LER-1982-083, /03L-0:on 821204,while Operating at 17% Rated Thermal Power,Turbine Control Sys Malfunctioned Causing Sudden Increase in Load,Resulting in Reactor Trip.Caused by Malfunction of Analog Converter |
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| 3381982083R03 - NRC Website |
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U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK / / / / / / / (1)
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)-
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LICENSEE CODE LICENSE NUMBER LICENSE TYPE CAT 0/1f RE O
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R DOCKET NUMBER EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10)
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/ On December 4, 1982, with Unit I at 17 percent of Rated Thermal Power, a mal-
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/ function of the Turbine Control System caused it to suddenly increase lead. A j
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/ Reactor Trip and SI resulted. All safety equipment responded as required. The /
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/ event was quickly terminated. The applicable LCO Action Statements were met.
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/ The public health and safety were not affected. This event is reportable pursu- /
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/ ant to T.S. 6.9.2 and T.S. 6.9.1.9.b.
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SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE
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SEQUENTIAL OCCURRENCE REPORT REVISION LER/R0 EVENT YEAR REPORT NO.
CODE TYPE NO.
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ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT MET 110D HOURS SUBMITTED FOM SUB. SUPPLIER MANUFACTURER
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27)
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/ A malfunction of a digital to analog converter in the turnine Electro-Hydraulic /
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/ _ Control (EllC) System caused the event. The plant was quickly stabilized and all /
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/ parameters restored to normal. All equipment was returned to normal status.
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/ The Turbine EllC System has been repaired.
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FACILITY METHOD OF
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DISCOVERY DISCOVERY DESCRIPTION (32)
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/ Operator Observation /
ACTIVITY CONTENT l
RELEASED OF RELEASE AMOUNT OF ACTIVITY (35)
LOCATION OF RELEASE (36)
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PERSONNEI EXPOSURES NUMBER TYPE DESCRIPTION (39)
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i PERSONNEL INJURIES NUMBER DESCRIPTION (41)
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LOSS OF OR DAMAGE TO FACILITY 3)
TYPE
DESCRIPTION
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PUBLICITY i
ISSUED DESCRIPTION (45)
NRC USE ONLY
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NAMF OF PRFPARER W. R. CARTWRIGHT PHONE (703) 894-5151 8301100314 821231 PDR ADOCK 05000338 S
PDR
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f Virginia Electric and Power Company North Anna Power Station, Unit No. 1 Attachment: Page 1 of 2 Docket No. 50-338 Attachment to LER 82-083/03L-0
Description of Event
On December 4, 1982 at 1650, with Unit 1 at 17 parcent of Rated Thermal Power and 100 MWe, turbine control was transferred from " IMP 4
OUT" (valve position reference control) to " IMP IN" (load or impulse pressure reference control).
The turbine EHC System malfunctioned and i
the turbine started ramping up at approximately 50 to 75 MWe per second.
The governor valves stopped opening at the " Valve Position Limiter" setting of 30 percent.
The load increase terminated at approximately 260 MWe.
The operator transferred to manual turbine control and an attempt was made to restore the governor valves to their original l
pretransient position manually; however the turbine transient was too severe to allow recovery.
The reactor tripped on a low steam generator level coincident with a steam flow / feed flow mismatch signal.
The Post Accident Analysis Log (PAAL) indicates that 183 milliseconds after the reactor trip the turbine tripped.
Automatic safety injection was initiated 350 milliseconds af ter the reactor trip from a high steamline flow - coincident with low reactor coolant average temperature SI signal.
l The reactor power increased from 17 to 23 percent prior to the reactor trip.
The minimum pressurizer level obtained during the event l
was 14.5 percent.
The lowest average reactor coolant temperature i
obtained during the event was 520 degrees fahrenheit.
The lowest reactor coolant system presrure obtained during the event was 2148 psig.
l Steam generator narrow range level wrs maintained throughout the event.
The primary system transient was mild.
All safety related equipment performed as designed.
No safety related equipoent failures occurred.
Approximately eight minutes after the event began, all conditions required by energency procedures to secure safety injection ware met and safety injection was terminated.
An unusual event was declared at 1650 when the event began.
By 1655 all parameters were within normal ranges for Mode 3 operation and preparations for returning equipment status to normal were being made.
The unusual event was terminated at 1655.
The NRC was informed of the unusual event within 15 minutes.
All emergency plan state and local notifications were completed by 1742.
The Control Room bottled air system which discharged during the event as designed was restored to operable status by 1730 in compliance with the Action Statement of the LCO for T.S.
3.7.7.1.
The Boron Injection Tank boron concentration was restored to T.S. 3.5.4.1 limits by 2145.
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Page 2 of 2 Unit 2 remained at 100 percent of Rated Thermal Power throughout the event and was not affected.
This event is reportable pursuant to T.S. 6.9.2 and T.S. 6.9.1.9.b.
This is the seventh ECCS actuation reportable pursuant to T.S. 6.9.2.
Probable Consequences of Occurrence All systems performed as designed.
The Action Statements of all applicable LCO's were met.
All parameters and equipment were quickly restored to notmal. No personnel injuries or equipment damage occurred.
The public health and safety were not affected.
Cc.use of Occurrence Both the reactor trip and safety injection were caused by a malfunction of a digital to analog converter in the Turbine EHC System.
Immediate Corrective Action
The appropriate emergency procedures were implemented, the plant was stabilized, and all parameters restored to normal.
All equipment was restored to normal status. The Turbine EHC System was repaired.
Scheduled Corrective Action No scheduled corrective actions are required.
Action Taken To Prevent Recurrence The Turbine EHC System has been repaired.
Generic Implications This event has no generic implications.
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| 05000339/LER-1982-001, Forwards LER 82-001/03L-0 | Forwards LER 82-001/03L-0 | | | 05000339/LER-1982-001-03, /03L-0:on 820101,RCS Leakage Increased to 15-30 Gpm.Caused by Missing Packing on RHR Isolation Valve. Packing Had Deteriorated & Passed Through Valve Leadoff Line.Valve Repacked,Leak Tested & Returned to Svc | /03L-0:on 820101,RCS Leakage Increased to 15-30 Gpm.Caused by Missing Packing on RHR Isolation Valve. Packing Had Deteriorated & Passed Through Valve Leadoff Line.Valve Repacked,Leak Tested & Returned to Svc | | | 05000338/LER-1982-001-03, /03L-0:on 820107,power Range Detector N-44 Drifted Low & Was Declared Inoperable.Quadrant Power Tilt Ratio Found Below Tech Spec Limit.Caused by Faulty Power Range Detector.Detector to Be Replaced During Refueling Outage | /03L-0:on 820107,power Range Detector N-44 Drifted Low & Was Declared Inoperable.Quadrant Power Tilt Ratio Found Below Tech Spec Limit.Caused by Faulty Power Range Detector.Detector to Be Replaced During Refueling Outage | | | 05000338/LER-1982-001, Forwards LER 82-001/03L-0 | Forwards LER 82-001/03L-0 | | | 05000338/LER-1982-002-03, /03L-0:on 820111,containment Particulate Activity detector,RM-159 & Containment Gaseous Activity Detector, RM-160,failed Low.Caused by Loose Electrical Connector on RM-159 & Drive Motor Failure on RM-160 | /03L-0:on 820111,containment Particulate Activity detector,RM-159 & Containment Gaseous Activity Detector, RM-160,failed Low.Caused by Loose Electrical Connector on RM-159 & Drive Motor Failure on RM-160 | | | 05000338/LER-1982-002, Forwards LER 82-002/03L-0 | Forwards LER 82-002/03L-0 | | | 05000339/LER-1982-002-03, /03L-0:on 820110,during Mode 1 Operation at 20% Power,C Reactor Coolant Loop Flow Lost.Caused by Loss of Power During Transfer from Reserve Transformer.Unit Tripped Manually & Pump Restarted When Power Restored | /03L-0:on 820110,during Mode 1 Operation at 20% Power,C Reactor Coolant Loop Flow Lost.Caused by Loss of Power During Transfer from Reserve Transformer.Unit Tripped Manually & Pump Restarted When Power Restored | | | 05000339/LER-1982-002, Forwards LER 82-002/03L-0 | Forwards LER 82-002/03L-0 | | | 05000338/LER-1982-003-03, /03L-0:on 820201 & 08,fire Door Between Rod Drive Room & Outside Would Not Latch.On 820203,1H Emergency Diesel Generator Access Door Would Not Latch.Caused by Inadequately Lubricated Latching Mechanisms | /03L-0:on 820201 & 08,fire Door Between Rod Drive Room & Outside Would Not Latch.On 820203,1H Emergency Diesel Generator Access Door Would Not Latch.Caused by Inadequately Lubricated Latching Mechanisms | | | 05000338/LER-1982-003, Forwards LER 82-003/03L-0 | Forwards LER 82-003/03L-0 | | | 05000339/LER-1982-003, Forwards LER 82-003/03L-0 | Forwards LER 82-003/03L-0 | | | 05000339/LER-1982-003-03, /03L-0:on 820110,individual Rod Position Indication(Ipri)For Rod J-07 & Group Demand Position for Shutdown Bank B Differed by 12 Steps.On 820111,IRPI for Rod B-08 Drifted.Caused by Voltage Drift in Circuitry | /03L-0:on 820110,individual Rod Position Indication(Ipri)For Rod J-07 & Group Demand Position for Shutdown Bank B Differed by 12 Steps.On 820111,IRPI for Rod B-08 Drifted.Caused by Voltage Drift in Circuitry | | | 05000338/LER-1982-004-03, /03L-0:on 820116,at 100% power,1J Emergency Diesel Generator Door Would Not Latch.Fire Watch Posted.Caused by Loose Latch Cover Plate Preventing Door from Latching Properly.Latch Repaired | /03L-0:on 820116,at 100% power,1J Emergency Diesel Generator Door Would Not Latch.Fire Watch Posted.Caused by Loose Latch Cover Plate Preventing Door from Latching Properly.Latch Repaired | | | 05000338/LER-1982-004, Forwards LER 82-004/03L-0 | Forwards LER 82-004/03L-0 | | | 05000339/LER-1982-004, Forwards LER 82-004/03L-0 | Forwards LER 82-004/03L-0 | | | 05000339/LER-1982-004-03, /03L-0:on 820110,containment Isolation Steam Operator Blowdown Valve TV-BD-200C Would Not Remain Closed from Control Room.Caused by Excessive Moisture in Limit Switch Housing.Housing Drained | /03L-0:on 820110,containment Isolation Steam Operator Blowdown Valve TV-BD-200C Would Not Remain Closed from Control Room.Caused by Excessive Moisture in Limit Switch Housing.Housing Drained | | | 05000339/LER-1982-005, Forwards LER 82-005/03L-0 | Forwards LER 82-005/03L-0 | | | 05000339/LER-1982-005-03, /03L-0:on 820222,in Mode 1,2J Emergency Diesel Generator Fire Door (S71-16) Between Diesel Room & Turbine Bldg Would Not Latch.Caused by Door Lock Tumbler Rotating on Axis & Not Engaging Latch.Lock Tumbler Tightened | /03L-0:on 820222,in Mode 1,2J Emergency Diesel Generator Fire Door (S71-16) Between Diesel Room & Turbine Bldg Would Not Latch.Caused by Door Lock Tumbler Rotating on Axis & Not Engaging Latch.Lock Tumbler Tightened | | | 05000338/LER-1982-005-03, /03L-0:on 820211,w/unit in Mode 1,RCS Unidentified Leakage Was Determined in Excess of Tech Specs.Caused by Packing Leak on 1-RC-129 Level Instrument Isolation Valve. Valves 1-RC-129 & 1-RC-130 Closed | /03L-0:on 820211,w/unit in Mode 1,RCS Unidentified Leakage Was Determined in Excess of Tech Specs.Caused by Packing Leak on 1-RC-129 Level Instrument Isolation Valve. Valves 1-RC-129 & 1-RC-130 Closed | | | 05000338/LER-1982-005, Forwards LER 82-005/03L-0 | Forwards LER 82-005/03L-0 | | | 05000338/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | | 05000338/LER-1982-006-03, /03L-0:on 820305,during Mode 1 at 100% Power,A Svc Water Return Header from Units 1 & 2 Charging Pumps & Air Compressors Were Isolated to Repair Pinhole Leak in Return Line.Caused by Aggressive Water Corrosion | /03L-0:on 820305,during Mode 1 at 100% Power,A Svc Water Return Header from Units 1 & 2 Charging Pumps & Air Compressors Were Isolated to Repair Pinhole Leak in Return Line.Caused by Aggressive Water Corrosion | | | 05000339/LER-1982-006-03, /03L-0:on 820216,during Mode 1 Operation,B Quench Spray Subsystem Removed from Svc Contrary to Tech Specs. Subsystem Removed from Svc to Repair body-to-bonnet Leak on B Quench Spray Pump Suction valve,MOV-QS-200B | /03L-0:on 820216,during Mode 1 Operation,B Quench Spray Subsystem Removed from Svc Contrary to Tech Specs. Subsystem Removed from Svc to Repair body-to-bonnet Leak on B Quench Spray Pump Suction valve,MOV-QS-200B | | | 05000339/LER-1982-006, Forwards LER 82-006/03L-0 | Forwards LER 82-006/03L-0 | | | 05000339/LER-1982-007, Forwards LER 82-007/03L-0 | Forwards LER 82-007/03L-0 | | | 05000338/LER-1982-007-03, /03L-0:on 820214,in Mode 1,fire Door S71-7 Declared Inoperable.On 820216,fire Doors A19-1 & A44-1 Declared Inoperable.Caused by Failure of Closures & Latching Mechanisms Due to Excessive Use.Locks Readjusted/Repaired | /03L-0:on 820214,in Mode 1,fire Door S71-7 Declared Inoperable.On 820216,fire Doors A19-1 & A44-1 Declared Inoperable.Caused by Failure of Closures & Latching Mechanisms Due to Excessive Use.Locks Readjusted/Repaired | | | 05000338/LER-1982-007, Forwards LER 82-007/03L-0 | Forwards LER 82-007/03L-0 | | | 05000339/LER-1982-007-03, /03L-0:on 820312,during Mode 5,emergency Diesel Generators 2H & 2J Were Not Operable.Caused by Failure of Voltage Regulator for 2J Causing Bus Voltage to Peg High & Open 1J Output Breaker 25J2 | /03L-0:on 820312,during Mode 5,emergency Diesel Generators 2H & 2J Were Not Operable.Caused by Failure of Voltage Regulator for 2J Causing Bus Voltage to Peg High & Open 1J Output Breaker 25J2 | | | 05000338/LER-1982-008, Forwards LER 82-008/01T-0 | Forwards LER 82-008/01T-0 | | | 05000338/LER-1982-008-01, /01T-0:on 820329,Westinghouse Determined That Six Output Slave Relays Did Not Have Qualified Latching Mechanisms.Caused by Use of Two Different Types of Latches. Latching Mechanisms Will Be Replaced | /01T-0:on 820329,Westinghouse Determined That Six Output Slave Relays Did Not Have Qualified Latching Mechanisms.Caused by Use of Two Different Types of Latches. Latching Mechanisms Will Be Replaced | | | 05000339/LER-1982-008-01, /01T-0:on 820307,prior to Refueling Outage,Power Restored to Accumulator Isolation Valves & Valves Closed W/ Pressurizer Pressure 1,000 Psig.Caused by Personnel Error. Valves Automatically Reopened W/Increased Pressure | /01T-0:on 820307,prior to Refueling Outage,Power Restored to Accumulator Isolation Valves & Valves Closed W/ Pressurizer Pressure 1,000 Psig.Caused by Personnel Error. Valves Automatically Reopened W/Increased Pressure | | | 05000339/LER-1982-008, Forwards LER 82-008/01T-0 | Forwards LER 82-008/01T-0 | | | 05000338/LER-1982-009, Forwards LER 82-009/99L-0 | Forwards LER 82-009/99L-0 | | | 05000338/LER-1982-009-99, /99L-0:on 820216,electric Driven Fire Pump 1-FP-P-1 Was Tagged Out & Declared Inoperable for Longer than 7 Days.Caused by Required Maint on 1B Circulating Water Pump.Redundant Source of Fire Water Provided | /99L-0:on 820216,electric Driven Fire Pump 1-FP-P-1 Was Tagged Out & Declared Inoperable for Longer than 7 Days.Caused by Required Maint on 1B Circulating Water Pump.Redundant Source of Fire Water Provided | | | 05000339/LER-1982-009-03, /03L-0:from 820308-10,pressurizer Power Operated Relief Valves Declared Inoperable Three Times While Cooling Down for Refueling Outage.Caused by Excessive Nitrogen Sys Demand,Excessive Sys Leakage & Inadequate Makeup Supply | /03L-0:from 820308-10,pressurizer Power Operated Relief Valves Declared Inoperable Three Times While Cooling Down for Refueling Outage.Caused by Excessive Nitrogen Sys Demand,Excessive Sys Leakage & Inadequate Makeup Supply | | | 05000339/LER-1982-009, Forwards LER 82-009/03L-0 | Forwards LER 82-009/03L-0 | | | 05000339/LER-1982-010, Forwards LER 82-010/03L-0 | Forwards LER 82-010/03L-0 | | | 05000338/LER-1982-010, /03L-0:on 820505,valves MOV-FW-154A,B & C & TV-1884A,B & C Found W/Identical Control Circuits as Reported in LER 82-010 for Unit 2.Design Permits Operator to Open Valves W/O Resetting Phase a Isolation Signal | /03L-0:on 820505,valves MOV-FW-154A,B & C & TV-1884A,B & C Found W/Identical Control Circuits as Reported in LER 82-010 for Unit 2.Design Permits Operator to Open Valves W/O Resetting Phase a Isolation Signal | | | 05000338/LER-1982-010-03, /03L-0:on 820223,post-reactor Trip Specific Activity Samples of RCS Indicated Dose Equivalent I-131 Level Greater than Tech Spec Limit.Caused by Fuel Element Defect.Sampling Frequency Accelerated | /03L-0:on 820223,post-reactor Trip Specific Activity Samples of RCS Indicated Dose Equivalent I-131 Level Greater than Tech Spec Limit.Caused by Fuel Element Defect.Sampling Frequency Accelerated | | | 05000338/LER-1982-011, Forwards LER 82-011/03L-0 | Forwards LER 82-011/03L-0 | | | 05000339/LER-1982-011-03, /03L-0:on 820410,fire Door M-80-2 Blocked Open W/O Fire Watch.On 820412,fire Door A-80-2 Would Not Close & Latch.Caused by Failure to Follow Procedures for Breeching Fire Barriers & Reclosure Device Being Out of Adjustment | /03L-0:on 820410,fire Door M-80-2 Blocked Open W/O Fire Watch.On 820412,fire Door A-80-2 Would Not Close & Latch.Caused by Failure to Follow Procedures for Breeching Fire Barriers & Reclosure Device Being Out of Adjustment | | | 05000338/LER-1982-011-03, /03L-0:on 820223,at 90% Power & Decreasing,Axial Flux Difference Deviated Greater than -5% from Target for 23 Minutes.Caused by Rapid Power Reduction Necessitated by Leak in Turbine Gland Steam Exhaust Sys | /03L-0:on 820223,at 90% Power & Decreasing,Axial Flux Difference Deviated Greater than -5% from Target for 23 Minutes.Caused by Rapid Power Reduction Necessitated by Leak in Turbine Gland Steam Exhaust Sys | | | 05000339/LER-1982-011, Forwards LER 82-011/03L-0 | Forwards LER 82-011/03L-0 | | | 05000339/LER-1982-012-03, /03L-0:on 820313,fire Door M80-2 Between Rod Control Room & Outside Would Not Close.On 820326,fire Door A80-2 Between Rod Control Room & Auxiliary Bldg Would Not Close.Caused by Improper Alignment Due to Excessive Use | /03L-0:on 820313,fire Door M80-2 Between Rod Control Room & Outside Would Not Close.On 820326,fire Door A80-2 Between Rod Control Room & Auxiliary Bldg Would Not Close.Caused by Improper Alignment Due to Excessive Use | | | 05000339/LER-1982-012, Forwards LER 82-012/03L-0 | Forwards LER 82-012/03L-0 | | | 05000338/LER-1982-012, Forwards LER 82-012/03L-0 | Forwards LER 82-012/03L-0 | | | 05000338/LER-1982-012-03, /03L-0:on 820223,emergency Condensate Storage Tank (Ecst) Dropped Below Min Required Vol Twice.Caused by Adding Water from Ecst to Steam Generators Due to Inoperable Condensate Sys | /03L-0:on 820223,emergency Condensate Storage Tank (Ecst) Dropped Below Min Required Vol Twice.Caused by Adding Water from Ecst to Steam Generators Due to Inoperable Condensate Sys | | | 05000339/LER-1982-013-03, During Periodic Surveillance Test,One Diesel Generator & One Offsite Power Supply for Emergency Bus 2H Became Temporarily Inoperable. Caused by Deficiency in Procedure.Periodic Test Changed | During Periodic Surveillance Test,One Diesel Generator & One Offsite Power Supply for Emergency Bus 2H Became Temporarily Inoperable. Caused by Deficiency in Procedure.Periodic Test Changed | | | 05000338/LER-1982-013-03, /03L-0:on 820401,post-reactor Trip Specific Activity Samples of RCS Indicated Dose Equivalent Level Greater than Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core.Accelerated Sampling Frequency Implemented | /03L-0:on 820401,post-reactor Trip Specific Activity Samples of RCS Indicated Dose Equivalent Level Greater than Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core.Accelerated Sampling Frequency Implemented | | | 05000338/LER-1982-013, Forwards LER 82-013/03L-0 | Forwards LER 82-013/03L-0 | |
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