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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D0201994-04-25025 April 1994 LER 94-007-01:on 931014,high Head Safety Injection Flow Balance Testing Found to Be Below TS Requirement.Caused by Unaccounted for Uncertainties.Cold Leg Safety Injection Leg Throttle Valve adjusted.W/940425 Ltr ML20045G9391993-07-0808 July 1993 Lr 93-017-00:on 930616,containment Hydrogen Analyzer Heat Trace Channel Calibration Not Performed on Staggered Test Basis Due to Inadequate Implementation of TS Amend.Test Procedure Satisfactorily performed.W/930708 Ltr ML20044H1591993-05-27027 May 1993 LER 93-016-00:on 930509,discovered That Containment Hydrogen Analyzer Pressure Switch PS-3 Sensing Line Disconnected in Local Panel.Caused by Personnel Error. Pressure Switch Calibr & Line reconnected.W/930527 Ltr ML20044D5711993-05-14014 May 1993 LER 93-002-00:on 930416,automatic Reactor Trip Initiated from Turbine Trip Due to Over Excitation of Main Generator. Emergency Procedure 2-E-0 Entered & Individuals Involved in Event Received Remediated training.W/930514 Ltr ML20044D2281993-05-12012 May 1993 LER 93-003-00:on 930424,manual Reactor Trip Initiated Due to Erratic Feedwater Flow Indications to SG C & Excessive Main Feedwater Regulating Valve Oscillations.Caused by Design Instabilities.Secondary Sys secured.W/930512 Ltr ML20044C9541993-05-0707 May 1993 LER 93-015-00:on 930427,discovered That Portions of Containment Pressure Channels That Input to Containment Spray hi-hi Pressure Not Tested Monthly.Caused by Personnel Error.Test Procedures changed.W/930507 Ltr ML20044C9811993-05-0606 May 1993 LER 93-014-00:on 930411,as-found Speed Setting of Steam Driven AFW Pump 1-FW-P-2 Found Below Required TS Limit. Caused by Incorrect Speed Control Setting.Pump Speed Adjusted & Maint Personnel counseled.W/930506 Ltr ML20024G6841991-04-18018 April 1991 LER 91-006-00:on 910403,discovered That Ac Offsite Power Source Surveillance Not Performed Due to Personnel Error. Surveillance Initiated Immediately & Positive Discipline Administered to supervisor.W/910418 Ltr ML20029B5601991-03-0606 March 1991 LER 91-005-00:on 910209,containment Building Penetrations Breached.Caused by Inadequate Procedural Controls.Core Mapping & Cavity Pump Down Activities Secured,Air Hose Removed & Hydrolase Hose capped.W/910306 Ltr ML20029A6471991-02-22022 February 1991 LER 91-004-00:on 910206,sealed Radioactive Source in Storage Not Leak Tested Prior to Use.Caused by Inadequate Procedures for Verifying Leak Testing of Sources.Procedures Revised.W/ 910222 Ltr ML20028H6681991-01-18018 January 1991 LER 90-009-01:on 900719,discovered That Response Time Testing of Pressurizer High Level Reactor Trip Function Not Performed in Accordance W/Tech Spec 3.3.1.1,Table 3.3-2. Caused by Personnel Error.Procedures revised.W/910118 Ltr ML20043H8321990-06-22022 June 1990 LER 90-007-00:on 900523,discovered That Two Sets of Concrete Roof Blocks on Svc Water Pump House Not in Required Safety Position.Caused by Lack of Administrative Controls.Blocks Restored to Required locations.W/900622 Ltr ML20043D5801990-06-0404 June 1990 LER 90-006-00:on 900504,casing Cooling Pump Not Put Into Alert Status & Surveillance Missed.Caused by Personnel Error.Pump 1-RS-P-3B Placed in Alert status.W/900604 Ltr ML20012E3301990-03-27027 March 1990 LER 90-003-00:on 900228,52 Valves Identified Not Included in Tech Spec Required Monthly Containment Integrity Verification Surveillance Program.Caused by Personnel Error & Inadequate Procedure.Procedure revised.W/900327 Ltr ML20012B6441990-03-0808 March 1990 LER 90-001-00:on 900215,inadvertent Partial Train a ESF Actuation of Containment Depressurization Sys Occurred. Caused by Human Error.Evaluation to Be Performed to Determine If Test Points Can Be moved.W/900308 Ltr ML20006E2371990-02-0808 February 1990 LER 90-001-00:on 900123,reactor Trip Occurred on Steam Feedwater Flow Mismatch.Caused by Failed Circuit Driver Card on Feedwater Regulating Valve.Feedwater Regulating Valve Driver Card replaced.W/900208 Ltr ML20006E3771990-02-0505 February 1990 LER 90-002-00:on 900127,fuel Bldg Ventilation Sys Not Aligned to Discharge Through Auxiliary Bldg HEPA Filter & Charcoal Adsorber Assembly During Fuel Movement.Caused by Personnel Error.Disciplinary Action taken.W/900205 Ltr ML20006A8531990-01-19019 January 1990 LER 89-019-00:on 891228,discovered That Outer Door of Containment Equipment Escape Air Lock Was Drawing in Air & Inner Door Noted as Not Being in Fully Closed Position.Cause Undetermined.Sys Enhancements Being evaluated.W/900119 Ltr ML20005F8781990-01-11011 January 1990 LER 89-018-00:on 891219,determined That Three Pressurizer Pressure Safety Injection Instrumentation Channels May Not Have Adequate Margin Between Actuation Setpoint & Bottom of Instrument span.W/900111 Ltr ML19332D5471989-11-22022 November 1989 LER 85-003-03:on 890907,determined That Situation Could Arise Where Water Level Would Rise to 264 Ft Before Next Required Surveillance Interval.Cause Not Determined.Dike to Be constructed.W/891122 Ltr ML20024B7821983-07-0606 July 1983 LER 83-048/03L-0:on 830606 & 17,intermediate Range Channels N35 & N36 High Neutron Flux Reactor Trip Setpoints Exceeded Tech Spec Requirements.Caused by Administrative Error. Setpoints reduced.W/830706 Ltr ML20024C1361983-06-30030 June 1983 LER 83-031/03L-0:on 830614,w/unit at 100% Power,Fire Door S54/5 from Emergency Switchgear Room to Cable Vault Would Not Latch.Fire Watch Posted Immediately.Caused by Misaligned Strike.Door Repaired within 1 h.W/830630 Ltr ML20024C3721983-06-30030 June 1983 LER 83-042/03L-0:on 830606,vital Bus 1-I Momentarily Deenergized While Trying to Clear Inverter Trouble Alarm. Caused by Operator Error.Bus energized.W/830630 Ltr ML20024B9891983-06-28028 June 1983 LER 83-047/03L-0:on 830530,emergency Diesel Generator 2J Tripped on High Crankcase Pressure During Surveillance Testing.Cause Not Determined.Diesel Tested Satisfactorily. W/830628 Ltr ML20024C2941983-06-23023 June 1983 LER 83-044/03L-0:on 830526,during Mode 3,one Recirculation Valve on Each of Two Casing Cooling Pumps Found Open.Caused by Procedure Inadequacy.Valves Closed Immediately.Maint Procedure Will Be revised.W/830623 Ltr ML20024C3071983-06-22022 June 1983 LER 83-034/03L-0:on 830525,during Mode 1,one Header of Control Room Bottled Air Pressurized Sys Had Lower than Required Pressure.Probably Caused by Leak from B Bank of Air Bottles.Header repressurized.W/830622 Ltr ML20024C0971983-06-22022 June 1983 LER 83-045/03L-0:on 830614,Fire Door S71-18,between Emergency Diesel Generator Room 2H & Turbine Bldg,Would Not Latch & Lock.Caused by Stuck Latch.Latch Adjusted & Lubricated.Door Designs modified.W/830622 Ltr ML20023E0951983-06-0101 June 1983 LER 83-027/03L-0:on 830505,one Header (42 Bottles) of Control Room Bottled Air Pressurized Sys Found to Have Lower than Required Pressure (2,290 Vs 2,300 Psig).Probably Caused by Leakage When Compressor malfunctioned.W/830601 Ltr ML20023E0721983-05-26026 May 1983 LER 83-029/03L-0:on 830509,following Rapid Rampdown from 100% to 4% power,I-131 Dose Equivalent Exceeded 1.0 Uci/G. Caused by Unidentified Fuel Element Defect Worsened by post-rampdown Conditions.Sampling increased.W/830526 Ltr ML20023D5371983-05-13013 May 1983 LER 83-022/03L-0:on 830412,review of ASME XI Iwv Program Identified 192 Valves Not Exercised &/Or Stroke Timed.Caused by Fragmented Implementation of Testing Program.Programs Upgraded ML20023D2491983-05-11011 May 1983 LER 83-032/03L-0:on 830412,during Mode 5,visual Insp of Hydraulic Snubber 2-WGCB-HSS-3B Revealed Damaged Reservoir W/O Fluid.Caused by Personnel Working in Area.Snubber Replaced ML20023C5371983-05-10010 May 1983 LER 83-021/03L-0:on 830411,Fire Door S-71-7 Between Svc Bldg Health Physics Area & Auxiliary Bldg Would Not Self Close.Caused by Removal of Reclosure Device for Maint of Closure Coupling.Reclosure Device Reinstalled ML20023B5931983-04-27027 April 1983 LER 83-029/03L-0:on 830402,during Mode 4,automatic Actuation of ECCS Occurred.Caused by Maint Personnel Standing on Conduit Resulting in Loss of lo-lo Pressurizer Pressure Safety Injection Block.Maint Personnel Reinstructed ML20023B5701983-04-27027 April 1983 LER 83-008/03L-0:on 830410,review Revealed That Procedure Used to Restore Boron Injection Tank Concentration Introduced Potential Unanalyzed Injection Flow Diversions. Caused by Oversight.Emergency Procedures Revised ML20028G6541983-02-0909 February 1983 LER 83-003/03L-0:on 830122,during Mode 5,RHR Flow Was Lost for 4 Minutes.Caused by Failure of 15 Kv a Inverter to Ac Vital Bus 1-III,de-energizing Auxiliary Relay for Pressure Channel P-1403.Vital Bus 1-III & RHR Flow Restored ML20028G6311983-02-0909 February 1983 LER 83-016/03L-0:on 830115 & 16,both Open & Closed Containment Isolation Valves TV-SI-200 & TV-CC-204C,train a Position Indication Lights Found Lit.Caused by Leaking Steam Generator Chemical Feed Line Vent Valve ML20028G0781983-01-31031 January 1983 LER 83-001/03L-0:on 830112,primary Grade Water Isolation Valve to Blender 1-CH-217 Remained Open Longer than Tech Spec Requirements.Caused by Personnel Error.Responsible Operator Reinstructed ML20028G0381983-01-28028 January 1983 LER 83-002/03L-0:on 830104,two of Four 2H Emergency Diesel Generator Surveillance Tests Required by Tech Spec Missed During Nov-Dec 1982.Caused by Scheduling Error.Test Frequency Increased to Meet Tech Spec Requirements ML20028G0131983-01-28028 January 1983 LER 83-011/03L-0:on 821119,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps.Caused by Instrument Drift.Indicator Channel for Rods B-09 & 02 & F-06 Recalibr ML20028F3501983-01-19019 January 1983 LER 83-008/03L-0:on 830107,during Mode 3,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps While Withdrawing Shutdown Bank B. Caused by Instrument Drift.Rods Recalibr ML20028E0391983-01-11011 January 1983 Updated LER 82-079/03X-1:on 821126,flow Path from Boric Acid Tanks to RCS Found Inoperable.Caused by Ruptured Diaphragm of Boric Acid Transfer Pump Suction Header Isolation Valve 1-CH-80.Valve Diaphragm Replaced ML20028E0441983-01-11011 January 1983 LER 82-085/03L-0:on 821215,w/unit at Full Power,Emergency Diesel Generator 2J Removed from Svc for 7 H to Adjust Voltage Regulator Response Time.Caused by Voltage Regulator Drift.Procedures Will Be Revised ML20028E0201983-01-11011 January 1983 LER 82-084/03L-0:on 821216,during Full Power,Input from Range Nuclear Instrument N-42 to Comparator Drawer N-50 Was in Defeat.Caused by Failure to Take N-42 Out of Defeat After Deviation Alarm Determination.Operators to Be Reinstructed ML20028E0781983-01-11011 January 1983 LER 82-078/03X-1:on 821125,w/unit in Mode 3,120-volt Ac Vital Bus 1-IV Lost Voltage.Caused by Failure of Normal Power Supply Inverter 1-VB-I-04,due to Failed Oscillator Board,Transformer & Fuse.Components Replaced ML20028D1311983-01-0505 January 1983 LER 82-083/03L-0:on 821213,emergency Diesel Generator 2J Removed from Svc.Caused by Failure of 40X Unexcitation Alarm Relay Coil.Carbon Deposits & Arcing Damage of 40/76 Relay Contact Prevented Good Contact ML20028D1571983-01-0505 January 1983 Updated LER 81-071/03X-2:on 810911,hydraulic Snubber on Main Steam Line Discovered Inoperable Due to Loss of Oil from Reservoir.Caused by Leak Due to Scored Brass Bushing on Piston Shaft.Snubber Purged & Refilled.Reach Rod Retorqued ML20028C5191982-12-31031 December 1982 LER 82-083/03L-0:on 821204,while Operating at 17% Rated Thermal Power,Turbine Control Sys Malfunctioned Causing Sudden Increase in Load,Resulting in Reactor Trip.Caused by Malfunction of Analog Converter ML20028A8651982-11-16016 November 1982 LER 82-067/03L-0:on 821019,suction to RHR Sys Pumps a & B Lost for 36 Minutes.On 821020,pump Suction Lost for 33 Minutes.Caused by Ambiguous RCS Level Indication While Water Drained to Centerline of Nozzles.Water Added ML20028A8821982-11-16016 November 1982 LER 82-060/03L-0:on 821019,station Battery I-IV Failed 18- Month Discharge Surveillance Test.Caused by Natural End of Life.Battery Replaced ML20028A9781982-11-16016 November 1982 LER 82-071/03L-0:on 821027,control Power for B Casing Cooling Pump Found de-energized.Caused by Opened Circuit Breaker Unintentionally Disturbed by Workers.Circuit Breaker Closed & Power Verified 1994-04-25
[Table view] Category:RO)
MONTHYEARML20029D0201994-04-25025 April 1994 LER 94-007-01:on 931014,high Head Safety Injection Flow Balance Testing Found to Be Below TS Requirement.Caused by Unaccounted for Uncertainties.Cold Leg Safety Injection Leg Throttle Valve adjusted.W/940425 Ltr ML20045G9391993-07-0808 July 1993 Lr 93-017-00:on 930616,containment Hydrogen Analyzer Heat Trace Channel Calibration Not Performed on Staggered Test Basis Due to Inadequate Implementation of TS Amend.Test Procedure Satisfactorily performed.W/930708 Ltr ML20044H1591993-05-27027 May 1993 LER 93-016-00:on 930509,discovered That Containment Hydrogen Analyzer Pressure Switch PS-3 Sensing Line Disconnected in Local Panel.Caused by Personnel Error. Pressure Switch Calibr & Line reconnected.W/930527 Ltr ML20044D5711993-05-14014 May 1993 LER 93-002-00:on 930416,automatic Reactor Trip Initiated from Turbine Trip Due to Over Excitation of Main Generator. Emergency Procedure 2-E-0 Entered & Individuals Involved in Event Received Remediated training.W/930514 Ltr ML20044D2281993-05-12012 May 1993 LER 93-003-00:on 930424,manual Reactor Trip Initiated Due to Erratic Feedwater Flow Indications to SG C & Excessive Main Feedwater Regulating Valve Oscillations.Caused by Design Instabilities.Secondary Sys secured.W/930512 Ltr ML20044C9541993-05-0707 May 1993 LER 93-015-00:on 930427,discovered That Portions of Containment Pressure Channels That Input to Containment Spray hi-hi Pressure Not Tested Monthly.Caused by Personnel Error.Test Procedures changed.W/930507 Ltr ML20044C9811993-05-0606 May 1993 LER 93-014-00:on 930411,as-found Speed Setting of Steam Driven AFW Pump 1-FW-P-2 Found Below Required TS Limit. Caused by Incorrect Speed Control Setting.Pump Speed Adjusted & Maint Personnel counseled.W/930506 Ltr ML20024G6841991-04-18018 April 1991 LER 91-006-00:on 910403,discovered That Ac Offsite Power Source Surveillance Not Performed Due to Personnel Error. Surveillance Initiated Immediately & Positive Discipline Administered to supervisor.W/910418 Ltr ML20029B5601991-03-0606 March 1991 LER 91-005-00:on 910209,containment Building Penetrations Breached.Caused by Inadequate Procedural Controls.Core Mapping & Cavity Pump Down Activities Secured,Air Hose Removed & Hydrolase Hose capped.W/910306 Ltr ML20029A6471991-02-22022 February 1991 LER 91-004-00:on 910206,sealed Radioactive Source in Storage Not Leak Tested Prior to Use.Caused by Inadequate Procedures for Verifying Leak Testing of Sources.Procedures Revised.W/ 910222 Ltr ML20028H6681991-01-18018 January 1991 LER 90-009-01:on 900719,discovered That Response Time Testing of Pressurizer High Level Reactor Trip Function Not Performed in Accordance W/Tech Spec 3.3.1.1,Table 3.3-2. Caused by Personnel Error.Procedures revised.W/910118 Ltr ML20043H8321990-06-22022 June 1990 LER 90-007-00:on 900523,discovered That Two Sets of Concrete Roof Blocks on Svc Water Pump House Not in Required Safety Position.Caused by Lack of Administrative Controls.Blocks Restored to Required locations.W/900622 Ltr ML20043D5801990-06-0404 June 1990 LER 90-006-00:on 900504,casing Cooling Pump Not Put Into Alert Status & Surveillance Missed.Caused by Personnel Error.Pump 1-RS-P-3B Placed in Alert status.W/900604 Ltr ML20012E3301990-03-27027 March 1990 LER 90-003-00:on 900228,52 Valves Identified Not Included in Tech Spec Required Monthly Containment Integrity Verification Surveillance Program.Caused by Personnel Error & Inadequate Procedure.Procedure revised.W/900327 Ltr ML20012B6441990-03-0808 March 1990 LER 90-001-00:on 900215,inadvertent Partial Train a ESF Actuation of Containment Depressurization Sys Occurred. Caused by Human Error.Evaluation to Be Performed to Determine If Test Points Can Be moved.W/900308 Ltr ML20006E2371990-02-0808 February 1990 LER 90-001-00:on 900123,reactor Trip Occurred on Steam Feedwater Flow Mismatch.Caused by Failed Circuit Driver Card on Feedwater Regulating Valve.Feedwater Regulating Valve Driver Card replaced.W/900208 Ltr ML20006E3771990-02-0505 February 1990 LER 90-002-00:on 900127,fuel Bldg Ventilation Sys Not Aligned to Discharge Through Auxiliary Bldg HEPA Filter & Charcoal Adsorber Assembly During Fuel Movement.Caused by Personnel Error.Disciplinary Action taken.W/900205 Ltr ML20006A8531990-01-19019 January 1990 LER 89-019-00:on 891228,discovered That Outer Door of Containment Equipment Escape Air Lock Was Drawing in Air & Inner Door Noted as Not Being in Fully Closed Position.Cause Undetermined.Sys Enhancements Being evaluated.W/900119 Ltr ML20005F8781990-01-11011 January 1990 LER 89-018-00:on 891219,determined That Three Pressurizer Pressure Safety Injection Instrumentation Channels May Not Have Adequate Margin Between Actuation Setpoint & Bottom of Instrument span.W/900111 Ltr ML19332D5471989-11-22022 November 1989 LER 85-003-03:on 890907,determined That Situation Could Arise Where Water Level Would Rise to 264 Ft Before Next Required Surveillance Interval.Cause Not Determined.Dike to Be constructed.W/891122 Ltr ML20024B7821983-07-0606 July 1983 LER 83-048/03L-0:on 830606 & 17,intermediate Range Channels N35 & N36 High Neutron Flux Reactor Trip Setpoints Exceeded Tech Spec Requirements.Caused by Administrative Error. Setpoints reduced.W/830706 Ltr ML20024C1361983-06-30030 June 1983 LER 83-031/03L-0:on 830614,w/unit at 100% Power,Fire Door S54/5 from Emergency Switchgear Room to Cable Vault Would Not Latch.Fire Watch Posted Immediately.Caused by Misaligned Strike.Door Repaired within 1 h.W/830630 Ltr ML20024C3721983-06-30030 June 1983 LER 83-042/03L-0:on 830606,vital Bus 1-I Momentarily Deenergized While Trying to Clear Inverter Trouble Alarm. Caused by Operator Error.Bus energized.W/830630 Ltr ML20024B9891983-06-28028 June 1983 LER 83-047/03L-0:on 830530,emergency Diesel Generator 2J Tripped on High Crankcase Pressure During Surveillance Testing.Cause Not Determined.Diesel Tested Satisfactorily. W/830628 Ltr ML20024C2941983-06-23023 June 1983 LER 83-044/03L-0:on 830526,during Mode 3,one Recirculation Valve on Each of Two Casing Cooling Pumps Found Open.Caused by Procedure Inadequacy.Valves Closed Immediately.Maint Procedure Will Be revised.W/830623 Ltr ML20024C3071983-06-22022 June 1983 LER 83-034/03L-0:on 830525,during Mode 1,one Header of Control Room Bottled Air Pressurized Sys Had Lower than Required Pressure.Probably Caused by Leak from B Bank of Air Bottles.Header repressurized.W/830622 Ltr ML20024C0971983-06-22022 June 1983 LER 83-045/03L-0:on 830614,Fire Door S71-18,between Emergency Diesel Generator Room 2H & Turbine Bldg,Would Not Latch & Lock.Caused by Stuck Latch.Latch Adjusted & Lubricated.Door Designs modified.W/830622 Ltr ML20023E0951983-06-0101 June 1983 LER 83-027/03L-0:on 830505,one Header (42 Bottles) of Control Room Bottled Air Pressurized Sys Found to Have Lower than Required Pressure (2,290 Vs 2,300 Psig).Probably Caused by Leakage When Compressor malfunctioned.W/830601 Ltr ML20023E0721983-05-26026 May 1983 LER 83-029/03L-0:on 830509,following Rapid Rampdown from 100% to 4% power,I-131 Dose Equivalent Exceeded 1.0 Uci/G. Caused by Unidentified Fuel Element Defect Worsened by post-rampdown Conditions.Sampling increased.W/830526 Ltr ML20023D5371983-05-13013 May 1983 LER 83-022/03L-0:on 830412,review of ASME XI Iwv Program Identified 192 Valves Not Exercised &/Or Stroke Timed.Caused by Fragmented Implementation of Testing Program.Programs Upgraded ML20023D2491983-05-11011 May 1983 LER 83-032/03L-0:on 830412,during Mode 5,visual Insp of Hydraulic Snubber 2-WGCB-HSS-3B Revealed Damaged Reservoir W/O Fluid.Caused by Personnel Working in Area.Snubber Replaced ML20023C5371983-05-10010 May 1983 LER 83-021/03L-0:on 830411,Fire Door S-71-7 Between Svc Bldg Health Physics Area & Auxiliary Bldg Would Not Self Close.Caused by Removal of Reclosure Device for Maint of Closure Coupling.Reclosure Device Reinstalled ML20023B5931983-04-27027 April 1983 LER 83-029/03L-0:on 830402,during Mode 4,automatic Actuation of ECCS Occurred.Caused by Maint Personnel Standing on Conduit Resulting in Loss of lo-lo Pressurizer Pressure Safety Injection Block.Maint Personnel Reinstructed ML20023B5701983-04-27027 April 1983 LER 83-008/03L-0:on 830410,review Revealed That Procedure Used to Restore Boron Injection Tank Concentration Introduced Potential Unanalyzed Injection Flow Diversions. Caused by Oversight.Emergency Procedures Revised ML20028G6541983-02-0909 February 1983 LER 83-003/03L-0:on 830122,during Mode 5,RHR Flow Was Lost for 4 Minutes.Caused by Failure of 15 Kv a Inverter to Ac Vital Bus 1-III,de-energizing Auxiliary Relay for Pressure Channel P-1403.Vital Bus 1-III & RHR Flow Restored ML20028G6311983-02-0909 February 1983 LER 83-016/03L-0:on 830115 & 16,both Open & Closed Containment Isolation Valves TV-SI-200 & TV-CC-204C,train a Position Indication Lights Found Lit.Caused by Leaking Steam Generator Chemical Feed Line Vent Valve ML20028G0781983-01-31031 January 1983 LER 83-001/03L-0:on 830112,primary Grade Water Isolation Valve to Blender 1-CH-217 Remained Open Longer than Tech Spec Requirements.Caused by Personnel Error.Responsible Operator Reinstructed ML20028G0381983-01-28028 January 1983 LER 83-002/03L-0:on 830104,two of Four 2H Emergency Diesel Generator Surveillance Tests Required by Tech Spec Missed During Nov-Dec 1982.Caused by Scheduling Error.Test Frequency Increased to Meet Tech Spec Requirements ML20028G0131983-01-28028 January 1983 LER 83-011/03L-0:on 821119,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps.Caused by Instrument Drift.Indicator Channel for Rods B-09 & 02 & F-06 Recalibr ML20028F3501983-01-19019 January 1983 LER 83-008/03L-0:on 830107,during Mode 3,individual Rod Position Indication Deviated from Group Demand Position by Greater than 12 Steps While Withdrawing Shutdown Bank B. Caused by Instrument Drift.Rods Recalibr ML20028E0391983-01-11011 January 1983 Updated LER 82-079/03X-1:on 821126,flow Path from Boric Acid Tanks to RCS Found Inoperable.Caused by Ruptured Diaphragm of Boric Acid Transfer Pump Suction Header Isolation Valve 1-CH-80.Valve Diaphragm Replaced ML20028E0441983-01-11011 January 1983 LER 82-085/03L-0:on 821215,w/unit at Full Power,Emergency Diesel Generator 2J Removed from Svc for 7 H to Adjust Voltage Regulator Response Time.Caused by Voltage Regulator Drift.Procedures Will Be Revised ML20028E0201983-01-11011 January 1983 LER 82-084/03L-0:on 821216,during Full Power,Input from Range Nuclear Instrument N-42 to Comparator Drawer N-50 Was in Defeat.Caused by Failure to Take N-42 Out of Defeat After Deviation Alarm Determination.Operators to Be Reinstructed ML20028E0781983-01-11011 January 1983 LER 82-078/03X-1:on 821125,w/unit in Mode 3,120-volt Ac Vital Bus 1-IV Lost Voltage.Caused by Failure of Normal Power Supply Inverter 1-VB-I-04,due to Failed Oscillator Board,Transformer & Fuse.Components Replaced ML20028D1311983-01-0505 January 1983 LER 82-083/03L-0:on 821213,emergency Diesel Generator 2J Removed from Svc.Caused by Failure of 40X Unexcitation Alarm Relay Coil.Carbon Deposits & Arcing Damage of 40/76 Relay Contact Prevented Good Contact ML20028D1571983-01-0505 January 1983 Updated LER 81-071/03X-2:on 810911,hydraulic Snubber on Main Steam Line Discovered Inoperable Due to Loss of Oil from Reservoir.Caused by Leak Due to Scored Brass Bushing on Piston Shaft.Snubber Purged & Refilled.Reach Rod Retorqued ML20028C5191982-12-31031 December 1982 LER 82-083/03L-0:on 821204,while Operating at 17% Rated Thermal Power,Turbine Control Sys Malfunctioned Causing Sudden Increase in Load,Resulting in Reactor Trip.Caused by Malfunction of Analog Converter ML20028A8651982-11-16016 November 1982 LER 82-067/03L-0:on 821019,suction to RHR Sys Pumps a & B Lost for 36 Minutes.On 821020,pump Suction Lost for 33 Minutes.Caused by Ambiguous RCS Level Indication While Water Drained to Centerline of Nozzles.Water Added ML20028A8821982-11-16016 November 1982 LER 82-060/03L-0:on 821019,station Battery I-IV Failed 18- Month Discharge Surveillance Test.Caused by Natural End of Life.Battery Replaced ML20028A9781982-11-16016 November 1982 LER 82-071/03L-0:on 821027,control Power for B Casing Cooling Pump Found de-energized.Caused by Opened Circuit Breaker Unintentionally Disturbed by Workers.Circuit Breaker Closed & Power Verified 1994-04-25
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N9281999-10-20020 October 1999 Special Rept:On 991003,PZR PORV Actuation Mitigated RCS low- Temp Overpressure Transient.Caused by a RCP Facilitating Sweeping of Entrained Air Out of RCS Loops.Operating Procedure 2-OP-5.1 Will Be Revised ML20217H3631999-10-14014 October 1999 Rev 0 to COLR for North Anna 2 Cycle 14 Pattern Su ML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML20212J9251999-10-0101 October 1999 Safety Evaluation Accepting Licensee Relief Request IWE-3 for Second 10-year ISI for Plant ML20217D6851999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for North Anna Power Station,Units 1 & 2.With ML20211N2611999-09-0808 September 1999 Safety Evaluation Concluding That Proposed Irradiation of Fuel Rods Beyond Current Lead Rod Burnup Limit & Clarification of Terminology with Respect to Reconstituted Fuel Assemblies Acceptable ML20211J2561999-08-31031 August 1999 Safety Evaluation Accepting Elimination of Augmented ISI Program for Pressurizer Spray Lines at North Anna Unit 2 ML20216E5011999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Naps,Units 1 & 2. with ML20211J2421999-08-31031 August 1999 Safety Evaluation Supporting Removal of Augmented Insp Program on RCS Bypass Lines from Licensing Basis of North Anna,Units 1 & 2 ML20210T0791999-08-13013 August 1999 Safety Evaluation Concluding That Revised Withdrawal Schedules for North Anna Units 1 & 2 Satisfy Requirements of App H to 10CFR50 & Therefore Acceptable ML20210S1411999-07-31031 July 1999 Monthly Operating Repts for July 1999 for North Anna Power Station.With ML20210Q9931999-07-31031 July 1999 Rev 1 to COLR for North Anna Power Station,Unit 2 Cycle 13 Pattern Ud ML20209E5641999-06-30030 June 1999 Monthly Operating Repts for June 1999 for North Anna Power Stations,Units 1 & 2.With ML20195G1901999-05-31031 May 1999 Monthly Operating Rept for May 1999 for NAPS Units 1 & 2. with ML20206L4831999-05-10010 May 1999 SER Accepting Request to Delay Submitting Plant,Unit 1 Class 1 Piping ISI Program for Third Insp Interval Until 010430, to Permit Development of Risk Informed ISI Program for Class 1 Piping ML20206Q6671999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for North Anna Power Station,Units 1 & 2.With ML20205S0391999-04-21021 April 1999 SER Accepting Request for Relief IWE5,per 10CFR50.55a(a)(3) & Proposed Alternatives for IWE2,IWE4,IWE6 & IWL2 Authorized Per 10CFR50.55a(a)(3)(ii) ML20205K3041999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for North Anna Power Station,Units 1 & 2.With ML20207K5921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for North Anna Power Station,Units 1 & 2.With ML20207E1731999-02-18018 February 1999 Informs Commission of Status of Preparations of IAEA Osart Mission to North Anna Nuclear Power Plant Early Next Year ML20205A0241998-12-31031 December 1998 Summary of Facility Changes,Tests & Experiments,Including Summary of SEs Implemented at Plant During 1998,per 10CFR50.59(b)(2).With ML20199C8781998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for North Anna Power Station,Units 1 & 2.With ML20198H9541998-12-0303 December 1998 Safety Evaluation Authorizing Proposed Alternative for Remainder of Second 10-yr Insp Interval for Plant ML20198J5561998-12-0303 December 1998 ISI Summary Rept for North Anna Power Station,Unit 1 1998 Refueling Outage Owner Rept for Inservice Insps ML20197G8551998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for North Anna Power Station,Units 1 & 2.With ML20196G1381998-11-0303 November 1998 Safety Evaluation Authorizing Rev to Relief Request NDE-32 for Remainder of Second 10-yr Insp Interval for Each Unit ML20195D0571998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for North Anna Power Station,Units 1 & 2.With ML20154L0691998-10-14014 October 1998 COLR for North Anna Power Station Unit 1 Cycle 14 Pattern Xy ML20155J6911998-10-0909 October 1998 Staff Response to Tasking Memorandum & Stakeholder Concerns ML20154H4001998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for North Anna Power Station,Units 1 & 2.With ML20151X8011998-09-10010 September 1998 Special Rept:On 980622,groundwater Level at Piezometer P-22 Was Again Noted to Be Above Max Water Level by 0.71 Feet. Increased Frequency of Piezometer Monitoring & Installed Addl Piezometers at Toe of Slope Along Southwest Section ML20151W4711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for North Anna Power Station Units 1 & 2.With ML20237A4341998-07-31031 July 1998 Monthly Operating Repts for July 1998 for North Anna Power Station,Units 1 & 2 ML20236V1251998-07-14014 July 1998 ISI Summary Rept for Naps,Unit 2,1998 Refueling Outage Owners Rept of Isis ML20236K5531998-07-0707 July 1998 SER Accepting Request for Change in ISI Commitment on Protection Against Pipe Breaks Outside Containment ML20236M3381998-06-30030 June 1998 Monthly Operating Repts for June 1998 for North Anna Power Station,Units 1 & 2 ML20248M1011998-05-31031 May 1998 Monthly Operating Repts for May 1998 for North Anna Power Station,Units 1 & 2 ML20248C8831998-05-29029 May 1998 SER Accepting Alternatives Proposed by Licensee for Use of Code Case N-535,pursuant to 10CFRa(a)(3)(i) in ASME Section XI Inservice Insp Program ML20247K9281998-05-15015 May 1998 Special Rept:On 980428,letdown PCV Exhibited Slow Response When C RCP Was Started.Cause to Be Determined.Review of Operating Procedure Will Be Performed to Determine If Enhancements Are Necessary ML20216A8971998-05-0606 May 1998 Rev 0 to Cycle 13 Pattern Ud COLR for North Anna Unit 2 ML20247F4441998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for North Anna Power Station,Units 1 & 2 ML20217B5321998-04-20020 April 1998 Safety Evaluation Supporting Proposed Alternative to ASME Code for Surface Exam of Seal Welds on Threaded Caps for Plant Reactor Vessel Head Penetrations for part-length CRDMs ML20217H9611998-04-0707 April 1998 Special Rept:On 980216,groundwater Level at Piezometer P-22, Again Noted to Be Above Max Water Level by 0.41 Feet.Design Package for Installation of Addl Standpipe Piezometers at Toe of Slope Southeast Section,Developed ML20216B1891998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for North Anna Power Station,Units 1 & 2 ML20216E8801998-03-0606 March 1998 Safety Evaluation Authorizing Licensee Request for Relief from ASME Code Requirements,Paragraph IWA-2400(c) (Summer Edition W/Summer 1983 Addenda),For Upcoming Naps,Unit 1 Outage,Per 10CFR50.55a(a)(3)(ii) ML20216E2561998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for North Anna Power Station,Units 1 & 2 ML20199J6431998-02-0202 February 1998 Safety Evaluation Approving Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Code Class 3 SW Piping for North Anna,Unit 1,as Submitted in ISI Relief Request NDE-46 on 971218 ML20202D5811998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for North Anna Power Station,Units 1 & 2 ML20198S7571998-01-15015 January 1998 Safety Evaluation Accepting Licensee Request for Approval to Repair Flaws IAW GL-90-05 for ASME Code Class 3 Svc Water Piping ML20198P1351997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for North Anna Power Station,Units 1 & 2 1999-09-08
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VOPCO VIRGINIA ELECTRIC AND POWE R COMPANY NORTH AN h A POWE R S TATION
- P. O. BO K 4 02 WIN E RAL. VIRGINI A 23117 t
10 CFR 50.73 May 12,1993 1.
U. S. Nuclear Regulatory Commission NAPS:M?W ,
Attention: Document Control Desk Docket No- 50-339 Washington, D.C. 20555 License No. NPF-7 >
Dear Sirs:
The Virginia Electric and Power Company hereby submits the following Licensee Event Report applicable to Nonh Anna Unit 2.
Repon No. 50-33993-003-00 This Report has been reviewed by the Station Nuclear Safety and Operating Committee and i will be forwarded to the Corporate Management Safety Review Committee for its review. ;
Very Truly Yours, G. E. e I Station Manager Enclosme: j a: U.S. Nuclear Regulatory Commission 101 Marietta Street, N.W.
Suite 2900 Atlaea, Georgia 30323 Mr. D. R. Taylor NRC Resident Inspector Nonh Anna Power Station 170139 l
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NRC FoRW ke US kJCLI AR REGULATQ3V CAMO gppitDVED OWB NO. 3?504104 f4 Epi EXPIRES:GTAl2 '
ESTlWATED BURDEN PER RESPONSE TO CoWPLY WITH THis WFORMATON i NTON REWESn no HRS. FORWARD CoWWENU REGARDWG BURDEN UCENSEE EVENT REPORT (LER) ESTadATE TO THE RCCoR3S AND REPORTS MANAGEWENT BRANCH (P $33. U.S.
NUCEEAR REGULATORY CoWWISSION, WASHINGTON DC 20655. AND TO THE PAPERWORK REDUCTON PROJECT (31504104L OFFICE oF WANAGEWENT AND 6
BUDGET. WASHINGTON.DC 205c3.
FaciLTTY NAME 0) DOCKET Muud R gn *G m North Anna Power Station Unit 2 nitIninio!3l319 1 lOQOj4 TITLE tal MANUAL RFACTOR TRIP INITIATED DUE TO EXCESSIVE MAIN FEE 0 WATER REGUIATING VALVE OSCILIATIONS EVENT DATE (5) LER NUWBE R (e) REPORT DATE (7) OTHER FACILITIE3 INv0LVED (8)
WCDITH DAY YEAR YEAR SE0VEN RIN WONTH DAY VEAR NT WWW NJuBER aruuSER clsiciolol I !
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UCEN5E E CONTACT FOR IH15 LER O2)
NAME TELEPHONE NUWBER ;
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l lll lfl EXPECTED MONTH DAY YEAR SUBWISSON YES te r e tzgettD avnessace Data NO CATE C5) l l l ABS TR ACT fumn m *4ac spense a e swomme==, ==en s.g gp. neur mesi O 6)
On April 24, 1993, at 0530 hours0.00613 days <br />0.147 hours <br />8.763227e-4 weeks <br />2.01665e-4 months <br /> with Unit 2 in Mode 1, 71 percent power, a manual reactor trip was initiated due to erratic feedwater flow indications to the "C" Steam Generator, abnormally high vibration alarms for the "B" Reactor Coolant Pump, and suspected water and steam leakage from the "C" Main Feedwater line. Emergency procedures were entered and immediate actions were performed. All Engineered Safety Feature system equipment responded as designed. At 0602 hours0.00697 days <br />0.167 hours <br />9.953704e-4 weeks <br />2.29061e-4 months <br /> an " Alert" was declared, based on Shift Supervisor judgment, in accordance with Emergency Plan Implementing Procedures and the required notifications were made. A 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> report was made to the NRC at 0620 hours0.00718 days <br />0.172 hours <br />0.00103 weeks <br />2.3591e-4 months <br /> pursuant to 10CFR50. 72 (a) (ii) (3) . At 0816 hours0.00944 days <br />0.227 hours <br />0.00135 weeks <br />3.10488e-4 months <br /> with the unit in a '
stable condition the " Alert" classification was down graded to a Notification Of Unusual Event (NOUE) . The NOUE was terminated at 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br /> on April 24, i 1993. The event is reportable pursuant to 50.73 (a) (2) (iv) .
The cause of the event has been attributed to the inherent instabilities with l the design of the main feedwater regulating valve and positioner controls. J
}
1 No significant safety consequences resulted f rom the main feedwater concerns because auxiliary feedwater was available and provided cooling to the steam generators throughout the event. Therefore, the health and safety of the public were not af fected at any time during this event.
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l NRC FoRW 3EA US CM11AA REGULATORY CouME510h AppitDVED oWB No. 3160.osos De {
EXPIRES: &JG'92 I ESTauATED BURDEN PER RESPONSE To COMPLY WITH THIS INFoRuATON UCENSEE EVENT REPORT (LER) couiCTON REcuEST: 50.0 HRS. FORWARD CoWWENTS REGARDING BURoEN TEXT CONTINUATION ESTlWATE To THE RECORDS AND REPORTS MANAGEWENT BRANmi(P430L U.S.
NUCLEAR REGULATORY CoWWLSSON, WASHINGTON. DC 20555. AND To THE PAPERWORK REDUCTON PROJECT (3tS0 010sk orFCE oF MANAGEWENT AND BUDGET, WASHINGTON.DC 20h01
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0 l 0 I3 O l0 012 or 014 TEzT pm mi. ww eee emc *w= nu a 07) i 1_0 Dmriptinn cf the Event On April 24, 1993, at 0530 hours0.00613 days <br />0.147 hours <br />8.763227e-4 weeks <br />2.01665e-4 months <br /> with Unit 2 in Mode 1, 71 percent power, a manual reactor trip was initiated due to erratic feedwater flow indications to the "C" Steam Generator (EIIS System AB, Component SG), abnormally high ,
vibration alarms (EIIS System IV, Component VA) for the "B" Reactor Coolant Pump (EIIS System AB, Component P), and suspected water and steam leakage from ,
the "C" Main Feedwater line (EIIS System SJ). Emergency procedures were entered and immediate actions were performed. All Engineered Safety Feature system (EIIS System JE) equipment responded as designed. At 0602 hours0.00697 days <br />0.167 hours <br />9.953704e-4 weeks <br />2.29061e-4 months <br /> an
" Alert" was declared, based on Shift Supervisor judgment, in accordance with i Emergency Plan Implernent ing Procedures and the required notifications were made. A 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> report was made to the NRC at 0620 hours0.00718 days <br />0.172 hours <br />0.00103 weeks <br />2.3591e-4 months <br /> pursuant to '
10CFR50.72 (a) (ii) (3) . At 0816 hours0.00944 days <br />0.227 hours <br />0.00135 weeks <br />3.10488e-4 months <br /> with the unit in a stable condition the
" Alert" classification was down graded to a Notification Of Unusual Event (NOUE) . The NOUE was terminated at 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br /> on April 24, 1993. The event is reportable pursuant to 50.73 (a' (2) (iv) .
On April 24, 1993, at 0255 hours0.00295 days <br />0.0708 hours <br />4.21627e-4 weeks <br />9.70275e-5 months <br /> "C" Steam Generator (SG) feed flow began to
- oscillate. At 0320 hours0.0037 days <br />0.0889 hours <br />5.291005e-4 weeks <br />1.2176e-4 months <br /> "B" SG feed flow escillated for approximately 10 minutes then reached steady state. At 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> "B" SG feed flow began to oscillate again. At 0517 hours0.00598 days <br />0.144 hours <br />8.54828e-4 weeks <br />1.967185e-4 months <br /> "C" feed flow oscillation worsened and both "B" and "C" Main Feed Regulating Valves (MFRV) (EIIS System SJ, Component FCV) l were placed in manual. An operator was dispatched to the Mechanical Equipment Room and reported that the feed lines were moving and the "C" MFRV was cycling. Feedline noises and pipe movement worsened. The "B" Reactor Coolant Pump vibrations alarm was received and the "B" SG Loose Parts alarm (EIIS System II, Component ALM) was received.
At 0530 hours0.00613 days <br />0.147 hours <br />8.763227e-4 weeks <br />2.01665e-4 months <br /> after vibrations were felt and heard in the Control Room the Senior Reactor Operator ordered a manual reactor trip. The immediate actions of Emergency Procedure 2-E-0, Reactor Trip or Safety Injection, were performed. Initially, Reactor Coolant System (RCS) (EIIS System AB) pressure decreased to approximately 2000 psig and temperature decreased to approximately 538 degrees F. All Engineered Safety Feature system equipment i responded as designed. Upon transition to Emergency Procedure 2-ES-0.1, Reactor Trip Response, the secondary systems were secured. At this point the noises and vibrations were no longer heard or felt in the Control Room. At 0602 hours0.00697 days <br />0.167 hours <br />9.953704e-4 weeks <br />2.29061e-4 months <br /> an " Alert" was declared, based on Shift Supervisor judgment, in ,
accordance with Emergency Plan Implementing Procedures. Notification of State and Local Governments occurred at 0609 hours0.00705 days <br />0.169 hours <br />0.00101 weeks <br />2.317245e-4 months <br />. The NRC Emergency Operations !
Center was notified of the " Alert" at 0620 hours0.00718 days <br />0.172 hours <br />0.00103 weeks <br />2.3591e-4 months <br /> pursuant to 10CFR5 0.72 (a) (ii) (3) . At 0816 hours0.00944 days <br />0.227 hours <br />0.00135 weeks <br />3.10488e-4 months <br /> with the unit in a stable condition the ,
" Alert" classification was down graded to a Notification Of Unusual Event (NOUE). The NRC was notified at 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br /> that the NOUE was terminated. At 1253 hours0.0145 days <br />0.348 hours <br />0.00207 weeks <br />4.767665e-4 months <br /> the unit entered Hot Shutdown with RCS temperature less than 350 ;
degrees F. At 1735 hours0.0201 days <br />0.482 hours <br />0.00287 weeks <br />6.601675e-4 months <br /> the unit entered Cold Shutdown wit h RCS temperature less than 200 degrees F. ;
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%AC FORet 2n6A US CACW RhTARSDRV N aPPRo0ED ouB No. 31500104 4em EXPIRES: 4'3CvD2 ESTIMATED BURoEN PER RESPONSE To CCWPLY WITH THis INFORMATON UCENSEE EVENT REPORT (LER) CouECTON REC 1 JEST: 50.0 HRS. FORWARD CoWWENTS REGARDh3 BURDEN TEXT CONTINUATION ESNATE To THE RECORDS AND REPORTS MANAGEWENT BRANCH (P-EX)L U.S.
NUCLEAR REGULATORY CoWW:SSON WASHNGioN. Oc 2065&. AND To THE PAPERWORK REDUCTON PROJECT (315acios). OFFCE OF WANAGEWENT AND BUDGET, W ASHINGToN.DC 20603.
FOCILITY %AME p) DOMET NautR 2 LER nguitp 4) P&CiE @
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O l0 0I3 cf 0l4 TLET irme =am = w u amene.wie re= asen es 07) 2.0 Sionificant Safety Cen=erences and Irrlications No significant safety consequences resulted from the main feedwater concerns because auxiliary feedwater was available to provide cooling to the steam generators throughout the event. Therefore, the health and safety of the public were not affected at any time during this event.
3.0 Cause of the Event The cause of the event has been attributed to the inherent instabilities with the design of the main feedwater regulating valve and positioner controls.
4.0 I m diate Corrective Actions Following the manual reactor trip Emergency Procedure 2-E-0, Reactor Trip or Safety Injection, was entered and the immediate actions performed.
1.0 Additional Corrective Actions Upon transition to Emergency Procedure 2-ES-0.1, Reactor Trip Response, the secondary systems were secured. The unit was brought to cold shutdown without incident.
The flow and pressure transmitters for the "C" main feedwater lines were satisfactorily calibrated and verified operable. The MFRVs and Main Feedwater Bypass Regulating Valves were visually inspected, stroked, calibrated, and verified operable. The feedwater piping and supports downstream of "C" MFRV up to and including the feed ring inside "C" SG were inspected. Adjustments were made to the MFRVs pneumatic boosters to reduce sensitivity and overshoot.
6.0 Actions to Prevent Recurrena Guidance to mitigate oscillations was provided to all operations shifts.
Early recognition of feedwater system oscillation during power ascension will allow appropriate operator actions to occur to preclude a similar event.
Parameters that will be monitored include: feedwater pump suction pressure, feedwater header pressure, feedwater flow, and the individual pressure indications at the discharge of each MFRV.
Requirements are in place to ensure the reactor trip event is included in the Licensed Operator Requalification Program. Actions taken are sufficient to preclude recurrence.
7.0 Similar Events None am e- ma im
NRC FoRW 38hA US NgCdAR RKmKSTDV NWh gpp g g g g 3 g g N' EKPERES: W3MI2 EST:WATED BURDEN PER RESPONSE TO CoWPLY W:TM THIS INFORWATON UCENSEE EVENT REPORT (LER) COLLECTION REQUEST: 504 HRS. FORWARD CoWWENTS REGARDING BURDEN TEXT CONTINUATION ESWATE TO NE RECORDS AND REPORTS WANAGEMENT ERANCH (P430L U.S.
NUCLEAR REGULATORY COWWISSON. vt ASHINGTON. DC 20555 AND TO THE PAPERwoRat REDUCTION PROJECT (315t>ctoak OFTCE OF WANAGEWENT AND BUDOET.% ASHINGTON.DC 20hD1.
F ACILITY NAME (1) DCXAET mMER 2 GA mR ts) pace m 9 E, SE;hJEETag m Rete,A North Anna Power Station wa M WJaeER Unit 2 al ci a l $ l a l31319 913 -l1 0 l0 i 3 -l O
! IO 014 0F 014 luTin . e .e. mac e anamn(17) 9.0 Additional Inf0N21 tion Component failures resulting from the main feedwater line oscillations ,
include: broken air line to the "B" Main Feedwater Regulating Valve, broken.
air line to the "B" Main Feedwater Bypass Regulating Valve, broken snubber extension rod on the "C" Main Feedwater Bypass line, broken spring hanger on ,
"C" Feedwater line, and a broken yoke en "C" main feedwater bypass regulating i valve.
The broken air lines to the "B" MFRV and "B" Main Feedwater Bypass Regulating Valve were repaired. The "C" Main Feedwater Bypass line snubber was replaced.
Snubbers were also replaced on the "A" and "C" feedwater headers. The spring hanger on "C" Feedwater line was repaired and the yoke on "C" main feedwater i bypass regulating valve was replaced.
Unit I was in Mode 1, 100 percent power, and was not affected by the event.
The Unit 1 MFRVs were modified during the recent refueling outage with a [
] pneumatic open and close operator. This modification was performed to eliminate oscillations of the MFRVs. The Unit 1 MFRV are of a different '
I design than Unit 2 and experience to date indicates they do not have similar instabilities. ,
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