LER-1983-029, /03L-0:on 830402,during Mode 4,automatic Actuation of ECCS Occurred.Caused by Maint Personnel Standing on Conduit Resulting in Loss of lo-lo Pressurizer Pressure Safety Injection Block.Maint Personnel Reinstructed |
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4 U.S. NUCLEAR RECULATORY COMMISSION LICENSEE EVENT REPORT h
CONTROL BLOCK / / / / / / / (1)
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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LICENSEE CODE LICENSE NUMBER LICENSE TYPE CAT IUlI#
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/0/4/2/7/8/3/ (9) g DOCKET NUMBER EVENT DATE REPORT DATE-EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10).
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/ On March 2, 1983 with Unit 2 in Mode 4 an automatic actuation'of the Emergency
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/ Core Cooling System occurred due to the loss of a Lo-Lo Pressurizer Pressure'S.I./
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ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP. COMPONENT j
.TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FORM SUB. SUPPLIER MANUFACTURER
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27) l
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/ The ECCS actuation was due to the loss of'Lo-Lo Pressurizer Pressure S.I. Block._/
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/ PCV-2456 lif ted when pressurizer pressure reached its low temperature setpoint of/
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/ 470 psig due to the influx of injection water. The loss of block was caused by a/
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/ SSPS train "B" power supply spike.
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PERSONNEL INJURIES NUMBER DESCRIPTION (41)
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LOSS OF OR DAMAGE TO FACILITY (43) 8305050215 830427
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PDR ADOCM 05000339 S
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NRC USE ONLY
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NAME OF PREPARER E. WAYNE HARRELL PHONE (703) 894-5151
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a Virginia Electric and Power Company North Anna Power Station Unit No. 2 Attachment: Page 1 of 2 Docket No. 50-339 Report No. LER 83-029/03L-0
Description of Event
On March 2, 1983, at 2009 hours0.0233 days <br />0.558 hours <br />0.00332 weeks <br />7.644245e-4 months <br /> with Unit 2 in Mode 4 cooling down for refueling, an automatic actuation of the Emergency Core Cooling System occurred due to the loss of the Lo-Lo Pressurizer Pressure Safety Injection Block in the train "B" logic of the Solid State Protection System.
Initial conditions of the Reactor Coolant System were as follows; RCS Temperature 321*F, Pressurizer Pressure 410 PSIG and Pressurizer Level 20 percent.
Upon inj ection of water into the RCS pressurizer pressure and level increased rapidly.
At 2011 and 2012 hours0.0233 days <br />0.559 hours <br />0.00333 weeks <br />7.65566e-4 months <br /> power operated relief valve, PCV-2456, lifted at its low temperature over pressure protection setpoint of 470 psig.
Safety injection was reset at 2013 hours0.0233 days <br />0.559 hours <br />0.00333 weeks <br />7.659465e-4 months <br /> and the injection flow terminated.
During the event the refueling water storage tank dropped below T.S.
minimum level and control bottle air banks discharged, both normal conditions during a safety injection.
All equipment performed as designed during the event except breaker 25C6, power supply breaker to main S/G feedwater pump motor 2-FW-P-102.
This event is reportable pursuant to T.S. 6.9.1.9.b and serves as a special report in accordance with T.S.
3.4.9.3 action C and T.S.
3.5.3 action C reportable pursuant to T.S. 6.9.2.
This was the fifth S.I. to occur on Unit 2.
Probable Consequences of Occurrence The Emergency Core Cooling System is designed to inject borated water into the Reactor Coolant System and maintain coolant inventory in the event of a loss of coolant accident or rapid cooldown from a main steam line break.
Since the ECCS System and related equipment performed as required and an actual condition requiring the ECCS did not occur the health and safety of the public were not affected.
Breaker 25C6 trip is part of the main S/G feedwater isolation.
Since isolation valves associated with the isolation of the feedpumps did close the health and safety of the public were not affected.
Cause of Occurrence The power supply to the Solid State Protection System train "B" logic cabinet is provided by two redundant power supplies to assure a positive power source to the logic cards.
Number one power supply is fed from 120 VAC Vital bus 2-III and number two power supply is fed from 120 VAC Vital bus 2-IV.
Seventeen minutes prior to the receipt of the Emergency Core Cooling actuation a SSPS train " P,"
trouble alarm was received in the main Control Room. Upon investigation it was determined that the alarm was brought in by a blown fuse in the power supply line from 120 VAC Vital bus 2-IV to the number two D.C. power supply.
The fuse blew because of a short to ground in the number four turbine throttle valve limit switch.
The short was caused by maintenance i
personnel standing on the conduit to the limit switch while performing maintenance.
,k e
Attachment: Page 2 of 2 The loss of power to SSPS train "B" from 120 VAC Vital bus 2-lV left only one D.C.
power supply to the logic cabinet.
A power supply spike is the suspected cause of the loss of the Lo-Lo pressurizer pressure block. The cause of the suspected spike in 120 VAC bus 2-III was investigated and could not be determined.
The failure of breaker 25C6 to trip on ECCS actuation is under investigation and will be repaired prior to re-entering Mode 4.
Immediate Corrective Action
Immediate corrective actions were to restore the Refueling Water Storage Tank level and Control Room bottled air to operable status in accordance with their associated T.S.
Action Statements.
Maintenance personnel involved were reinstructed upon the dangers of using conduit for supports.
Scheduled Corrective Action Determine cause of failure of 25C6 to trip on an ECCS actuation and repair prior to re-entering Mode 4.
Actions Taken to Prevent Recurrence None required.
Generic Implications None
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| 05000338/LER-1983-001-03, /03L-0:on 830112,primary Grade Water Isolation Valve to Blender 1-CH-217 Remained Open Longer than Tech Spec Requirements.Caused by Personnel Error.Responsible Operator Reinstructed | /03L-0:on 830112,primary Grade Water Isolation Valve to Blender 1-CH-217 Remained Open Longer than Tech Spec Requirements.Caused by Personnel Error.Responsible Operator Reinstructed | | | 05000338/LER-1983-001, Forwards LER 83-001/03L-0 | Forwards LER 83-001/03L-0 | | | 05000339/LER-1983-001-03, /03L-0:on 830123,charging Pump 2-CH-P-1C Secured from Operation During High Lube Oil Temp Evaluation on Pump Speed Changer.Caused by Faulty Temp Indicator.Excess Oil Drained & Temp Returned to Normal.Temp Indicator Replaced | /03L-0:on 830123,charging Pump 2-CH-P-1C Secured from Operation During High Lube Oil Temp Evaluation on Pump Speed Changer.Caused by Faulty Temp Indicator.Excess Oil Drained & Temp Returned to Normal.Temp Indicator Replaced | | | 05000339/LER-1983-001, Forwards LER 83-001/03L-0 | Forwards LER 83-001/03L-0 | | | 05000339/LER-1983-002, Forwards LER 83-002/03L-0 | Forwards LER 83-002/03L-0 | | | 05000338/LER-1983-002-03, /03L-0:830104,meteorological Delta Temp Recorder Determined Out of Tolerance.Caused by Instrument Drift. Recorder Recalibr | /03L-0:830104,meteorological Delta Temp Recorder Determined Out of Tolerance.Caused by Instrument Drift. Recorder Recalibr | | | 05000338/LER-1983-002, Forwards LER 83-002/03L-0 | Forwards LER 83-002/03L-0 | | | 05000339/LER-1983-003-03, /03L-0:on 830104,middle Level Corner Support Temp for Steam Generator a Indicated Less than 225 F for 12 H. Caused by Condensation Due to High Secondary Steam Leakage from body-to-bonnet Leak of Blowdown Isolation Valve | /03L-0:on 830104,middle Level Corner Support Temp for Steam Generator a Indicated Less than 225 F for 12 H. Caused by Condensation Due to High Secondary Steam Leakage from body-to-bonnet Leak of Blowdown Isolation Valve | | | 05000339/LER-1983-003, Forwards LER 83-003/03L-0 | Forwards LER 83-003/03L-0 | | | 05000338/LER-1983-003, Forwards LER 83-003/03L-0 | Forwards LER 83-003/03L-0 | | | 05000338/LER-1983-003-03, /03L-0:on 830122,during Mode 5,RHR Flow Was Lost for 4 Minutes.Caused by Failure of 15 Kv a Inverter to Ac Vital Bus 1-III,de-energizing Auxiliary Relay for Pressure Channel P-1403.Vital Bus 1-III & RHR Flow Restored | /03L-0:on 830122,during Mode 5,RHR Flow Was Lost for 4 Minutes.Caused by Failure of 15 Kv a Inverter to Ac Vital Bus 1-III,de-energizing Auxiliary Relay for Pressure Channel P-1403.Vital Bus 1-III & RHR Flow Restored | | | 05000339/LER-1983-004, Forwards LER 83-004/03L-0 | Forwards LER 83-004/03L-0 | | | 05000339/LER-1983-004-03, /03L-0:on 830105,casing Cooling Pump B Removed from Svc.Caused by Need to Repair Small Leak in Discharge Flange of Pump.Repair Made & Pump Returned to Svc | /03L-0:on 830105,casing Cooling Pump B Removed from Svc.Caused by Need to Repair Small Leak in Discharge Flange of Pump.Repair Made & Pump Returned to Svc | | | 05000338/LER-1983-004-03, /03L-0:on 830125,svc Water Supply Valves MOV-SW- 103B & C & Discharge Valve MOV-SW-104C to Recirculation Spray HXs Would Not Open.Caused by Problems in Valve Operators.Valves Removed & Cleaned | /03L-0:on 830125,svc Water Supply Valves MOV-SW- 103B & C & Discharge Valve MOV-SW-104C to Recirculation Spray HXs Would Not Open.Caused by Problems in Valve Operators.Valves Removed & Cleaned | | | 05000338/LER-1983-004, Forwards LER 83-004/03L-0 | Forwards LER 83-004/03L-0 | | | 05000338/LER-1983-005, Forwards LER 83-005/03L-0 | Forwards LER 83-005/03L-0 | | | 05000338/LER-1983-005-03, /03L-0:on 830313,individual Rod Position Indication for Rod G-13 in Shutdown Bank a Deviated from Group Demand Position.Caused by Instrument Drift.Problem Generic to Westinghouse Analog Position Indication Sys | /03L-0:on 830313,individual Rod Position Indication for Rod G-13 in Shutdown Bank a Deviated from Group Demand Position.Caused by Instrument Drift.Problem Generic to Westinghouse Analog Position Indication Sys | | | 05000339/LER-1983-005, Forwards LER 83-005/03L-0 | Forwards LER 83-005/03L-0 | | | 05000339/LER-1983-005-03, /03L-0:on 830108,valve Monitoring Sys Cabinet de-energized for Maint,Causing Loss of Valve Position Indication for Pressurizer Safety & Porvs.Caused by Open Breakers.Breakers Closed After Maint | /03L-0:on 830108,valve Monitoring Sys Cabinet de-energized for Maint,Causing Loss of Valve Position Indication for Pressurizer Safety & Porvs.Caused by Open Breakers.Breakers Closed After Maint | | | 05000338/LER-1983-006-03, /03L-0:on 830125,triaxial Peak Accelegraphs on RHR HX & Safety Injection Pipe Found Inoperable from Corrosion Damage on Internal Parts.Caused by Moisture Entering Accelegraphs.Units Replaced | /03L-0:on 830125,triaxial Peak Accelegraphs on RHR HX & Safety Injection Pipe Found Inoperable from Corrosion Damage on Internal Parts.Caused by Moisture Entering Accelegraphs.Units Replaced | | | 05000338/LER-1983-006, Forwards LER 83-006/03L-0 | Forwards LER 83-006/03L-0 | | | 05000339/LER-1983-006, Forwards LER 83-006/03L-0 | Forwards LER 83-006/03L-0 | | | 05000339/LER-1983-006-03, /03L-0:on 830106,MOV-RS-255B,recirculation Spray Pump 2B Suction Isolation Valve Failed to Reopen After Periodic Test,Rendering 2-RS-P-2B Inoperable.Caused by Motor Operator Torquing Out from Jammed Seal Cap.Cap Reset | /03L-0:on 830106,MOV-RS-255B,recirculation Spray Pump 2B Suction Isolation Valve Failed to Reopen After Periodic Test,Rendering 2-RS-P-2B Inoperable.Caused by Motor Operator Torquing Out from Jammed Seal Cap.Cap Reset | | | 05000338/LER-1983-007-03, /03L-0:on 830202,during Mode 5,high Head Safety Injection Throttle Valve Found Out of Alignment by 7/8 of Turn.Caused by Miscount of Valve Handle Turns During Type C 821109 Test or 821108 Valve Verification Procedure | /03L-0:on 830202,during Mode 5,high Head Safety Injection Throttle Valve Found Out of Alignment by 7/8 of Turn.Caused by Miscount of Valve Handle Turns During Type C 821109 Test or 821108 Valve Verification Procedure | | | 05000339/LER-1983-007-03, /03L-0:on 830201,svc Water Supply Header to Charging Pump Lube Oil Coolers & Air Compressors Isolated to Repair Pinhole Leaks.Caused by Aggressive Water & Bacterial Reduction of Mild Steel Piping.Piping Replaced | /03L-0:on 830201,svc Water Supply Header to Charging Pump Lube Oil Coolers & Air Compressors Isolated to Repair Pinhole Leaks.Caused by Aggressive Water & Bacterial Reduction of Mild Steel Piping.Piping Replaced | | | 05000339/LER-1983-007, Forwards LER 83-007/03L-0 | Forwards LER 83-007/03L-0 | | | 05000338/LER-1983-007, Forwards LER 83-007/03L-0 | Forwards LER 83-007/03L-0 | | | 05000338/LER-1983-008, Forwards LER 83-008/03L-0 | Forwards LER 83-008/03L-0 | | | 05000338/LER-1983-008-03, /03L-0:on 830410,review Revealed That Procedure Used to Restore Boron Injection Tank Concentration Introduced Potential Unanalyzed Injection Flow Diversions. Caused by Oversight.Emergency Procedures Revised | /03L-0:on 830410,review Revealed That Procedure Used to Restore Boron Injection Tank Concentration Introduced Potential Unanalyzed Injection Flow Diversions. Caused by Oversight.Emergency Procedures Revised | | | 05000339/LER-1983-008-03, /03L-0:on 830107,during Mode 3,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps While Withdrawing Shutdown Bank B. Caused by Instrument Drift.Rods Recalibr | /03L-0:on 830107,during Mode 3,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps While Withdrawing Shutdown Bank B. Caused by Instrument Drift.Rods Recalibr | | | 05000339/LER-1983-008, Forwards LER 83-008/03L-0 | Forwards LER 83-008/03L-0 | | | 05000338/LER-1983-009-03, /03L-0:on 830218,control Room Operator Observed Indications of Cavitation on RHR Pumps a & B.Cause Unknown. Pumps Secured & Vented.No Air Observed While Venting Pumps | /03L-0:on 830218,control Room Operator Observed Indications of Cavitation on RHR Pumps a & B.Cause Unknown. Pumps Secured & Vented.No Air Observed While Venting Pumps | | | 05000338/LER-1983-009, Forwards LER 83-009/03L-0 | Forwards LER 83-009/03L-0 | | | 05000339/LER-1983-009, Forwards LER 83-009/03L-0 | Forwards LER 83-009/03L-0 | | | 05000339/LER-1983-009-03, /03L-0:on 830112,train a Reactor Trip Breaker Bypassed for More than Allowed 2 H During Solid State Protection Sys Surveillance Testing.Cause Due to Necessity to Replace Damaged Universal Logic Card | /03L-0:on 830112,train a Reactor Trip Breaker Bypassed for More than Allowed 2 H During Solid State Protection Sys Surveillance Testing.Cause Due to Necessity to Replace Damaged Universal Logic Card | | | 05000338/LER-1983-010-03, /03L-0:on 830304,while in Mod 3,fire Door S71-17 Between 1J Emergency Diesel Generator Room & Turbine Bldg Declared Inoperable.Caused by Warping Due to Closing Door During Diesel Operation.Closure Device Readjusted | /03L-0:on 830304,while in Mod 3,fire Door S71-17 Between 1J Emergency Diesel Generator Room & Turbine Bldg Declared Inoperable.Caused by Warping Due to Closing Door During Diesel Operation.Closure Device Readjusted | | | 05000338/LER-1983-010, Forwards LER 83-010/03L-0 | Forwards LER 83-010/03L-0 | | | 05000339/LER-1983-010-03, /03L-0:on 830109,fire Door S54-13 Between Control Room Air Handler Room & Control Room Chiller Room Would Not Consistently Close.Caused by Loose Door Hinges & Out of Adjustment Reclosure Device.Hinges Tightened | /03L-0:on 830109,fire Door S54-13 Between Control Room Air Handler Room & Control Room Chiller Room Would Not Consistently Close.Caused by Loose Door Hinges & Out of Adjustment Reclosure Device.Hinges Tightened | | | 05000339/LER-1983-010, Forwards LER 83-010/03L-0 | Forwards LER 83-010/03L-0 | | | 05000338/LER-1983-011, Forwards LER 83-011/03L-0 | Forwards LER 83-011/03L-0 | | | 05000338/LER-1983-011-03, /03L-0:on 830304,while in Mode 3,turbine Driven Auxiliary Feedwater Pump Tripped on Overspeed During Testing.Caused by Incorrect Setting of Turbine Governor on 830228.New Governor Installed & Pump Tested Satisfactorily | /03L-0:on 830304,while in Mode 3,turbine Driven Auxiliary Feedwater Pump Tripped on Overspeed During Testing.Caused by Incorrect Setting of Turbine Governor on 830228.New Governor Installed & Pump Tested Satisfactorily | | | 05000339/LER-1983-011, Forwards LER 83-011/03L-0 | Forwards LER 83-011/03L-0 | | | 05000339/LER-1983-011-03, /03L-0:on 821119,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps.Caused by Instrument Drift.Indicator Channel for Rods B-09 & 02 & F-06 Recalibr | /03L-0:on 821119,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps.Caused by Instrument Drift.Indicator Channel for Rods B-09 & 02 & F-06 Recalibr | | | 05000338/LER-1983-012-03, /03L-0:on 830304,individual Rod Position Indication for Rod D-04 in Control Bank C Indicated Zero Steps & Deviated from Group Demand Position.Caused by Faulty Signal Conditioning Module.Conditioning Module Replaced | /03L-0:on 830304,individual Rod Position Indication for Rod D-04 in Control Bank C Indicated Zero Steps & Deviated from Group Demand Position.Caused by Faulty Signal Conditioning Module.Conditioning Module Replaced | | | 05000338/LER-1983-012, Forwards LER 83-012/03L-0 | Forwards LER 83-012/03L-0 | | | 05000339/LER-1983-012-03, /03L-0:on 830114,delta T Indicator Associated W/Delta T Protection for Loop a Read 6% High.Caused by Failed Relay Card on Delta T Hot Loop A,TE-2412B,output. Card Replaced | /03L-0:on 830114,delta T Indicator Associated W/Delta T Protection for Loop a Read 6% High.Caused by Failed Relay Card on Delta T Hot Loop A,TE-2412B,output. Card Replaced | | | 05000339/LER-1983-012, Forwards LER 83-012/03L-0 | Forwards LER 83-012/03L-0 | | | 05000338/LER-1983-013-03, /03L-0:on 830317,steam Generator a Steam Flow Channel IV Failed Low.Cause Unknown.Failed Channel Placed in Tripped Condition | /03L-0:on 830317,steam Generator a Steam Flow Channel IV Failed Low.Cause Unknown.Failed Channel Placed in Tripped Condition | | | 05000338/LER-1983-013, Forwards LER 83-013/03L-0 | Forwards LER 83-013/03L-0 | | | 05000339/LER-1983-013, Forwards LER 83-013/03L-0 | Forwards LER 83-013/03L-0 | |
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