ML20197D211

From kanterella
Revision as of 00:01, 21 December 2021 by StriderTol (talk | contribs) (StriderTol Bot change)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
Insp Rept 50-354/97-09 on 971005-1115.Apparent Violation Being Considered for Escalated Ea.Major Areas Inspected: Licensee Operations,Engineering,Maint,Plant Support & Site Security Programs
ML20197D211
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 12/10/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20197D206 List:
References
50-354-97-09, 50-354-97-9, NUDOCS 9712290003
Download: ML20197D211 (29)


See also: IR 05000354/1997009

Text

.

.

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Do:ket No:- 50 354

License Nos: NPF 57

Report No. 50 3E4/97 09

Licensee: Pubhc Service Electric and Gas Company

Facility: Hope Creek Nuclear Generating Station

Location: P.O. Box 236

Harscocks Bridge, New Jersey 08038

Dates: October 5,1997 November 15,1997 ,

'

inspectors: S. A. Morris, Senior Resident inspector

J. D. Orr, Resident Inspector ,

G. C. Smith Senior Physical Security inspector .

E. B. King, Physical Security Inspector .,

E. H. Grav, Senior Reactor Engineer

Approved by: James C. Linville, Chief, Projects Branch 3

Division of Reactor Projects

,

t

9712290003 971210

PDR ADOCK 05000354 i

G PDR u.

.. - -

.-. . - . . . , - - . . _ _ - - --- . - . - . . - . - - . . - .. . . ,


.. - - . - . .. -- - _ - _ ...- - - - - .

!

< * 1

!

l

.

l'

EXECUTIVE SUMMARY

, Hope CreJk Generating Station

NRC Inspection Report 50 354/97 09

'

j

] This integrated inspectior. includes aspects of licensee operations, engineering,

maintenancc, and plant support. The report covers a six week period of resident -

inspection; in addition, it includes the results of announced inspections by three regional .

inspectors, one who reviewed PSE&G follow up activities to the core spray norzle through j

wallleak event and two who evaluated the effectiveness of site security programs and i-

-

practices.

! QacIations 1

!

Operators demonstrated inconsistent performance overall, and exhibited notable

.

- weaknesses with respect to attention to detail and awareness of equipment status. i

4

(Section 01.1)  !

PSE&G personnel displayed excellent overall performance in the development, pre bricling,

, and implementation of the plan to drain down the reactor cavity and vessel to support core

]

- spray nozzle repair efforts. (Section 01.2) ,

Operators exhibited poor performance during the conduct of an infrequently performed l

shutdown margin demonstration in that a stuck control rod procedure was not followed  ;

and conservative decision making with regard to reactivity management was not

4 demonstrated. Additionally, these actions and decisions were not sufficiently challenged

by control room observers. (Section 04.1)

,

The inspectors judged that Quality Assurance findings were well supported, independent,

-

and promptly referred to station management for action. Quality Assurance oversight of

control room activities was usua'ly good. (Section 07)

Maintenance  ;

!

- Maintenance department technicians exhibited adequate performance during the conduct of

outage work activities and testing. While procedure and work order usage was generally

good, deficiencies in interdepartmental coordination and foreign material exclusion controls

were evident. (Section M1.1)

Numerous unplanned emergency diesel generator start attempts and equipment restoration

delays were encountered as a result of poor work centrols over mechanical govemor

maintenance and replacements. (Section M4.1)

Maintenance technicians improperly set up the mechanical overspeed trip device for the 4

. reactor core isolation cooling turbine in part due to weak procedural guidance, which

complicated a subsequent tutbine overspeed event. Insufficient verting of the turbine

control oil system, again partly because of limited proceduro guidance, was judged to be

the primary cause of the overspeed event. (Section M4.2)

ii

4

h

e

-+-m+ s-,-w .----s,, wm -~-w-nse, e A -- - m-me-w.* s m~ m-em.~-n--..,mSm -rw-,,-w-+,,w e mm t.e + mv- ,--r e. - , <p-w- mm nn gn--,-.--e---- a m n v m ,- wv mm w n , , ,.$

_ _ ._ _ . _ _ . . _ . _ _ . _ _ _ _ _ _ _ _ . _ . _ _ _ _ . _ . . _ _ ._ __ _ _ .. _

. I

!

'

,

PSE&G performed a detailed and thorough evaluation of the f ailed core spray nozzle weld

j history, previous nondestructive testing, and through wallleak causal f actors. Proposed-

corrective actions were judged to be reasonable and appropriately focused on preventing

recurrence. However, the f ailure to detect and repair a weld flaw in 1995 during a focused i

ultrasonic inspection of the noted core spray nozzle highlighted weaknesses in the Hope  ;

Creek inservice inspection program. (Section M8.1) i

inadequate surveulance test procedure development led to the undetected inoperability of

,

one train of the filtration, recirculation, and ventilation system. Corrective actions were  ;

-

effective. (Section M8.3)

Enaineerina -

PSE&G promptly developed and implemented an acceptable design cho. ige packege to  !

resolve a self identified issue involving bracket weld cracks on jet pump instrument lines. l

(Section E1.1)  !

Engineering department prepared safety evaluations were of good quality and were

appropriately focused on the potential nuclear safety impact of the plrnt design or

equipment changes. (Section U2.1)

PSE&G acted promptly and effectively in the resolution of a self identified issue involving a

potential secondary containment bypass leakage pathway. (Section E8.4)

'

!

Plant Suonort

PSE&G maintained an effective site security program. Management support of program

'

objectives was evident. Performance of security department person.nc! cnd equipment

were generally good.

,

PSE&G's provisions for land vehicle control measures satisfied regulatory requirements and

licensee commitments. The site protected area barrier was properly installed and

maintained, and satisfied the requirements of the NRC approved security plan.

!

s i

l

iii

- . - . _ _ _ . _ _ _ _ _ . _ _ , _ _ _ _ _ _ _ _ _ _ _ _ - - . .__ _ _ . _ _ . _ _... _ _ ..

.

.

TABLE OF CONTENTS

EX E C UTIVE SU M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

T A B L E O F C O N T E N T S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv

1. O p e r a t i o n s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.1 General Observations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.2 Reactor Cavity and Vessel Drain Down Evolution ............ 2

04 Operator Knowledge and Performance . . . . . . . . . . . . . . . . . . . . . . . . . 3

04.1 Shutdown Margin Demonstration . . . . . . . . . . . . . . . . . . . . . . . . 3

07 Quality Aseurance in Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

08 Miscellaneous Operations issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

08.1 (Closed) LER 50 354/9713 01: Unplanned high pressure coolant

injection system inoperability ..........................6 ,

ll . M a in t e n a nc e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

M1 Conduct of Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

M1.1 General Observations of Maintenance and Surveillance ........ 6

M4 Maintenance Staf f Knowledge and Performance . . . . . . . . . . . . . . . . . . 7

M4.1 Emergency Diesel Generator Maintenance and Testing . . . . . . . . . 7

M4.2 Reactor Core Isolation Cooling System Maintenance and Testing .9

M8 Miscellaneous Maintenance issues . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

M8.1 (Closed) URI 50 354/97 07 02:"A" core spray nozzle (N50) sofe end

leak, non-destructive examination and repair . . . . . . . . . . . . . . . 10

M8.2 (Closed) LER 50 354/97 23: core spray nozzle weld through wallleak

..............................................11

M8.3 (Closed) LER 50-354/97 26:*E" filtration, recirculation, and

ventilation system recirculation unit inoperability due to tripped high-

high temperature switch - procedure deficiency . . . . . . . . . . . . . 11

Ill . E ng ine e r ing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 2

E1 Conduct of Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

E1.1 Jet Pump Instrument Line Bracket Weld Cracking . . . . . . . . . . . 12

E2 Engineering Support of Facilities and Equipment ................. 13

E2.1 Design Change Package and Safety Evaluation Review ....... 13

E8 Miscollaneous Engineering Issues . . . . . . . . . . . . . . . . . . , . . . . . . . . . 14

E8.1 (Closed) LER 50 354/96-09: operation in an unanalyzed condition due

to inappropriate service water system / safety auxiliaries cooling

system throttle valve settings . . . . . . . . . . . . . . . . . . . . . . . . . 14

E8,2 (Closed) LER 50-354/9615: potential to operate in an unanalyzed

condition due to a design deficiency in the (service water emergency)

overboard discharge line . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

E8.3 (Closed) LER 50 354/97-24:as found values for safety relief valve lif t

setpoints exceed technical specification allowable limits ...... 15

E8.4 (Closed) LER 60 354/97 25: design deficiency potential for an

unmonitored release path through the station service water system

iv

_ _ - . _ -_

l

-  ;

l

i

i

.

..............................................16 l

E8.5 (Closed) URI 50 354/96 04 06:non conservative rnaximum ultimate l

'

heat sink temperatura limit . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

E8.6 (Closed) VIO 50 354/E96 28104013: inappropriate service

water / safety auxiliaries cooling system throttle valve settings . . . 16  !

l

IV. Pl a nt S u pp or t . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

S1 Conduct of Security and Safeguards Activities . . . . . . . . . . . . . . . . . . 16 l

S2 Status of Security Facilities and Equipment . . . . . . . . . . . . . . . . . . . . . 17

S2.1 Protected Area Access Control of Vehicles . . . . . . . . . . . . . . . . 17

S2.2 Alarm Stations, Communications and Assessment Aids . . . . . . . 17

S2.3 Testing, Maintenance and Compensatory Measures . . . . . . . . . . 18

S5 Security and Safeguards Staff Traininn and Qualification . . . . . . . . . . . 19

S6 Security Organization and Administration . . . . . . . . . . . . . . . . . . . . . . 19

S7 Ouality Assurance in Security and Safeguards Activities ...........20

S7.1 Audits .........................................20  !

S8 Miscellaneous Security and Safeguards issues ............. . . . . 21 l

S8.1 Vehicle Barrier System . . . . . . . . . . . . . ................21 .

S8.2 Bomb Dia st Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21 l

S8.3 Procedural Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 2

V. M a nag eme nt M e e ting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 2

X1 Exit Meetine Summ ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 2 i

X2 Review of Updated Final Safety Analysis Report . . . . . . . . . . . ..... 22 i

i

v  :

-- - - . , ._ ,_

.

,

Report Details

1, 0Refstions

01 Conduct of Operations

.

QM General Observatlora

a. jnsocution Scone 171707)

Throughout the report period, the inspectors routinely reviewed and obserwd

operator performance with respect to technical specification (TS) action statement

tracking, proceduto compliance, attention to detail, and reportable event accuracy

and timeliness. Quality assurance (OA) efforts were also assessed.

b. Qb.tmiyations and Findinas

The inspectors witnessed inconsistent performance by operators during their

conduct of routine and off normal activities. For example, reactor fuel reload

activities were executed very well, in contrast to the offload activities earlier in the

outage. All fuel moves were performec'in a single dimension, and no errors were

noted in bundle selection or placement. As noted in section 01.2 below, efforts

involving the reactor cavity drain down were conducted effectively. Shutdown

cooling and spent fuel pool decay heat removal system flow paths were closely

controlled and protected. Control room operators were generally f amiliar with most

work being conducted in the plant.

OA inspector coverage in the control room was frequent and provided generally

good independent assessment of plant activities. Of particular note, a OA inspector

questioned operators on whether a decision to commence core alterations

(operational condition') from operational condition 5 was consistent with TS 3.0.4

since two trains of the filtration, Iacirculation and ventilation system (FRVS) were

inoperable. TS 3.0.4 mandates that entry into an operational condition shall not be

made when conditions for the limiting conditions for operation (LCO) are not met

and the associated action statement ultimately requires a plant shutdown. The

FRVS TS 3.6.5.3 LCO requires that all six FRVS recirculation units be operable in

operatii, ial condition'. Because of OA intervention in this issue, a potential TS

violation was avoided during the operational condition change.

The inspectors noted other performance deficiencies during the report period.

Specifically, on November 7,1997, relieving operating shitt personnel questioned

off going operators about the status of the safety parameter display system. At

that point off going operatorr reallred that the system had been inoperable for

nearly 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, since the degraded condition was first identified and

communicatsd to engineering personnel for resolution earlier in their shif t. Operators

appropriately recognized that this condition required a non-emergency 10 CFR

50.72 report to the NRC as a " major loss of emergency assessment capability" in

accordance with the Hopa Creek emergency classification guide. Operations

management concluded that this reportable event resulted from inadequate

turnovers, follow up, and communichtions.

,

,. -

rv- r- . ,- , - , - - - - - ,- -,--n--e,

. ..--_. - ._ - . . - - _ __. . . ._ _- - _ _ .

.

.

2 I

Othat weaknesses were identified as well. A loss of offsite power / loss of coolant

accident (LOP /LOCA) surveillance of the *B" 4100 VAC vital bus had to be rapeated >

when the *B" residual heat removal system pump failed to start because the motor

supply breaker switch was inadvertently lef t in " pull to lock." Implementation of

several test procedures, including a reactor core isolation cooling system valve

inservice test procedure observed by the inspectors, did not meet department

expectetions for placekeeping. A reactor auxiliaries cooiing system head tank

overflowed while troubleshooting continued on an emergency diesel generator  ;

control system because operators did not maintain full cognizance of system status.

Though not anticipated, a service water pump automatically started as designed i

during a remote shutdown panel test because the pump controls were left in

automatic during the activity. While performing core alterations, secondary

containment pressure went positive with respect to atmospheric conditions during

recovery from a LOP /LOCA surveillance when a reactor building ventilaCon

subsystem tripped. The unreliability of this subsystem had been demonstrated by

earlier unexplained trips, and caused the inspectors to question the decialen (af ter

the f act) to continue fuel movements during the noted LOP /LOCA tert.

c. C,onclusiont

Operators demenstrated inconsistent performance overall, and exhibited notable

weaknesses with respect to attention to detail and awareness of equipment status..

Quality assurance oversight of control rooms activities was usually good.

QL2 Reactor Cavity and Vessel Drain Down Evolution

a. Impection Scope (71707)

The inspectors observed portions of the planning, briefing, and implementation of a

first time evolution involving a reactor cavity and vessel drain down to suoport weld

repair efforts on the "A" core spray line nozzle.

b. Observations and Findinos

Weld repairs for the through wallleakage on the "A" core spray nozzle (see NRC

Inspaction Report 50 354/97 07 for details) required that the vessel penetration be

drained of water. Because this penetration is not isolable from the reactor vessel,

operators devised a plan for draining the cavity and vessel to a level below the

nozzle to support the work. The reactor fuel bundles were completely offloaded

into the spent fuel storage pool. The inspectors reviewed the newly prepared

procedure, which was in part based on other industry experience, and jedged it to

be of good depth and quality. PSE&G completed thorough reviews of the

procedure, which included a final approval by the station operations review

committee.

The pre evolution briefing was timely and comprehensive, and was attended by a

wide array of direct and peripheral evolution participants. Contingency measures

were thoroughly discussed, and effective communications were stressed.

_ _ _ _ _ _ __

_ _ _ .. _ . - . _ _ _ _ _ _

_ _ . _ _ _ _ _ _ _ . _ - _ _ _ ,

[

4

3 [

'

Because the entire core had been transferred to the spent fuel storage pool,

operators planned a functional test of the residual heat removal fuel pool cooling

assist mode bnfore the fuel pool getes were installed. The inspectors observed the

functional terit, an activity which had not been perforrned since Hope Creek pre-

operational testing. Based in part on a prior detailed procedure walk through, the  ;

test was completed without error or incident.

Operators properly conducted the drain down evolution using the newly developed

procedure. Appropriate actions were taken upon discovery that the equipment pool

gate seals were leaking water at a rate of several hundred gallons per minute, ,

Oulck recognition and timely response !n accordance with pre planned contingencies

and briefings ensured that no additional complications were encountered. The gate

seals were repairet, and the drain down was completed successfully. The

inspectors witnessed excellent management oversight and interdepartmental l

coordination during this activity. +

c. Conclu11ong

PSE&G personnel displayed excellent overall performann ir* the development, pre-

bilefing, and impleninntation of the plan to drain down the reactor cavity and vessel

to support core spray norrie repair efforts.

04 Operator Knowlvdge and Performance ,

QL1 Shutdown Maroin flamonstration

a. ADippetion Scone U1707)

The inspectors observed portions of a post refueling reactor shutdown margin

demonstration performed to demonstrate compliance with technical specification 3.1.1.

b. Observations and Findinas

On November 12,1997, with the plant in operational condition 5 (reactor vessel

head removed). control roon, operators began a core shutdown margin

demonstration in accordance with procedure HC.RE ST.ZZ 0007(O). This test  ;

'

involved the full withdrawal of twenty control rods (of 185 total) selected by the

reactor engitioering .tarf. Operamrs invoked "special test exception" TS 3.10.3 to

permit conduct of this infrequently p9rformed svolution since the test required the

mode switch to be placed in the **.tartup" pc ition, defeating the one-rod out

interlock normally required le operational condition 5. The inspectors verified that all

associated TS required conditions were satisfied during performance of the test,

which included reactor protection system (RPS) shorting link removal and the need '

fo % dependent oversight and verification of test procedure compliance by a

" technically qualified member of the staff," in this case the reactor engineering

department supervisor, since the rod worth minimiter was inoperable.

_ _-, __ - . - - . _. __

.

.

4 -

Operators experienced difhculty withdrawing several of the test-designated control

rods. As cuch, early in the evolution during an initial observation, the inspectors ,

noted that operators appropriately implemented step 4.6 of the stuck control rod l

procedure, HC.OP AB.ZZ 104(O), which requires that control rod drive (CRD)

hydraulic system drive water pressure be " raised in 50 psiincrements" until the

tod(s) were freed during single notch attempts, at which time the pressure "should

be immediately restored to the norrnal range" (260 270 psi). However, later in the

evolution during a subsequent observation, the inspectors noted that one control

rod appeared to withdraw from the core abnormally f ast, and determined that drive

water prewsure was still at an elevated level (approximately 400 psi), indicating that

drive pressure was not returned to the normal range following successfulinitial

movement. Additionally, operators did not return the drive water pressure to the

normal range prior to selecting and withdrawing the next rod in sequence. This

latter observation indicated that operators inappropriately remained M the stuch rod

procedure without first meeting the prerequisite of unsuccessful control rod

movement with normal drive water pressure. The inspectors questioned this

practice because it appeared to be contrary to the noted proceduro guldance, and

because continuous rod withdrawals from position 00 to 48 were being performed.

,

The senior reactor operator (SRO) supervising the evolution stated that he felt

justified in departing from the stuck rod procedure (both the prerequisites for usage

and step 4.6 regarding the incrementalincreases in drive pressure) in part because.

he was concerned that repeated cycling of the CRD pressure control valve was

distracting his reactor operator from monitoring the source range count rate nuclear

instrumentation. Further, the SRO stated that he " knew," based on experience, that

every rod in the test sequence would require an elevated drive water pressure in

order to be withdrawn. He further stated that the on duty operations

superintendent also endorsed this practice. The reactor engineering department

supervisor monitoring the evolution did not express a concern. The inspectors

shared their observations with a quality assurance inspector also present in the

control room but that individual did not independently pursue resolution of the issue

with station management. Finally, no narrative log entries were made describing

the basis for departing from the specific requirements of the abnormal operating

procedure.

The inspectors judged that operator's acted non-conservatively when they elected

not to adhere to the requirements of the stuck control rod abnormal operating

procedure, in that they permitted reactivity additions at potentially unknown or

uncontrolled rates. Specifically, operators performed an infrequent evolution which

added positive reactivity to an essentially now, untested reactor core with several

new control rod blades using CRD mechanisms and hydraulic control units which

had undergone either complete replacements or large scale maintenance, with their

operability not yet fully demonstrated. Defense-in-depth from a potential fission

product release was reduced since one of the principal barriers was degraded (i.e

the vessel head was removed). The one rod-out interlock was defeated because the

reactor mode switch was in "startup" to support performance of the test.

Moderator temperature was below 100 degrees F, increasing core reactivity. The

rod worth minimizer was inoperable and was being compensated by additional

- . . . - . - ___ _ __

_ _ ._ . .

.

. I

1

5

human oversight Collectively, the inspectors judged that these conditions 6Sould

have warranted increased vigilance by reactor operators adding reactivity to the

core, especially during an evolution that is designed to verify that the reactor will

remain sufficiently ruberitical with twenty rods fully withdrawn.

The inspectors reviewed other PSE&G procedures prescribing expectations for

reactivity management and conservative decision making. The inspectors identified

two procedures, NC.NA AP.ZZ 0005(O) (NAP 5) and HC.0P AS.ZZ 0002(Z), which

provide guidance la these areas. Sections 5.21 and 6.30 of NAP-5 prescribe station .

'

policy on the use of reactivity controls and specifies that personnel "act

conservatively when f aced with adverse conditions which could affe-t reactor

safety." The latter noted procedure, which is a specific Hope Creek operations

department performance standard, requires operators to adhere to reactivity

manipulation procedures " alertly and cautiously," and to move control rods in a

" deliberate, :arefully controlled manner." The inspectors judged that the standards

of performance defined in these two documents were not met during the November

12,1997 shutdown margin demonstration.

Until the inspectors discussed their observations with senior site management on

November 13,1997, the significance of the noted issues went unrecognized by

station personnel. Station management demonstrated an appropriate response to

the issues, which included a formal debriefing with all of the station operators, and,

initiation of a formal root cause and fact finding investigation. Memorandums

reiterating expectations for maintaining " utmost caution" during reactivity

manipulations were also issued. The responsible on shif t operations superintendent

was reassigned to other duties.

The inspectors noted that no actual safety consequences resulted from performance

of the shutdown margin demonstration. Also, actual measured control rod speeds

during the test were later determined to be within the analyzed envelope. However,

plant eperation outside established reactivity manipulation procedures under the

described circumstances reflected a poor operating practice and was judged to be

an apparent violation of TS 6.8.1 procedure requirements. (eel 50 354/97 09 01)

c. Conclusions

Operators exhibited poor performance during the conduct of an infrequently

performed shutdown margin demonstration in that a stuck control rod procedure

was not followed and conservative decision making with regard to reactivity

management was not demonstrated. Additionally, these actions and decisions were

not sufficiently challenged by control room observers.

07 Quality Assurance in Operations

The Quality Assurance (QA) departrnent conducted a detailed team review and audit

of Hope Creek operations department performance with focus on technical

specification (TS) implementation and action tracking during the report period. The

inspectors observed portions of the audit and discussed relevant QA findings with

.

4

0

lead oversight personnel. The QA team concluded that verbal communications,

peer checking, infrequent evolution pre job briefs, and senior reactor operator

oversight of control room activities were good. No improper operability

determinations were identified. Howrver, the team Judged that procedure

placekeeping and documentation, as well as TS action statement tracking, were

weak. The team also concluded that there appeared to be a negative trend with

respect to conservative decision making. Several examples, including the above-

described shutdown margin demonstration issue, were used as a basis for reaching

this conclusion. The inspectors judged that QA findings were well supported,

independent, and promptly referred to station management for action.

08 Miscellaneous Operations issues

QL1 (Closed) LER 50 354/9713 01: unplanned high pressure toolant injection system

inoperability. This event was described in detailin NRC Inspection Report 50-

354/97 04 and resulted in issuance ci a violation of 10 CFR 50 Appendix B

Criterion XVI. This supplemental LER was submitted to describe in greater detail

the impact and significance of the event. Specifically, plant operators failed to enter

TS 3.0.3 and commence a plant shutdown because the inoperability of the high

pressure coolant injection (HPCI) system was not recognized during the period of

time when two trains of the residual heat removal system were inoperable for on-

line maintenance. The inspectors judged that the LER accurately described the

circumstances of the event and that proposed corrective actions were reasonable.

No additional new information was provided by this LER.

II. Maintenang_t

M1 Conduct of Maintenance

M 1.1 General Observations of Maintenance and Surveillanca

a. inspection Scope (71707)

Throughout the report period, the inspectors conducted frequent observations of

station maintenance and surveillance activities to verify proper procedures were in

use, adequate retests were completed or scheduled, monitoring and test equipment

(M&TE) was within calibration, housekeeping and foreign material exclusion

standards were satisfied, and coordination between departments was evident.

Additionally, the inspectors reviewed PSE&G actions taken in response to self-

identified or self revealing issues involving maintentnce or testing. A sample of

safety-related equipment tagouts were evaluated for adequacy of development and

implementation. Detailed assessments of specific observations and reviews are

described in section M4.

- - . . .. . _ _ - _ -.____-_ - - - _... . - - - _ _ . _. -- - . - _ - -- - -__ - .

'

.

i

/ ,

,

b. Observations and Findinas

,

The inspectors observed inconsistent performance with respect to maintenance

department activities. While most work orders reviewed spelfied adequate post-

maintenance retest activities, some were noted to be deficient because the

proposed tests were too narrowly focused. Though inspector verifications of

equipment tagouts did not identify any deficiencies, several self identified "near-

misses" were docurnented. Most observed maintenance was adequately supervised

and coordinated between engineeri ,g and operations, however on one instance

security grates were partially removed from circulating water system piping without

prior notification of security personnel to ensure that appropriate compensatory

measures were in place.

Weld overlay repairs of the through wallleak on the NSB core spray nozzle were

well planned, coordinated and executed. Underwater work in the primary

containment suppression pool to replace the *D" residual heat removal suction

strainer was aiso well executed. Torus cleaning activities were judged to be

excellent; the inspectors conducted an extensive pre closeout tour of the torus and

found only minor deficiencies.

Howover, several performance deficiencies were also noted. For example, foreign

~

.

material exclusion practices on the refuel floor were initially poor in that several

objects were inadvertently dropped into the reactor cavity while the reactor vessel

head was removed. Subsequent actions to improve performance in this area were

effective, including more strict use of lanyards, tool controls, etc. A vital bus loss

of power / loss of coolant accident surveillance test activity had to be repeated

because maintenance technicians improperly set up the M&TE used for test data

collection. Poor coordination with operations personnel during conduct of scram

discharge volume (SDV) flushing resulted in the generation of an unexpected half-

scum signal when water level exceeded SDV the trip setpoint.

,

c. Conclusions

Maintenance department technicians exhibited inconsistent performance during the

conduct of outage work activities and testing. While procedure and work order

usage was generally good, deficiencies in interdepartms. ital coordination and foreign

material exclusion controls were evident.

M4 Maintenance Staff Knowledge and Performance

M4.1 Emeroency Diesel Generator Maintenance and Testina

a. Inspection Scone fQ2707)

The inspectors reviewed the circumstances surrounding several f ailed post-

maintenance tests and surveillances of the emergency diesel generators (EDG).

Additionally, the inspectors observed the startup and troubleshooting of the "A"

EDG on November 6,1997. Discussions related to the testing failures were held

with control room operators, engineers, and maintenance supervisors,

i

-. , _ . _ . , -_,.-~e_. ,. - .-.- _ . . . - - .._ . , , . , . . ...., , . _ . _,. . ,,m- m . _ . . . .m . _ _

-- .. . .

.

8

b. Observations and Findinas

Following a scheduled electronic governor replacement, maintenance technicians

began overspeed trip testing on the "B" EDG on September 27,1997. The

technicians noted during restoration from the %st that the mechanical governor

speed control adjustment, used during the o tspeed test, could not be returned to

its original pre test setting. The entire mechanical governor assembly was then

replaced based on a vendor recommendation, and the damaged unit was shipped

offsite to a repair f acility. PSE&G reviewed the maintenance history on the *D" EDG

mechanical governor and determined that the most likely failure of the speed control

was an over adjustment of the speed knob on September 27,1997 con blned with

inadequate tightening of internal governor dial stops in December 1994.

On September 29,1997, two attempts were made to start the "B" EDG for post-

maintenance testing af ter the mechanical governor replaccment. On both attempts

the EDG tripped on low lube ol' pressure. PSE&G later determined that the initial

setup of the new mechanical governor did not ellow the engine to develop sufficient

speed to clear the low lube oil pressure trip. PSE&G subsequently developed a new

procedure which provides guidance for performing initial diesel generator mechanical

governor setups af ter maintenance or replacement (" Diesel Generator Speed / Load

Control System Alignment," HC.MD CM.KJ-0015(O)h The inspectors learned that

previous mechanical governor maintenance was conducted with direct oversight by-

vendor representatives using work orders ind vendor technical references as

guidance.

On November 6,1997, following outage work, the "A" EDG was carrying the

10A401 vital bus in accordance with " Integrated Emergency Diesel Generator

1 AG400 Test 18 Months," HC.OP ST.KJ-0005(O). During the test, the control

room operators discovered that the EDG would not respond to speed changes. The

EDG was shut down and engineering personnel developed an action plan to

troublesnoot the control problem. Technicians subsequently determined that the

mechanical governor was improperly set, controlling the engine speed at too low a

value which prevented the electronic governor from effecting speed changes.

Further investigation by PSE&G determined that the speed knob on the mechanical

governor was not restored to the proper position at the conclusion of an earlier

overspeed test.

The inspectors noted that none of the affected EDG's described above were

required to be operable at the time of the maintenance or testing. Additionally, all

of the applicable technical specification EDG surveillance tests were completed

satisfactorily for each machine prior to restoring them to an operable status,

c. Conclusions

Namerous unplanned emergency diesel generator start attempts and equipment

restoration delays were encountered as a result of weak work controls over

mechanical governor maintenance and replacements.

- -- - _. - _ -.----_- - - -.- - - - - -

.  !

!

l

9  !

M4.2 Reactor Core Isolation Coolina System Maintenance and lestina >

a, lasoection Scone (62707)

The inspectors reviewed the maintenance conducted prior to and following a reactor

'

core isolation cooling (RCIC) system turbine overspeed trip event du'ing testing,

b. Observations and Findinos

On November 9,1997, with the rtuctor plant in operational condWnn 6,

maintenance technich.ns attempted to perform an overspeed trip test of the RCIC

turbine using auxiliary steam in accordance with procedure HC.MD PM.FC 0001(O),

  • Reactor Core isolation and Cooling Steam Turbine Inspection and P.M." The pre.

Job brief for the evolution was good in that Individuals were assigned specific

4 actions should unforeseen e.ircumstances arise during the test. As required, the t

'

turbine was uncoupled from the pump and turbine speed was controlled from a local

potentiometer and was raised in 50 rpm increments, with an overspeed trip t

expected at approximately 5625 rpm. At 4900 rpm, the RCIC turbine unexpectedly  ;

accelerated to about 7500 rpm. A maintenance technician in the RCIC room

immediately tripped the turbine with the local trip device after recognizing the

,

overspeed condition, as assioned during the pre job brief. The RCIC system was

not required to be operable at the time of the test.

The inspectors judged the PSE&G's troubleshooting plans and follow up actions to

the overspeed event to be adequate. Based in part on vendor recommendations,

RCIC turbine inspections were conducted to verify that the no equipment damage

resulted. PSE&G determined that one of the causes of the event was that the

mechanical overspeed trip device was not properly set up during the previous

system maintenance, primarily bucause the work procedure did not provide

sufficient detail to ensure consistent implementation. PSE&G revised the HC.MD-

PM.FC 0001(Q) procedure to include a detailed verification that the mechanical

overspeed trip device is properly set prior to operating the turbine. Engineers

determined the most likely cause of the overspeed event, aside from the failure of '

the trip mechanism, was air entrapment in the turbine governor control oil following

a filter change. PSE&G enhanced the RCIC turbine operating procedures by adding

additional oil system venting activities to minimize the potential for air introductlen

during RCIC operation.

c. Conclusions

Maintenance technicians improperly set up the mechanical overspeed trip device for

'

the RCIC turbine in part due to weak procedural guidance, which complicated a

subsequent turbine overspeed event, insufficient venting of the turbine control oil

wystem, again partly because of limited procedure guidance, was judged to be the

primary cause of the overspeed event.

. ~ . _ . _ _ , . - _ _ _ _ __ _. _ _ _ _ - - _ _ - - _ _ _ _ _ _ _.-

.

10

M8 Miscellaneous Maintenance issues

M8.1 (Closed) URI 50-354/97 07-02:"A" core spray nozzle (NSB) safe end laak, non-

destructive examination and repair.

a. htmgetion Scoce (73115)

This inspection was conducted as a followup to an issua 8M' unresolved following a

recent inservice inspection program assessment. The W ..ivolved the f ailure to

identify degradation prior to the development of a through wallloak in the NSB core

spray nozzle to safe end weld. The process employed to repair the lock (weld

overlay with .emperbead welding) on the low alloy steel nozzle was also reviewed.

b. Q32servations and Findinos

The inspectors reviewed PSE&G's formal root cause evaluation report for the NSB

core spray injection nozzle through-wallleak, dated November 4,1997, af ter

meeting with some of the participants on the evaluatio.: team. The inspectors

found ti at extensive fact gathering and root cause analysis were performed with

appropriate corrective actions either proposed or implemented. The safety

significance of the degraded NSB weld were discussed in the report, which stated

that there were no actual consequences and that there was no impact on public

health and safety. Though an increass in unidentified drywellleakage (from 0.3 to

0.0 gallons per minute) was noted in August 1997 during plant operation, this

increased leakage was withh TJ limits and was not associated with an increase in-

radiation. Because the crack exhibited the * leak before break" behavior expected

for the materials of construction, any further crack propagation with the plant

operating would have resulted in an increased unidentified leak rate followed by a

normal plant shutdown prior to a catastrophic pipe f ailure. Postulation of

consequences of the worst case event, that is a failure of the core spray line

initiated by a transient (e.g. seismic event) was evaluated by the PSE&G engineers

and found to be within the plant's design and licensing bases.

PSE&G identified one of the causal f actors of this issue was ineffective computer-

based ultrasonic testing (UT) dats evaluation. Recent re review of 1995 UT data

identified a misdiagnosed degrav'.d condition to have been present in 1995. The

1995 UT analyst noted the presence of a recordable indication, but judged that

there was no requirement for either supplemental non destructive examination (NDE)

or UT examination of the area containing the indication. PSE&G's recent review of

UT data on 19 other similar welds, including the conduct of UT on six of these

welds in 1997, did not identify any similar problems. On another set of 16 welds

that were examined by the somo UT process as the NSB weld, a reexamination of

six of these in 1997 by manual UT did not identify degradation. Other than the NSB

wold UT problem, no other incidents of a f ailure to identify potentially significant

flaws were found.

The 1995 UT analyr t dispositioned the NSB weld indication as acceptable based on

the nozzle weld data provided which indicated that the material was INCONEL 82

.

B

11

and was therefore not susceptible to stress corrosion cracking. During the

licensee's root cause analysis, it was determined that the construction material

should have been recorded as INCONEL 182 which is susceptible to cracking.

Immediate corrective actions to resolve the through-wallleakage included the repair

of the NSB weld by weld overlay. The corrective actions directed toward improving

the effectiveness of UT of welds similar to NSB included specific instructions to

Level 111 UT examiners for dissimilar welds, procedure reviews to clarify data

interpretation actions, industry involvement to improve UT of dissimilar welds,

additional review of causes and corrective actions, requirement for indepeMent

review of UT data by a second analyst for category D welds, consolidatice nd

review by data analysts of as-built data for each weld, and review of site specific

flaws and reflectors by the data analysts prior to review of new NDE data.

The failure to promptly idenufy the degraded core spray nozzle weld in 1995, a

condition adverse to quality, coupled with the f ailure to reques supplernental

nondestructive evaluation or supplemental ultrasonic examination of the area when

the indication was initially discovered, represented an inadequacy in the inservice

inspection program. As such, this event was deemed to be a violation of 10 CFR

50 Appendix B, Criterion XVI Corrective Action. However, because this violation

was non repetitive, and because of the prompt and thorough development of root

causes and corrective actions, thlF violation is being treated as a Non-Cited

Violatiore, consistent with Section Vll.B.1 of the NRC Enforcement Policy (NUREG-

1600). (NCV 50 345/97 09 02)

c. Conclusions

PSE&G performed a detailed and thorough evaluation of the failed core spray nozzle

weld history, previous nondestructive testing, and through wall leak causal f actors.

Proposed corrective actions were judged to be reasonable and appropriately focused

on preventing recurrence. However, the failure to detect and repair a weld flaw in

1995 during a focused ultrasonl< inspection of the noted core spray nozzle

highlighted weaknesses in th.: Hope Creek inservice inspection program.

M3.2 (Closed) LER 50 354/97 23: core spray nozzle weld through wallleak. This event is

described in dew in NRC Inspection Report 50-354/97 07 and was left unresolved

pending an NRC assessment of the completed root cause evaluation for why

analyses of a previot3.nna.t nic tes't of this nozzle failed to detect a weld flaw.

This assessment was wu sh I during the current report period with the results

described in section M8.1 above. No new information was provided by this LER.

M8.3 (Closed) LER 50-354/97-26:"E" filtration, recirculation, and ventilation system

recirculation unit inoperability due ,o tripped high-high temperature switch -

procedure deficiency. This LER describes a self-identified issue in which the "E"

filtration, recirculation, and ventilation system (FRVS) recirculation unit was found

to be inoperable just prior -o conducting a monthly technical specification (TS)

surveillance test on Sept inber 12,1997. PSE&G determined that the unit had

been inoperable since the conclusion of the previous monthly test completed on

- _- - . .

.

.

12

August 17,1997, because of a recent surveillance tcat procedure change which

was deficient. Specifically, the FRVS test procedure was recently modified to

change the method used to verify heater power consumption at the end of a ten

hour heater run. However, no provision was included to allow the f an to run after

the heaters were deenergized to cool the coils. As such, when the unit ,is secured

following the August 17 test, the heater high-high temperature switch unsnowingly

tripped, rendering the unit inoperable. PSE&G recognized in t.'to LF.R discussion that

because the FRVS unit was inoperable for greater than sev',n days ithe TS allowed

outage time for one inoperable FRVS unit), the plant should have commenced a

shutdown on August 24,1997.

The inspectors verified that the FRVS surveillance test procedure was appropriately

revised following identification of this issue and that subsequsnt FRVS test runs

have not experienced any similar problems. This licensee-identified and corrected

technical specification violation is being treated as a Non-Cited Violation, consistent

with Section Vil of the NRC Enforcement Policy (NUREG 1600). (NCt! 50 354/97-

09-03)

111. Enaineerina

E1 Conduct of Engineering

ELj. Jet Pumo Instrument Line Bracket Weld Crackina

a. Inspection Scope (37051)

The inspectors reviewed PSE&G's actions in response to a self identified discovery

of three jet pump sensing line bracket weld cracks,

b. Observations and Findinas

Oming in-vessel visual inspections of jet pumps, PSE&G inspectors determined that

rn pump numbers 8,9, and 15 all exhibited instrument line bracket weld cracks

v nich required repair. Station engineering personnel proposed the use of

" temporary" clamps to secure the affected sensing lines rather than repair the

deficient welds. Hope Creek staff also performed comprehensive inspections of all

20 jet pumps, including the lower elbows next to the inside of the vessel where

cracking had been recently discovered at the Peach Bottom Atomic Power Station

(GE-BWR4). No cracking was noted in these areas at Hope Creek.

A conference call between NRC and PSE&G technical staff was held on November

14,1997 to discuss the issues related to the proposed jet pump clamp repair

methodology. The clamp design was developed for use at the Susquehanna Steam

and Electric Station (GE-BWR4) where similar jet pump instrument line bracket weld

i

cracking was detected in 1994. The installed clamps had been inspected at that

station during two subsequent refueling outages with no noted degradation.

PSE&G performed a detailed analysis of the potential effects on reactor operation

should a jet pump instrument line break while at power, and concluded that there

l

l

l

. . . - .-. -

_ ._ _ _ __ _ _ _ . . _ . _

.

(

--

g

13

would be no impact on safe plant operation. No concerns were raised during the .

course of the conference call.

The inspectors reviewad the design change package and associated evaluation for

installation of the jet pump clamps, and judged them to be acceptabla. Additionally,

thi inspectors observed portions of the actual clamp installation process, including a

review of the installation procedure, and did not identify 6ny deficiencies. Based on

the results of future refu(I outage inspections of these cumps, these jet pump

modifications may become a permanent installation.

c. Conclusiong

PSE&G promptly developed and implemented an acceptable design change pa::kage

,

to resolve a seliidentified issue involving bracket weld cracks on jet pump -

, instrument lines.

E2 Engineering Support of Facilities and Equipment

. Q1 Desian Chanae Packsae and Safetv Evaluation Review

a. Insoection Scoce (37551)

The inspectors reviewed the 10 CFR 50.59 safety evaluations associated with the

following plant system design modifications implemented during this report period:

  • lsofoam in the turbine auxiliaries cooling system (TACS) accumulator floating roof
  • Ultrasonic Test Scanner bearing cap - potentiallost part in reactor vessel
  • Alternate air supply to SACS flow control valve for safety-related chiller units

Additionally, the inspectors observed the installation of several other engineering

design change packages needed before the restart from the RF07 refuelinr, outage,

including:

  • Jet pump instrument line clamps
  • Rod sequence control system elimination

.

b. Observations and Findinas

PSE&G engineering developed approximately 70 design change packages for

installation during the RFO7 refueling outage, several of which were not part of the

original outage work scope but were deemed necessary as a result of self identified

adverse or degraded conditions. For instance, a safety evaluation was prepared on

November 12,1997, to assess the impact of plant operation with an unrecovered

loose part in the reactor vessel. Specifically, a 1" x 2" steel bearing cap which had

fallen ' ff an ultrasonic testing rig used for in-vessel weld inspections was never

-- - - - -_

_ _ - __ _ _ _ _ _ ____ _


- - .

. . . - _. _ -

~

l

.

14

recovered despite extensive efforts to locate and retrieve the item. The safety

evaluation thoroughly assessed the potential concerns associated with this lost part,

including possible effects on control rod movement, core flow restrictions, etc., and ,

judged that even though the issue involved a " change" to the facility as described ir,

the UFSAR,it did not result in the need for prior NRC review and approval.

Several other engineering saf sty evaluations were reviewed and judged to be

acceptable.10 CFR 50.59 " applicability reviews" and unreviewed safety question

determinations included sufficient scope, detail and analysis to justify tha final

conclusions. The inspectors determined that none of the plant modifications

reviewed resulted in final installed conditions which were inconsistent with.

continued safe plant operation. In fact, most of the 70 change evaluations

completed during the outage were developed to enhance safe and uneventful plant

operation, as opposed to simply accepting degraded conditions "as is" or providing

.

for operational conveniences. ,

Based on the limited sample of evaluations reviewed, the inspectors judged that the

quality of the 10 CFR 50.59 process had improved over the past operating cycle.

Process improvements such as evaluation " grading," cross disciplinary peer

roviewing, independent auditing, and focused engineering department training

resulted in better and more thorough safety evaluations. Based on interviews with

engineering management personnel, the inspectors learned that the process will

continue to evolve based on recently issued regulatory and industry guidanco,

c. Conclusions

Engineering department prepared safety evaluations were of good quality and were

appropriately focused on the potential nuclear safety impact of the r! ant design or

equipment changes.

E8 Miscellaneous Engineering issues

EQJ fClosed) LER 50-354/96-09: operation in an unanalyzed condition due to

inappropriate service water system / safety auxiliaries cooling system throttle valve-

settings. This LER describes a self-identified issue involving a March 1996

discovery that station service water (SSW) system throttle valves were set

improperly in November 1992 after a design change which replaced these valves,

that would have prevented adequate SSW cooling flow to the safety auxiliaries

cooling system (SACS) heat exchangers during design basis accident conditions.

PSE&G recognized that while no safety consequence resulted from this failure to

maintain appropriate system configuration control, the plant was operated for nearly

four years outside of the design and licensing basis (see NRC Inspection Report 50-

354/96 06). PSE&G attributed the cause of this deficiency to an inadequate

engineering design modification process, which in 1992 did not require design

calculation assumptions to be verified by field data collected after modification

installation.

- - _ .

.

.

15

The inspectors determined that PSE&G's design change process was modified to

include the need to conduct field verifications of design calculation assumptions.

Additionally, PSE&G conducted a thorough design bases validation of the SSW and

SACS systems by performing an independent service water system operational

performance inspection, an NRC review of which was documented in NRC

inspection Report 50-354/97-06. Lastly, in direct response to the issue described in

this LER, on October 23,1996, the NRC issued a violation of TS 3.7.1.2.b, which

requires that an operable service water flow path be maintained to ensure adequate

cooling to the SACS heat exchangers (see section E8.6 below).

kBJ (Closed) LER 50 354/9615: potential to operate in an unanalyzed condition due to

a design deficiency in the (service water emergency) overboard discharge line.

During station service water (SSW) system design bask reviews performed in

response to previously identified discrepancies, engineering personnel identified an

error in SSW design calculations in that emergency discharge point dynamic flow

conditions were not properly accounted for. This discovery rendered the technical

specification (TS) limit on maximum ultimate heat sink (UHS) temperature non-

conservatively high (see NRC inspection Reports 50 354/96 04,96 06, and 97-01).

A public meeting between the NRC and PSE&G was held on July 18,1996, to

discuss this and other related SSW and SACS system design issues, as well as

instituted compensatory measures and proposed corrective actions. Compensatory

measures included placement of an administrative limit on maximum UHS

temperature and development of specific operator actions in the event of a loss of

one SSW or SACS loop. Corrective actions included the conduct of an independent

service water system operational performance inspection, followed by the submittal

of any needed license change requests.

PSE&G completed its SSW/ SACS / UHS design basis review in May 1997, and

submitted associated TS amendment requests for NRC review promptly thereafter.

An independent NRC inspection of the design basis review effort was documented

in NRC Inspection Report 50 354/97-06. NRC review of PSE&G-proposed licenso

changes was completed in October 1997, and were issued as TS Amendment 106.

The NRC safety evaluation report included with this amendment did not identify any

concerns with the PSE&G-proposed changes.

EDJ (Closed) LER 50-354/97-24:as found values for safety relief valvo lift setpoints

exceed technical specification allowable limits. This LER was written to document a

repeat issue involving main steam line safety relief valve (SRV) setpoint drift outside

technical specification (TS) limits. As found " bench testing" of the 14 Hope Creek

SRV's, which are a two-stage Target Rock design, determined that ten of the valves

had excessive drift (worst case was + 9.4%). The setpoint drift issue has been an

on-going industry-wide concern and several industry-driven corrective actions have

been proposed. The inspectors determined that PSE&G has been aggressively

pursuing resolution of this issue, which has included design changes to SRV pilot

valve seating materials. All SRV setpoints wera verified to be within TS allowable

drif t limits prior to reinstallation in the main steam system.

.

16

EBA (Closed) LER 50 354/97 25: design deficiency potential for an unmonitored release

path through the station service water system. This LLR describes a self identified

discovery of a potential secondary containment bypass leakage pathway. After a

postulated loss of power accident, station service water (SSW) system solenoid-

operated vacuum breakers would fall open allowing the reactor building atmosphere

to communicate directly with SSW piping, which discharges water outside the

secondary containment. This design deficiency was recognized by technicians

performing maintenance on the noted sotenoids. PSE&G promptly developed a

design change packagt to re-route the vacuum breaker vent piping to the outside

environment rather than from inside the reactor building. The inspectors reviewed

the design change package and the associated safety evaluation, es well as walked

down the modified piping after installation was complete. No defic!sncies were

noted. The inspectors judged that PSE&G acted promptly and effectively in the

resolution of this issue.

,

ESJ (Closed) URI 50-354/96 04-06:non-conservative maximum ultimate heat sink

temperature limit. This issue was left unresolved pending NRC review of PSE&G

corrective actions to self identified discrepancies in the service water and safety

auxiliaries cooling system design bases. These discrepancies resulted in the need

for several compensatory measures to be put in place to ensure that the ncted

systems remained operable. A detailed discussion of the NRC and PSE&G follow up

to this and other related issues is described in sections E8.1 and E8.2 above.

EQJ (Closed) VIO 50-354/E96 281-04013: inappropriate service water / safety auxiliaries

cooling system throttle valve settings. This issue was described in detailin NRC

Inspection Report 50 354/96-06,LER 50-354/96-09,and section E8.1 above. The

inspectors verified that corrective actions stated in PSE&G's violation response

letter dated November 22,1996, were completed. These actions included (1) a

comprehensive service water system flow balance in which engineering flow

calculation assumptions were validated with field data, (2) the engineering process

for making design modifications was enhanced with additional specific training

provided, and (3) an independent service water system operational performance

inspection was conducted.

IV. Plant Scoport

S1 Conduct of Security and Safeguards Activities

a. Insoection Scone

A focused review was performed to determine whether the PSE&G security

program, as implemented, met the licensee's commitments in the NRC-approved

security plan (the Plan) and NRC regulatory requirements. The security program

was inspected during the periods of November 3-7 and November 12,1997. Areas

inspected included: management support; audits; alarm stations, communications,

and assessment aids; testing, maintenance and compensatory measures; training

and qualification; protected area access centrol of vehicles; and the vehicle barrier

system.

. . . . - . - - _- - - -. . - . . , . . _ .

.

,

17

b. Observations and Findinas

Management support was ongoing as evilenced by the procurement and installation

of four X ray machines for access searco * packages, installation and

implementation of hand geometry, and range upgrades to enhance tactical response

training. Audits were thorough and in depth, alarm station operators were

knowledgeable of their duties, communications requirements were performed in

accordance 'vith the Plan, and assessment aids had adequate picture quality.

Vehicles requiring protected area access were controlled as required in the Plan.

Applicable procedures and security equipment were tested and maintained in

accordance with the Plan, and security training was performed in accordance with

the NRC approved training and qualification (T&O) plan.

Based on the observations and discussions with security management and plant "

.

engineering personnel, the inspectors determined that the PSE&G's provisions for

land vehicle control measures satisfied regulatory requirements and licensee

commitments,

c. Conclusions

PSE&G conducted security and safeguards activities in a manner that protected

public health and safety and that the program, as implemented, met the licensee's -

commitments and NRC requirements.

S2 Status of Security Facilities and Equipment

E2d Protected Area Access Control of Vehicles

a. inspection Scoce

The inspectors evaluated whether PSE&G controlled access of all vehicles to the

protected area in conformance with the Plan and regulatory requirements.

! b. Observations. Findinas and Conclusion

On November 5 and 6,1997, the inspectors observed security force members

(SFMs) performing vehicle searches. Additionally, the inspectors discussed vehicle

authorization and escort requirements with security management and SFMs and

determined that vehicles requiring protected area access were controlled as required

d

in the Plan and applicable procedures.

S2J Alarm Stations. Lommunications and Assessment Aids

a. Insoection Scoce

The inspectors determined whether the Central Alarm Station (CAS) and Secondary

Alarm Station (SAS) are: (1) equipped with appropriate alarm, surveillance and

communication capability, (2) continuously manned by operators, and (3) use

_ _ _ ,

- . . - . . .- _ - - - . ~ - --

i

.

18

independent and diverse systems so that no single act can remove the capability of

detecting a threat and calling for assistance, or otherwise responding to the threat,

as required by NRC regulations,

b. Observations and Findinos

i inspector observations of CAS and SAS operations verified that the alarm stations

were equipped with the appropriate alarm, surveillance, and communication

capabilities. Interviews with CAS and SAS operators found them knowledgeable of

their duties and responsibilities. The inspectors also ver!fied through observations  ;

'

and interviews that the CAS and SAS operators were not required to engage in

activities that would interfere with the assessment and response functions, and that

.the licensee had exercised communication methods with the local law enforcement

agencies as committed in the Plan.

,

Additionally, on November 5,1997, the inspectors evaluated the effectiveness of

the assessnient aids, by observing on closed circuit television, a walkdown of the

4

protected area. The inspectors determined that the assessment aids in both cf the

alarm stations had adequate picture quality,

c. Conclusion

' The alarm stations and communications adequately implemented PSE&G's Plan

commitments and NRC requirements.

SM Testino, Maintenance and Comoensatorv Mean!ntt

, a. Inspection Scope

The inspectors determined whether programs were implemented to ensure the

reliability of security related equipment, including proper installation, testing and

, maintsnance to replace defective or marginally effective equipment. Additionally,

the inspectors evaluated the effectiveness that the compensatory measures put in

place when security related equipment fails,

b. Observations and Findinas

Tht, inspectors reviewed testing and maintenance records for security related

equipment and found that documentation was on file to demonstrate that the

licensee was testing and maintaining systems and equipment as committed to in the

Plan. A priority status was being assigned to each work request and repairs were

normally completed the same day a work request necessitating compensatory

i measures was generated. The inspectors also noted that the working relationship

between security and maintenance departments was improving and tracking and

trending programs to monitor recurring equipment problems to determine when

,

engineering support was required, were being implemented.

. - . - - .- --

._ . . _ . _ _ _ . .. _ __ ._ . _ _ . _ _

.

.

19

c.. Conclusions

Documentation on file confirmed that security equipment was tested and maintained

as required. Repair work was timely and the use of compensatory measures was

found to be appropriate and minimal.

S5 Security and Safeguards Staff Training and Qualification

a. insoection Scone

The inspectors evaluated whether members of the security organization were

trained and qualified to perform each assigned security related job task or duty in

accordance with the NRC approved T&Q plan,

b. Observations and Findinas

On November 5,1997, the inspectors randomly selected and reviewed the T&Q

records of thirteen security force members (SFMs). Physical and firearms

requalification records were inspected for armed SFMs and security supervisors.

The inspectors found that the training had been conducted in accordance with the

T&Q Plan and was properly documented.

During discussions with the security training staff and security management, the  ;

inspectors were informed that new response weapons were purchased to enhance l

the licensee's tactical response capabilities. However, the new weapons will not be l

issued until all SFMs have been properly trained and qualified with the new

weapons. Further discussions revealed that the licensee was in the process of

upgrading its firing range. On November 6,1997, the inspectors toured the firing

range and determined, based on observations, that the upgrades would enhance

tactical response training. Additionally, the inspectors interviewed a number of

'

SFMs to determine if they possessed the requisite knowledge and ability to carry

out their assigned duties,

c. Conclusions

The inspectors determined that training had been conducted in accordance with the

T&Q plan. Based on the security force members responses to the inspectors *

questions and observations, the training provided by the security staff was

considered effective.

S6 Security Organization and Administration

a. insoection Scoce

The inspectors conducted a review of the level of management support for PSE&G's

physical security program.

_

_ . _ - _ . ._ _ _ _ _ . _ _ _ _ _ _.

.

.

20

b. Observations and Findinas

The inspectors reviewed various program enhancements made since the last NRC-

in@ection, which was conducted in April 1997. These enhancements included the

procurement and installation of four X ray machines for access search of packages,

and installation and implementation of hand geometry and range upgrades to

enhance tactical response training.

The inspectors reviewed the Manager - Nuclear Security's position in the

organizational structure and reporting chain. The Manager - Nuclear Security

reports to the General Manager Salem Operations, who reports directly to the

Senior Vice President - Nucleer Operations, who reports directly to the Chief Nuclear

Officer and President Nuclear Business Unit.

c. Conclusions ,

Management support for the physical security program was judged to be effective.

No problems with the organizational structure that could be detrimental to the

effective implementation of the security and safeguards programs were noted.

S7 Quality Assurance in Security and Safeguards Activities

S2d Audits

a. Insnection Sco.ag

The inspectors reviewed the licensee's Quality Assurance (QA) report of the NRC-

required security program audit to determine if the licensee's commitments as

contained in the Plan were being satisfied,

b. Observations and Findinas

The inspectors reviewed the 1997 combined QA audit of the security, access

authorization and fitness for-duty (FFD) programs, conducted May 19-30,1997,

(Audit No.97-031). The audit was found to have been conducted in accordance

with the Plan and FFD regulation. To enhance the effectiveness of the audit, the

PSE&G's QA audit team included four independent technical specialists.

The audit included findings in the security, access authorization and FFD areas,

however, the inspectors determined that the findings were not indicative of major

programmatic weaknesses. The inspectors further determined, based on

discussions with security management and FFD staff and a review of the responses

to the findings, that the resultant corrective actions were effective.

c. Conclusions

A recent Quality Assurance Audit of security was very comprehensive in scope and

depth, and at,dit findings were reported to the appropriate levels of management.

The inspectors judged that the audit program was being effectively administered.

I

- - _ _ -_

.-. . . . . - ._-

,

,.

21

88 Miscellaneous Security and Safeguards issues

Sfld Vehicle Barrier System (VBS)

General

On August 1,1994, the Commission amended 10 CFR Part 73, " Physical Protection

of Plants and Materials," to modify the design basis threat for radiological sabotage

to include the use of a land vehicle by adversaries for transporting personnel and

their hand carried equipment to the proximity of vital areas and to include the use of

,

a land vehicle bomb. The amendments required reactor licensees to install vehicle

control measures, including VBSs, to protect against the malevolent use of a land

vehicle. Regulatory Guide 5.68 and NUREC/CR-6190 were issued in August 1994

to provide guidance acceptable to the NRC by which the licensees could meet the

requirrments of the amended regulations.

Letters dated February 28,1996 and June 19,1996 from PSE&G to the NRC

forwarded Revisions 6 and 7 to its physical security plan that detailed the actions

implemented to meet the requirements of 10 CFR 73.55 (c)(7),(8), and (9) and the

design goals of the " Design Basis Land Vehicle" and " Design Basis Land Vehicle

Bomb." A NRC July 6,1996, letter advised the licensee that the changes

submitted had been reviewed and were determined to be consistent with the .

provisions of 10 CFR 50.54(p) and were acceptable for inclusion in the NRC-

approved security plan.

This inspection, conducted in accordance with NRC Inspection Manual Temporary

Instruction 2515/132," Malevolent Use of Vehicles at Nuclear Power Plants," dated

January 18,1996, assessed the implementation of the licensee's vehicle control

measures, including vehicle barrier systems, to determine if they were

commensurate with regulatory requirements and the licensee's physical security

plan.

The inspectors reviewed documentation that described the VBS and physically

inspected the as-built VBS to verify that it was consistent with the licensee's

summary description submitted to the NRC. The inspectors' walkdown of the VBS

and review of the VBS summary description disclosed that the as-built VBS was

consistent with the summary description and met or exceeded the specifications in

NUREG/CR-6190. The inspectors determined that there were no discrepancies in

the as-built VBS or the VBS summary description.

$12 Bomb Blast Analysis

The inspectors reviewed the licensee's documentation of the bomb blast analysis

and verified actual standoff distances provided by the as-built VBS. The inspectors'

review of the licensee's documentation of the bomb blast analysis determined that

it was consistent with the summary description submitted to the NRC. The

inspectors also verified that the actual standoff distances provided by their as-built

VBS were consistent with the minimum standoff distances calculated using

__ _ _.

.- - - - - . - _ . -. .

.

.

22-

'

NUREG/CR-6190. The standoff distances were verified by review of scaled-

drawings and actual field measurements. No discrepancies were noted in the

documentation of bomb blast analysis or actual standoff distances provided by the

as-built VBS.

, ESJ Procedural Controls

The inspectors reviewed applicable procedures to ensure that they had been revised

to include the VBS. The inspectors reviewed the licensee's procedures for VBS

access control measures, surveillance and compensatory measures. The procedures

contained effective controls to provide passage through the VBS, provide adequate

surveillance and inspection of the VBS, and provide adequate compensation for any

degradation of the VBS. The inspector's review of the procedures applicable to the

VBS disclosed no discrepancies.

V. Manaaement M_tafirnt

X1 Exit Meeting Summary

The inspectors presented their findings and conclusions to members of licensee

management at the conclusion of the report period on November 21,1997. The licensee

acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

X2 Review of Updated Finst Safety Analysis Report (UFSAR)

A recent discovery of a licensee operating its f acility in a manner contrary to the UFSAR

description highlighted the need for a special focused review that compares plant practices,

procedures, and parameters to the UFSAR description. Since the UFSAR does not

specifically include security program requirements, the in:;pectors compared licensee

activities to the NRC approved physical security plan, which is the applicable document.

While performing the inspection discussed in this report, the inspectors reviewed

Section 4.1.2 of the Plan, titled " Protected Area - Physical Barrier Description" was

reviewed. The inspectors determined, by observations, that the protected erea barrier was

properly installed, maintained and satisfied the requirements of the Plan.

-

.

.

23

- INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations

IP 71707: Plant Operations

IP 73755: Inservice inspection - Data Review and Evaluation

IP 81700: Physica! Security Prograrn for Po ner Reactors

ITEMS OPENED, CLOSED, AND DISCUSSED

OpentLd

50-354/97-09-01 eel Shutdown margin demonstration, apparent TS 6.8.1

violation

Onened/CloLqd

50-354/97 09 02 NCV Violation of 10 CFR 50 Appendix B, Criterion XVI

Corrective Action

50-354/97-09-03 NCV FRVS recirculation unit inoperability

Q219d

50-354/E96-281-04013 VIO Inappropriate service water / safety auxiliaries cooling

system throttle valve settings

50 354/96-04-06 URI Non-conservative maximum ultimate heat sink

temperature limit

50 354/97-07-02 URI 'A' core spray nozzle (N5B) safe end leak, NDE and

repair

50-354/96-09 LER Operation in an unanalyzed condition due to

inappropriate SWS/ safety auxiliaries cooling system

throttle valve settings

50 354/96-15 LER Potential to operate in an unanalyzed condition

50 354/97-13 01 LER Unplanned HPCI inoperability

50 354/97 23 LER Core spray nozzle weld through-wallleak

50-354/97 24 LER As found values for safety relief valve lift setpoints

exceed TS allowable limits

50 354/97 25 LER Design deficiency - potential for an unmonitored release

path through the SSW system

50-354/97 26 LER "E" FRVS recirculation unit inoperability

. . - . . - .

-.

- 1 .

24 j

h

LIST OF ACRONYMS USED

CAS Central Alarm System

- CRD. Control Rod Drive

EDG Emergency Diesel Generator ,

FFD Fitness For Duty .

FRVS- - Filtration, Recirculation and _ Ventilation System

HPCI High Pressure Coolant injection

LER Licensee Event Report

LCO ~ Limiting Conditions for Operation

LOP /LOCA - Loss of Offsite Power / Loss of Coolant Accident

- M&TE Monitoring & Test Equipment

- NDE- Non-destructive Examination ,

,

- NRC Nuclear Regulatory Commission

_

PDR- Public Document Room .

PSE&G Public Service Electric and Gas

OA: Quality Assurance -

,

RCIC Reactor Core Isolation Cooling

RG Regulatory Guide

RHR- Residual Heat Removal

RP&C_' Radiological Protection & Chemistry

RPS Reac. tor Protection System

SACS Safety Auxiliaries Cooling System

SAS Secondary Alarm System

SDV Scram Discharge Volume

SFM Security Force Members

SRO. Senior Reactor Operator

SRV Safety Relief Valve

SSW- Station Service Water

T&O Training and Qualification

TACS Turbine Auxiliaries Cooling System

the Plan- NRC approved Physical Security Plan

TS -Technical Specification

UFSAR Updated Final Safety Analysis Report

UHS Ultimate Heat Sink

'

UT Ultrasenic Testing

- VBS

. Vehicle Barrier System

-

1

e

-

-. w -p_ .- y y - v_, -

.m-_._-- _eg .ge.g .w g, y y ,,e