ML20129D089

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Insp Rept 50-354/96-07 on 960804-0921.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20129D089
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 10/18/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20129D067 List:
References
50-354-96-07, 50-354-96-7, NUDOCS 9610240196
Download: ML20129D089 (40)


See also: IR 05000354/1996007

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U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No:

50-354

License Nos:

NPF-57

Report No.

50-354/96-07

Licensee:

Public Service Electric and Gas Company

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Facility:

Hope Creek Nuclear Generating Station

Location:

P.O. Box 236

Hancocks Bridge, New Jersey 08038

Dates:

August 4,1996 - September 21,1996

Inspectors:

R. J. Summers, Senior Resident Inspector

S. A. Morris, Resident inspector

N. T. McNamara, Emergency Preparedness inspector

F. J. Laughlin, Emergency Preparedness Inspector

A. L. Della Grecca, Senior Reactor inspector

D. A.Jaffe, Senior Project Manager

Approved by:

Larry E. Nicholson, Chief, Projects Branch 3

Division of Reactor Projects

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9610240196 961018

PDR

ADOCK 05000354

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EXECUTIVE SUMMARY

Hope Creek Generating Station

NRC Inspection Report 50-354/96-07

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers a 7-week period of resident inspection;

in addition, it includes the results of announced inspections by regional inspectors in the

Emergency Preparedness area; follewup inspection activities in engineering support and

operations; and, a program assessment of the 50.59 process by the NRR project manager.

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During the report period, a security program inspection was conducted by region-based

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specialist inspectors; however, the details of that inspection are contained in NRC

Inspection Report 50-354/96-08.

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Operations

Operators responded appropriately to an inadvertent reactor core isolation cooling system

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isolation. Despite their inability to establish a definitive root cause, good engineering

department involvement in troubleshooting the suspected instrument drawer ensured

prompt restoration of the RCIC system to operability. A strong determination to promptly

identify the component failure mechanism was also evident. (Section 01.2)

Station operators exhibited good awareness and questioning attitude in the identification of

a minor steam leak in a normally inaccessible area of the reactor building. Engineering

personnel developed an appropriate safety evaluation to address an abnormal valve

configuration that temporarily minimizes the impact of the noted steam leak. (Section

01.3)

Although the initial response to a potential tampering event at Salem appeared to be

minimal, subsequent actions, including direct communication of management expectations

and the development of an operational directive for reacting to suspected tampering events

were thorough. Verification of the operability of remote shutdown equipment following a

suspected sabotage event at another utility was timely and comprehensive. (Section 04.1)

Though a plant operator failed to self-check prior to implementing an important step in a

procedure, no damage to safety related equipment resulted and licensee response to the

event was good. (Section 04.2)

SORC activities were conducted in accordance with plant technical specifications. In

addition, SORC questions were of sufficient depth to ensure that station activities were

conducted safely. (Section 07.1)

The corrective action program performance indicators were effective for monitoring

problems identified by station personnel and in ensuring that timely corrective actions were

taken. (Section 07.2)

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Maintenance / Surveillance

Control and conduct of maintenance and surveillance activitics was good. Similarly,

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procedure adherence was good. Schedule adherence, especially for significant on-line

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activities, like the "A" emergency diesel generator, and response to emergent work was

good. (Section M1.1)

Plant operators exhibited a timely and conservative response to indications of improper oil

in two residual heat removal pump motor bearings. Good coordination with maintenance

technicians resulted in the prompt restoration of affected equipment. Root cause

assessment and corrective actions were comprehensive. (Section M2.1)

The backlog of corrective maintenance activities is high; however, licensee management

has continuously assessed the backlog for impact on Operations and prioritization of

maintenance. (Section M2.2)

Operator recognition of inoperable drywell leak detection system instrumentation that

required a plant shut down was not timely; however, the condition was subsequently

recognized avoiding any violation of the plant technical specifications. Subsequent

response was appropriate, including prompt implementation of TS-required actions and

documentation of the event in accordance with the corrective action program. (Section

M4.1 )

Enaineerina

PSE&G's framework for the 10 CFR 50.59 program was generally good. Two examples of

changing the plant without an appropriate 10 CFR 50.59 evaluation were identified and

resulted in a violation of NRC regulations. (Section E1.1, E1.2 & S8)

Plant operators modified the controls of a safety related component (valve 1EGHV-2522E),

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without use of proper engineering support to assess if this resulted in either a necessary

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change to the plant technical specifications or an unreviewed safety question. Once this

concern was identified, operators restored the valve to its normal configuration in a timely

manner. (Section E1.2)

Operators exhibited a good, conservative desire to maximize overall service water system

reliability due to the impending severe weather by requesting engineering personnel to

devise a means to restore the function of an associated subsystem made inoperable by

partialimplementation of a design change package. However, a review of the

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documentation associated with the modification to satisfy the operations department

request highlighted weaknesses in the process for controlling and justifying design change

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package revisions. (Section E2.1)

The NAP-59 procedure for addressing the 10 CFR 50.59 process is well written, provides

clear assignment of responsibility, and provides the user with good directions. (Section

E3.1)

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Certain aspects of the training program for 10 CFR 50.59 were good; however,

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qualification requirements had not yet been developed to ensure that personnel involved in

the use of 10 CFR 50.59 had been appropriately trained. (Section E5.1)

The Offsite Safety Review Group review of safety evaluations were not consistently-

performed. PSE&G's corrective actions for similar prior findings were ineffective at Hope

Creek in that sponsoring organizations at Hope Creek continued to be inconsistent in

providing safety evaluations for OSRG review. Finally, the OSRG lacked reasonable

initiative in ensuring that they received these safety evaluations from the sponsoring

organizations. (Section E7.1)

Plant Suooort

The inspectors conducted numerous tours of the facility and noted that all required

radiological postings and locked areas met regulatory requirements. Further, areas were

clear of unnecessary equipment, wellilluminated and free of safety hazards. (Section R2)

While some activities associated with effluent grab sampling and analysis were not

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conducted in a timely manner, overall performance of radiation protection program

requirements were good. (Section R4)

A QA department audit of the radioactive waste program met the requirements of the Hope

Creek technical specifications and provided good self-assessment of this area. (Section

R7)

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PSE&G maintained an adequate emergency preparedness program. The emergency plan

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and implementing procedures were current and effectively implemented. The emergency

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facilities, equipment, instruments and supplies were maintained in a state of readiness. All

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required 1995 and 1996 surveillance tests were completed. In the past six months, there

have been EP management and organizational changes and it appears that these changes

have not had an adverse effect on the EP program. A sampling of emergency response

organization (ERO) personnel training records indicated that training qualifications were

current. Routine verification that specified ERO personnel have maintained respirator

requalification training was not being conducted. Reports indicated that quality assurance

audits were thorough and satisfied NRC requirements. (Section P)

PSE&G's implementation of a design change package to replace the Hope Creek fire

protection computer was generally acceptable, although interim compensatory measures

were not properly evaluated to ensure that no unreviewed safety question existed.

(Section F2)

Based on observed drill response, the inspectors concluded that the compensatory

measures were effective in providing appropriate fire panel indication and alarm information

-to the control room for response to postulated fires in the f acility. (Section F4)

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TABLE OF CONTENTS

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EX EC UTIV E S U M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii

TABLE O F CO NTENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . vi

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1. O pe r a t io n s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

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11. M a i nt e n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

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lli. Engineering

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I V. Pl a nt S u ppo rt . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

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V. Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

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Report Details

Summarv of Plant Status

Hope Creek began the inspection period at 100 percent power. Full power operations were

maintained throughout the period spanning August 4,1996 to September 21,1996,

except for minor power reductions to support maintenance and testing activities.

1. Operations

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Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. In general, the conduct of operations was professional

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and safety-conscious; specific events and noteworthy observations are detailed in

the sections below.

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01.2 , Reactor Core Isolation Coolina System Isolation

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insoection Scope (71707,62707)

The inspectors observed PSE&G's response to an engineered safety feature

actuation that resulted in an automatic isolation of the reactor core isolation cooling

(RCIC) system,

b.

Observations and Findinas

On August 21,1996, the RCIC system steam inlet valve and turbine trip throttle

valve both closed in response to an isolation signal generated by the steam leak

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detection system. Station operators surmised that the actuation was the result of

an instrumentation failure since a prompt inspection of the RCIC equipment room

indicated that all conditions were normal. Operators verified that the system

responded as expected to the isolation signal, implemented the applicable LCO

action statements per TS 3.7.4, and reported the occurrence to the NRC operations

center as required by 10 CFR 50.73. The inspectors witnessed appropriate concern

by station management in response to this event, specifically because members of

the TS surveillance improvement project were coincidentally reviewing the adequacy

of past operability testing of the high pressure coolant injection system.

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Initial troubleshooting by maintenance technicians identified multiple hardware

problems on various cards internal to the RCIC system "NUMAC" instrumentation

and control drawer, the device which houses the steam leak detection and actuation

logic. However, the engineering department system manager subsequently

determined that none of the discrepancies identified should have resulted in the

observed RCIC system isolation. Discussions with the NUMAC vendor and a search

of industry operating experience data, though a good initiative, did not assist in

finding the root cause of the condition. Additionally, a search of maintenance

history on other installed NUMAC drawers at Hope Creek determined that no

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adverse equipment performance trend was evident. In order to minimize the duration

of the unplanned RCIC system outage, station management elected to replace the

entire NUMAC drawer with a spare. The inspectors observed that subsequent

instrument calibration and testing was completed satisfactorily. The RCIC system

was inoperable for less than two days.

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PSE&G engineering personnel stated that, because of the inconclusive

troubleshooting, and because much of the internal functional design of the

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component is proprietary, the suspect NUMAC drawer would be shipped to the

vendor for additional testing and root cause analysis.

c.

Conclusion

Operators responded appropriately to an inadvertent reactor core isolation cooling

system isolation. Despite their inability to establish a definitive root cause, good

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engineering department involvement in troubleshooting the suspected instrument

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drawer ensured prompt restoration of the RCIC system to operability. A strong

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determination to promptly identify the component failure mechanism was also

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evident.

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01.3 Steam Leak From Main Steam Line Drain Pioina

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a.

Insoection Scoce (71707,37551)

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The inspectors observed the process by which a small steam leak in the steam

tunnel was identified and (temporarily) resolved, including the steps taken by the

operations department to locate the source of the leak and the follow up analysis

performed by engineering personnel to justify a temporary change in an established

isolation valve line up.

b.

Observations and Findinas

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On August 7,1996, sYation operators detected a slight rising trend on the reactor

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building exhaust ventilation radiation monitor. Operators subsequently correlated a

slowly rising steam tunnel temperature indication to the reactor building exhaust

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readings. Suspecting a steam leak, operations, engineering, and radiation protection

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department personnel coordinated an effort which ultimately resulted in a

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determination that the source of the leak was from main steam line drain piping.

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Operators closed the drain line outboard containment isolation valve,1 ABHV-F019,

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and placed it under administrative control (caution tag); this action resulted in an

immediate reduction in steam tunnel temperature and reactor building exhaust

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radiation levels.

Because thorough investigation and repair of the drain line piping would result in

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relatively high exposures to personnel in the vicinity, station management elected to

defer the corrective maintenance until an outage of sufficient duration. As a result,

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since the UFSAR indicates that the 1 ABHV-F019 valve is open during normal

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operation, engineering appropriately prepared a 10 CFR 50.59 safety evaluation for

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the extended temporary condition during which the valve would remain closed. The

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inspectors reviewed the evaluation and observed the station operations review

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committee (SORC) deliberations on the merits of the assessment, and judged both

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to be appropriately focused on the design and safety implications. The evaluation

was approved primarily since the valve remained operable (even though closed), and

that it was placed in its design basis (safe) position.

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c.

Conclusion

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Station operators exhibited good awareness and questioning attitude in the

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identification of a minor steam leak in a normally inaccessible area of the reactor

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building. Engineering personnel developed an appropriate safety evaluation to

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address an abnormal valve configuration that temporarily minimized the impact of

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the noted steam leak.

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Operator Knowledge and Performance

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04.1 Station Response to Potential Tamoerina Events

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Insoection Scope (71707. 71750)

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The inspectors reviewed the Hope Creek operations department response to reports

and indications of suspected or actual tampering events at other commercial nuclear

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power stations.

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b.

Observations and Findinas

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On August 7,1996, just prior to shift turnover, the Hope Creek senior nuclear shift

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supervisor-(SNSS) was informed by his Salem station counterpart that Salem

operators discovered mis-positioned valves (closed versus locked open) in a safety

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system, and that tampering was being considering as a possible explanation. The

inspectors initially learned of the event from the relieving SNSS during his plant

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status briefing to station management. Based on a initial perception of minimal

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interest in this issue, the inspectors subsequently questioned the operating shift on

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their response to this issue, and, upon noting little appreciation of the nature of the

issue by shift personnel, expressed the concern to senior PSE&G management.

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Before substantive actions could be implemented, Hope Creek management learned

that the Salem issue had been traced to a status control error in the tagging system.

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However, shortly afterward, the operations department issued a draft directive that

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provided specific guidance for expected operations response to suspected tampering

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events. Additionally, the inspectors noted that management expectations for

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handling tampering concerns were clearly expressed to the operating shifts,

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including an entry in the " night orders."

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On August 15,1996, Hope Creek management learned that an Unusual Event was

declared at the St. Lucie plant in Florida because of suspected sabotage of the

remote shutdown system (glue found in various keylock switches, rendering them

inoperable). The inspectors witnessed an excellent response to this event.

Specifically, the event was promptly communicated to appropriate station personnel

with emphasis on its potential consequences, and, more significantly, the operations

department conducted a comprehensive walkdown of all remote shutdown

equipment at the station using the applicable integrated operating procedure as a

guide. No discrepancies were found.

Later, on August 28,1996, Salem reported to the Hope Creek SNSS that mis-

positioned switches on safety-related battery chargers at Salem appeared

suspicious, and that tampering had not been ruled out. The inspectors noted that,

despite a subsequent determination that tampering was not involved, the Hope

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Creek operations department response was prompt and thorough, and followed the

expectations outlined in the newly established directive,

c.

Conclusions

Although the initial response to a potential tampering event at Salem appeared to be

minimal, subsequent actions, including direct communication of management

expectations and the development of an operational directive for reacting to

suspected tampering events were thorough. Verification of the operability of

remote shutdown equipment following a suspected sabotage event at another utility

was timely and comprehensive.

04.2 Ooerator Error Durina Post-Maintenance Testina of the "A" Emeraency Diesel

Generator

The inspectors reviewed an event on September 4,1996, involving an operator

error. At the time, post-maintenance testing was in progress on the "A" emergency

diesel generator. An equipment operator was about to remove the EDG from

service, which involved opening the output breaker. However, instead of opening

the output breaker, the operator erroneously pressed the engine stop button. This

caused the engine to stop with the generator output breaker still closed.

Subsequently, the output breaker opened automatically on a reverse power

condition (as designed). No damage to the equipment occurred as a result of this

event because the automatic breakers controls performed appropriately.

The inspector observed that the licensee treated this condition seriously and

performed an acceptable review of the causes for the operator error and to establish

the extent of damage to the equipment.

The inspector concluded that while the operator failed to self check prior to

implementing an important step in a procedure, no damage to safety related

equipment resulted and licensee response to the event was good.

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06

Operations Organization and Administration

06.1 Operations Department Manaaement Chanae:

Just after the close of the inspection period, the licensee announced that the

Operations Department Director resigned from the organization. The department

management responsibilities will be temporarily charged to the Operating Engineers.

The operating shifts will continue to report to H. Hanson, Acting Operations

Manager and current SRO-license holder. The licensee plans to recruit a

replacement for the Operations Department Director.

07

Quality Assurance in Operations

07.1 Station Operations Review Committee (SORC) Meeting Observations

The inspectors observed several routine SORC meetings during the inspection

period. The inspectors verified that the SORC membership requirements of the

plant technical specifications were met. The observed discussions were of

excellent quality. Noteworthy examples included discussions on: operability

determinations; the aggregate impact of degraded, but operable equipment; review

of an event involving observed leakage from the emergency overboard discharge

line of the service water system; and, review of the plans for retiring certain

radioactive waste handling equipment.

The inspectors concluded that the SORC activities were conducted in accordance

with plant technical specifications. In addition, SORC questions were of sufficient

depth to ensure that station activities were conducted safely.

07.2 Station Corrective Action Proaram (CAP) Performance Indicators

The inspectors reviewed the current CAP performance indicators for the months of

July and August,1996. Improved performance was noted in schedule adherence

for corrective actions, for example 98 percent of the scheduled corrective actions

for August were completed on time. The average time to complete corrective

actions (57 days) remained within the licensee's goals; and, the number of overdue

corrective actions was reduced from 60 in July to 10 in August.

The inspectors concluded that the licensee's CAP performance indicators were

effective for monitoring problems being identified by station personnel and in

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ensuring that timely corrective actions.

08

Miscellaneous Operations issue

08.1 (Closed) LER 50-354/96023: Reactor Core Isolation Cooling system isolation due to

a failed steam leak detection monitor. This issue is discussed in detail in section

01.2 of this report. No new issues were revealed by this LER.

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08.2 (Closed) URI 50-354/93-11-01: This item involved apparent deficiencies in the

licensee's corrective action program. The licensee subsequently modified this

program in July 1995, with additional minor improvements being noted by the

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inspector since that time. The NRC has evaluated the licensee's program

implementation and determined that the deficiencies identified in this prior

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inspection have been corrected.

08.3 (Closed) Violation 50-354/94-09-04: mis-operation of the refueling bridge. The

inspector verified the corrective actions described in the licensee response letter,

dated December 8,1994, to be reasonable and complete. Further, it was noted

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during the most recent refueling outage that no similar event occurred.

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08.4 _(Closed) Soecial Reoort 50-354/94-003-01: operation of the facility in excess of the

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licensed thermal power limits. This was a required supplemental report of two

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events of operation above licensed thermal power limits. While additional

assessment of the significance of these events and revised corrective actions were

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provided, no new significant issue were revealed by the supplemental report. The

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inspector considered the corrective actions to be reasonable and complete.

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11. Maintenance

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Conduct of Maintenance

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M1.1 General Comments

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a.

Insoection Scope (62703 and 61726)

The inspectors observed all or portions of the following work activities:

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"D" service water pump replacement

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1CD-447125 Volt battery cell equalizing charge

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service water traveling screen on-line maintenance

high pressure coolant injection jockey pump repairs

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"A" emergency diesel generator on-line maintenance

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modification of the Hope Creek fire protection computer per DCP 4EC-3296

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Bailey module replacement affecting allindication and control for non-1E

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breakers

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reactor core isolation cooling system NUMAC drawer replacement

south plant vent flow monitor repairs

electrical backseating of valve 1 ABHV 2016B

The inspectors observed all or portions of the following surveillance procedure (s):

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high pressure coolant injection jockey pump check valve in-service test

"B" service water pump in-service test

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b.

Observations and Findinas

in general, the inspectors found that the work performed during the conduct of the

above noted maintenance and surveillance activities were in accordance with

approved station procedures and work control programs.

Pre-job work briefings were observed to be appropriate for the planned tasks. The

inspectors frequently observed maintenance supervisors and system engineers

monitoring the activities and providing necessary support. When applicable

appropriate radiation protection controls were observed to be followed.

The inspectors noted that on-line maintenance activities were conducted in

accordance with pre-approved risk-based work schedules and LCO maintenance

plans. For example, the "A" emergency diesel generator on-line maintenance

activities were completed an hour prior to the planned activity schedule.

The inspectors observed that the licensee continued to self-assess the

implementation of the work week schedules and when necessary, provide corrective

actions to prevent recurrence of significant scheduler problems.

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Emergent work activities, like the repeat failures of the south plant vent monitor,

and the failure of the RCIC NUMAC drawer, were appropriately controlled, and

where applicable, associated plant technical specification action statements

implemented. While some planned activities were interrupted by the emergent

work, the inspectors noted that overall schedule adherence was very good

throughout the inspection period.

The licensee appropriately implemented 10 CFR 50.59 controls in support of the

electrical backseating of valve 1 ABHV-20168. This valve is a main steam system

valve that provides steam flow to the "B" steam jet air ejector. The licensee

determined that the valve packing had a steam leak that was worsening. The

backseating of the valve reduced the steam leakage considerably and restored

environmental conditions in the steam tunnel and turbine building to normal. The

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inspector observed the SORC review of the associated 10 CFR 50.59 safety

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evaluation and found the level of questioning to be appropriately detailed.

c.

Conclusions

The inspectors concluded that the control and conduct of maintenance and

surveillance activities was good. Similarly, procedure adherence was good.

Schedule adherence, especially for significant on-line activities, like the "A"

emergency diesel generator, and response to emergent work was good.


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Maintenance and Material Condition of Facilities and Equipment

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M2.1 Imorooer Oil Discovered in Residual Heat Removal Pumos

a.

Insoection Scope (62707)

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The inspectors reviewed and evaluated PSE&G's response to a self-identified

condition in which an incorrect oil type was discovered in the residual heat removal

(RHR) system pumps.

b.

Observations and Findinas

On August 14,1996, while performing a post-maintenance surveillance run of the

"C" RHR pump, operators observed an abnormal oil level condition on the pump's

upper motor bearing concurrent with a " burning" smell. The pump was promptly

secured and declared inoperable. Technicians determined that a small amount of oil

had leaked down from the upper bearing area into the motor. This condition was

subsequently corrected. In addition, oil samples were taken from both upper and

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lower bearing oil sumps. This analysis identified that the lower bearing sump

contained an oil type not permitted by station configuration control documents.

Upon learning of the discrepancy, maintenance technicians replaced the improper oil

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with the correct type. Operations initiated an action request to address causal

factors and required the oil in the redundant RHR pump motors (as well as core

spray, SACS and service water) be sampled to determine the extent of the adverse

condition. It was later determined that the "A" RHR pump motor was similarly

affected. Concurrently, specialty engineering personnel provided an assessment of

pump motor operability and concluded that the use of the incorrect oil in the RHR

motor bearings would not adversely impact pump reliability or functionality. In spite

of this assessment, plant operators, upon restoration of the "C" RHR pump,

voluntarily removed the "A" RHR pump from an operable status to replace the

improper oil in the motor bearing. The inspectors observed good coordination

between operations and maintenance personnel during the ensuing work and the

RHR pump was promptly restored to service.

The inspectors reviewed the root cause assessment performed by engineering

personnel in response to this event and concluded that it thoroughly addressed the

relevant issues in their recommended corrective actions. Specifically, engineering

determined through a search of work order history that the wrong oil had been used

during recent motor bearing oil changes. Several factors that likely contributed to

this improper oil substitution, including the use of similar oil storage containers and

storage locations, were all adequately addressed to preclude recurrence of this

condition. Use of the wrong oil was considered a violation of station procedures;

however, the oilin question did not adversely affect the equipment and the concern

was both timely identified and corrected by the licensee. This licensee-identified

and corrected violation is being treated as a Non-Cited Violation, consistent with

Section Vll.B.1 of the NRC Enforcement Poliev.

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c.

Conclusions

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Plant operators exhibited a timely and conservative responce to indications of

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with maintenance technicians resulted in the prompt restoration of affected

improper oil in two residual heat removal pump motor beaiings. Good coordination

equipment. Root cause assessment and corrective actions were comprehensive.

M2.2 Maintenance Backloas

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The inspectors reviewed the maintenance backlog during the inspection period and

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the licensee's response in order to maintain the outstanding workload to a

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a

reasonable level. As of September 9,1996, the non-outage backlog of corrective

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maintenance (CM) activities was about 1400 activities, with a goal of about 400 by

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Refueling Outage 7 (currently scheduled for September 1997). The backlog of

overdue non-outage preventative maintenance (PM) activities was about 130

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3

activities, with a goal of O overdue by November 1996. Due to recent emphasis on

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reducing the overdue PM backlog, the CM backlog remained about the same over

the last few inspection periods. Of the non-outage backlog activities, approximately

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450 of the work orders were on-hold for various reasons, including: about 100 on-

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hold for parts, and about 250 on-hold for engineering support. This exceeded the

station goal of having no more than 150 work orders on-hold.

,

While the backlogs were consistently above the licensee's expectations throughout

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the inspection period, the inspectors noted the following: (i) work-week schedule

adherence has improved and remained above 90% adherence throughout the

inspection period; and, (ii) licensee efforts to reduce the overdue PM backlog has

been effective. Once the overdue PM backlog is eliminated, additional resources

will be available to begin a reduction of the CM backlog, in the interim period, the

inspectors observed increased management focus and assessment to ensure that

the backlog is a station priority and to assess the impact of the outstanding work on

safe operations. As an example, all cms associated with control room indicators

and alarms are considered a high priority and receive special management.

However, the number of control room deficiencies remains high.

The inspectors concluded that the outstanding corrective maintenance work is high;

however, licensee management has continuously assessed the backlog for impact

on operations and prioritization of maintenance.

M4.1 Both Channels of Drvwell Leak Detection Inocerable

a.

Insoection Scooe (71707,62707,61726)

The inspectors reviewed and evaluated the operations department response to a

self-identified event in which both channels of the drywellleak detection system

instrumentation were discovered to be simultaneously inoperable.

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b.

Observations and Findinas

On August 23,1996, while Hope Creek maintenance technicians were performing a

surveillance test on the drywell leak detection (DLD) system noble gas radiation

monitor, radiation protection department personnel noted that the drywell floor drain

sump flow instrument indicated an " operate failure." After receiving this report,

plant operators reviewed the alarm chronology print out in the control room and

determined that the floor drain sump flow monitor had failed 36 minutes earlier.

The shift supervisor quickly determined that, as a result of this instrument failure, in

combination with the redundant channel of DLD being inoperable (due to the in-

progress surveillance on the noble gas monitor), the station did not satisfy the

requirements of TS 3.4.3.1 (RCS Leakage Detection Systems). Action "d" of this

TS mandates that the plant be placed in hot shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Despite the good questioning attitude exhibited by radiation protection personnel in

this event, the inspectors judged that plant operators failed to recognize the

inoperable floor drain instrument in a timely manner. The shift supervisor

determined that 36 minutes had passed from the time when the station should have

recognized the hot shut down action statement until the condition was recognized.

An additional twenty minutes passed until maintenance technicians could

successfully complete the DLD noble gas monitor surveillance, effectively

terminating the hot shut down requirement about an hour after it began.

Operations department follow up to this adverse condition was appropriate. The

" pre-planned manual calculation" for quantifying floor drain cump in-leakage per TS 3.4.3.1 action a.1 was properly implemented until the floor drain monitor was

repaired. In addition, the operators involved in this event initiated an action request

in accordance with PSE&G's corrective action program, and developed a list of

" lessons learned" from the event that was promptly communicated to all of the

other operating shifts. Significant among the issues raised in this "self-assessment"

was a reinforcement of the expectation that reactor operators question the validity

of each alarm received on the radiation monitoring system display; in the noted

event the inspectors learned that an operator acknowledged the alarm indicating the

initial failure of the floor drain instrument but (in part) assumed that it was attributed

to the in progress surveillance on the noble gas monitor,

c.

Conclusions

Operator recognition of inoperable drywell leak detection system instrumentation

that required a plant shut down was not timely; however, the condition was

subsequently recognized avoiding any violation of the plant technical specifications.

Subsequent response was appropriate, including prompt implementation of TS-

required actions and documentation of the event in accordance with the corrective

action program.

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M8

Miscellaneous Maintenance issues

M8.1 (Closed) Violation 50-354/94-09-01: containment integrated leak rate test (Type A>.

The inspector verified the corrective actions described in licensee response letter,

dated December 8,1994, to be reasonable and complete.

M8.2 (Closed) LER 50-354/96005: inadequate surveillance testing for the residual heat

removal system suppression pool and spray modes of operation due to unaccounted

for RHR heat exchanger bypass valve leakage. This even' was discovered by the

licensee during the last refueling outage and involved en inadequate surveillance

test procedure. The procedure failed to consider design leakage through the RHR

i

heat exchanger bypass valves in determining the flow through the heat exchangers.

1

Since actual flow from the RHR pumps was about 10,000 gallons per minute total,

the flow through the heat exchanger (about 9650 gpm) was calculated to be less

than the technical specification minimum (10,000 gpm) required for the suppression

1

pool cooling test. The licensee deermined that this event was caused by the lack

'

of a rigorous design review when developing the plant technical specifications. The

licensee also determined that the Operational Experience Feedback process had an

'

opportunity to identify this poblem in 1992 based on the report of a similar problem

at the Limerick Generating Station.

The licensee provided corrective actions, including: a proposed change to the

technical specifications to correctly account for the design leakage through the RHR

bypass valves; changes to the OEF process that should better screen such

information to determine if external issues are applicable to Hope Creek; and,

incorporating lessons learned from this event into the Technical Specification

Surveillance improvement Process. The inspector had no further questions and

found the licensee's corrective actions to be reasonable and complete.

M8.3 (Closed) LER 50-354/96020: operations prohibited by technical specification -

failure to perform actions for inoperable radioactive gaseous effluent monitoring

instrumentation. This event involved less than timely actions to the grab sampling

requirements due to a failed South Plant Vent radiation monitor. On several

occasions grab samples were not taken within the specified 12-hour requirements.

The licensee implemented corrective actions to ensure more timely sampling and

analysis for conditions required by the plant technical specifications. This licensee

identified and corrected violation is being treated as a Non-Cited Violation,

consistent with Section Vll.B.1 of the NRC Enforcement Policy. This LER is closed.

M8.4 (Closed) LER 50-354/95-033. Sucolements 7. 8. 9 and 10: technical specification

surveillance requirement implementation deficiencies identified by the TSSIP.

These LER supplements document additional findings of the licensee's long-term

!

corrective action for surveillance testing inadequacies originally described in LER 95-

033. While different surveillance requirements were identified in these reports as

not having been appropriately demonstrated, the associated root causes and

corrective actions were the same as previously identified in addition, the

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equipment was subsequently tested and determined to be operable. No other new

issues were revealed by the supplements.

111. Enaineerina

E1

Conduct of Engineering

E1.1

10 CFR 50.59 Activities

a.

Insoection Scope (37551)

,

The inspector reviewed those 10 CFR 50.59 activities described in Table 1 for Hope

Creek. The 10 CFR 50.59 activities were conducted at Hope Creek during the

period of January 1995 to June 1996 with an emphasis on more recent activities.

.

b.

Observations and Findinos

,

For each activity, the inspector requested that the licensee provide a NAP-59 safety

evaluation or a NAP-59 Applicability Review. Test procedure, THC.OP-SO.GO-

0002, (item 3 of Table 1), was determined by the licensee to require a safety

evaluation. However, the inspector found that the safety evaluation had not been

prepared until after the activity had been initiated which is a violation of 10 CFR 50.59(a)(1). The requirements of 10 CFR 50.59(a)(1) allow the licensee to make

changes in the facility, as described in the FSAR, provided that the change does not

involve a USQ or a change to the TSs. Since the licensee did not prepare a safety

evaluation to determine if the activity involved a USO, or to determine if a change

to the TSs was involved, prior to undertaking this activity, this is a violation of 10 CFR 50.59(a)(1). The inspector noted that the licensee identified this violation and

terminated use of the procedure until a safety evaluation was prepared and

approved, which was considered an effective corrective action. This licensee-

identified and corrected violation is being treated as a Non-Cited Violation,

consistent with Section Vll.B.1 of the NRC Enforcement Policv.

The inspector found that the licensee did riot prepare a NAP-59 Applicability Review

or NAP-59 safety evaluation in connection with a March 18,1996 revision to the

design change package,4EC-3546, Package 12, Revision 1, (item 13 of Table 1).

The inspector noted the revision involved changing the leak test method from

" hydrostatic" to "in-service leak test." The inspector noted that, while a procedure

to perform a test associated with a design change may be included in a design

change package, the procedure change should still be subjected to the 10 CFR 50.59 process in that the new test may pose its own safety issues, independent of

the design change. Although the example discussed here did not result in a

violation of 50.59, it does point to a vulnerability in the process that governs

revisions to design changes.

The remaining activities reviewed by the inspector (see Table 1) were observed to

be of generally good quality and in accordance with NRC requirements.

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c.

Conclusions

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The inspector concluded that, in general, PSE&G had a good framework for the 10 CFR 50.59 program.

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E1.2 Station Auxiliary Coolino System Valve 1EGHV-2522E Operation

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a.

Insoection Scope (71707 and 37551)

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The inspectors observed PSE&G's response to a possible oilleak in the hydraulic

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operator associated with safety auxiliaries cooling system (SACS) valve 1EGHV-

2522E.

b.

Observations and Findinos

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On August 13,1996, operators suspected that the hydraulic operator of valve

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1EGHV-2522E had an internal oil leak. This condition, if left uncorrected, could

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lead to the valve not operating properly and possibly resulting in a transient

condition due to a loss of turbine auxiliaries cooling system (TACS) water.

'

Based on a review of the UFSAR Sections 9.2 and 9.5, the inspectors determined

7

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that TACS is a non-safety related " load" that is cooled by the safety-related SACS

sy. stem. The TACS system is designed to lesser quality standards than the SACS

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aystem and, as a result, during the initial licensing of the facility, PSE&G considered

the effects of a postulated break in the TACS pipe. To account for the

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hydrodynamic effects, accumulators were placed in the SACS lines to act as

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dampeners for possible water hammer. To account for possible inventory losses to

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the SACS system, two fast-acting hydraulically-operated isolation valves (1EGHV-

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2522E and F) were installed in series in the TACS supply piping. The 2522E and F

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valves are automatically closed on any indicated low pressure in the SACS to TACS

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supply line that possibly results from a catastrophic failure of the TACS line.

Normally, one of the two SACS subsystems is lined up to supply cooling water to

TACS. While there are no logical or physical barriers preventing the operators from

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lining up both SACS subsystems to provide TACS cooling, the system operating

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procedure does not permit this alignment. In addition, such an alignment could lead

to sluicing water inventory from one SACS head tank to the redundant counterpart

in the other subsystem, which could lead to operational transients. The TACS

system is isolated from the SACS system by two pairs of isolation valves on the

supply side (one pair from each SACS subsystem) and by a pair of isolation valves

on the return side of SACS. All of these valves receive automatic closure signals in

response to LOCA or LOP actuations. These valves are similar to the TACS

isolation valve 2522E, except their closure response time is significantly longer

(about 20 seconds vs.10 seconds for 2522E).

It is not clear in the UFSAR that the TACS isolations valves (2522E and F) provide a

safety function; although, they do perform a required isolation function to limit

SACS coolant inventory loss on a postulated TACS line break. In addition, while

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14

the isolation valves are considered part of the safety-related portions of the SACS

system, the instrumentation that initiates closure of the valves are not safety

related.

On August 13,1996, in response to the possible valve operator hydraulic leak,

station operators " locked" open the 2522E valve by blocking its fluid vent port.

This action was not a specified action in either the system operating or alarm

response procedure. As such, it resulted in the system not being able to operate as

described in the UFSAR and no safety evaluation was conducted to determine

whether that change in the component operation constituted an unreviewed safety

question. While the inspectors noted that the valve function did not include

automatic response to LOCA or LOP accident signals, it was designed to mitigate a

large or complete break of the largest non-safety related TACS line and prevent a

functional failure of the associated safety-related SACS system. Once the

inspectors communicated this concern to the operators, the valve controls were

restored to a normal configuration (for a total of about three hours in the abnormal

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configuration). This issue was considered a violation of 10 CFR Part 50.59(a)(1).

(VIO 50-354/96-07-01)

c.

Conclusions

The inspectors concluded that plant operators modified the controls of a safety

related component, valve 1EGHV-2522E, without use of proper engineering support

to assess whether this action resulted in either a necessary change to the plant

technical specifications or an unreviewed safety question. Once this concern was

identified, operators restored the valve to its normal configuration in a timely

manner.

E2

Engineering Support of Facilities and Equipment

C

E2.1

Station Service Water Travelina Screen Controls Modification

a.

Insoection Scope (37751)

The inspectors reviewed the documentation associated with a modification to an

approved design change package for the station service water system traveling

screen controls. The inspectors interviewed appropriate licensee representatives

associated with this modification, using established station procedures governing

design changes and safety evaluations as a basis for assessment.

b.

Observations and Findinas

During July 1996, Hope Creek maintenance technicians implemented an approved

design change package which upgraded the station service water system traveling

screen controls to resolve long-standing performance problems and improve overall

system reliability. On July 12,1996, with the work on the "D" screen controls only

partially completed, operations personnel requested that the engineering department

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devise a means to restore the function of the screen temporarily due to the

anticipated arrival of Hurricane Bertha the next day.

Since the "D" service water subsystem was already inoperable due to the in-

progress design change, engineering management concluded that a temporary

modification and associated 10 CFR 50.59 evaluation was not necessary to make

the traveling screen available for operation, but not operable. Instead, a manual

change request (MCR #78) was approved that modified the original screen control

design change package (DCP 4EC-3599) permitting the installation of jumpers in the

control logic to allow manual high speed operation of the traveling screen. The

inspectors reviewed the MCR and judged that the supporting documentation was

weak, specifically because the technical basis for justifying the revision to the

original design change package was not provided.

Based on this review, the inspectors noted that the MCR process (defined in design

engineering procedure NC.DE-AP.ZZ-0017 (O)) requires that a " revision justification

sheet" be completed and approved. This justification sheet implements a screening

process like that mandated by 10 CFR 50.59, but does not require a documented

basis for why revisions to a design change package do not invalidate the original

safety evaluation. As a result, though MCR #78 of DCP 4EC-3599 met the

requirements of the governing station procedure, it was not clear to the inspector

that the implementation of jumpers in the traveling screen control logic was not

considered a major revision to the overall design change package, and therefore

invalidate the conclusion of the original supporting safety evaluation.

]

During interviews with engineering department supervision, the inspectors agreed

that MCR #78 was technically adequate and met the requirements of station

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procedures, primarily because this design change package revision also ensured that

the screen control logic jumpers would be removed from the affected service water

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subsystem prior to returning the subsystem to an operable status. In spite of the

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licensee's assurance that the MCR provided sufficient control to ensure the design

change would be appropriately installed, the inspector noted that the MCR resulted

in a change to the system configuration different than analyzed. While noting that

the system was not considered operable during the time that the MCR was in

effect, the inspector considered the supporting analysis to be weak,

c.

Conclusions

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Operators exhibited a good, conservative desire to maximize overall service water

system reliability due to the impending severe weather by requesting engineering

personnel to devise a means to restore the function of a an associated subsystem

made inoperable by partial implementation of a design change package. However, a

review of the modification engineering personnel developed for installation to satisfy

the operations department request highlighted weaknesses in the process for

controlling and justifying design change package revisions.

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E3

Engineering Procedures and Documentation

E3.1

10 CFR 50.59 Reviews and Safety Evaluations

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The inspector reviewed procedure NC.NA-AP.ZZ-0059(O) Rev. 4, "10 CFR 50.59

j

Applicability Reviews and Safety Evaluations," referred to as NAP-59. The strategy

of NAP-59 is to apply the procedure to a wide range of activities where 10 CFR 50.59 may, or may not, be applicable. The user is required to first perform an

,

" Applicability Review" to determine if a particular activity is within the scope of 10

,

CFR 50.59. If the results of the Applicability Review show that 10 CFR 50.59 is

4

not applicable, the Applicability Review form is saved for future reference. If the

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Applicability Review indicates that 10 CFR 50.59 is applicable, the user is required

to perform a safety evaluation. The NAP-59 procedure also provides procedural

i

interfacing with the FSAR update program of NAP-35, should the subject activity

require a change to the FSAR.

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The NAP-59 procedure is based on the industry guidance in NSAC-125, " Guidance

for 10 CFR 50.59 Safety Evaluations," draft dated June 1989. Consequently, NAP-

>

l

59 indicates that a smallincrease in the probability or consequences of an accident

i

or malfunction previously evaluated in the safety analysis report may not indicate

that the activity involves an Unreviewed Safety Question (USQ). The NRC issued

guidance on this issue in an April 9,1996 revision to the NRC Inspection Manual,

Part 9900, " Interim Guidance on the Requirements Related to Changes to Facilities,

Procedures and Tests." The guidance indicates that a smallincrease in the

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probability or consequences of an accident or malfunction previously evaluated in

i

the safety analysis report does indicate that the activity involves an Unreviewed

Safety Question (USQ). The licensee's memorandum of July 12,1996 informs

j

those involved in the 10 CFR 50.59 process of NRC's April 9,1996 positions on 10 CFR 50.59.

a

In summary, the inspector found that NAP-59 is well written, provides clear

assignment of responsibility, and provides the user with good directions for

,

addressing the 10 CFR 50.59 process.

E5.1

Staff Trainina and Qualification on 10 CFR 50.59 Reviews

!

The inspector reviewed the 10 CFR 50.59 aspects of the training program. The

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lesson plans for initial training (L.P. No. 0905-300.20-5059ZZ-03) and periodic

i

retraining (L.P. 0905 300.99N-5059-03) were reviewed. The lesson plans were

l

found to be clearly written with good examples to demonstrate the use of NAP-59.

Conversations with the licensee indicated that periodic 10 CFR 50.59 training is not

1

a program requirement.

With regard to qualifications, the inspector ascertained through conversations with

the licensee that no PSE&G-wide qualifications have been established for those

<

individuals involved in the 10 CFR 50.59 process. The licensee also stated that a

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soon-to-be-released revision of NAP-59 will provide additional guidance on this.

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The inspector concluded that certain aspects of the training program for 10 CFR 50.59 were good; however, qualification requirements had not yet been developed

to ensure that personnel involved in the use of 10 CFR 50.59 had been

appropriately trained.

4

E7

Quality Assurance in Engineering Activities

E7.1

Safety Review Committee Activities for 10 CFR 50.59 Evaluations

Hope Creek TS 6.5.1.6.e requires that the Site Operations Review Committee

(SORC) perform a review of the safety evaluations that have been completed under

the provisions of 10 CFR 50.59. In reviewing the activities described in Table 1

i

(attached to this report), the inspector noted evidence that the SORCs had

performed the required safety evaluation reviews. Attendance at a Hope Creek

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SORC meeting gave the inspector the impression that the SORCs set a fairly high

standard for approval of 10 CFR 50.59 safety evaluations. ' The rejection rates for

,

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safety evaluations presented to SORCs is trended and varied from approximately 10

to 20 percent during the period of August 1995 to January 1996 with an improving

trend at the end of the period; during the same period, the Hope Creek SORC

rejection rate varied from approximately 5 to 35 percent, also with an improving

trend at the end of the period.

The Hope Creek Offsite Safety Review Group (OSRG) also has a role in reviewing

10 CFR 50.59 safety evaluations as required by Hope Creek TS 6.5.2.4.2.a. The

inspector requested that the licensee provide evidence that the activities described

in Table 1 had been reviewed by the OSRG. In response, the licensee indicated that

activities 1,3,18,19 and 20 in Table 1 had not been reviewed by OSRG because

,

they had not been received from the sponsoring organizations. Hope Creek TS 6.5.2.4.2.a requires that the OSRG review all safety evaluations prepared pursuant

to 10 CFR 50.59. The failure of the OSRG to review the noted activities in Table 1

is a violation of the facility technical specifications. (VIO 50-354/96-07-02)

The inspector determined that the OSRG had previously known that sponsoring

organizations were not consistently forwarding safety evaluations for OSRG review.

A memorandum dated October 19,1994, from Nuclear Safety Review to the Salem

and Hope Creek General Managers, noted this fact.

The inspector concluded that OSRG review of safety evaluations were not

consistently performed. This led to a violation of NRC requirements. The inspector

further concluded that the licensee's corrective actions for similar prior findings

were ineffective at Hope Creek in that sponsoring organizations at Hope Creek

continued to be inconsistent in providing safety evaluations for OSRG review.

Finally, the inspector concluded that the OSRG lacked reasonable initiative in

ensuring that they received these safety evaluations from the sponsoring

organizations.

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E8

Miscellaneous Engineering issues

l

E8.1

(Closed) Unresolved item (50-354/96-03-05): on January 31,1996,PSE&G

declared four Hope Creek radiation detectors inoperable. PSE&G had found that the

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detectors were being used outside their design temperature range. The detectors

monitor beta radiation in the intake of the control room ventilation system and on

high radiation, initiate an alarm and redirect the control room air from the outside to

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a filter train.

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)

PSE&G's subsequent review of the detector design determined that, besides low

temperature, high humidity was also an issue requiring resolution. As described in

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NRC inspection report 50-354/93-06, after consultation with the detector vendor,

PSE&G concluded that the low temperature was not a concern. Regarding

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humidity, calculations performed by PSE&G determined that a film of vapor droplets

4

could form on the aluminum foil end of the detector, limit the amount of beta

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radiation entering the detector, and attenuate the radiation signal. PSE&G

calculated that the maximum film thickness could be 0.0048 inches, correspondinD

to an attenuation coefficient of 44%. This attenuation, when included in the

detector error analysis, was accepMble and within the current beta allowable

settings for the control room.

l

To confirm the calculations, PSE&G hired a consultant to build a full scale mockup

of the control room ventilation ducting and test the detector within the postulated

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limiting environmental conditions. In this experiment two beta energy sources were

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used and the temperature and relative humidity were slowly changed. In the end

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the film thickness was less than that calculated and the measured attenuation

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coefficients due to moisture were 38% with the low energy beta source, and 26%

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with the high energy source. Based on the results of their analyses and experiment,

PSE&G concluded that the installed detectors were always operable over all

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temperature and humidity ranges.

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As a result of the above review, PSE&G found that exposure to moisture could

cause pitting of the foil. Therefore, they decided that the foil should be changed

each time the detectors would be calibrated. The 18-month period between

calibrations, and foil changes, was based on the results of their surveillance of the

detectors as well as calculations.

Based on a review of the above calculations and test results, the inspector

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concluded that PSE&G had properly addressed and resolved the issue.

E8.2 (Closed) Violation 50-354/95-10-01: failure to update the Hope Creek Generating

Station FSAR in accordance with 10CFR50.71(e)(4). The licensee responded to the

violation by letter dated September 11,1995 providing the following corrective

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actions: (1) elimination of the change notice backlog, (2) update of the Salem and

Hope Creek FSARs and (3) review of procedures to assure proper assignment of

responsibility.

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The inspector reviewed PSE&G procedure NC.LR-AP.ZZ-0013(Z) - Revision 0,

"UFSAR Maintenance Process", dated February 1,1996. The inspector found the

procedure to be well written with clear assignment of program responsibility and

correctly reflecting the requirements of 10 CFR 50.71(e). The inspector interviewed

the UFSAR Coordinator and found this individual to be knowledgeable concerning

program requirements. The UFSAR Coordinator indicated that the change notice

backlog had been eliminated and the Hope Creek UFSAR had been brought up-to-

date with UFSAR Revision 7, dated December 28,1995. The next Hope Creek

UFSAR update is scheduled for September 25,1996, which is 6 months following

restart from the refueling outage in accordance with 10 CFR 50.71(e). The UFSAR

Coordinator indicated that the Salem change notice file was also current, the last

FSAR update having been made on June 10,1996. The schedule for Salem UFSAR

update is uncertain due to the continuing unit outages.

The inspector reviewed UFSAR update packages associated with activities 6,8 and

16 of Table 1 for Hope Creek. The inspector concluded that PSE&G had taken

effective corrective action for this violation.

1

E8.3 (Closed) Violation 50-354/94-13-0_2: RHR system suppression pool suction valve

(BC-HV-F004A) could not be controlled properly from the remote operating switch

in accordance with plant design. The inspector verified the corrective actions

described in licensee response letter, dated October 18,1994, to be reasonable and

complete. No similar examples were identified.

IV. Plant Support

R2

Status of RP&C Facilities and Equipment

During this inspection, the inspector conducted numerous tours of the facility during

operating conditions and noted that all required radiological postings and locked

areas met regulatory requirements. Further, areas were clear of unnecessary

equipment, well illuminated and free of safety hazards.

,

R4

Staff Knowledge and Performance in RP&C

During this inspection, the licensee identified neveral missed technical specification

required sampling and analysis activities due to poor tracking of such, coincident

with inoperable effluent monitoring equipment. This matter is described in Section

M8.3 of this report. The licensee has directed all departments to decrease the

required action times for technical specification action statements in order to better

achieve requirect results. For example,12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> actions will be scheduled every

eight hours, etc.

In addition, Hope Creek operators observed a minor increase on two of the effluent

radiation monitors associated with the turbine building exhaust. The inspectors

considered the troubleshooting of the associated detectors and investigation of the

.

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20

possible causes of the minor increase in radiation levels to be appropriate. The

inspectors also noted that no releases were made in excess of technical

specification requirements. Further, once the licensee corrected the minor packing

leak in the steam tunnel associated with main steam valve,1 ABHV-2016B,

monitored turbine building exhaust ducting returned to normal conditions.

The inspector concluded that while some activities associated with effluent grab

sampling and analysis were not conducted in a timely manner, overall performance

of radiation protection program requirements were good.

R7

Quality Assurance in RP&C Activities

The inspectors reviewed Audit Report 96-151/152, Radioactive Material Control,

issued September 9,1996. The inspector observed that the audit scope was

sufficiently detailed to ensure that the Hope Creek Process Control Program and

implementing procedures for processing and packaging radioactive wastes was

successfully maintained. Several concerns were identified, including: deficiencies in

radiation monitoring system equipment and missed compensatory sampling;

deficient QA oversight of the program; deficient procedure adherence. All of the

deficient conditions were appropriately entered into the licensee's corrective action

program. One positive attribute was identified associated with technical knowledge

,

of responsible individuals and ownership of the radioactive waste transportation

'

program.

The inspector concluded that the QA audit of the Hope Creek radioactive waste

program met the requirements of the Hope Creek technical specifications and

provided good self-assessment of this area.

P1

Conduct of Emergency Preparedness (EP) Activities

P1.1

Effectiveness of Licensee Controls

a.

Inspection Scoce (82701)

The inspectors reviewed the licensee's tracking systems used for tracking EP

related action items. Also, the EP self-assessment program was reviewed to

determine the effectiveness of licensee controls.

b.

Observations and Findinas

Procedure NC.NA-AP-ZZ-0000(Q), PSE&G Nuclear Business Unit " Action Request

(AR) Process," describes the licensee's method for reporting conditics requiring

,

corrective action, program enhancement or interdepartmental support. ARs are

tracked by a newly developed automated system termed the Performance

improvement Review System (PIRS), which is maintained by the audit department

staff who screen, classify and distribute the ARs. ARs are assigned significance

.

.

21

levels (one to four, in descending priority) depending on circumstances, conditions

or at management discretion. All ARs are given significant management attention

and the highest significance levels (one and two) require a root cause analysis.

The inspectors requested a demonstration of the PIRS but the licensee was not able

to locate any recently closed ARs. Licensee individisals stated that PIRS is not

" user-friendly" and has the potential for losing data if a user incorrectly inputs

information. Due to these problems, the EP staff utilizes three other internal office

systems for tracking repetitive EP activities required by E-Plan commitments,

procedure /E-Plan changes, drill / exercise critiques, training classes reviews and EP.

administrative review items. The inspectors discussed the problems noted during

,

the demonstration of the PIRS with members of the audit department. They stated

j

that they were aware of the computer program problems and are currently

modifying the program for easier and more efficient use. Once the problems are

resolved, it is the licensee's intent that the PlRS will become the sole tracking

system for Salem and Hope Creek.

The inspectors reviewed several ARs and found them to be very detailed, thorough

,

and were reviewed by management.

i

The licensee had recently implemented an "EP Group Planned Self-assessment

Program" to evaluate the effectiveness and performance of the EP program. The

inspectors reviewed several self-assessment reports and found them to include

evaluation plans, strengths, weaknesses and/or potential areas for improvement.

As the self-assessment program develops, the licensee plans to become more self-

critical, establish trending data and closely evaluate repeat findings.

)

c.

Conclusions

)

1

The EP staff uses the AR process plus three other automated systems for tracking

issues such as audit findings, procedure changes and self-assessment findings. The

systems are effective and ensure adequate management attention. The recent

addition of a self-assessment program is a good initiative for the EP program.

j

P1.2 Relationshio with Offsite Aaencies

a.

Insoection Scope (82701)

The inspectors interviewed state and county representatives from the States of

New Jersey and Delaware to assess the licensee's relationship with offsite

agencies.

i

b.

Observations and Findinas

The inspectors interviewed the Radiological Administrator for the Delaware

Emergency Management Agency, the Manager, Bureau of Nuclear Engineering

(BNE), New Jersey, and the Deputy Coordinator for the Department of Emergency

Services, Salem County, New Jersey, to discuss the licensee's relationship with

.

e

22

those agencies. Both Delaware and Salem County, NJ representatives stated that,

overall, the licensee worked hard to maintain an excellent rapport with their

agencies.

However, the Manager, BNE stated that while the communications and information

flow between the licensee and the State has improved since October,1995, further

improvement is needed in the following areas: 1) planning of the Emergency

Operational Facility (EOF) renovation; 2) quality of the station status checklists used

for transmitting event information; and 3) the verification of information contained in

press releases from the licensee's emergency news center. He further stated that

recent communications with the licensee on the proposed NUMARC EALs was

constructive.

c.

Conclusions

Overall, the licensee maintained good rapport with the offsite agencies. However,

the Manager, BNE identified some issues where coordination and communication

between the licensee and the State of New Jersey could be improved.

P2

Status of EP Facilities, Equipment and Resources

P2.1

Operational Readiness of Emeraency Facilities

a.

Insoection Scope (82701)

The inspectors toured the following Salem facilities: the EOF, Control Room (CR),

Technical Support Center (TSC), Operations Support Center (OSC), and Control

Point. The Hope Creek facilities were evaluated during the May,1996 annual

exercise and found to be operationally ready. The inspectors also reviewed 1996

facility equipment inventories and surveillance tests for completeness and accuracy.

b.

Observations and Findinas

The inspectors checked the inventory of several emergency equipment lockers and

one field monitoring team emergency kit for completeness and equipment readiness.

One locker contained two radiation survey instruments with dead batteries, which

were immediately replaced. All other survey meters inspected were calibrated and

operational. The inspectors found two unshielded Cesium-137 check sources in

supply lockers located in the EOF and TSC, used for verifying instrument response.

The check sources are routinely stored near a supply of personnel

thermoluminescent dosimeters (TLDs) used for offsite field monitoring teams.

These sources could potentially produce an erroneous radiation dose to the field

TLDs prior to use in an actual emergency. The licensee acknowledged this problem

and agreed that the check sources and TLDs should be stored in separate lockers.

While touring the TSC, the inspectors noticed that a key for a radiation protection

(RP) locker was missing. Apparently, an RP staff member had changed the lock,

/

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23

without informing the EP staff, and stored the key at the Salem control point.

According to the licensee's emergency plan implementing procedure (EPIP) 203S,

the key is to be stored near the locker. Relocation of the key could potentially

result in the locker being inaccessible to field teams during an emergency. The

licensee initiated a procedure change to ensure that during emergency conditions,

an RP technician, assigned to the TSC, would bring the locker key from the control

point and unlock the locker.

The licensee was in the process of constructing a new OSC inside the CR

ventilation boundary and renovating the existing EOF. During construction, a

temporary OSC, outside the CR, was being utilized in case of an actual emergency

event. The inspectors concluded that the EOF and temporary OSC were adequate if

needed for this purpose.

The inspectors determined that equipment inventories, communication surveillance

tests, and siren surveillance tests were conducted at correct frequencies, and

inventory checklists were properly completed and reviewed. Identified deficiencies

and corrective actions were well documented.

l

C.

Conclusions

j

The inspectors concluded that the licensee maintained an effective inventory and

surveillance test program and that the Salem / Hope Creek emergency facilities and

equipment were operationally ready.

P3

EP Procedures and Documentation

a.

Inspection Scope (82701)

The inspectors reviewed emergency plan (E-Plan) and EPIP revisions in the regional

office, prior to the inspection, to determine if the changes reduced the effectiveness

of the E-Plan. While onsite, the inspectors reviewed the documentation for the last

E-Plan changes.

b.

Observations and Findinas

The inspectors reviewed the licensee's 10 CFR 50.59 safety evaluation and 10 CFR 50.54(q) licensee review for Revision 5 to Section 2 of the E-Plan. The inspectors

concluded that these were thorough, well-documented, and adequate for making

this revision. EPIP revision changes were documented in NRC Inspection Report

50-354/96-01, 50-272 & 311/96-01 and no additional revisions were reviewed

prior to this inspection.

.

.

24

c.

Conclusions

The inspectors determined that the reviewed E-Plan and EPIP changes did not

reduce the effectiveness of the E-Plan. Also, the licensee's procedure change

process was good.

P5

Staff Training and Qualification in EP

a.

Insoection Scope (82701)

The inspectors reviewed EP training records, training procedures, lesson plans,

EPIPs and the licensee's E-Plan to evaluate the licensee's EP training program. The

inspectors also conducted interviews with Salem Senior Reactor Operators (SROs)

to assess the licensee's EAL classification training.

b.

Observations and Findinas

The EP off-site supervisor maintained the EP training records for emergency

response organization (ERO) responders. The inspectors randomly selected the

training records of approximately 75 responders from Salem and Hope Creek and

verified that the ERO responders were qualified to fill their assigned emergency

response positions. Approximately a quarter of the responders are required to have

respirator training which is provided by RP. EP does not routinely track the RP

training to ensure that all responder training requirements are met, in early 1996,

the EP off-site supervisor, discovered that respirator training for 9 out of 16

maintenance workers on the ERO list had elapsed. Also, in August 1996, it was

reported in the licensee's morning management meeting, that an Instrument and

Control tech.. :ian was reported not to have current respirator qualifications and

was listed on the current ERO list. The EP staff appeared to be unaware of this

incident.

The inspectors stated to the licensee that although the RP Department is

responsible to provide respirator training, the EP staff is responsible to ensure that

all members on the ERO list meet the required qualifications stated in the Emergency

Plan and EPIPS. The licensee plans to review this area of concern and to review the

RP records to ensure that allindividuals on the current ERO list meet all training

requirements. Additionally, the licensee mentioned plans to have one automated

training tracking system for better utilization by the EP staff.

The licensee had made changes to their EP training program due to problems

identified in drills and exercises. The licensee was conducting quarterly

unannounced call-out muster drills, weekly pager tests, and were completely

revising procedures and EP overview lesson plans. In addition, a letter was sent

from upper management to the ERO members addressing their EP roles and

responsibilities.

.

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25

The inspectors interviewed two Salem SROs to assess the quality of the licensee's

present EAL training. Both SROs stated that the NUMARC EAL training was good,

however, they did not think the one-hour training session on the present EAL

i

scheme was very thorough or detailed. They both stated that if the NUMARC EALs

are not approved prior to restart of Salem 1 & 2, they would expect comprehensive

retraining on the present EALs.

The inspectors stated to the licensee that until the NUMARC EALs are approved,

adequate and appropriate training should be provided to the SRO's for classifying

events using the present EALS.

'

The inspectors reviewed training records for annual offsite emergency response

,

i

training for medical, fire-fighting, and media personnel. The inspectors found that

the required drills had been conducted and were well-documented. Media training

was offered by the licensee, but may not have been implemented in accordance

with the E-Plan (see Section P8). With this onc exception, all on-site and off-site

required drills, exercises and training were conducted in 1995 and 1996 in

accordance with the licensee's E-Plan.

l

The licensee conducted monthly pager drills for all four duty ERO teams and weekly

drills for the on-call duty team. Additionally, they conducted quarterly muster

exercises where the duty team must actually report to the site, alternating between

Salem and Hope Creek. The inspectors noted that documentation regarding these

drills and exercises indicated an overall improvement in ERO response. However, in

May 1996, NRC inspectors attended an unannounced call-out drill and observed

poor drillmanship and command and control. (See Section P8.3)

The inspectors reviewed the training records for annual EAL training with the states

'

and counties and found them to be satisfactory.

c.

Conclusions

The inspectors determined that the ERO members, for whom training was reviewed,

were currently qualified. However, the EP department was not fully effective at

ensuring that individuals listed on the ERO list meet all training requirements to fill

their position. Training of offsite agencies and support organizations is of good

quality and completed as required.

The inspectors concluded that the periodic pager tests and mustering drills, as well

as holding ERO responders accountable for their responsibilities is a positive step to

upgrade their overall emergency response capability. Overall, the inspectors

assessed this area as adequate.

._

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26

P6

EP Organization and Administration

a.

Insoection Scope (82701)

The inspectors reviewed the licensee's EP staffing and management to determine

the changes that have occurred since the last program inspection (August 1994),

and to assess if those changes had any adverse effect on the EP program.

b.

Observations and Findinas

The EP Department has had several management and organization changes in the

past year. In January 1996, the Manager, EP & Radiological Safety was replaced.

In September 1996, this position is being eliminated and split into two management

positions. The intentions are to add an experienced EP manager and an experienced

radiological health manager. In July, the EP and Radiological Support Division was

moved from Site Support Services and placed in the Nuclear Training Center (NTC)

Division. The Director, NTC reports directly to the Sr. Vice President, Nuclear

Operations. The licensee is planning additional changes in the responsibilities of the

EP staff members.

Discussions with the Sr. Vice President and Director, NTC indicated that

management is committed to bringing a serious EP attitude to the ERO members.

They also stated that the addition of a manager with EP experience will enhance EP

staff performance.

c.

Conclusions

Discussions with the members of the EP staff, the inspectors determined that the

recent organizational changes have not had an adverse effect on the EP staff. At

this time, it does not appear that these changes have reduced the ability to

administer the EP program effectively.

P7

Quality Assurance (QA)in EP Activities

a.

Insoection Scope (82701)

The inspectors reviewed Audit Reports No.95-030 and 96-030, of the EP

Department, conducted in 1995_and 1996, respectively. The inspectors also

reviewed audit plans, checklists procedures and interviewed personnel from the QA

Department regarding the process for conducting a program audit.

b.

Observations and Findinas

Based on document review and interviews, the inspectors determined that the

audits were conducted utilizing an audit plan and checklists, and that the audit team

included several technical specialists from other nuclear utilities with EP experience.

_ . _ _ _ _ _ _ _ _ .._ _ _ _

.

,

27

The audit reports were appropriately detailed and rnet the requirements specified in

10 CFR 50.54(t). No programmatic problems were identified.

c.

Conclusion

The audit reports were comprehensive and the audit plan was extensive. The use

of independent technical specialists is particularly noteworthy. The reports met the

requirements of 10 CFR 50.54(t) and the inspectors assessed this area as very

'

good.

P8

Miscellaneous EP issues

P8.1

Updated Final Safety Analysis Report (UFSAR) Inconsistencies

A recent discovery of a licensee operating its facility in a manner contrary to the

UFSAR description highlighted the need for a special focused review that compares

'

plant practices, procedures, and/or parameters to the UFSAR description. Since the

<

UFSAR does not specifically include EP requirements, the inspectors compared

licensee activities to the E-Plan, which is the applicable document. The following

inconsistences were noted between the E-Plan and licensee activities by the

inspectors.

1.

Section 9, paragraph 4.4 of the E-Plan discusses additional radiological

instrumentation located in the licensee's Training Center laboratory to be

!

available as backup to the EOF. The inspectors determined that the

instrumentation had never been calibrated and the laboratory is currently

being dismantled.

2.

Section 8, paragrbph 3.0 of the E-Plan, states that annually, an information

program is provided to local news representatives and covers specific

outlined topics on nuclear energy, radiation and emergency planning. It also

states that this program may take place as part of the annual exercise. A

public information (PI) representative stated that media training actually

consisted of an information calendar sent to local media personnel, followed

by a phone call, inviting them to the licensee's annual exercise. This is

inconsistent with the commitments in the E-Plan.

The inspectors discussed these issues with the licensee, and E-Plan changes have

been submitted to delete the use of the Training Center laboratory as a backup to

the EOF and to provide a better description of media training. These concerns are

considered unresolved pending NRC review and approval of the proposed changes.

(URI 50-354/96-07-03)

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28

P8.2 Missed Alert Declaration

During this inspection, the inspectors reviewed the missed alert declaration for an

event that occurred at Salem on June 7,1995. Details of this inspection are

contained in Salem inspection report 50-272,311/96-15.

S1

Conduct of Security and Safeguards Activities

Du@g this inspection, the inspector observed some conditions that were not in

accordance with the licensee's security plan and its implementing procedures.

These activities are fully discussed in NRC Inspection Report 50-354/96-08.

S8

Miscellaneous Security and Safeguards issues

S8.1

(Closed) Followuo item 50-354/93-28-01: inspection followup of perimeter

assessment aid upgrades. The upgrade project has been completed on the Hope

Creek site. The inspectors have noted that routine maintenance is now effective at

maintaining these aids available. Some additional planned work is still to be

completed on the Salem upgrades and those issues will be reviewed separately;

however, the Hope Creek portion of this item is considered closed.

F2

Status of Fire Protection Facilities and Equipment

.

The inspectors toured various portions of the licensee facilities and observed that

fire protection response equipment was maintained appropriately. During this

inspection period, the licensee initiated a previously approved design change

package (DCP 4EC-3296) to replace the Hope Creek fire protection computer. This

activity was conducted on-line, which resulted in a temporary loss of the fire

protection alarm and indication function in the control room. As a result,

compensatory measures were established to provide fire watch monitors of local

fire panels for indication and alarm for all safety related portions of the facility.

These monitors included use of closed circuit television (CCTV) for certain local

panels in lieu of a watchstander.

The inspectors reviewed the use of CCTVs, which is described in procedure HC.FP-

AP.ZZ-0004(O), " Actions for inoperable Fire Protection - Hope Creek," dated

September 9,1996. In lieu of using a specific safety evaluation for installing the

CCTVs, the licensee relied upon acceptance criteria provided in a radiation

protection procedure for use of this same equipment. That procedure required

associated cables for the CCTVs not be placed within one inch of any safety related

cab le tray, cable or conduit. The inspectors walked down the installation of the

CCTV cables for this fire protection procedure change and observed that several

cables did not meet the established criteria. In addition, the licensee subsequently

informed the inspectors that the one inch criteria was not really meant to pre-

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29

j

approve installation of CCTV cables over open safety-related cable trays or

traversing multiple trains of safety-related cable trays, as was the condition

identified by the inspectors.

After the inspectors identified this condition, licensee individuals took immediate

corrective actions to remove all CCTV cables in close proximity to safety-related

cables, cable trays, and conduit.

The inspectors determined that the safety evaluation associated with this procedure

revision failed to address that use of CCTVs resulted in a hardware change to the

facility, especially regarding placing non-safety related cables over and in close

,

proximity to safety related cables, cable trays and conduit. These conditions were

not previously evaluated by the licensee per 10 CFR 50.59 (a) (1) as required to

ensure that the necessary cable runs for the CCTVs did not result in an unreviewed

!

. safety question. This matter was considered another example of a violation of 10

j

CFR 50.59. (VIO 50-354/96-07-01)

l

The inspectors concluded that the licensee's implementation of the design change

package to replace the Hope Creek fire protection computer was generally

-

acceptable; although interim compensatory measures were not properly evaluated to

,

ensure that no unreviewed safety question existed.

F4

Fire Protection Staff Knowledge and Performance

The inspectors observed two fire department drills to evaluate the effectiveness of

'

the previously described (section F2) fire alarm outage contingency plan. The drills

were appropriately developed and implemented. The inspectors concluded that the

compensatory measures were effective in providing appropriate fire panel indication

'

and alarm information to the control room for response to postulated fires in the

,

facility.

V. Manaaement Meetinas

X1

Exit Meeting Summary

A recent discovery of a licensee operating their facility in a manner contrary to the UFSAR

description highlighted the need for a special focused review that compares plant practices,

procedures and/or parameters to the UFSAR descriptions. While performing the

inspections discussed in this report, the inspectors reviewed the applicable portions of the

UFSAR that related to the areas inspected. The inspectors verified that the UFSAR

wording was consistent with the observed plant practices, procedures and/or parameters.

On October 1,1996, the inspectors presented the inspection results to members of

licensee management. Licensee management acknowledged the presented findings.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

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PARTIAL LIST OF PERSONS CONTACTED

PSE&G

M. Bezilla, Hope Creek General Manager

C. Banner, Emergency Preparedness

J. McMahon, Director, Nuclear Training Center

.,

J. Polyak, Manager, Radiological Safety

L. Storz, Sr. VP, Nuclear Operations

J. Benjamin, Manager, Quality Assurance

New Jersev Bureau of Nuclear Enaineerina

K. Tosch, Manager

Delaware Emeraency Manaaement Acency

P

E. Falone, Radiological Administrator

Department of Emeraency Services. Salem County, New Jersey

C. Wentzell, Deputy Coordinator

I

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INSPECTION PROCEDURES USED

IP 61726:

Surveillance Observations

-

IP 62707:

Maintenance Observations

IP 71707:

Plant Operations

j

IP 37551:

Onsite Engineering

IP 71750:

Plant Support

IP 82701:

Emergency Preparedness Program

,

1

IP 92901:

Plant Operations Followup

!

IP 92902:

Maintenance Followup

IP 92903:

Engineering Followup

l

IP 92904:

Plant Support Followup

IP 93702:

Event Response

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5

e'

9

4

d

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3

4

,

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I

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2

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l:..

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ITEMS OPENED, CLOSED, AND DISCUSSED

!

Opened

50-354/96-07-01

VIO

Two examples of licensee failure to evaluate changes to the

facility in accordance with 10 CFR 50.59, including temporary

installation of cables associated with fire protection

compensatory measures; and, blocking open a safety auxiliary

cooling system isolation valve.

l

l

50-354/96-07-02

VIO

Failure of the offsite safety review group to review safety

evaluations in accordance with technical specifications.

!

50-354/96-07-03

URI

Media Training not being conducted in accordance to the E-

Plan (UFSAR item); and, Training Center Laboratory

radiological equipment not maintained to meet the intentions

stated in the E-Plan.

Closed

50-354/96023

LER

Reactor Core Isolation Cooling system isolation due to a failed

,

steam leak detection monitor.

'

50-354/93-11-01

URI

This item involved apparent deficiencies in the licensee's

corrective action program.

!

50-354/94-09-04

VIO

Mis-operation of the refueling bridge.

50-354/94-003-01 SR

Operation of the facility in excess of the licensed thermal

!

power limits.

!

50-354/94-09-01

VIO

Containment integrated leak rate test (Type A) deficiencies.

l

50-354/96005

LER

Inadequate surveillance testing for the residual heat removal

system suppression pool and spray modes of operation.

50-354/96020

LER

Operations prohibited by technical specification - failure to

perform actions for inoperable radioactive gaseous effluent

monitoring instrumentation.

!

50-354/95-033

LER

Supplements 7,8,9 and 10: technical specification

surveillance requirement implementation deficiencies identified

,

l

by the TSSIP.

l

50-354/96-03-05

URI

Event on January 31,1996, when PSE&G declared four Hope

Creek radiation detectors inoperable.

50-354/95-10-01

VIO

Failure to update the Hope Creek Generating Station FSAR in

accordance with 10CFR50.71(e)(4).

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2

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50-354/94-13-02

VIO

RHR system suppression pool suction valve (BC-HV-F004A)

l

could not be controlled properly from the remote operating

switch in accordance with plant design.

50-354/93-28-01

IFl

Inspection followup of perimeter assessment aid upgrades.

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o

e

LIST OF ACRONYMS USED

AR

Action Request

BNE

Bureau of Nuclear Engineering (NJ)

BP

Business Process

CR

Condition Resolution

e

CR

Control Room

CM

Corrective Maintenance

EAL

Emergency Action Level

ED

Emergency Director

EOF

Emergency Operations Facility

E-PLAN

Emergency Plan

,

EPlP

Emergency Plan Implementing Procedures

i

EP

Emergency Preparedness

ERO

Emergency Response Organization

ECG

Event Classification Guide

CCTV

Closed Circuit Television

j

l&C

Instrument & Control

~

LOCA

Loss of Coolant Accident

LOP

Loss of Offsite Power

NUMARC

Nuclear Management and Resources Council

NTC

Nuclear Training Center

OSC

Operations Support Center

!

PIRS

Performance improvement Review System

Pi

Public Information

OA

Quality Assurance

i

RHR

Residual Heat Removal

RP

Radiation Protection

SACS

Safety Auxiliaries Cooling System

SNSS

Senior Nuclear Shift Supervisor

SRO

Senior Reactor Operator

STA

Shift Technical Advisor

SERT

Significant Event Review Team

TACS

Turbine Auxiliaries Cooling System

TS

Technical Specifications

TSC

Technical Support Center

TLD

Thermoluminescent Dosimeter

UFSAR

Updated Final Safety Analysis Report

r

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