ML20006A853

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LER 89-019-00:on 891228,discovered That Outer Door of Containment Equipment Escape Air Lock Was Drawing in Air & Inner Door Noted as Not Being in Fully Closed Position.Cause Undetermined.Sys Enhancements Being evaluated.W/900119 Ltr
ML20006A853
Person / Time
Site: North Anna Dominion icon.png
Issue date: 01/19/1990
From: Kane G
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-89-019-02, LER-89-19-2, N-89-026, N-89-26, NUDOCS 9001300354
Download: ML20006A853 (5)


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10 CFR 50.73 i VIRGINI A ELECTRIC AND PODER COMP ANY NORTM ANN A POSCR $T ATION I P. O. Box 402 [

ulNE R AL, VIRGINI A 23117 r January 19, 1990  ;

U. S. Nuclear Regulatory Commission Serial No. N 89-026 '

Attention: Document Contml Desk NAPS /DEQ:deg Washington, D.C. 20555 & Let No. 50 338 i t

l License No. NPF-4 '

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Dear Sirs:

The Virginia Electric and Power Company hereby submits the following Licensee Event Report l applicablc to North Anna Unit 1.

i Report No. LER 89-019-00 l t

f This Report has been reviewed by the Station Nuclear and Operating Committee and will be forwarded to Safety Evaluation and Control for their review, i l

Very Truly Yours,

/ di.b. Kane Station Manager  ;

i

Enclosure:

cc: U.S. Nuclear Regulatory Commission 101 Marietta Street, N.W.

Suite 2900 .

Atlanta, Georgia 30323 Mr. J. L. Caldwell NRC Senior Resident Inspector North Anna Power Station

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[ No l l l 3 . ,. . . ,,,. .. . . , n e i At 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br /> on December 28, 1989, with Unit I at 100 percent power <

(Mode 1 ), llcalth Physics personnel performing their weekly survey rounds reported that the outer door of the containment equipment escape air lock was drawing in air. Prior to performing a Periodic Test to quantify the leakage, the  !

inner door was noted as not being in the fully closed position and was subsequently closed, thus restoring containment integrity. This event has been determined to be reportable pursuant to 10CFR50.73(a)(2)(li). A one hour report was made in accordance with 10CFR50.72(b)(ii). Additionally, an engineering calculation has determined that the leakage from the containment +

cscape air lock door during this event was greater than the maximum leakage allowed by Technical Specifications 3.6.1.2 and 3.6.1.3. Consequently, this event is also reportable pursuant to 10CFR50.73(a)(2)(1)(B).

Investigation could not identify why the inner door was not fully closed.

Procedural and system enhancements, recommended as a result of an event j investigation, will be evaluated and implemented as necessary.  :

This event posed minimal significant safety implications because the i containment remained subatmospheric throughout this event. The health and I safety of the general public were not affected at any time during this event, j I

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1.0 Description of the Event At 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br /> on December 28, 1989, with Unit 1 at 100 percent power  ;

(Mode 1 ), ficalth Physics personnel performing their weekly survey rounds reported that the outer door of the containment equipment escape air lock '

(Ells System identifier Nil , Component identifier AL) was drawing in air.

Following discovery of the outer door leakage, actions were initiated to perform Periodic Test (PT) 62.3,

  • Equipment llatch Escape Lock Door Seals Testing," to quantify the seal leakage. At 0040 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> on December 29, 1989, prior to performing PT 62.3, the inner door was noted as not being in the i fully closed position and was immediately closed, thus restoring containment ,

integrity. Since the Surveillance Requirement of Technical Specification  ;

4.6.1.3 requires that both the inner and outer doors of the containment equipment air lock be demonstrated operable within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> following closing, preparations continued to perform PT 62.3. At 0115 hours0.00133 days <br />0.0319 hours <br />1.901455e-4 weeks <br />4.37575e-5 months <br /> on December 29, 1989, the outer door failed to pass PT 62.3 and the Action Statement of Technical Specification 3.6.1.3 was entered for one containment i escape air lock door being inoperable. The O rings on the outer door were cleaned and reinserted and PT 62.3 was satisfactorily completed on the outer door. The outer door was opened to provide access to the inner door. The inner door was successfully tested in accordance with 1 PT 62.3. The outer door was subsequently reclosed and satisfactorily tested as required by 1 PT. ,

62.3. The Action Statement of Technical Specification 3.6.1.3 was cleared at approximately 0315 hours0.00365 days <br />0.0875 hours <br />5.208333e-4 weeks <br />1.198575e-4 months <br /> on December 29, 1989. t At 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br /> on December 29, 1989, Station Management discussed the containment escape air lock door events. Upon completion, the event was determined to be four hour reportable pursuant to 10CFR50.72(b)(iii)(C) and .

30 day reportable pursuant to 10CFR50.73(a)(2)(ii). At 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> on December 29, 1989, the Station Nuclear Safety and Operating Committec  ;

conveined to reevaluate the events and discuss the engineering assessment of ,

the event. At that time, the event was determined to be one hour reportable pursuant to 10CFR50.72(b)(ii). At 1040 hours0.012 days <br />0.289 hours <br />0.00172 weeks <br />3.9572e-4 months <br />, a one hout report was made in accordance with 10CFR50.72(b)(ii).

Prior to this event Unit 1 experienced a reactor trip on December 5, 1989. In preparation for Unit startup following the reactor trip, the containment equipment escape air lock was verified to be closed and scaled by satisfactory completion of 1 PT 62.3,1 PT 62.2, " Containment Air Locks -

Interlocks," 1 PT 61.2.3, " Containment Type B Test - Equipment llatch," 1 PT.

61.2.3.1, " Containment Type B Test Equipment flatch "AS FOUND" Leak Rate )

Test," on December 8, 1989, llowever, preceding unit startup, a ground  !

occurred on the 'B' Reactor Coolant Pump (RCP) and the containment equipment escape air lock was removed on December 12, 1989 to facilitate replacement of the 'B' RCP motor. After completion of the 'B' RCP motor replacement, the containment escape air lock was reinstalled and verified on

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December 17, 1989 to be scaled by satisfactory completion of 1 PT 61.2.3,  !

" Containment Type B Test - Equipment flatch,", In addition, on December 24, i 1989, the Security Department performed an alarm test on the security ?oor at the containment equipment escape air lock and did not observe increased noise levels due to escape air lock leakage, j An engineering calculation has determined that the leakage from the i containment escape air lock door during this event was greater than the l maxirnum leakage allowed by Technical Specifications 3.6.1.2 and 3.6.1.3. '

Consequently, this event is also reportable pursuant to 10CFR50.73(a)(2)(1)(B). j 2.0 Sicnifiennt S afety Conscauences and implientions This event posed minimal significant safety implications because the '

containment remained subatmospheric throughout this event. Therefore, there was no positive pressure differential to force any radioactive gas through the unsealed air locks. The health and safety of the general public were not affected at any time during this event.

3.0 Cause of the Event Investigation could not identify why the inner door was not fully closed.

4.0 Immediate Corrective Action ,

As an immediate corrective action, a procedure deviation was written .

and approved to test the outer door of the containment equinment escape air lock in an attempt to quantify the leakage. Prior to testing the outer door, the inner door was identified as not being fully closed and was immediately closed, thus restoring containment integrity.

5.0 Additional Corrective Action i I

After the inner door was fully closed, the outer door of the containment equipment escape air lock was tested in accordance with the Technical Specifications. The outer door failed to pass the periodic test and the Action Statement of Technical Specification 3.6.1.3 was entered. The o.

rings on the outer door were adjusted and PT-62.3 was satisfactorily completed on the outer door. The outer door was opened to 1.rovide access to the inner door. The inner door was successfully tested in accordance with 1 PT-62.3.

The outer door was subsequently closed and satisfactorily tested as required by 1 PT-62.3. The Action Statement of Technical Specification 3.6.1.3 was subsequently cleared.

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.trw - .m . . n-s uc s m .nm 5.0 Additional Corrective Action Cont'd.

i The following procedural and system enhancements, resulting from an event investigation, will be evaluated and implemented as necessary:

1. Installing break away plastic seals to the inner and outer door operators of the equipment hatch escape air locks to provide positive indication of operator movement.
2. Revising appropriate periodic tests and operating procedures to document and verify the seals are properly installed and I maintained intact. I
3. Adding placecards to the equipment hatch escape air locks that address the need for Control Room notification when the doors are operated.

An engineering calculation was also performed in an attempt to .

quantify the leakage.

6.0 Actions to Prevent Recurrence This is believed to be an isolated event, llowever, corrective actions identified from the event investigation will be evaluated and implemented as necessary to prevent recurrence of similar events.

7.0 Simlar Events On September 21, 1987, both Unit 2 containment air lock doors were discovered to be open in Mode 6 (Refueling) during control rod latching as a result of a procedure inadequacy and personnel error. This event was J reported in LER N2/87 010 00.  !

8.0 Additional In form ation l Several followup inspections have been made to verify that both containment equipment air lock doors have remained closed. Also, Unit 2 was checked and  !

no problems were identified. l

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