|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M7571999-10-22022 October 1999 Advises That Attachment 1 to ,Marked as Proprietary,Re Safety Limit MCPR & Fuel Vendor Change Will Be Withheld from Public Disclosure Per 10CFR2.790(b)(5) ML20217M2101999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Requal Pass Dates ML20217H8471999-10-18018 October 1999 Discusses Completion of Licensing Action for GL 98-01 & Suppl 1, Yr 2000 Readiness of Computer Sys at Npps, to All Holders of Operating Licenses for NPPs ML20217K8441999-10-15015 October 1999 Submits Revised Commitment to NRC Bulletin 90-01,Suppl 1 for Hope Creek Generating Station ML20217H9771999-10-13013 October 1999 Forwards SRO & RO Initial Exam Rept 50-354/98-302,suppl Rept on 990125-29,mtg Meeting on 990322,990429-30 & 0617-18 in-office Review & 990720 Telcon on Appeal Results.Overall, 11 of 16 Applicants Received NRC Licenses ML18107A5561999-10-0707 October 1999 Requests Relief Associated with Containment Examinations at Hope Creek & Salem Generating Stations.Attachment 1 Includes Proposed Alternatives & Supporting Justification for Relief Requests ML20217C4391999-10-0606 October 1999 Informs That Util Authorized to Administer Initial NRC Retake Written Exam to Applicant Listed,During Week of 991011 ML18107A5501999-10-0505 October 1999 Provides Current Status of Pse&G Actions Re GL 98-01, Y2K Readiness of Computer Sys at Npps, for Salem Nuclear Generating Station,Units 1 & 2 & Hope Creek Nuclear Generating Station ML18107A5521999-10-0505 October 1999 Encourages NRC to Support Abb Combustion Engineering Nuclear Power Request for Priority Review of Generic TR Re Crossflow Ultrasonic Flow Measurement Sys ML20217A9601999-10-0404 October 1999 Forwards Errata Redressing Deficiencies & Correcting Two Typos to Ufsar,Rev 10.Incorporate Attached Pages/Figures Into Controlled Copies of UFSAR ML20217A6861999-10-0101 October 1999 Forwards Insp Rept 50-354/99-05 on 990711-0829.Four Violations Occurred Re Areas of Fire Protection,Operation at Reduced Feedwater Inlet Temp & safety-related Battery Charging Operation & Being Treated as NCVs LR-N990430, Forwards Rev 10 to Hope Creek Generating Station Ufsar,Iaw 10CFR50.71(e).Details Re Each Change Also Attached to Facilitate NRC Review1999-09-28028 September 1999 Forwards Rev 10 to Hope Creek Generating Station Ufsar,Iaw 10CFR50.71(e).Details Re Each Change Also Attached to Facilitate NRC Review ML18107A5341999-09-22022 September 1999 Provides Data Re Operator Licensing Exam for Salem & Hope Creek Station,In Response to NRC Form 536 (7-1999) ML20217K7781999-09-16016 September 1999 Forwards Discharge Monitoring Rept for Hope Creek Generating Station for Month of Aug 1999. Rept Is Required by & Prepared Specifically for EPA & Nj Dept of Environ Protection ML20212B3631999-09-14014 September 1999 Forwards Rev 13 to Salem - Hope Creek Security Plan,Iaw 10CFR50.54(p).Summary of Proposed Changes to Plan,Encl. Encl Withheld ML20212B4021999-09-13013 September 1999 Submits Supplemental Info Related to Hope Creek License Change Request (LCR) H98-08,submitted to NRC on 981230, Re Flood Protection TS Changes ML18107A5221999-09-0808 September 1999 Requests Approval to Use ASME Code Case N546,which Provides Alternative Qualification Requirements That Allow Personnel Most Familiar with Walkdown of Plant Sys,Like License Operators to Perform VT-2 Examinations ML20211N5421999-09-0808 September 1999 Forwards Amend 121 to License NPF-57 & Safety Evaluation. Amend Revises TSs by Relocating Procedural Details of RETS to Offsite Dose Calculation Manual LR-N990395, Provides Comments on NRC Ltr Dtd 990714, Closure of TAC Number MA1194 - Response to RAIs to GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity, for Hope Creek Generating Sation. Revised GE Report Encl Also1999-09-0101 September 1999 Provides Comments on NRC Ltr Dtd 990714, Closure of TAC Number MA1194 - Response to RAIs to GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity, for Hope Creek Generating Sation. Revised GE Report Encl Also ML20211B5341999-08-20020 August 1999 Forwards RAI Re 2nd 10-yr ISI Interval Relief Requests Re Plant.Info Requested to Be Provided within 60 Days of Receipt of Ltr ML18107A4911999-08-20020 August 1999 Forwards Revised Plant Attribute Libraries for Salem & Hope Creek Generating Stations,Iaw 10CFR50,App E,Vi, Emergency Response Data Sys, 3.b.Changes Are Identified by Rev Bars ML18107A4801999-08-13013 August 1999 Requests That Pse&Gs Contact in NUREG-0383, Directory of Compliance for Radioactive Matl Packages, Be Changed ML20210R4911999-08-11011 August 1999 Forwards Insp Rept 50-354/99-04 on 990530-0711.No Violations Noted.Inspectors Reviewed Performance Indicators Submitted as Part of Pilot Program for New Regulatory Oversight Process & Verified Data ML18107A4751999-08-0505 August 1999 Forwards Fitness for Duty Performance Data Rept for Six Month Period Ending 990630 ML20210H9241999-07-26026 July 1999 Informs That State of Nj Dept of Environ Protection Has No Comments on Licensee 990517 Request for Amend to TS by Adding TS 3.3.10, Instrumentation of OPRM Sys ML20210F3271999-07-22022 July 1999 Forwards SE Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3 Re First 10-year Interval for ISI Program at Hope Creek ML20210D3971999-07-16016 July 1999 Forwards Discharge Monitoring Rept for Hope Creek Generating Station, for June 1999.Rept Is Required by & Prepared for EPA & Nj Dept of Environ Protection 05000354/LER-1999-007, Forwards LER 99-007-00,re License Condition Violation - Class-1E Battery Charging Operation.Commitments Made by Util Encl1999-07-14014 July 1999 Forwards LER 99-007-00,re License Condition Violation - Class-1E Battery Charging Operation.Commitments Made by Util Encl ML20209G2831999-07-14014 July 1999 Disclosure Closure of TAC MA1194 Re Licensee Response to RAI to GL 92-01,Rev 1,Suppl 1, Rc Structural Integrity, for Plant LR-N990250, Provides Proposed Alternative & Supporting Justification for Relief from Augmented Inservice Requirements of 10CFR50.55a(g) for Volumetric Exam of RPV Circumferential Welds1999-07-0909 July 1999 Provides Proposed Alternative & Supporting Justification for Relief from Augmented Inservice Requirements of 10CFR50.55a(g) for Volumetric Exam of RPV Circumferential Welds ML20196J4421999-07-0101 July 1999 Forwards Request for Addl Info Re Increase of Allowable Main Steam Isolation Valve (MSIV) Leak Rate & Deletion of MSIV Sealing Sys for Plant LR-N990316, Responds to NRC Request for Info Re Y2K Readiness at Npps, Per GL 98-01,suppl 1.Disclosure Encl1999-06-30030 June 1999 Responds to NRC Request for Info Re Y2K Readiness at Npps, Per GL 98-01,suppl 1.Disclosure Encl ML18107A4131999-06-25025 June 1999 Provides Further Clarification of Licensing & Design Basis for 125 Vdc Battery Margins for Sgs & HCGS for Meeting Station SBO & Loca/Loop Loading Requirements,Per Util 990426 Ltr & Discussion with NRC ML20209B6441999-06-21021 June 1999 Offers No Comments on Licensee 990529 Request for Revs to Plant Radiological Effluent Ts,Per GL 89-01 ML20209C0621999-06-21021 June 1999 Forwards NPDES Discharge Monitoring Rept,May 1999, for Hcgs.Rept Prepared Specifically for EPA & Nj Dept of Environ Protection ML20196E6471999-06-21021 June 1999 Forwards Revised marked-up TS Page for HCGS License Change Requests H99-02 & H99-05,dtd 990329 & 0524,respectively. Revised Pages Do Not Alter Conclusions Reached in 10CFR50.92 No Significant Hazards Analysis Previously Submitted ML20196F9441999-06-21021 June 1999 Forwards Insp Rept 50-354/99-03 on 990419-0529.Violations Noted.Two Violations of NRC Requirements Occurred Re Reactor Bldg Ventilation Setpoints & Control Rod Drop Analyses ML20212J0541999-06-17017 June 1999 Responds to Requesting That NRC Staff ...Allow BWR Plants Identified to Defer Weld Overlay Exams Until March 2001 or Until Completion of NRC Staff Review & Approval of Proposed Generic Rept,Whichever Comes First ML20196E9631999-06-17017 June 1999 Informs That Util Has Made Change to Commitment Stated in NRC Ser,Suppl 5.Commitment That Has Been Changed Is Item Number 1 of First Paragraph on Page 9-3 of Ser,Suppl 5 LR-N990295, Submits Change 1 to Relief Request RR-A4,which Clarifies Requirements Re Snubber Visual Insps.Request Was Submitted as Part of Plant Second Interval ISI Program on 9905111999-06-16016 June 1999 Submits Change 1 to Relief Request RR-A4,which Clarifies Requirements Re Snubber Visual Insps.Request Was Submitted as Part of Plant Second Interval ISI Program on 990511 05000354/LER-1999-006, Forwards LER 99-006-00 Re Esfa B Channel Primary Containment Isolation Signal Actuation.Attachment a Lists Commitments Util Making to NRC Re LER1999-06-15015 June 1999 Forwards LER 99-006-00 Re Esfa B Channel Primary Containment Isolation Signal Actuation.Attachment a Lists Commitments Util Making to NRC Re LER ML20195J1051999-06-0707 June 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Jw Clifford Will Be Section Chief for Hope Creek Generating Station ML20195J1101999-06-0707 June 1999 Informs of Completion of Review of Providing Updated Status on Implementation of Commitments Made in Response to GL 89-13.Confirms Revs Made to Previous Commitments to Resolve Monitoring Pressure Drop Problem ML20207F2681999-06-0303 June 1999 Responds to by Forwarding Gfes & NRC Written Exam Grades for List of Hope Creek Operators Submitted by DE Jackson.Absence of Gfes Grade Indicates That Operator Previously Issued RO or SRO License.Without Encl ML20207D0201999-05-27027 May 1999 Discusses 990512 Meeting to Identify Insp Activities at Hope Creek Facility Over Next Six Months & Informs of Planned Insps in Order for Licensee to Have Opportunity to Prepare & Provide Region I with Feedback on Schedule Conflicts ML18107A3611999-05-27027 May 1999 Forwards Responses to NRC 990301 & 990323 RAIs for Salem & Hope Creek Generating Stations Relating to GL 96-05 ML20195B9931999-05-20020 May 1999 Forwards NPDES Discharge Monitoring Rept,Apr 1999, for Hgcs.Rept Prepared Specifically for EPA & Nj Dept of Environ Protection ML20207A3451999-05-20020 May 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECCS Strainers by Debris in Bwrs ML20206Q4461999-05-14014 May 1999 Forwards SE Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206U8451999-05-14014 May 1999 Forwards Insp Rept 50-354/99-02 on 990308-0418.Violations Re Fuel Handling Errors & Missed Temp Monitoring During Reactor Vessel Head Tensioning Occurred & Being Treated as non-cited Violation 1999-09-08
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217M7571999-10-22022 October 1999 Advises That Attachment 1 to ,Marked as Proprietary,Re Safety Limit MCPR & Fuel Vendor Change Will Be Withheld from Public Disclosure Per 10CFR2.790(b)(5) ML20217M2101999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Requal Pass Dates ML20217H8471999-10-18018 October 1999 Discusses Completion of Licensing Action for GL 98-01 & Suppl 1, Yr 2000 Readiness of Computer Sys at Npps, to All Holders of Operating Licenses for NPPs ML20217H9771999-10-13013 October 1999 Forwards SRO & RO Initial Exam Rept 50-354/98-302,suppl Rept on 990125-29,mtg Meeting on 990322,990429-30 & 0617-18 in-office Review & 990720 Telcon on Appeal Results.Overall, 11 of 16 Applicants Received NRC Licenses ML20217C4391999-10-0606 October 1999 Informs That Util Authorized to Administer Initial NRC Retake Written Exam to Applicant Listed,During Week of 991011 ML20217A6861999-10-0101 October 1999 Forwards Insp Rept 50-354/99-05 on 990711-0829.Four Violations Occurred Re Areas of Fire Protection,Operation at Reduced Feedwater Inlet Temp & safety-related Battery Charging Operation & Being Treated as NCVs ML20211N5421999-09-0808 September 1999 Forwards Amend 121 to License NPF-57 & Safety Evaluation. Amend Revises TSs by Relocating Procedural Details of RETS to Offsite Dose Calculation Manual ML20211B5341999-08-20020 August 1999 Forwards RAI Re 2nd 10-yr ISI Interval Relief Requests Re Plant.Info Requested to Be Provided within 60 Days of Receipt of Ltr ML20210R4911999-08-11011 August 1999 Forwards Insp Rept 50-354/99-04 on 990530-0711.No Violations Noted.Inspectors Reviewed Performance Indicators Submitted as Part of Pilot Program for New Regulatory Oversight Process & Verified Data ML20210F3271999-07-22022 July 1999 Forwards SE Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3 Re First 10-year Interval for ISI Program at Hope Creek ML20209G2831999-07-14014 July 1999 Disclosure Closure of TAC MA1194 Re Licensee Response to RAI to GL 92-01,Rev 1,Suppl 1, Rc Structural Integrity, for Plant ML20196J4421999-07-0101 July 1999 Forwards Request for Addl Info Re Increase of Allowable Main Steam Isolation Valve (MSIV) Leak Rate & Deletion of MSIV Sealing Sys for Plant ML20196F9441999-06-21021 June 1999 Forwards Insp Rept 50-354/99-03 on 990419-0529.Violations Noted.Two Violations of NRC Requirements Occurred Re Reactor Bldg Ventilation Setpoints & Control Rod Drop Analyses ML20212J0541999-06-17017 June 1999 Responds to Requesting That NRC Staff ...Allow BWR Plants Identified to Defer Weld Overlay Exams Until March 2001 or Until Completion of NRC Staff Review & Approval of Proposed Generic Rept,Whichever Comes First ML20195J1101999-06-0707 June 1999 Informs of Completion of Review of Providing Updated Status on Implementation of Commitments Made in Response to GL 89-13.Confirms Revs Made to Previous Commitments to Resolve Monitoring Pressure Drop Problem ML20195J1051999-06-0707 June 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Jw Clifford Will Be Section Chief for Hope Creek Generating Station ML20207F2681999-06-0303 June 1999 Responds to by Forwarding Gfes & NRC Written Exam Grades for List of Hope Creek Operators Submitted by DE Jackson.Absence of Gfes Grade Indicates That Operator Previously Issued RO or SRO License.Without Encl ML20207D0201999-05-27027 May 1999 Discusses 990512 Meeting to Identify Insp Activities at Hope Creek Facility Over Next Six Months & Informs of Planned Insps in Order for Licensee to Have Opportunity to Prepare & Provide Region I with Feedback on Schedule Conflicts ML20207A3451999-05-20020 May 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECCS Strainers by Debris in Bwrs ML20206U8451999-05-14014 May 1999 Forwards Insp Rept 50-354/99-02 on 990308-0418.Violations Re Fuel Handling Errors & Missed Temp Monitoring During Reactor Vessel Head Tensioning Occurred & Being Treated as non-cited Violation ML20206Q6211999-05-14014 May 1999 Informs That on 990119 Licensee Provided NRC with Several Revised TS Bases Pages for Plant.Ts Bases Pages B 3/4 6-1 & B 3/4 6-2 Were Revised ML20206Q4461999-05-14014 May 1999 Forwards SE Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206R2691999-05-12012 May 1999 Informs That During 990504 Telcon Between J Caruso & H Hanson,Arrangements Were Made for Administration of Licensing Written Retake Exam at Hope Creek Nuclear Generating Station During Week of 990927 ML20206C8431999-04-22022 April 1999 Forwards SER Authorizing Util 980728 Submitted Relief Requests Associated with Changes Made to Repair Plan for Core Spray Nozzle Weld N5B ML20205S7911999-04-19019 April 1999 Forwards Insp Rept 50-354/99-01 on 990124-0307.Violations Noted.Some Human Performance Errors Occurred During Numerous Outage Activities,Util Appropriately Reacted to Each of Errors & Initiated Corrective Actions ML20205R0861999-04-14014 April 1999 Informs That Final Review of Hard Copy of PPR Re Hope Creek, Issued 990409 Had Error.Electronic Version e-mailed Was Not Effected.Forwards Pp with Correction in Margin.Without Encl ML20205R0461999-04-14014 April 1999 Forwards Associated Page with Correction Marked in Margin of PPR of Salem Issued 990409.During Final Review of Hard Copy, Error Was Noted.Without Encl ML20205N2481999-04-0909 April 1999 Discusses Hope Creek Generating Station Plant Performance Review Conducted for Period April 1998 Through Jan 1999 & Informs of NRC Planned Insp Effort Resulting from Ppr. Historial Listing & Insp Plans for Next Few Months Encl IR 05000354/19983021999-04-0909 April 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-354/98-302 Issued on 990226.Response Indicates That Licensee Corrected Violation & Initiated Measures to Prevent Recurrence ML20205G5961999-03-19019 March 1999 Forwards Safety Evaluation of Relief Request Re ASME Code Case N-567, Alternate Requirements for Class 1,2 & 3 Replacement Components Section Xi,Div 1. Request Acceptable ML20205F8771999-03-18018 March 1999 Forwards SE Authorizing Licensee 971222 Relief Requests Re Second 10-year Interval for Pumps & Valves IST Program for Hope Creek Generating Station ML20207D5741999-03-0101 March 1999 Discusses Pse&G 980604 Updated Response to GL 96-05 Indicating Intent to Implement Provisions of JOG Program on MOV Periodic Verification at Hope Creek Generating Station. Forwards RAI Re GL 96-05 Program at Hope Creek ML20198H6211998-12-24024 December 1998 Forwards Notice of Withdrawal of 970826,as Suppl 980424 & 0924 Amend Request for FOL NPF-57.Proposed Change Would Have Modified Facility TSs Pertaining to Filtration,Recirculation & Ventilation Sys Surveillance Testing Requirements ML20198L3571998-12-22022 December 1998 Forwards Insp Rept 50-354/98-11 on 981101-1212.No Violations Noted.Insp Generally Characterized by safety-conscious Operations,Effective Engineering & Maint Practices & Careful Radiological Work Controls ML20198H6661998-12-17017 December 1998 Informs That Attachment 1 to Ltr LR-N98404,dtd 980825 Marked as Proprietary,Will Be Withheld from Public Disclosure Pursuant to 10CFR2.790(b)(5) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20196K1371998-12-0909 December 1998 Advises of Planned Insp Effort Resulting from Hope Creek Insp Review Planning Meeting Conducted on 981110.Details of Insp Plan for Next 6 Months Encl ML20197H3841998-12-0707 December 1998 Informs That Licensee Authorized to Administer Initial Written Exams to Listed Applicants on 981222.NRC Region I Operator Licensing Staff Will Administer Operating Tests ML20196H0301998-12-0101 December 1998 Informs That NEDC-32511P,rev 1,dtd Oct 1998 Marked as Proprietary,Will Be Withheld from Public Disclosure Pursuant to 10CFR2.790(b)(5) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20196F7991998-11-30030 November 1998 Forwards Rept Representing Results of 981026-29 Audit of Year 2000 Pragram at Hope Creek Generating Station.Audit Conducted as Followup to NRC GL 98-01, Year 2000 Readiness of Computer Sys at Npps, Issued 980511 ML20196D0711998-11-23023 November 1998 Forwards Insp Rept 50-354/98-10 on 980920-1031 & Notice of Violation Re Preforming Single Cell Charge on safety-related Battery Cell in Configuration Prohibited by Station Procedures ML20154Q7071998-10-16016 October 1998 Forwards Exam Rept 50-354/98-03OL Conducted by NRC During Periods of 980304-12,0519-21,22-28 & 0629.All Five Reactor Operator Applicants & Four of Five Senior Reactor Applicants Passed Exams ML20154J8501998-10-0909 October 1998 Forwards Insp Rept 50-354/98-08 on 980809-0919 & Notice of Violation Re Inadequate Corrective Actions to Resolve Steam Leaks from Piping Located in Torus Room ML20154P4011998-10-0909 October 1998 First Final Response to FOIA Request for Records.Records in App a Available in Pdr.Records in App B Partially Withheld (Ref FOIA Exemption 3) IA-98-323, First Final Response to FOIA Request for Records.Records in App a Available in Pdr.Records in App B Partially Withheld (Ref FOIA Exemption 3)1998-10-0909 October 1998 First Final Response to FOIA Request for Records.Records in App a Available in Pdr.Records in App B Partially Withheld (Ref FOIA Exemption 3) ML20154F1121998-10-0202 October 1998 Forwards Insp Rept 50-354/98-09 on 980817-26 & 0908.No Violations Identified.Major Areas Inspected:Maint, Engineering & Mgt Meeting ML20154B3341998-09-29029 September 1998 Requests That Encl Info on GE Rept NEDC-32511P Be Reviewed & Revised Proprietary Version of Subj Rept Be Submitted.Some Info in Rept Should Not Be Exempt from Public Disclosure & Should Be Released & Placed in PDR ML20154B3781998-09-25025 September 1998 Informs That Facility Scheduled to Administer NRC Generic Fundamentals Exam on 981007.Sonalysts,Inc Authorized Under Contract to Support NRC in Administration of Activities. Ltr & Encls Provide Instructions & Guidelines IR 05000354/19980061998-09-11011 September 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-354/98-06 Issued on 980721 ML20151Z5941998-09-11011 September 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-354/98-02 on 980423.Response Indicated Violations Corrected & Measures Initiated to Prevent Recurrence IR 05000354/19980021998-09-11011 September 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-354/98-02 on 980423.Response Indicated Violations Corrected & Measures Initiated to Prevent Recurrence 1999-09-08
[Table view] |
Text
SUBJECT:
NRC INSPECTION REPORT 50-354/98-05
Dear Mr. Keiser:
!
This letter refers to your July 6,1998 correspondence (LR-N980316),in response to our June 4,1998, letter regarding the Hope Creek facility.
Thank you for informing us of the corrective and preventive actions for the Notice of
Violation, as documented in your letter. The Notice of Violation identified four examples of
violations of NRC requirements. One violation involved the failure to maintain the residual l
heat removal system available during a 1990 refueling outage when the reactor was off-loaded. The remaining three violation examples were related to a modification that was installed during the Fall 1997 refueling outage and was associated with ventilation system safety related chillers.
Your response to the violation indicated that you have corrected the specific violations and have initiated measures to prevent recurrence. Your response to the violations will be examined during a future inspection.
Your cooperation with us is appreciated.
l
Sincerely, ORIGINAL SIGNED BY:
l James C. Linville, Chief
Projects Branch 3
'
Division of Reactor Projects
/
l Docket No. 50-354 9007290032 990721 f
PDR ADOCK 05000354 G
PDR fi:D E_
--
- - - - -
-
-
-_
)
-_ - _ - _-- -_-__ _ _ __-__ __-_.
- _ _ _ _ _ _ _ _ _ _.
l
.
.
j
-
.
I Mr. Harold !
l l
.
cc:
l L. Storz, Senior Vice President - Nuclear Operations E. Simpson, Senior Vice President - Nuclear Engineering E. Salowitz, Director - Nuclear Business Support l
M. Bezilla, General Manager - Hope Creek Operations J. McMahon, Director - QA/ Nuclear Training / Emergency Preparedness i
D. Powell, Director - Licensing / Regulation & Fuels A. C. Tepert, Program Administrator
,
,
cc w/cy of Licensee's Letter:
A. F. Kirby,111, External Operations - Nuclear, Delmarva Power & Light Co.
,
J. A. Isabella, Manager, Joint Generation Atlantic Electric R. Kankus, Joint Owner Affairs Jeffrey J. Keenan, Esquire Consumer Advocate, Office of Consumer Advocate l
William Conklin, Public Safety Consultant, Lower Alloways Creek Township l
State of New Jersey State of Delaware i
,
I l
l
i
<
<___m_m_.____
_ _.___. _. _ _ _ _.
_
___ ___ ___ - _ - - - ____-
!
.-
.
..
_,
.
I I
Mr. Harold W.' Keiser
l
- Distribution w/ copy of Licensee's Response Letter:
Region I Docket Room (with concurrences)
' J. Linville, DRP S. Barber, DRP C. O'Daniell, DRP
!-
- D.' Screnci, PAO
!
Nuclear Safety Information Center (NSIC)
l NRC Resident inspector B. McCabe, OEDO R. Ennis, Project Manager, NRR R. Capra, PD1-2, NRR inspection Program Branch, NRR (IPAS)
jl R. Correia, NRR F. Talbot, NRR l-DOCDESK l
PUBLIC -
i l
-
l.
i r
j I
.
l
!
!
!:
~
f-
'
!
l l
,
~ DOCUMENT NAME: G:\\BHANCH3\\1-HC\\9805 RESP.lR
, TJ receive e copy of this doonmert. Indicate in the box:
"C" = Copy without ettechmerWenclosure
- E" = Copy with ettschment/ enclosure
"N" = No copy f
.
0FFICE RI/DRP.
l RI/ORP
,3/fl
/
l l
l NAME --
Pindale/meo Linville\\fI DATE 07/21/98 07/1
/988 07/
/98 07/
/98 07/
/98
'
0FFICIAL RECORD COPY i
E
-
-
-
e
g
.
.
,
-
e i
.
.4.". 4*
Public Service j
Electric and Gas Company H r:ld Pubhc Service Electne and Gas Company PO Box 236, Hancocks Bndge. NJ 08038 609-339-1100 Chief Nuclear Officer & President Nuclear Business Unit LR-N980316 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
REPLY TO NOTICE OF VIOLATION INSPECTION REPORT 354/98-05 HOPE CREEK GENERATING STATION j
FACILITY OPERATING LICENSE NPF-57 j
DOCKET NO. 50-354 Pursuant to the provisions of 10 CFR 2.201, Public Service Electric and Gas Company
!
(PSE&G) hereby submits a reply to the Notice of Violation (NOV) issued to the Hope Creek Generating Station in a letter dated June 4,1998.
l The PSE&G response for this violation is contained in the Attachment to this letter. If you have any questions or comments on this transmittal, please contact Paul Duke at (609) 339-1466.
,
i
Sincerely,
/
\\
M l
Attachment l
l
[
MO 7/@WQ
,
- - - - - - - _ _ - -. _ - - - - - - - - - - - - - - - - - - - - - -. - - - - - - - - _ _ _ _ _ _ _ _ _ _ _ _
.
.
,
,-
.
,
'
JUL 061998
.
I Document Co@pi Desk-2-
- LR-N980316 C
Mr. H. Miller, Administrator - Region l U. S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA '9406 Mr. R. Ennis, Licensing Project Manager - Hope Creek U. S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Mail Stop 14E21 Rockville, MD 20852
i Mr. S. Pindale (X24)
USNRC Senior Resident inspector-HC l
Mr. K. Tosch, Manager IV i
Bureau of Nuclear Engineering P. O. Box 415
,
I Trenton, NJ 08625
-
,
'
l
l l
'
l f
t f
L
,
. _ _.
.__ _______ _ - _ _ _
e
-
.
J
!
.
'
JUL 061998 Document. Content Desk-3-LR-N980316 PRD BC CNO & President - NBU (N09)
Senior Vice President - Nuclear Engineering (N19)
Senior Vice President - Nuclear Operations (XO4)
Genere! Manager - Hope Creek Operations (H07)
i Director-QA/NT/EP (X01)
J Director-System Engineering (H16)
Director-Design Engineering (N23)
Director - Engineering Assurance (N25)
Director - Licensing / Regulation and Fuels (N21)
Manager - Financial Control & Co-Owner Affairs (N07)
-
Operations Manager - Hope Creek (H01)
Manager - Hope Creek Maintenance (H07)
' Manager - Hope Creek System Engineering (H18)
Mechanical Design Manager (N24)
Manager-Quality Assessment-NBU (X16)
Program Manager - Nuclear Review Board (N38)
Manager-Hope Creek Licensing (N21)
J. Keenan, Esq. (N21)
Records Management (N21)
.
Microfilm Copy File Nos.1.2.1,3.1 (HC iP,354/98-05)
i
!
!
F-
-
-
.
-
.
l*
l j
. -u ATTACHMENT
.
l
'
RESPONSE TO NOTICE OF VIOLATION INSPECTION REPORT NO. 50-354/98-05 HOPE CREEK GENERATING STATION DOCKET NO. 50-354
A.10 CFR 50.59 Violation l
1. Description of the Notice of Violation 10 CFR 50.59, " Changes, tests and experiments," in part, permits the licensee to make changes to its facility and procedures as described in the final safety analysis report (FSAR) and conduct tests or experiments not described in the safety analysis report without prior Commission approval provided the change does not involve a change in the technical specifications or an Unreviewed Safety Question (USO). The licensee shall maintain records of changes in the l
facility and these records must include a written safety evaluation which provides the bases for the determination that the change does not involve a USQ.
"
FSAR Section 9.1.3.2.3 establishes that the design and operation of the fuel pool cooling and cleanup systems for the decay heat associated with a full core offload is based, in part, on the operation or availability of the residual heat removal (RHR) system to augment the fuel pool cooling and cleanup (FPCC)
system.
Contrary to the above, during refueling outage a F03 in December 1990, the i
licensee did not maintain the RHR system in operation or available to augment l
the FPCC system which represented a change to the facility as described in the FSAR and did not perform a review of this change to demonstrate that the l
change did not involve a USQ.
l This is a Severity Level IV violation (Supplement 1).
2. Reply to Notice of Violation PSE&G agrees with the violation.
l 3. Reason for the Violation
!
PSE&G attributed the cause for this violation to inadequate procedures for outage reviews and controls. Altemate means of decay heat removal were evaluated before the RFO3 full core offload to ensure sufficient decay heat removal capacity. However, the requirement to compare the alternate decay heat removal methods with those described in the Hope Creek Up6;ted Final Safety Analysis Report (UFSAR) and to evaluate deviations in accordance with 10 CFR 50.59 was not recognized.
Page 1 of 6
.
- - - - - - _ _ _ _ - _ _ - _ _ _ - - _ _.
_
L*
.
.
Attachment'
LR-N980316
-
'4
....w.
l 4. Corrective Steps that Have Been Taken and Results Achieved The interschon among Nuclear Fuels, System Engineering and Outage (.
Management has been proceduralized. The station outage risk management l
procedure was revised to include guidance on the development of decay heat l
load estimates and heat-up curves for outage planning. The guidance includes l
verification of adequate decay heat removal capability throughout the outage j
schedule.
i For the full core offload performed during refueling outage RFO7, completed in December 1997, the decay heat removal method was evaluated in accordance with 10 CFR 50.59 and found not to involve an Unreviewed Safety Question.
5. Corrective Steps that Will Be Taken to Avoid Further Violations No additional corrective actions are planned.
i 6. Date When Full Compliance Will be Achieved i
Hope Creek achieved full compliance when the RHR system was returned to l
available status and the core reload was completeu during RFO3.
l
[
B.10 CFR 50 Appendix B Criterion XI Violation 1. Description of the Notice of Violation 10 CFR 50 Appendix B Criterion XI requires, in part, that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service be identified and performed in accordance with written test procedures
,
which incorporate the requirements and acceptance limits contained in l
applicable design documents. The test program shall include, as appropriate, proof tests prior to installation and operational tests during nuclear power plant operation of structures, systems, and components.
l Contrary to the above, two examples of inadequate testing requirements l
associated with a design change modification to the Hope Creek safety-related control area chilled water system chillers were identified as follows:
(1) As of April 7,1998, a complete proof test prior to installation and an operational test had not been performed to verify that check valves 1KBV-1243 through 1KVB-1250 [ sic) would provide a relatively leak tight boundary and ensure that the backup safety-related pneumatic supplies for the chiller condenser cooling water pressure control valves would remain available for four hours after a loss of power event.
(2) On April 8,1998, the backup safety-related pneumatic preseure regulators (1KBPCV-11464, -11466, and -11467) for the chiller condenser cooling water l
Page 2 of 6
)
L
__
. _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _
____
_-
!
.
. Atta:hment
LR-N980316
.
I I
pressiird'c6ntrol valves were found set below minimum design requirements.
Operational tests had also not been performed to ensure that pressure regulators 1KBPCV-1164 (sic] through 1KBPV-1171 [ sic] would remain property set in accordance with design requirements.
This is a Severity Level IV violation (Supplement I).
2. Reply to Notice of V%Iation i
PSE&G agrees with the violation.
.
l 3. Reason for the Violation Example (1)
PSE&G attributed the cause of the failure to establish inservice testing (IST)
!
. requirements and to periodically perform ISTs to personnel error. Personnel preparing the design change package (DCP) and performing design specialty reviews did not ensure the DCP was reviewed by the IST group. Deficiencies in the standard DCP format contributed to the violation. The design interface record had a single signoff for IST and for valve programs.
As part of the post-modification testing, an external leak check was perfomied l
and the valves were functionally tested. Both tests were satisfactory. However, l
since the design change packages that added the check valves for the backup pneumatic supply were not reviewed by the IST group, IST requirements for the valves were not established.
Example (2)
,
l PSE&G attributed the cause of the failure to maintain the backup pneumatic pressure regulator settings to personnel error, most likely after the modification j
was completed. The regulator settings were verified as part of the post-modification testing. The most likely scenario is misadjustment by an operator l
i during rounds or during a routine maintenance activity. Deficiencies in the
!
procedure changes and in operator training for the design change package contributed to the violation.
4. Corrective Steps that Have Been Taken and Results Achieved Example (1)
a. The check valves were tested satisfactorily.
b. IST procedures for the check valves have been developed.
c. The format for the design change interface record was revised to require a separate signoff for the IST review.
l Page 3 of 6
_ _ _ _ _ _ _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
. _ _ _ _ _ _.
_ _ _ _ _
r.
Atta:hment LR-N980316
-
,
,
...u L
d. A detailed roll out of this event and its implications was provided to affected j
design engineering personnel.
e. Personnelinvolved were counseled concerning performance in this event.
l I
I l
Example (2)
a. The backup pneumatic supply regulator settings were restored to their
required values, b. Interim guidance on the operation of the backup pneumatic supply system was provided to operators.
l c. IST procedures for the check valves have been developed. The procedures include periodic verification of the pressure regulator settings for the backup pneumatic supply.
5. Corrective Steps that Will Be Taken to Avoid Further Violations Example (1)
No additional corrective actions are planned.
Example (2)
l a. This violation will be incorporated in operator continuing training by
- .
l September 1,1998.
i b. Lessons leamed from this violation will be communicated to Engineering personnel by September 30,1998.
6. Date When Full Compliance Will be Achieved l
Example (1)
Hope Creek achieved full compliance on April 8,1998 when the inservice testing was performed satisfactorily on the backup pneumatic supply check valves. The valves have been added to the IST program.
Example (2)
Hope Creek achieved full compliance on April 8,1998 when the backup pneumatic supply regulator settings were restored to their required values.
Page 4 of 6 I
L
_ _ - _ _ - _ - - _ _ _ - - - - - _ _ _ - _
-_ _ - -
.
.
. Atta:hment LR-N980316
.
l C.10 CFR 50-Appendix B Critorion XVI Violation 1. Description of the Notice of Violation
)
l 10 CFR Appendix B Criterion XVI (Corrective Action) requires, in part, that measures shall be established to assure that conditions adverse to quality, such l
as failures, malfunctions, deficiencies, deviations, and nonconformances are
promptly identified and corrected.
Contrary to the above, on December 10,1997, PSE&G engineers determined that the minimum cooling water inlet temperature for the safety-related control area chilled water system chillers should be changed in a more limiting direction to 70 degrees Fahrenheit from 55 degrees Fahrenheit. On April 9,1998, the operations department management, still unaware of any necessary change to the minimum allowed cooling water temperature, used 55 degrees Fahrenheit as I
a basis for determining inoperability when they made a four-hour event i
notification to the NRC. Hope Creek abnormal operating procedure, Loss of Instrument Air and/or Service Air, HC.OP-AB.ZZ-0131(Q) - Rev.14, and pending
change, HFSAR 97-080, to the Hope Creek Updated Final Safety Analysis Report (UFSAR) also incorrectly stated that 55 degrees Fahrenheit was the i
minimum cooling water temperature below which the safety-related backup i
pneumatic supply needed to remain operable. The change in minimum cooling water inlet temperature to a more limiting value was not corrected until May 7, 1998, when guidance was provided to operators specifying the new 70 degrees Fahrenheit minimum cooling water temperature.
l This is a Severity Level IV violation (Supplement 1).
I 2. Reply to Notice of Violatior
!
PSE&G agrees with the violation.
3. Reason for the Violation
i PSE&G attributed the cause for this violation to personnel error. In December, 1997, the responsible engineer concluded that the minimum Safety Auxiliaries
,
Cooling system (SACS) temperature for Control Room chiller operation with full SACS flow is higher (more limiting) than the minimum temperature used for design of the backup pneumatic supply modification. The 55 degrees Fahrenheit i
temperature was an appropriate limit for a fully loaded chiller; but it is more conservative to assume that the chiller is lightly loaded. The responsible engineer, who is no longer employed by PSE&G, recognized the need for corrective action but did not initiate an Action Request as required by PSE&G's Corrective Action Program to ensure the non-conservative design assumption was reviewed for its effect on chiller operability.
Page 5 of 6
___
_ _ _ _ _ _ _ _ _ _ - - _ _ _ _ - - _ _ _ _ _ _. _ _ _ _ _ _ _ _ _ _
,
'
Atta hment LR-N980316
,
.
a
,.
,
4. CorrectidSteps that Have Been Taken and Results Achieved a. An Action Request to document this condition was initiated.
b. The backup pneumatic supply was restored and the Control Room chillers were retumed to OPERABLE status on April 8,1998.
c. A detailed roll out of this event and its implications was provided to affected design engineering personnel.
5. Corrective Steps that Will Be Taken to Avoid Further Violations a. An evaluation to determine the correct minimum SACS temperature for chiller operation without the Instrument Air system or backup pneumatic supply will be completed by August 21,1998. Temporary administrative controls are in place to ensure the backup pneumatic supply remains in service when SACS temperature is less than 70 degrees Fahrenheit (for Control Room chillers) or 62 degrees Fahrenheit (for 1E Panel Room chillers).
b. Operating procedures will be revised as necessary by September 18,1998 to include the results of the evaluation described above.
c. Lessons learned from this violation will be communicated to Engineering personnel by September 30,1998.
6. Date When Full Compliance Will be Achieved Hopi Creek achieved full compliance on April 8,1998 when the backup pneumatic supply to the chiller pressure control valves was restored.
.
i
!
!
Page 6 of 6
.
.
__
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _. _ -. _ _ _ _ _. _ _ _ _ _ _ _. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _. _ _ _ _ _ _ _ _. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _. _. _ _ _ _... _ _. _ _ _. _ _ _. _ _ _ _ _