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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:RO)
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A9151999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Shearon Harris Npp. with 991012 Ltr ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18017A8621999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Harris Nuclear Plant.With 990908 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18017A8361999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Shearon Harris Nuclear Power Plant.With 990811 Ltr ML18016B0151999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Shearon Harris Npp. with 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990614 Ltr ML18017A8981999-05-12012 May 1999 Technical Rept Entitled, Harris Nuclear Plant-Bacteria Detection in Water from C&D Spent Fuel Pool Cooling Lines. ML18016A9581999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990513 Ltr ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8941999-04-0505 April 1999 Revised Pages 20-25 to App 4A of non-proprietary Version of Rev 3 to HI-971760 ML18016A9101999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Shearon Harris Nuclear Power Plant.With 990413 Ltr ML18016A8661999-03-31031 March 1999 Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept. ML18017A8931999-02-28028 February 1999 Risks & Alternative Options Associated with Spent Fuel Storage at Shearon Harris Nuclear Power Plant. ML18016A8551999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Shearon Harris Npp. with 990312 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8531999-02-18018 February 1999 Non-proprietary Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFP 'C' & 'D'. ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18022B0631999-02-0404 February 1999 Rev 0 to Nuclear NDE Manual. with 28 Oversize Uncodable Drawings of Alternative Plan Scope & 4 Oversize Codable Drawings ML20202J1161999-02-0101 February 1999 SER Accepting Relief Requests Associated with Second 10-year Interval Inservice Testing Program ML18016A8041999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Shearon Harris Nuclear Power Plant.With 990211 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7801998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Shearon Harris Npp. with 990113 Ltr ML18016A7671998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Shnpp,Unit 1.With 981215 Ltr ML18016A9731998-11-28028 November 1998 Changes,Tests & Experiments, for Harris Nuclear Plant.Rept Provides Brief Description of Changes to Facility & Summary & of SE for Each Item That Was Implemented Under 10CFR50.59 Between 970608-981128.With 990527 Ltr ML18016A8351998-11-28028 November 1998 ISI Summary 8th Refueling Outage for Shearon Harris Power Plant,Unit 1. ML18016A7411998-11-25025 November 1998 Rev 1 to Shnpp Cycle 9 Colr. ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A7071998-11-0303 November 1998 Rev 0 to Harris Unit 1 Cycle 9 Colr. ML18016A7201998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Shearon Harris Nuclear Power Plant.With 981113 Ltr ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves ML18016A6201998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Harris Nuclear Power Plant.With 981012 Ltr ML18016A5971998-09-21021 September 1998 Rev 1 to Harris Unit 1 Cycle 8 Colr. ML18016A5881998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Shnpp,Unit 1.With 980914 Ltr ML18016A5071998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Shearon Harris Nuclear Plant.W/980811 Ltr ML18016A9431998-07-0707 July 1998 Rev 1 to QAP Manual. ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A9371998-06-30030 June 1998 Technical Rept on Matl Identification of Spent Fuel Piping Welds at Hnp. ML18016A4861998-06-30030 June 1998 Monthly Operating Rept for June 1998 for SHNPP.W/980715 Ltr ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18016A4521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Shearon Harris Nuclear Power Plant.W/980612 Ltr ML18016A7711998-05-26026 May 1998 Non-proprietary Rev 2 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris Spent Fuel Pools 'C' & 'D'. 1999-09-30
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.AC CEREBRATED EMO.STRE ON FT REGULATO~INFORMATION DISTRIBUTION SYSTEM (RIDS)I fA'ZESSION NBR:8812050217 DOC~DATE: 88/11/29 NOTARIZED; NO QACIL:50-~400 Shearon Harris Nuclear Power Plant, Unit 1', Carolina AUTHeN~E~AUTHOR AFFILIATION JOHNSON,J.R.
Carolina Powerl'ight Co.WATSON,R.A.
, Carolina Powerl'ight Co.RECIP.NAME RECIPIENT AFFILIATION DOCKET¹05000400
SUBJECT:
LER 88-032-00:on 881030,manual rea'ctor trip upon loss of main feedwater due to trip of heater drain pumps.W/881129 W/8 ltr.DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR I ENCL j SIZE: TITLE: 50.73 Licensee Event Report (LER), Incident Rptg etc.NOTES':Application for permit renewal fiied.05000400 RECIPIENT ID CODE/NAME PD2-1 LA BUCKLEYgB INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DSP/TPAB ARM/DCTS/DAB
.NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/ZSB 8D NRR/DEST/SGB 8K)NRR/DLPQ/QAB 10 NRR/DREP/RAB 10--BR*IS IB 9A EG F 02 RES//SR/PRAB EXTERNAL: EGGG WILLIAMSFS H ST LOBBY WARD NRC PDR NSIC MAYS,G COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 0 1 1 1 1 1 1 1'1.1 1, 1 1'1 1 1 1 4 4 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD2-1 PD ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP DEDRONRR/DEST/CEB 8H NRR/DEST/ICSB 7 NRR/DEST/MTB 9H NRR/DEST/RSB.8E NRR'/DLPQ/HFB 10 NRR/DOE&/EAB 11 NRR/DREP/RPB 10 NUDOCS-ABSTRACT-RES/DSIR/EIB RGN2 FILE Ol FORD BLDG HOY,A LPDR NSIC HARRISFJ COPIES LTTR ENCL~1.1 2 2 1 1 1.1 1 1 1 4 1 1 1 1 1 l.1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 h R D S h NOIE KO ALL'%ZCG" PLEASE HELP US IO REDUCE KQx~f CGÃ5KT'IHE DOQIMENT CXRZML DESKS RXN Pl-37 (EXT.20079)TO XZiIMZMGE K%K MME PRCH DIPI%GBUTIQN LISTS.MR IXXXIMENXS YOU DCKFT NEED!S TOTAL NUMBER OF COPIES REQUIRED: LTTR 43 ENCL 42 NAC Form 388 (983)LICENSEE EVENT REPORT (LER)U.S.NUCLEAR REQULATORY COMMISSION APPROVED OMB NO.31504104 EXPIRES: 8/31/88 FACILITY NAME'(ll Shearon Harris Nuclear Power Plant Unit 1 DOCKET NUMBER (2)PA 0 5 0 0 0 4 00 1 OFO 5"".'" Manual Reactor Trip Upon Loss of Main Feedwater Due to Trip of Heater Drain Pum s MONTH OAY YEAR EVENT DATE (5)LER NUMBER (SI YEAR gg SEQVENTIAL Srrr'UMBER REVISION NVMSER REPORT DATE 17I OAY YEAR MONTH DOCKET NUMBER(S)0 5 0 0 0 FACILITY NAMES OTHER FACILITIES INVOLVED (8)1 030 8 8 OPERATINO MODE (8)1 POWER LEYEL 0 9 8@Yvnrcrger<
0 5 0 0 0 2 9 8 8 0 3 2 0 0 8 8 73.71(III 73.71(c)50.73(s)(2)(lv) 50.73(s)(2)(vl 80.73(el(2)(vel 50.73(s)(2)(vLB)(A) s 50.75(e)12l(vill)(8)50.73(~)(2)(x)0 THE REQUIREMENTs oF 10 cFR g:/csece one'or more of tire follovt/no/
(11)THIS REPORT IS SUBMITTED PURSUANT T 20.405(cl 20AOS(s)(I IO)20,405(sl(1)(el 20.405(sl(1)(lll)SOM(c)(I)SOM(c)(2)50.73(s)(2)(l)50.73(e)(2)(ill 20A05(sl(1)(Iv)20.405(sl(1)(v)5073(s)(2)(ill)
OTHER/Specify In Abrtrect Oe/ore em/In Text, HRC Form 388A/LICENSEE CONTACT FOR THIS LER (12)NAME Joseph R.Johnson v Senior Specialist
-Regulatory Compliance s TELEPHONE NUMBER AREA CODE 919362-2083 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OESCRIBEO IN THIS REPORT 113)CAUSE SYSTEM COMPONENT MANUFAC.TURER EPORTABLE TO NPRDS F5@.:+(I CAUSE SYSTEM COMPONENT MANUFAC.TURER Tr EPORTABLE)TO NPRDS rA SUPPLEMENTAL REPORT EXPECTED (14)YES/lf yer, complete EIIPECZED SU84/ISSION DATE/X NO~AB$TRAGT/Llmlt to/400 spec'et, I e., epproxlmetr/y fifteen r/no/ecpece typevrrltten liner/(18)EXPECTED SUBMISSION DATE (15I MONTH OAY YEAR ABSTRACT: On October 30, 1988, the plant was operating in Mode 1 at 98/'ower.At 18:26:47 hours, the"B" Heater Drain Pump tripped causing an automatic turbine runback.Approximately 25 seconds'later, the"A" Heater Drain Pump tripped.Due to the rapid load reduction and sudden decrease in feedwater flow, the"B" Condensate Booster Pump tripped on high discharge pressure at 18:30:36.The control operator tripped the"B" Main Feedwater Pump at 18:31:00, and the"A" Main Feedwater Pump automatically tripped at 18:32:32, resulting in a loss of all feedwater flow.The control operator manually tripped the reactor at 18:32:44 and stabilized the plant in Mode 3.The event was initiated by the trip of the Heater Drain Pump which was attributed to a plywood cover inadvertently left inside Feedwater Heater 3A following maintenance.
In addition, the automatic turbine runback did not function as expected by the operators.
This.hindered their ability to stabilize the plant and avoid a reactor trip.The turbine runbacks were investigated and the response was in accordance with the design.The operators were retrained with the information obtained from the investigation of the runback functions.
The plywood cover was removed from the feedwater heater.8812050217 881129 PDR ADDCN 05000400 8 PNU NRC Form 388 (84)3)
NRC Form 3SSA ($83)LICENSEE EVENT'REPORT
{LER)TEXT CONTINUATION U.S.NUCLEAR RECULATORY COMMISSION APPROVED OMS NO.3'I50-010i EXPIRES: 8/31/88 FACILITY NAME (1 I Shearon Harris Nuclear Power Plant Unit 1 DOCKET NUMSER (2)LER NUMSER (5)YEAR/gal SEOUENTIAL jul NUMSER REVISION NUMSSR PACE (3)TEXT///more s/roce*nqakwt, oee aA55ond/I/RC Forrrr 38SA Sl (1 3)0 5 0 0 0 4 0 0 8 8 0 3 2 0 0 0 2 OF 0 5 DESCRIPTION:
I The:plant was operating-normally in steady.state..conditions:,at
-'98X'hermal power and producing I8771 net MWE.All'significant plant..control.
systems were in automatic, and all,Digital Electro-Hydraulic (DEH)Control System (EIIS:TG)feedback loops were operational.
The plant was in the process of returning to full power operation following refueling.
The 90X thermal power level was reached about 1700 on October 29, 1988..The.ascension to,-full power began about 1410 on October.30..As the power.-increase began, the"Low Delta P/Low Flow" alarm was periodically received for"B".Heater"Drain Pump (EIIS'.SN:P).
r The"Low NPSH" alarm'was actuat3.ng
'at regular intervals as power appr'oached 98X.By 1620, on October 30,,power was stabilized at.98X.There was no readily apparent reason for the Heat;er Drain System(fluctuations.
'I This transient was the result of a serf.es of complex plant interactions.
At 1826 the"Low Delta P/Low Flow"'larm actuated and"locked in." The"Low NPSH" alarm actuated, cleared, and actuated again.At 18:26:47 the"B" Heater ,Drain Pump (HDP)tripped.This started a turbine runback.The control operator expected the runback to stop at 86X turbine power.r Approximately 25 seconds'fter, the trip of the"B" HDP, the"A" HDP also tripped.The initial runback was still in progress due to overshoot caused by the turbine's (DEH)Control System'(EIIS:TG)P Reactor power at the time of the'A".HDP trip was'pproximately 93X as indicated by the Nuclear.Instrumentation System, and-approximately 70X turbine power.The turbine runback stopped when turbine power was approximately 54X at 18:27:32.As a result of the turbine load rejection, the Steam Dump Control System load rejection controller was armed and attempting to limit the increase in Reactor Coolant System average temperature caused by the mismatch'etween reactor power and turbine load.The Steam Dump valves to the condenser closed at 18:27:17 indicating that Reactor Coolant System average temperature was within 3 degrees of the reference value from turbine first stage pressure.Reactor power remained near 70X for approximately the next 3 minutes.During the transient, the Condensate Booster Pumps speed controller shifted to manual control due to discharge pressure increasing above a preset pressure.This was caused'y the decrease in feedwater flow and apparent overshoot by the Condensate Booster Pumps speed controller.
The control operator's were controlling steam generator water level by manually controlling the feedwater regulating valves, and were controlling the Main Feedwater Pump (EIIS:SJ:P) suction pressure by manually adjusting Condensate Booster Pump speed.However, the"B" Condensate Booster Pump (CBP)(EIIS:SG:P) tripped on high discharge pressure at 18:30:36.The operator expected the corresponding Main Feedwater Pump (MFP)to trip.When it did not, the operator.then manually tripped the"B" MFP at 18:31:00, because'he operators were trai.'ned that an automatic MFP trip should have resulted.NRC FORM 34OA (883)oU.S.GPO:1888 D82i.538/i55 NRC ForoI 388A (9431 LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U.S.NUCLEAR REOULATORY COMMISSION APPROVEO OMS NO.3150&ICE EXPIRES: 8/31/88 FACILITY NAME (1 I DOCKET NUMSER (ll LER NUMBER (Sl PACE (3)Shearon Harris Nuclear Power Plant Unit 1 m(T//F IIKoo OOoco/o Ioyo/CAE ooo aAWarW HRC Fom/355l3/(IT(DESCRIPTION (continued) 0 5 0 0 0 4 0 0 YEAR 1IAo EEOVENTIAL zlIN AEYIEION>p%NVM EA>><: NVMSEA 88-03 2-0 0 0 30F 0 5/Based on reactor power, the operators were expecting another-turbine runback upon, the trip of the"B",MFP,'ut it did not;.occur.
The runbackI did not occur'ecause the runback is based on turbine load, and it was already low enough to prevent the runback.An operator, believing that the automatic runback failed to occur, began a manual turbine runback, and started both motor driven Auxiliary Feedwater Pumps (EIIS:BA:P).
Steam Dump to'the condenser was agpin actuated, and the manual runback caused a reactor power change from approximately'0X to 60X'he Steam ,Dumps actuated from 18:32:02 tb 18:32:18.During this runback, the output of the"ALE CBP'was controlled manually to maintain discharge pressure.The"A" MFP suction pressure'ubsequently decreased to approximately 314 psig, and at 18:32!32, automatically tripped resulting in a loss of all main feedwater flow.Following these events, the reactor was manually tripped at 18.:32:44, and the plant was stabilized in Mode 3.Reactor power at the time of the trip was approximately 585.CAUSE There were two causal factors for this event.The loss of the heater drain pumps initiated the event, and the unexpected response of the DEH Control System during the turbine runback contributed to'the event.The'initial problems relating to the Heater Drain Pumps NPSH were attributed to an abnormal pressure drop across Feedwater Heater 3A, caused by a plywood cover that had been'inadvertently left inside the heater following maintenance activities during the previous refueling outage.The cover had been used to partially cover the feedwater inlet to the heater to allow workers a platform to stand on.Generally, individuals are allowed to follow good work practices on non-safety
'systems without detailed work procedures or inspection hold points.The failure to remove the plywood cover was a personnel error in failing to implement proper work practices.
Procedure MMM-011,"Cleanliness and Housekeeping," recommends a written record of the entry and exit of personnel and tools.The use of the record, however, is elective based on the judgment of the job supervisor.
The basic thrust of MMM-011 is to assure that the conduct of a specific job does not degrade the cleanliness of a system.The cover partially blocked the feedwater flow through the 3A&4A heaters, and in turn, increased the flow through the 3B&4B heaters.The increased flow through 3B&4B heaters caused increased condensed steam flow on the 4B heater shell si.de and decreased shell pressure.The"B" HDP takes suction from the 4B heater shell side.The heater level control system controls to a fixed level in the heater.The combined result was increased flow through the"B" HDP and decreased NPSH which caused the trip of the pump.NAC FOAM 3OOA (983 I*U.S.OPO:(988&828 538/455 NRC Form 3EEA (84(3 I LICENSEE'EVENT REPORT (LER)TEXT CONTINUATION U.S, NUCLEAR REGULATORY COMMISSION APPROVED OMB NO.3I SOMI04 EXPIRES: 8/31/88 FACILITY NAME (1 I DOCKET NUMBER (2I LER NUMBER (8)PAGE (3I Shearon Harris Nuclear Power Plant Unit 1 TEXT//F more epece/r/el/rkerL INe~HRC%%dr<<<<<<3RL/l lTI YEAR o s o o o 40 088 SEOVENTIAL NVM ER 0 3 2 REVISION NVMEER 00 04 OF 0 5 CAUSE (continued)
The:DEH Control System is designed such"that when the plant is operating above'90K<<thermal power, as sensed.by the turbine first,'.stage";impulse.
pressure, loss of either HDP will result in a turbine runback until turbine power is reduced to less than 86X.When the runback occurs, the DEH Control System removes the feedback loops from service and ramps down the reference counter (desired=load)at.1900 MW/min.until the runback signal.'has cleared, at wh'ich time it pill place the feedback loops back in service.The DEH Control System also , ramps the turbine governor valves shut using'alculated vaI.ues'valve management program)at a rate that should match the reference counter.However, experience has shown that, the governor valves will ramp shut at a slower rate than the reference counter.When the runback signal clears, and the feedback l,oops are placed back in service, the DEH Control System will continue closing the turbine governor valves until the reference counter and feedback signals match.This caused the DEH Control System to overshoot the turbine runback setpoints and create a 45X load rejection.
\The analysis of the event determined.
that the DEH Control System functioned properly as designed.However,"the-control operators were not trained to expect this response during a turbine runback with feedback loops in service.In addition, th'e operators did not recognize the magnitude of the load rejection.
These facts, coupled with-the rapid occurrence bf'events, hirfdered the operators'bility to, stabilize the condensate and feedwater system pressures to prevent the trip of the"B" CBP and"B" MFP.The operator expeCted the MFP to automatically trip after the trip of the"B" CBP, but it did not trip.However, the pump did function as designed.Present plant design does not cause hn automatic MFP trip upon high CBP discharge pressure.The pump will trip upon low flow or low suction pressure as a result of the loss of the CBP, but these trips have time delays of 5&30 seconds respectively.
Plant operators are trained to manually trip an MFP following a CBP trip, if it does not occur immediately.
The cause of the'rip of the"B" CBP was attributed to high discharge pressure.Although the highest discharge pressure recorded by the plant computer was 607 psig, (the CBP trip setpoint is 625 psig), the pressure switches that actuate the pump trip could have seen a momentary spike not recorded by the pressure transmitter that feeds the computer.The trip was found to be within the tolerance of the applicable pressure switches'he cause of the trip of the"A" MFP was attributed to incorrect calibration of the pressure switch for the low suction pressure trip.A post trip review found the switch set at 305 psig instead of the required setpoint of 250 psig.A NRC FORM 34EA (843 l 4 U.S.GPO:18804<<
024.838/4SS NRC ForrmI 344A I94LTI I LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U mL NUCLEAR REOULATORY COMMISSION APPROVED OMB NO.3160&194 EXPIRES: 8/31/88 FACILI'TY NAME Ill Shearon Harris Nuclear Power Plant Unit 1 DOCKET NUMBER ISI YEAR LER NUMBER (Sl Sl SEOVENTIAL QI.,.3 NVMSER Pm REVISION NVM ER PACE IS)TEXT//amore epece ie/I1/reed See//I/Ooe///RC Forer 34843/(ITI ANALYSIS OF EVENT: o s o o o 40 088-0 3 2-0 0 0 5 QF 0 5 There were no adverse safety.consequences-resulting.
from this-event.All plant systems responded as intended, and.'he:.plant'as stabilized in Mode,3 at normal no load temperature and pressure.Normal steam generator water levels were restored with the Auxiliary Feedwater System (EIIS:BA).
This event is being reported in accordance with.10CFR50.73(a)(2)(iv) as an actuation of an Engineer'ed Safeguards Feature and Reactor Protection System.~'Previous similar events associated with the loss of Heater Drain Pumps and resulting in reactor trips were reported in LERs 87-019-00, 87-024-00, 87-025-00, and 87-031-00; however, these events are, not directly related to'."his LER because of different root causes for the heater drain pump'trip and the concurrent large turbine load decrease.CORRECTIVE ACTION.I.1.Feedwater Heater 3A was opened and.inspected.
m.,A.plywood,.cover'as found inside the heater pnd'as removed.The heater was restored to service, 3~To prevent the overshoot of setpoints during a turbine runback, a design change to the DEH Control System wi11 be considered, which'ill ensure that the feedback loops, once taken out of service will not'e automatically placed back in service.Plant operators will be provided training on the event and the effect of feedback loops on turbine runback conditions.
4.An operations night order was issued that requires the feedback loops to be taken out of service before exceeding 90%power.A change to applicable procedures will be made.5.Disciplinary action was taken for the personnel responsible for leaving the cover in the 3A Feedwater Heater.6.A review of the current controls and closure inspections of systems will be conducted.
7.Retraining of applicable maintenance personnel on proper work practices for system cleanliness will be conducted.
NRC SORM 344A 1983l*U.S.OPO;19884-834 d38/4dS
@&54 Carolina Power 8 Light Company.HARRIS NUCLEAR PROJECT P.O.Box 165 New Hill, NC 27562 NOV 29 1988'File Number.SHF/10-13510C Letter Number: HO-880241 (0)U.S.Nuclear Regulator/
Commission ATTN: NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO.50-400 LICENSE NO.NPF-63 LICENSEE EVENT'REPORT 88-032~00 Gentlemen:
In accordance with Title 10 to the Code of Federal Regulations,'he enclosed Licensee Event Report is submitted This report'ulfills the requirement for a written'report within thirty (30)days of a reportable occurrence and is'n accordance with th'format set forth in NUREG-1022, September 1983.Very truly yours, JRJ:dj Enclosure R.A.Watson Vice President Harris Nuclear Project cc: Mr.W.H.Bradford (NRC-SHNPP)Mr.B.Buckley (NRR)Mr.M.L.Ernst (NRC-RII)MEM/LER-88-032/1/Osl
>r,.