ML20217H805

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Notice of Violation from Insp on 980222-0404.Violation Noted:Three Examples of Inadequate Accomplishment of Procedure Control Associated W/Temporary Equipment Installed in Plant Svc Water Intake Structure
ML20217H805
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 04/23/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20217H804 List:
References
50-354-98-02, 50-354-98-2, NUDOCS 9804300092
Download: ML20217H805 (2)


Text

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APPENDIX A NOTICE OF VIOLATION 1

Public Service Electric and Gas Company Docket No:

50-354 Hope Creek Generating Station License No: NPF-57 l

During an NRC inspection conducted on February 22,1998 to April 4,1998, violations of NRC requirements were identified. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," NUREG-1600, the violations are listed below:

10 CFR 50 Appendix B Criterion V requires in part that activities affecting quality shall be accomplished in accordance with established procedures. These procedures shallinclude appropriate quantitative or qualitative accomplishment criteria.

Contrary to the above, three examples of inadequate accomplishment of procedure controls associated with temporary equipment installed in the Hope Creek service water intake structure maintenance were identified as follows:

l (1)

On February 24,1998, maintenance technicians erected a scaffold work platform around the "B" service water pump strainer, and on March 31, 1998, maintenance technicians erected a scaffold work platform around the "D" service water pump strainer without performing the administrative controls and inspections required by maintenance procedure SH.MD-AP.ZZ-0023 (Q), Revision 0, " Scaffolding Erection, Mod;fication and Dismantling Guidelines."

(2)

On February 24,1998, several plugs were installed in the floor drains for both the " A" & "C" service water bay and the "B" & "D" service water bay without the administrative controls requ. red by PSE&G Nuclear Administrative Procedure NC.NA-AP.ZZ-0013 (Q), Revision 5, " Control of Temporary Modifications."

l (3)

On February 14,1998, equipment operators used a troubleshooting plan and j

installed a temporary discharge hose on the "A" & "C" service water bay j

sump pump system without completing a 10 CFR 50.59 safety evaluation.

l Hope Creek troubleshooting procedure, HC.OP-GP.ZZ-0008 (Q), Revision 1,

" Operations Troubleshooting," requires that a troubleshooting plan not be approved if a 10 CFR 50.59 safety evaluation is required. PSE&G engineers I

later determined that a 10 CFR 50.59 safety evaluation was required.

l This is a Severity Level IV violation (Supplement I).

j I

Pursuant to the provisions of 10 CFR 2.201, Public Service Electric and Gas Company is j

hereby required to submit a written statement or explanation to the U.S. Nuclear i

l 9804300092 980423 l

PDR ADOCK 05000354 j

G PDR j

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2 Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555 with a copy to the Regional Administrator, Region I, and a copy to the NRC Resident inspector at the facility that is the subject of this Notice, within 30 days of the date of the letter transmitting this Notice of Violation (Notice). This reply should be clearly marked as a

" Reply to a Notice of Violation" and should include for each violation: (1) the reason for l-the violation, or, if contested, the basis for disputing the violation or severity level, (2) the corrective' steps that have been taken and the results achieved, (3) the corrective steps that will be taken to avoid further violations, and (4) the date when full compliance will be achieved. Your response may reference or include previous docketed correspondence, if the correspondence adequately addresses the required response. If an adequate reply is not received within the time specified in this Notice, an order or a Demand for Information may be issued as to why the license should not be modified, suspended, or revoked, or why such other action as may be proper should not be taken. Where good cause is shown, consideration will be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response to the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001.

Because your response will be placed in the NRC Public Document Room (PDR), to the extent possible, it should not include any personal privacy, proprietary, or safeguards information so that it can be placed in the PDR without redaction. If personal privacy or i

proprietary information is necessary to provide an acceptable response, then please provide a bracketed copy of your response that identifies the information that should be protected i

and a redacted copy of your response that deletes such information. If you request withholding of such material, you mual specifically identify the portions of your response that you seek to have withheld and provide in detail the bases for your claim of withhold-4 ing (e.g., explain why the disclosure of information will create an unwarranted invasion of personal privacy or provide the information required by 10 CFR 2.790(b) to' support a request for withholding confidential commercial or financial information), if safeguards information is necessary to provide an acceptable response, please provide the level of j

protection described in 10 CFR 73.21.

Dated at King of Prussia, Pennsylvania this 23rd day of April,1998 l

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