the current refueling outage, investigations into the failure of 1131 204 Attachment page 5 of 5 the nain steam dump valve and the turbine reheat stop valve will be conducted by Vepco, Westinghouse and Copes Vulcan.
An engineering review of the letdown divert to the boron recovery system will be performed to determine if any improvements may be implemented to the present system.
A design change will be incorporated into the control room bottled air systen which will provide protection to the Bourdon tubes from over-pressurization.
A continued investigation into the ef fect of the transient on the plant is being performed by Vepco and Westinghouse.
Also, Vepco and Westinghouse are reviewing the problem of #3 seal leakoff from secured RCP's.
Actions Taken to Prevent Recurrence:
Corrective actions to the main steam dump valves and reheat stop valves will be performed when the results of the investigations are available.
An engineering review into the problem of high flow in the High Level Liquid Waste Tank vent line will be undertaken.
Any lessons learned from Vepco and Westinghouse reviews of the transient will be incorporated into Vepco procedures and will be forwarded to the Westinghouse Owners Group.
113 205.