|
---|
Category:INSPECTION REPORT
MONTHYEARIR 05000354/19990051999-10-0101 October 1999 Insp Rept 50-354/99-05 on 990711-0829.Four Violations of NRC Requirements Occurred & Being Treated as Ncvs.Major Areas Inspected:Mitigating Sys,Barrier Integrity & Performance Indicator Verification IR 05000354/19990041999-08-11011 August 1999 Insp Rept 50-354/99-04 on 990530-0711.No Violations Noted. Major Areas inspected:cornerstone-mitigating Sys,Pi Verification IR 05000354/19990031999-06-21021 June 1999 Insp Rept 50-354/99-03 on 990419-0529.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000354/19990021999-05-14014 May 1999 Insp Rept 50-354/99-02 on 990308-0418.Non-cited Violation Identified.Major Areas Inspected:Operations,Maint & Plant Support IR 05000354/19990011999-04-19019 April 1999 Insp Rept 50-354/99-01 on 990124-0307.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000354/19980111998-12-22022 December 1998 Insp Rept 50-354/98-11 on 981101-1212.No Violations Noted. Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support IR 05000354/19980101998-11-23023 November 1998 Insp Rept 50-354/98-10 on 980920-1031.Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000354/19980081998-10-0909 October 1998 Insp Rept 50-354/98-08 on 980809-1019.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000354/19980091998-10-0202 October 1998 Insp Rept 50-354/98-09 on 980817-26 & 0908.No Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000354/19980071998-08-25025 August 1998 Insp Rept 50-354/98-07 on 980628-0808.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000272/19982021998-07-0909 July 1998 Partially Deleted Insp Repts 50-272/98-202,50-311/98-202 & 50-354/98-202 on 980420-23.No Violations Noted.Major Areas Inspected:Conduct of Security & Safeguards Activities IR 05000354/19980801998-06-10010 June 1998 Insp Rept 50-354/98-80 on 980223-0319 & 0427-30.Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000354/19980011998-03-16016 March 1998 Insp Rept 50-354/98-01 on 980104-0221.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000354/19970101998-02-0303 February 1998 Insp Rept 50-354/97-10 on 971116-980103.Violations Noted. Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000354/19970091997-12-10010 December 1997 Insp Rept 50-354/97-09 on 971005-1115.Apparent Violation Being Considered for Escalated Ea.Major Areas Inspected: Licensee Operations,Engineering,Maint,Plant Support & Site Security Programs ML20199D3431997-11-13013 November 1997 Insp Rept 50-354/97-07 on 970824-1004.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000354/19970071997-11-13013 November 1997 Insp Rept 50-354/97-07 on 970824-1004.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000354/19970051997-09-15015 September 1997 Insp Rept 50-354/97-05 on 970713-0823.Noncited Violations Identified.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000354/19970061997-09-0404 September 1997 Insp Rept 50-354/97-06 on 961112-970529.Violations Noted. Major Areas Inspected:Engineering IR 05000354/19970041997-08-11011 August 1997 Insp Rept 50-354/97-04 on 970601-0712.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000354/19970031997-06-12012 June 1997 Insp Rept 50-354/97-03 on 970429-0531.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000354/19970021997-05-23023 May 1997 Insp Rept 50-354/97-02 on 970318-0428.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support.Routine Insp of Physical Protection & Security Program Also Conducted ML20148D2301997-05-23023 May 1997 Insp Rept 50-354/97-02 on 970318-0428.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support.Routine Insp of Physical Protection & Security Program Also Conducted ML20137W7811997-04-14014 April 1997 Insp Rept 50-354/97-01 on 970202-0317.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint, & Plant Support ML20135A3901997-02-21021 February 1997 Insp Rept 50-354/96-11 on 961222-970201.Violation Noted. Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000354/19960101997-01-27027 January 1997 Insp Rept 50-354/96-10 on 961110-1221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering,Plant Support & Security Program Plan IR 05000354/19960091996-12-0505 December 1996 Insp Rept 50-354/96-09 on 960922-1109.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support ML20129D0891996-10-18018 October 1996 Insp Rept 50-354/96-07 on 960804-0921.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000354/19950151996-02-14014 February 1996 Insp Rept 50-354/95-15 on 950905-1109.No Violations Noted. Major Areas inspected:safety-related Reactor Vessel Water Level Mod,Corrective Actons for Digital Feedwater Control Sys & RCIC Jockey Pump Corrective Action Process ML20084L7691995-05-30030 May 1995 Insp Rept 50-354/95-05 on 950406-21.No Violations Noted. Major Areas Inspected:Licensee Actions & Evaluations Associated W/Unplanned Release of Radioactive Matl from Hope Creek South Plant Vent That Occurred on 950405 IR 05000272/19940341994-12-23023 December 1994 Insp Repts 50-272/94-34,50-311/94-34 & 50-354/94-28 on 941212-15.No Violations Noted.Major Areas Inspected:Security Plan & Implementing Procedures,Previously Identified Item, fitness-for-duty & Contingency Plan Implementation IR 05000272/19940161994-06-30030 June 1994 Insp Repts 50-272/94-16,50-311/94-16 & 50-354/94-16 on 940613-17.Violations Noted.Major Areas Inspected:Protected Physical Barriers,Detection & Assessment Aids,Protected & Vital Area Access Control of Personnel,Packages & Vehicles IR 05000354/19930231993-12-15015 December 1993 Insp Rept 50-354/93-23 on 931004-1103.No Violations Noted. Major Areas Inspected:Review Licensee Corrective Actions of Previously Identified Edsfi Findings IR 05000354/19930191993-07-27027 July 1993 Insp Rept 50-354/93-19 on 930615-17.No Violations Noted. Major Areas Inspected:Organization,Staffing,Audits & Assessments,Alara Controls & Performance IR 05000272/19930181993-06-30030 June 1993 Physical Security Program Insp Repts 50-272/93-18, 50-311/93-18 & 50-354/93-17 on 930607-11.No Safety Concerns or Violations Noted.Major Areas Inspected:Security Program Plans & Protected & Vital Area Physical Barriers IR 05000354/19930121993-05-24024 May 1993 Insp Rept 50-354/93-12 on 930510-14.No Violations Noted. Major Areas Inspected:Licensee Radioactive Liquid & Gaseous Effluent Control Programs,Including Mgt Controls for Programs & Ability to Calculate Projected Doses IR 05000272/19930021993-03-25025 March 1993 Insp Repts 50-272/93-02,50-311/93-02 & 50-354/93-02 on Stated Date.No Violations Noted.Major Areas Inspected: Operations,Radiological Controls,Maint & Surveillance Testing,Emergency Preparedness & Security IR 05000354/19920191992-12-15015 December 1992 Insp Rept 50-354/92-19 on 921104-10.No Violations Noted. Major Areas Inspected:Licensees C/A for Mechanical Snubbers That Failed Functional Test & to Verify That Failed Snubbers Have Been Replaced or Restored to as-designed Condition ML20086H3621991-11-26026 November 1991 Physical Security Insp Repts 50-272/91-29,50-311/91-29 & 50-354/91-22 on 911104-08.No Violations Noted.Major Areas Inspected:Previously Identified Items,Followup Actions in Response to 910410-14 Regulatory Review & Security Programs IR 05000354/19910131991-06-21021 June 1991 Insp Rept 50-354/91-13 on 910520-24.No Violations Noted. Major Areas Inspected:Review of Several Open Items Remaining from Maint Team Insp 50-354/89-80 & Surveillance Test & Implementation IR 05000272/19910101991-04-26026 April 1991 Partially Withheld Insp Repts 50-272/91-10,50-311/91-10 & 50-354/91-07 on 910401-05.No Violations Noted.Major Areas Inspected:Mgt Support,Security Programs Plans & Audits & Protected Area Access Control of Personnel IR 05000272/19900231990-11-0707 November 1990 Insp Repts 50-272/90-23,50-311/90-23 & 50-354/90-19 on 900925-28.No Violations Noted.Major Areas Inspected:Licensee Action on Previously Identified Items IR 05000354/19900131990-07-26026 July 1990 Insp Rept 50-354/90-13 on 900618-22.No Violations Noted. Major Areas Inspected:Svc Water Intake Structure & Licensee Actions on Previous Insp Findings Re Svc Water Pipe Leak Examined IR 05000354/19900151990-07-19019 July 1990 Insp Rept 50-354/90-15 on 900625-29.No Violations Noted. Major Areas Inspected:Organization & Staffing,Training & Qualifications of Personnel,Procedures,Audits & Assessments, External & Internal Exposure Controls IR 05000354/19900091990-04-30030 April 1990 Insp Rept 50-354/90-09 on 900416-20.No Violations or Deviations Noted.Major Areas Inspected:Transportation & Solid Radwaste Programs,Including Mgt Controls,Qa & Implementation of Programs IR 05000354/19900051990-04-0505 April 1990 Insp Rept 50-354/90-05 on 900305-09.No Violations Noted. Major Areas Inspected:Radiological & Nonradiological Chemistry Programs,Including Confirmatory Measurements Radiological,Stds Analyses Chemistry & Lab Qa/Qc IR 05000354/19900021990-03-21021 March 1990 Insp Rept 50-354/90-02 on 900226-0302.No Violations Noted. Major Areas Inspected:Licensee Radioactive Liquid & Gaseous Effluent Control Programs,Including Mgt Controls, Implementation of ODCM & Calibr of Effluent Monitors IR 05000272/19900061990-03-15015 March 1990 Insp Repts 50-272/90-06,50-311/90-06 & 50-354/90-04 on 900226-0302.No Violations Noted.Major Areas Inspected: Radiological Environ Monitoring & Meteorological Monitoring Programs,Including Mgt Controls for Programs ML20246C4001989-08-15015 August 1989 Partially Deleted Insp Repts 50-272/89-19,50-311/89-17 & 50-354/89-15 on 890710-14 (Ref 10CFR73.21).Major Areas Inspected:Followup on Actions Taken in Response to Regulatory Effectiveness Review on 890410-14 IR 05000354/19890131989-07-20020 July 1989 Insp Rept 50-354/89-13 on 890626-30.No Violations Noted. Major Areas Inspected:Licensee Compliance to 10CFR50.62 ATWS Rule Pertaining to Alternate Rod Injection Sys 1999-08-11
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000354/19990051999-10-0101 October 1999 Insp Rept 50-354/99-05 on 990711-0829.Four Violations of NRC Requirements Occurred & Being Treated as Ncvs.Major Areas Inspected:Mitigating Sys,Barrier Integrity & Performance Indicator Verification IR 05000354/19990041999-08-11011 August 1999 Insp Rept 50-354/99-04 on 990530-0711.No Violations Noted. Major Areas inspected:cornerstone-mitigating Sys,Pi Verification IR 05000354/19990031999-06-21021 June 1999 Insp Rept 50-354/99-03 on 990419-0529.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000354/19990021999-05-14014 May 1999 Insp Rept 50-354/99-02 on 990308-0418.Non-cited Violation Identified.Major Areas Inspected:Operations,Maint & Plant Support IR 05000354/19990011999-04-19019 April 1999 Insp Rept 50-354/99-01 on 990124-0307.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000354/19980111998-12-22022 December 1998 Insp Rept 50-354/98-11 on 981101-1212.No Violations Noted. Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support IR 05000354/19980101998-11-23023 November 1998 Insp Rept 50-354/98-10 on 980920-1031.Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000354/19980081998-10-0909 October 1998 Insp Rept 50-354/98-08 on 980809-1019.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000354/19980091998-10-0202 October 1998 Insp Rept 50-354/98-09 on 980817-26 & 0908.No Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000354/19980071998-08-25025 August 1998 Insp Rept 50-354/98-07 on 980628-0808.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000272/19982021998-07-0909 July 1998 Partially Deleted Insp Repts 50-272/98-202,50-311/98-202 & 50-354/98-202 on 980420-23.No Violations Noted.Major Areas Inspected:Conduct of Security & Safeguards Activities IR 05000354/19980801998-06-10010 June 1998 Insp Rept 50-354/98-80 on 980223-0319 & 0427-30.Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000354/19980011998-03-16016 March 1998 Insp Rept 50-354/98-01 on 980104-0221.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000354/19970101998-02-0303 February 1998 Insp Rept 50-354/97-10 on 971116-980103.Violations Noted. Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000354/19970091997-12-10010 December 1997 Insp Rept 50-354/97-09 on 971005-1115.Apparent Violation Being Considered for Escalated Ea.Major Areas Inspected: Licensee Operations,Engineering,Maint,Plant Support & Site Security Programs ML20199D3431997-11-13013 November 1997 Insp Rept 50-354/97-07 on 970824-1004.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000354/19970071997-11-13013 November 1997 Insp Rept 50-354/97-07 on 970824-1004.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000354/19970051997-09-15015 September 1997 Insp Rept 50-354/97-05 on 970713-0823.Noncited Violations Identified.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000354/19970061997-09-0404 September 1997 Insp Rept 50-354/97-06 on 961112-970529.Violations Noted. Major Areas Inspected:Engineering IR 05000354/19970041997-08-11011 August 1997 Insp Rept 50-354/97-04 on 970601-0712.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000354/19970031997-06-12012 June 1997 Insp Rept 50-354/97-03 on 970429-0531.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000354/19970021997-05-23023 May 1997 Insp Rept 50-354/97-02 on 970318-0428.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support.Routine Insp of Physical Protection & Security Program Also Conducted ML20148D2301997-05-23023 May 1997 Insp Rept 50-354/97-02 on 970318-0428.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support.Routine Insp of Physical Protection & Security Program Also Conducted ML20137W7811997-04-14014 April 1997 Insp Rept 50-354/97-01 on 970202-0317.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint, & Plant Support ML20135A3901997-02-21021 February 1997 Insp Rept 50-354/96-11 on 961222-970201.Violation Noted. Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000354/19960101997-01-27027 January 1997 Insp Rept 50-354/96-10 on 961110-1221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering,Plant Support & Security Program Plan IR 05000354/19960091996-12-0505 December 1996 Insp Rept 50-354/96-09 on 960922-1109.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support ML20129D0891996-10-18018 October 1996 Insp Rept 50-354/96-07 on 960804-0921.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000354/19950151996-02-14014 February 1996 Insp Rept 50-354/95-15 on 950905-1109.No Violations Noted. Major Areas inspected:safety-related Reactor Vessel Water Level Mod,Corrective Actons for Digital Feedwater Control Sys & RCIC Jockey Pump Corrective Action Process ML20084L7691995-05-30030 May 1995 Insp Rept 50-354/95-05 on 950406-21.No Violations Noted. Major Areas Inspected:Licensee Actions & Evaluations Associated W/Unplanned Release of Radioactive Matl from Hope Creek South Plant Vent That Occurred on 950405 IR 05000272/19940341994-12-23023 December 1994 Insp Repts 50-272/94-34,50-311/94-34 & 50-354/94-28 on 941212-15.No Violations Noted.Major Areas Inspected:Security Plan & Implementing Procedures,Previously Identified Item, fitness-for-duty & Contingency Plan Implementation IR 05000272/19940161994-06-30030 June 1994 Insp Repts 50-272/94-16,50-311/94-16 & 50-354/94-16 on 940613-17.Violations Noted.Major Areas Inspected:Protected Physical Barriers,Detection & Assessment Aids,Protected & Vital Area Access Control of Personnel,Packages & Vehicles IR 05000354/19930231993-12-15015 December 1993 Insp Rept 50-354/93-23 on 931004-1103.No Violations Noted. Major Areas Inspected:Review Licensee Corrective Actions of Previously Identified Edsfi Findings IR 05000354/19930191993-07-27027 July 1993 Insp Rept 50-354/93-19 on 930615-17.No Violations Noted. Major Areas Inspected:Organization,Staffing,Audits & Assessments,Alara Controls & Performance IR 05000272/19930181993-06-30030 June 1993 Physical Security Program Insp Repts 50-272/93-18, 50-311/93-18 & 50-354/93-17 on 930607-11.No Safety Concerns or Violations Noted.Major Areas Inspected:Security Program Plans & Protected & Vital Area Physical Barriers IR 05000354/19930121993-05-24024 May 1993 Insp Rept 50-354/93-12 on 930510-14.No Violations Noted. Major Areas Inspected:Licensee Radioactive Liquid & Gaseous Effluent Control Programs,Including Mgt Controls for Programs & Ability to Calculate Projected Doses IR 05000272/19930021993-03-25025 March 1993 Insp Repts 50-272/93-02,50-311/93-02 & 50-354/93-02 on Stated Date.No Violations Noted.Major Areas Inspected: Operations,Radiological Controls,Maint & Surveillance Testing,Emergency Preparedness & Security IR 05000354/19920191992-12-15015 December 1992 Insp Rept 50-354/92-19 on 921104-10.No Violations Noted. Major Areas Inspected:Licensees C/A for Mechanical Snubbers That Failed Functional Test & to Verify That Failed Snubbers Have Been Replaced or Restored to as-designed Condition ML20086H3621991-11-26026 November 1991 Physical Security Insp Repts 50-272/91-29,50-311/91-29 & 50-354/91-22 on 911104-08.No Violations Noted.Major Areas Inspected:Previously Identified Items,Followup Actions in Response to 910410-14 Regulatory Review & Security Programs IR 05000354/19910131991-06-21021 June 1991 Insp Rept 50-354/91-13 on 910520-24.No Violations Noted. Major Areas Inspected:Review of Several Open Items Remaining from Maint Team Insp 50-354/89-80 & Surveillance Test & Implementation IR 05000272/19910101991-04-26026 April 1991 Partially Withheld Insp Repts 50-272/91-10,50-311/91-10 & 50-354/91-07 on 910401-05.No Violations Noted.Major Areas Inspected:Mgt Support,Security Programs Plans & Audits & Protected Area Access Control of Personnel IR 05000272/19900231990-11-0707 November 1990 Insp Repts 50-272/90-23,50-311/90-23 & 50-354/90-19 on 900925-28.No Violations Noted.Major Areas Inspected:Licensee Action on Previously Identified Items IR 05000354/19900131990-07-26026 July 1990 Insp Rept 50-354/90-13 on 900618-22.No Violations Noted. Major Areas Inspected:Svc Water Intake Structure & Licensee Actions on Previous Insp Findings Re Svc Water Pipe Leak Examined IR 05000354/19900151990-07-19019 July 1990 Insp Rept 50-354/90-15 on 900625-29.No Violations Noted. Major Areas Inspected:Organization & Staffing,Training & Qualifications of Personnel,Procedures,Audits & Assessments, External & Internal Exposure Controls IR 05000354/19900091990-04-30030 April 1990 Insp Rept 50-354/90-09 on 900416-20.No Violations or Deviations Noted.Major Areas Inspected:Transportation & Solid Radwaste Programs,Including Mgt Controls,Qa & Implementation of Programs IR 05000354/19900051990-04-0505 April 1990 Insp Rept 50-354/90-05 on 900305-09.No Violations Noted. Major Areas Inspected:Radiological & Nonradiological Chemistry Programs,Including Confirmatory Measurements Radiological,Stds Analyses Chemistry & Lab Qa/Qc IR 05000354/19900021990-03-21021 March 1990 Insp Rept 50-354/90-02 on 900226-0302.No Violations Noted. Major Areas Inspected:Licensee Radioactive Liquid & Gaseous Effluent Control Programs,Including Mgt Controls, Implementation of ODCM & Calibr of Effluent Monitors IR 05000272/19900061990-03-15015 March 1990 Insp Repts 50-272/90-06,50-311/90-06 & 50-354/90-04 on 900226-0302.No Violations Noted.Major Areas Inspected: Radiological Environ Monitoring & Meteorological Monitoring Programs,Including Mgt Controls for Programs ML20246C4001989-08-15015 August 1989 Partially Deleted Insp Repts 50-272/89-19,50-311/89-17 & 50-354/89-15 on 890710-14 (Ref 10CFR73.21).Major Areas Inspected:Followup on Actions Taken in Response to Regulatory Effectiveness Review on 890410-14 IR 05000354/19890131989-07-20020 July 1989 Insp Rept 50-354/89-13 on 890626-30.No Violations Noted. Major Areas Inspected:Licensee Compliance to 10CFR50.62 ATWS Rule Pertaining to Alternate Rod Injection Sys 1999-08-11
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000354/19990051999-10-0101 October 1999 Insp Rept 50-354/99-05 on 990711-0829.Four Violations of NRC Requirements Occurred & Being Treated as Ncvs.Major Areas Inspected:Mitigating Sys,Barrier Integrity & Performance Indicator Verification PNO-I-99-043, on 990916,Hurricane Floyd Was Approaching Ccnpp,Sgs,Hcgs & Ocnpp.Hurricane Was Centered at Latitude 36.0 North & Longitude 76.6 West & Moving north-northeast at Approx 25 Mph.Plants Remain at Power1999-09-16016 September 1999 PNO-I-99-043:on 990916,Hurricane Floyd Was Approaching Ccnpp,Sgs,Hcgs & Ocnpp.Hurricane Was Centered at Latitude 36.0 North & Longitude 76.6 West & Moving north-northeast at Approx 25 Mph.Plants Remain at Power IR 05000354/19990041999-08-11011 August 1999 Insp Rept 50-354/99-04 on 990530-0711.No Violations Noted. Major Areas inspected:cornerstone-mitigating Sys,Pi Verification IR 05000354/19990031999-06-21021 June 1999 Insp Rept 50-354/99-03 on 990419-0529.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000354/19990021999-05-14014 May 1999 Insp Rept 50-354/99-02 on 990308-0418.Non-cited Violation Identified.Major Areas Inspected:Operations,Maint & Plant Support IR 05000354/19990011999-04-19019 April 1999 Insp Rept 50-354/99-01 on 990124-0307.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint & Plant Support IR 05000354/19980111998-12-22022 December 1998 Insp Rept 50-354/98-11 on 981101-1212.No Violations Noted. Major Areas Inspected:Aspects of Licensee Operations, Engineering,Maint & Plant Support IR 05000354/19980101998-11-23023 November 1998 Insp Rept 50-354/98-10 on 980920-1031.Violations Noted. Major Areas Inspected:Operations,Maint & Engineering ML20196D0911998-11-23023 November 1998 Notice of Violation from Insp on 980920-1031.Violation Noted:On 981001,electricians Placed Single Degraded Cell Associated with Operable 1E Battery Bank on Single Cell Charge PNO-I-98-053, on 981115,plant Experienced Turbine Trip While Operating at 95% Power Due to High Level Condition on One of Two Moisture Separators.Reactor Automatically Shut Down.Util Evaluating Incorrect Sys Drawing.States of Nj & DE Notifie1998-11-16016 November 1998 PNO-I-98-053:on 981115,plant Experienced Turbine Trip While Operating at 95% Power Due to High Level Condition on One of Two Moisture Separators.Reactor Automatically Shut Down.Util Evaluating Incorrect Sys Drawing.States of Nj & DE Notifie ML20154Q7381998-10-16016 October 1998 Second Suppl to NRC Exam Rept 50-354/98-03OL for Tests Administered on 980304-12,0519-21,22-28 & 0629.Five of Five Reactor Operator Applicants & Four of Five Senior Reactor Applicants Passed Exams IR 05000354/19980031998-10-16016 October 1998 Second Suppl to NRC Exam Rept 50-354/98-03OL for Tests Administered on 980304-12,0519-21,22-28 & 0629.Five of Five Reactor Operator Applicants & Four of Five Senior Reactor Applicants Passed Exams IR 05000354/19980081998-10-0909 October 1998 Insp Rept 50-354/98-08 on 980809-1019.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20154J8611998-10-0909 October 1998 Notice of Violation from Insp on 980809-0919.Violation Noted:On 980831,licensee Did Not Promptly Correct Condition Adverse to Quality in That C Residual Heat Removal Pump Rendered Inoperable IR 05000354/19980091998-10-0202 October 1998 Insp Rept 50-354/98-09 on 980817-26 & 0908.No Violations Noted.Major Areas Inspected:Maint & Engineering IR 05000354/19983011998-09-0404 September 1998 Exam Rept 50-354/98-301OL Conducted on 980810-12.Exam Results:Four SRO Candidates Performed Well on Both Written & Operating Portions of Exam.All Four Were Issued Licenses IR 05000354/19980071998-08-25025 August 1998 Insp Rept 50-354/98-07 on 980628-0808.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20237E4981998-08-25025 August 1998 Notice of Violation from Insp on 980628-0808.Violation Noted:As of 980810,util Had Not Corrected Known Deficiency in Verifying MSIV Full Closed During Springs Only Full Stroke Closing Tests ML20236T1601998-07-21021 July 1998 Notice of Violation from Insp on 980517-0627.Violation Noted:As of Oct 1997,chemistry Technicians Did Not Sample & Analyze Diesel Fuel Oil Deliveries for Particulates & Did Not Report Results by Written Notification within 14 Days IR 05000272/19982021998-07-0909 July 1998 Partially Deleted Insp Repts 50-272/98-202,50-311/98-202 & 50-354/98-202 on 980420-23.No Violations Noted.Major Areas Inspected:Conduct of Security & Safeguards Activities IR 05000354/19980801998-06-10010 June 1998 Insp Rept 50-354/98-80 on 980223-0319 & 0427-30.Violations Noted.Major Areas Inspected:Maint & Engineering ML20249A2031998-06-10010 June 1998 Notice of Violation from Insp on 980223-0319 & 0427-30. Violation Noted:Conditions Adverse to Quality Were Not Promptly Identified & Corrected IR 05000354/19980991998-06-0808 June 1998 SALP Rept 50-354/98-99 for Period of 961110-980516 ML20249A1071998-06-0404 June 1998 Notice of Violation from Insp on 980405-0516.Violation Noted:During Refueling Outage RF03 in Dec 1990 Licensee Did Not Maintain RHR Sys in Operation ML20217N6221998-04-24024 April 1998 Notice of Violation from Investigation Conducted by Oi. Violation Noted:Safeguard Event Log,Required to Be Maintained by Licensee,Was Not Complete & Accurate in All Matl Aspects ML20217H8051998-04-23023 April 1998 Notice of Violation from Insp on 980222-0404.Violation Noted:Three Examples of Inadequate Accomplishment of Procedure Control Associated W/Temporary Equipment Installed in Plant Svc Water Intake Structure ML20217C6711998-03-20020 March 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:On 971112,while Reactor Was in Cold Shutdown W/Rv Head Removed,Operators Did Not Verify That CR Position Did Not Change During Withdrawal ML20217D8291998-03-17017 March 1998 EN-98-013:informs That NOV & Proposed Imposition of Civil Penalty in Amount of $55,000 Will Be Issued on or About 980330 to Pse&G.Civil Penalty Based on Violation Involving Failure by Operating Crew to Follow Procedures IR 05000354/19980011998-03-16016 March 1998 Insp Rept 50-354/98-01 on 980104-0221.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000354/19970101998-02-0303 February 1998 Insp Rept 50-354/97-10 on 971116-980103.Violations Noted. Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support ML20199L4791998-02-0303 February 1998 Notice of Violation from Insp on 971126-980103.Violation Noted:On 971124,maint Technicians Failed to Follow HC.IC-DC.ZZ-0140(Q),Rev 3, Device/Equipment Calibration Masonleilan Pressure & Temperature Controllers IR 05000354/19970091997-12-10010 December 1997 Insp Rept 50-354/97-09 on 971005-1115.Apparent Violation Being Considered for Escalated Ea.Major Areas Inspected: Licensee Operations,Engineering,Maint,Plant Support & Site Security Programs ML20199D3431997-11-13013 November 1997 Insp Rept 50-354/97-07 on 970824-1004.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support IR 05000354/19970071997-11-13013 November 1997 Insp Rept 50-354/97-07 on 970824-1004.Violations Noted. Major Areas Inspected:Operations,Engineering,Maintenance & Plant Support ML20199D3171997-11-12012 November 1997 Notice of Violation from Insp on 970824-1004.Violation Noted:On 970914,electric motor-driven Fire Pump Supply Breaker Opened During Electrical Bus Swap Which Rendered Pump Inoperable ML20196J6531997-10-20020 October 1997 Notice of Violation from Insp on 970202 & 0317.Violation Noted:In Apr 1994,licensee Made Changes to Facility That Involved USQ Without Prior Commission Approval IR 05000354/19970081997-10-15015 October 1997 NRC Operator Licensing Exam Rept 50-354/97-08OL for Tests Administered on 970929-1002.Exam Results:Four Candidates Passed All Portions of License Exam.One Candidate Failed Written Exam ML20198L9531997-10-15015 October 1997 NRC Operator Licensing Exam Rept 50-354/97-08OL for Tests Administered on 970929-1002.Exam Results:Four Candidates Passed All Portions of License Exam.One Candidate Failed Written Exam IR 05000354/19970051997-09-15015 September 1997 Insp Rept 50-354/97-05 on 970713-0823.Noncited Violations Identified.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000354/19970061997-09-0404 September 1997 Insp Rept 50-354/97-06 on 961112-970529.Violations Noted. Major Areas Inspected:Engineering IR 05000354/19970041997-08-11011 August 1997 Insp Rept 50-354/97-04 on 970601-0712.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support ML20210N9061997-08-11011 August 1997 Notice of Violation from Insp on 970601-0712.Violation Noted:Inoperable HPCI Sys Injection Valve Was Not Promptly Identified ML20217E7851997-07-25025 July 1997 Investigation Rept 1-96-024 on 970725.No Noncompliance Noted.Major Areas Investigated:Allegations Re Failure to Make 10CFR73.71 Notification by Station Security Dept ML20140J3811997-06-12012 June 1997 Notice of Violation from Insp on 970429-0531.Violation Noted:Failing to Adhere to Established Procedural Guidance for safety-related Activities Were Identified,Significant Condition Adverse to Quality IR 05000354/19970031997-06-12012 June 1997 Insp Rept 50-354/97-03 on 970429-0531.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support ML20148D2011997-05-23023 May 1997 Notice of Violation from Insp on 970318-0428.Violation Noted:On 970423,operators Failed to Shut Six of Twelve Cylinder Indicator Test Cocks Following Completion of C Emergency Diesel Generator pre-start Checks ML20148D2301997-05-23023 May 1997 Insp Rept 50-354/97-02 on 970318-0428.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support.Routine Insp of Physical Protection & Security Program Also Conducted IR 05000354/19970021997-05-23023 May 1997 Insp Rept 50-354/97-02 on 970318-0428.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support.Routine Insp of Physical Protection & Security Program Also Conducted ML20137W7701997-04-14014 April 1997 Notice of Violation,App a for Insp on 970202-0317.Violation Noted:On 970226,scaffolds Installed in safety-related Areas, Including a & B RHR Pump Rooms & Standby Liquid Control Pump Room in Rb,Lacked Appropriate Construction Documentation ML20137W7811997-04-14014 April 1997 Insp Rept 50-354/97-01 on 970202-0317.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint, & Plant Support 1999-09-16
[Table view] |
Text
.. _. _
.. _.
_
_
.-
.
.
_
_
_
.
-
. _ _
,
i
~
n U. S. NUCLEAR REGULATORY COMMISSION i
REGION I
,
REPORT / DOCKET NOS. 50-354/93-23 LICENSE NO.
NPF-57
.
LICENSEE:
Public Service Electric and Gas Company
,
P. O. Box 236 11ancocks Bridge, New Jersey
..
FACILITY NAME:
Ilope Creek Nuclear Generating Station.
INSPECTION AT:
Hancocks Bridge, New Jersey INSPECTION DATES:
October 4-7,1993 and November 1-3, 1993
[
!
,
INSPECTORS:
Scott Morris, Reactor Engineer, DRP Douglas Weaver, Reactor Engineer, DRP
s, M, b--l to ( %
Ram Bhatia, Reactor Engineer Date
'
Electrical Section, EB, DRS
APPROVED BY:
l/
m
/
/
[%
William II. Ruiand, Chief Date Electrical Section, EB, DRS i
i i
1 9401140046 931229 PDR ADOCK 05000354 G
PDR
-,
.
.
-,
-
. - -
_
.
,
.
-
_
_.
-
... -
,
l
.
l Areas Inspected: This was an announced inspection to review the licensee's corrective -
!
actions of previously identified electrical distribution system functional inspection (EDSFI)
findings.
-i Results: No violations or deviations were identified. Six open items reviewed were found to
[
be adequate and the items are closed. The inspector noted that your staff evaluation of the i
fast-transfer design scheme and the root cause analysis of the load tap changer problems were i
comprehensive and thorough.
I i
!
!
I t
!
t I
i
i l
f I
l i
t i
!'
!
f
.
.
i
>
i
-!
!
,
"
)
,
?
i.
. _ - -
,
_,_,m.
.
.
-.
.
,_
-.
.-
-
-
-
-
..
.
.
DETAILS
,
1.0 PURPOSE
,
The purpose of this inspection was to review and verify the licensee's corrective actions for previously identified NRC findings during the 1992 Electrical Distribution System Functional Inspection (EDSFI) for Hope Creek Generating Station.
2.0 FOLLOWUP OF PREVIOUSLY IDENTIFIED FINDINGS 2.1 (Closed) Unresolved Item 50-354/92-80-02 pertaining to the study to review plant fast transfer scheme logic design verification
During the followup EDSFI inspection in October 1992, the inspectors noted that the hcensee
!
had completed the design review of the transfer scheme design operational concern and determined that the recovery voltages for the 4.16 kV and 480 Volt motors would remam
<
above the 90% perbrmance values under LOCA conditions for all safety load sequence i
steps. In addition, the licensee determined that under a degraded voltage condition, the
'
4.16 kV bus voltages would not approach the degraded relay pick up setpoint of 92% Also, to prevent an operational flip / flop concern, the licensee had implemented an administrative control and revised the applicable procedures for blocking this condition by utilizing the existing designed push buttons to keep them in the depressed mode (energized position). The
'
inspectors had no concerns with this portion of the issue at that time; however, this item was left open because of an event, which occurred on May 13,1993, where a transient fault on the 13.8 kV ring bus feeder resulted in transfer to an alternate source and eventually to the emergency diesel generators (EDGs) because of a low voltage condition suspected during the
'
bus transfer condition.
During this inspection, the intpector reviewed the licensee's May 13, 1993, event analysis, computer simulation analysis, and additional study completed by the licensee's contractors to
confirm the voltage conditions experienced during this event and the existing design adequacy. This study focused on evaluatin;; the adequacy of the existing fast transfer design of the Hope Creek under transient condition.
The inspectors noted that the licensee had concluded that the Hope Creek electrical power distribution system performed as designed during the transient faulted condition on the 13.8 kV feeder of the ring bus. The licensee further concluded that sufficient controls remained in place for the operators to.nanually take control of the alternate source infeed breaker for l
!
closing had the onsite ac power failed to start and supply the emergency buses under the-accident conditions to mitigate the accident. Based on the inspectors review of the existing control scheme drawings and the licensee's evaluation of the event, the inspectors found no concerns. The inspectors review of the computer simulated analysis study (PSE&G Calculation No. E-15.10, PTl Report # R 52-93) revealed that to achieve a successful fast.
transfer of the 1E buses, the 13.8 kV source voltage should be above 0.92 pu and 4.16 kV Class IE bus voltages should be above 0.70 pu, respectively. In addition, these minimum voltages also had to exist simultaneously. The simulated analysis of the May 13,1993, event
1
.
_
_
E
<
.
.
determined that both the above system voltage levels were determined to be below the minimum acceptable values. The analysis concluded that the alternate power source voltas;e had dropped below the 0.92 pu, while the Class 4.16 kV IE bus voltages rose from 0.4 pu to 0.65-0.8 pu as the recovery began. Since the low voltage conditions on both affected safety buses were below the acceptable values, this event led to starting of the respective EDGs.
i The inspectors review of this analysis revealed no concerns. In addition, the review of the i
study completed by the contractor did not identify any major concern; however, it concluded that the present design could be further improved under transient faulted conditions.
Per discussion with the licensee, the inspector determined that the licensee was in the process of reviewing the recommendations of the contractor study. Upon completion of the above review, any additional improvements considered necessary by the licensee in 4.16 kV fast bus transfer system design would be done under routine design changes at a later date, based on the station priority system.
I Based on the review of the above completed evaluations to confirm that the present design
was adequate, as per the present design requirements, and no concerns were identified by the i
inspectors during this inspection review, and the additional design improvements could be
followed up during the NRC routine engineering inspections, the inspectors concluded that
this item is closed.
2.2 (Closed) Unresolved Item 50-354/92-80-07 regarding the inadequate documentation for the EDG crankcase exhaust piping mounting condition (
!
During the EDSFl inspection, the team noted that the licensee's Hope Creek seismic II/I evaluation program identified potential II/I interactions between the emergency diesel generator (EDG) engme and the crankcase exhaust (vacuum) system. Documentation submitted by the licensee at the time of the original inspection did not indicate that a proper seismic analysis of the exhaust piping had ever been done. The team was concerned that a
>
failure of the crankcase exhaust system piping could result in explosive gas accumulation in
.
I the diesel engine room and affect the performance of the EDGs operation.
,
To resolve the above concern, the licensee performed an evaluation of all applicable design documentation (HCGS UFSAR, Volume 14, Chapter 9, P&ID M-30-1, Drawing 1-P-KJ-09)
!
and determined that all the EDGs crankcase exhaust piping system was adequately supported j
as classified in their design drawings as seismic, Category II.
The inspectors reviewed the above design documentation and identified no concerns. The i
inspectors also confirmed by visual inspection that the installation of EDG crankcase exhaust system piping and hangers were in accordance with the design drawings and identified no i
concerns. All EDGs systems were found to be configured as per the design drawings.
l Based on the inspector's verification and adequate design in place by the licensee, the I
inspectors concluded that this item is closed.
.-.
- -
_
_
_
_._. _
.
_
.
.
.
_
!
.
'
'i
.
2.3 (Closed) Unresolved item 50-354/92-80-10 pertaining to the auto load tap changer failures on station transformers
!
During the previous EDSFI inspection, the team determined that four automatic load tap
>
changer (LTC) failures occurred on the 1 AX501 and IBX.501 station service transformers in i
the previous three years. The root causes of these failures were not known to the licensee at that time. The team was concerned that a failure of station service transformer LTCs could
i affect the available voltage at the 480 Volt motor control centers loads (MCCs) and affect their performance. In addition, on May 4,1993, a similar LTC failure was observed by the licensee on the I AX501 station service transformer.
,
During this inspection, the inspectors noted that the licensee had completed an extensive
investigation to review the LTC failure concern by reviewing similar concerns with other utilities, vendors and inspection of failed components. In addition, the licensee had changed the operations log and procedure to alert the operators of a potential LTC concern. The minimum and maximum allowed bus voltage values were also added in the procedure to alert operators of potential LTC problems, should bus voltage fall outside the acceptable values.
i Based on the licensee's investigation and the inspectors visual inspection of the selected LTC '
failed circuit cards, evidence of corrosion was on the cards. Per discussion with the licensee, the inspectors determined that the licensee had concluded the cause of the LTC failures was due to the existence of corrosion on the solid-state LTC control cards. These l
control cards are located inside the control housings of the station transformers. The licensee's inspection determined that corrosion was visible only on the control cards associated with the transformers that had LTC failures and no corrosion was evident on the units that did not fail.
.
!
The inspectors noted that the licensee had taken the following corrective. actions to prevent future LTC failures.
-
Replaced station service transformer LTC control cards with new improved cards (scaled relays, solder etched on both sides, better control transformer, and covering with a conformal coating to protect against corrosion and moisture),
t
-
Revised the preventive maintenance procedure to inspect the internals of the transformer control housing and examination of the LTC control card for evidence of.
,
corrosion.
-
Performed the walkdown of all similar transformer control cabinets to verify integrity of the door seals and latches and operation of the internal space heaters.
'i Based on the inspectors' review'of the licensee's corrective actions, documentation review,
'
and visual inspection of both the old and new control cards, and no abnormal LTC transients
!
i noted since the above actions, the inspector concluded that this item is closed
,
,
-
,
+nn e
.-
-
.
.
2.4 (Closed) Unresolved Item No. 50-354/92-80-12 pertaining to the test record i
documentation concerns identified in 1986 pre-operational test During the previous EDSFI inspection, the licensee was not able to provide adequate documentation to justify this resolution for several concerns identified by the team. The specific areas of concerns were identified with respect to the fuel oil day tank size, fuel oil l
consumption rate and other issues identified in the emergency diesel generators pre-operational test (PTP-BB-3, Part A). At that time, the team did ec consider any one of these issues to be an operability concern. The licensee committed to evaluate these concerns and demonstrate that adequate corrective actions were taken to resolve this issue.
l During this inspection, the licensee had collected all of the applicable documentation from
'
the above pre-operation test and completed the evaluation of the above test exemption concerns identified in the 1986 test. The licensee found that all test concerns had been adequately resolved and appropriate followup actions had been completed to adequately resolve the test concerns. Based on this evaluation performed, no additional actions were required to address the above issue. The inspectors review of the documentation pertaining to the pre-operational test conducted in 1986 revealed a total of 45 test exemptions.
To satisfy the above team concern, the inspectors randomly selected eight test exemption (TE) items from the previous inspection concerns. These items pertained to the EDG fuel oil day tank capacity, fuel oil day tank size and other concerns (TE-27, 29, 32, 33, 34, 35, 36 and 38). The inspectors review of the licensee's corrective actions taken to satisfy the EDG pre-operational test documentation revealed no concerns. A brief description and its resolution of each item observed by the inspectors during this inspection is noted below:
hem Concern Resolution TE-27 and The EDG A, B and D fuel oil The fuel oil day tank level alarms
day tank level alarm were readjusted and calibrated.
annunciated in 24 minutes instead of required specified 70 minutes, per the test procedure
-.
TE-32 Three core spray pumps Troubleshooting found missing (AP206, CP206 and DP206)
wires in switchgear cubicles, after started in 10 seconds instead of rewired as required per design and 6 seconds time after the bus re-successfully completed test on energization specified in test 2/16/86.
procedure.
l l
l
_.
_
_
_.
_.
.
,
..
'
.
i TE-33 The EDGs day tank fuel volume Technical evaluation made by the
'
was not available (recorded) to licensee used only the storage calculate the fuel consumption capacity tank differential level and rate, only the storage tank level assumption was made that the day
'
differential data was used to tank level would stay approximately I
calculate fuel consumption rate the same after the run. The
.
licensee evaluation concluded that L adequate fuel oil was available in the storage tank (53,000 gallons i
good for 179.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />) to satisfy the 168 hour0.00194 days <br />0.0467 hours <br />2.777778e-4 weeks <br />6.3924e-5 months <br /> (7 days) for each EDG -
required time in the storage tank.
TE-34 The EDGs lube oil consumption Technical evaluation concluded that j
rate was found to be slightly 1.63 gallons / hour rate was not l
higher (1.63 gallons / hour) than excessive. In addition, the licensee
!
the manufacturer's keeps a minimum of 550 gallons of recommended value of 1.55 lube oil onsite in their warehouse to gallons / hour as listed in the test satisfy the UFSAR question procedure and it failed to meet response 430.131 to the NRC as the 7 days storage requirements.
committed. It is more than adequate for makeup for EDGs demand in the emergency.
TE-35 EDG "D" fuel consumption Technical evaluation made by the calculated to be 163.07 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> licensee used only the storage tank versus 168 hours0.00194 days <br />0.0467 hours <br />2.777778e-4 weeks <br />6.3924e-5 months <br /> to satisfy the capacity differential level and Regulatory Guide 1.137 assumption was made that the day requirements of 7 days fuel oil tank level would stay approximately -
storage requirements the same after the run. The licensee evaluation concluded that adequate fuel oil was available'in '
the storage tank (53,000 gallons good for 179.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />) to satisfy the l
168 hour0.00194 days <br />0.0467 hours <br />2.777778e-4 weeks <br />6.3924e-5 months <br /> (7 days) for each EDG required time in the storage tank.'
TE-36 The actual EDG test data The licensee evaluation found that'
-j obtained did not match with the the design data specified in the
-
values specified in the pre-procedure was not accurate for the i
operational procedure for no
"no load" EDG conditions. The ~
load conditions, such as KVAR procedure values were revised i
rating, field amperes, etc.
accordingly,
.
TE-38 The A, C and D EDGs The engineering evaluation exhibited excessive frequency determined that the momentary overshoot during initial starting overshoot of the frequency observed (63.8,62.8 and 62.0 hertz) for EDGs A, C, and D, above the nominal 60 hertz value was acceptable. No conflict with the UFSAR requirements or design deficiency was determined during this test.
i The inspector's review of the above selected documents, including the technical evaluations, startup deviation reports, design modifications, procedure changes, startup test and supplemental test results revealed no concerns. The inspector concluded that the licensee had taken adequate corrective action to resolve the pre-operational concerns of 1986 testing and had adequate documentation to demonstrate their resolution. Therefore, this item is closed.
2.5 (Closed) Unresolved Item (50-354/92-80-14) pertaining to excessive EDG time response for an accident condition during the monthly surveillance testing i
During the EDSFI inspection, the team observed that the "B" EDG was inoperable for a long I
time while it was being " barred over" just prior to the monthly surveillance test. The team was concerned that during this EDG preparation period, the surveillance test procedure contained no precautions designed to limit the amount of time the diesel would be inoperable.
The diesel was observed to be inoperable for approximately 30 minutes during that test.
In a February 26,1992, letter to the NRC, the licensee agreed to establish various
.
precautionary steps to alleviate the potential consequence of an inoperable EDG dunng testing. These steps include: 1) limiting the inoperable time to 15 minutes each test; 2)
dispatching an operator to the EDG room to provide prompt response to the control room
demand: 3) not scheduling an EDG test when a redundant train is inoperable; and 4)
providing additional training to operators and technicians of the potential problem during EDG testing.
During this mspection, the inspectors reviewed the licensee EDG Operating Procedure HC.OP-SO.KJ-001(Q), Rev.13. The procedure contained specific prerequisites and precautions to limit the amount of time the diesel could be inoperable prior to performing the monthly surveillance with a stated goal of 15 minutes. The inspectors reviewed several of the log entries related to this surveillance and noted an average inoperable time of approximately 8 minutes was achieved by the licensee staff. The inspector also conducted interviews with licensed operators and personnel involved with the scheduling of surveillance. Each person interviewed displayed a clear understanding of the status of the diesel requirements prior to and during the monthly surveillance testin _. _ -
.
.
However, during the above review, the inspectors noted that some disparity existed among j
operators in the documentation being performed when Technical Specification Action j
Statements were entered for brief periods during surveillance. Specifically, some operators consider this and document the entry and exit in the Action Statement Tracking Log and some do not. The procedure which governs the Action Statement Tracking Log, HC.OP-AP.ZZ-0108(Q), Rev. 6, " Removal and Return of Equipment to Service," was noted to be ambiguous with respect to whether all Action Statement entries needed to be logged.
To address the above concern, the licensee initiated a revision of the above procedure.
Operators will be required to document in the operating log the time the engine was barred
,
over. The procedure update was expected to be completed by the end of this year and was t
being tracked on the ATS system as Item No. 354/92-80-14.
Based on the adequate licensee's corrective actions taken, including procedural changes and
'
interviews with plant personnel and time verification from the past surveillance tests, the inspectors concluded that this concern had been adequately addressed by the licensee. Since the above minor documentation concern were being monitored by the licensee on their tracking system, the inspectors concluded that this item is closed.
2.6 (Closed) Unresolved Item 50-354/92-80-15 pertaining to the inadequate transformer oil analysis During the previous EDSFI inspection, the team reviewed the licensee's station transformer
.
oil analysis program for both main power and station service transformers. The team also
!
'
conducted independent evaluations of transformer oil sample data by means of the industry accepted Roger's Method in accordance with ANSI /IEEE C57.104. Based on this independent assessment, the team concluded that the adequacy of the Hope Creek oil analysis program for important-to-safety transformers was questionable, and that the material condition of some of the transformers may be degraded.
.
l In a followup EDSFI inspection (50-354/93-10), the inspector concluded after reviewing i
various input data from the licensee and their contractor analysis, that there was no problem with the station transformers, even though the oil data indicated a previous heating and i
degradation of some of the units. However, the inspectors also noted that the continued
,
trending of the oil data was necessary to verify the integrity of the transformers.
During this inspection, the inspector reviewed the licensee evaluation 'and station transformer i
oil sample _ data for the main power and station service transformers to evaluate their current condition and the evaluation process. In addition, discussions with system engineers were i
conducted to determine the methodology by which the data were evaluated.
!
t
>
s w
-
._
_
.__
_
_
_
-
.
.
.
The licensee did not dispute, based on all available analysis, that some overheating and
,
degradation was experienced in the noted transformers in the past. However, the gases
,
generated from these past events were retained in the oil and were not likely to ever diffuse
out of the system. Therefore, in reviewing, the post-overheating event oil data were being
taken into consideration for the new higher baseline levels for generated gases. Deviations
-
from the new baseline levels were being evaluated for potential transformer degradation.
!
The inspectors review of all oil data since the initial overheating events indicated no-significant rising trend in the evolution of gases. The inspectors noted that, in the main -
power transformers, levels of total combustible gases had actually been slowly decreasing.
The licensee had effectively documented the above findings, and had taken further steps to i
ensure the adequacy of transformer cooling (radiator cleaning, etc.). The licensee's current _
,
method of sampling, analyzing, and documenting transformer oil data appeared to be
!
adequate and technically sound.
Based on this review, the inspector concluded that the licensee has acceptably resolved this issue and that this item is closed.
3.0 EXIT MEETING The inspector met with licensee representatives denoted in Attachment 1 on November 3,1993. The inspector summarized the purpose, scope and findings of the
,
inspection. The licensee's representatives acknowledged the findings and did not express any disagreement with them,
!
)
i i
l l
I l
l
~-
-
.-
-
__
i i
ATTACHMENT 1
Persons Contacted and Exit Meeting Attendees i
Public Service Electric and Gas Comnany
)
i
- V. Ciarlante, Senior Supervisor - ALARA
- J. Clancy, Technical Manager - Hope Creek l
S. Funsten, Maintenance Manager, Hope Creek
- M. Gray, Licensing Engineer
,
R. Griffins, Manager, Station QA - Hope Creek
- R. Hovey, General Manager - Hope Creek B. O'Malley, OPS Manager - Hope Creek J. Rucki, Technical Engineer - Hope Creek
,
- B. Smith, Licensing Engineer
,
U. S Eugjear Regulatory Commission f
- C. Marschall, Sr. Resident Inspector
- Denotes attendance at the exit meeting on November 3,1993.
The inspector also contacted other licensee personnel during the course of the inspection.
1