ML20148D230
ML20148D230 | |
Person / Time | |
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Site: | Hope Creek |
Issue date: | 05/23/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
To: | |
Shared Package | |
ML20148D196 | List: |
References | |
50-354-97-02, 50-354-97-2, NUDOCS 9705300121 | |
Download: ML20148D230 (26) | |
See also: IR 05000354/1997002
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U. S. NUCLEAR REGULATORY COMMISSION
REGION I
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Docket No: 50-354
License Nos: NPF-57
Report No. 50-354/97-02
Licensee: Public Service Electric and Gas Company
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Facility: Hope Creek Nuclear Generating Station
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Location: P.O. Box 236
Hancocks Bridge, New Jersey 08038
Dates: March 18,1997 - April 28,1997
Inspectors: R. J. Summers, Senior Resident inspector
S. A. Morris, Resident inspector
G. C. Smith, Senior Physical Security inspector
E. B. King, Physical Security inspector
D. T. Moy, Reactor Engineer
J. D. Orr, Reactor Engineer
Approved by: James C. Linville, Chief, Projects Branch 3
Division of Reactor Projects
9705300121 970523
PDR ADOCK 05000354
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EXECUTIVE SUMMARY
Hope Creek Generating Station
NRC Inspection Report 50-354/97-02
This integrated inspection included aspects of licensee operations, engineering,
maintenance, and plant support. The report covers a 6-week period of resident inspection;
in addition, it includes the results of announced inspections by regional inspectors in the
areas of plant operations, physical protection and engineering support. A routine core
inspection of the security program was conducted during the period of March 17-21 and
April 14-17,1997. The conclusions and major assessment finding of that inspection are
contained in this report; however, the entire details of that inspection are contained in NRC
Inspection Report 50-272/97-07;50-311/97-07.
Operations
The inspectors concluded that operator response to the plant events was good, in that the
necessary immediate actions were taken; the events were properly classified in accordance
with the licensee's Event Classification Guide (Emergency Plan); and, NRC reporting
requirements were met. (Section 01.2)
Operators safely operated the Hope Creek Station. However, the Nuclear Shift Supervisors
were challenged with a large number of administrative tasks not directly associated with
safe and reliable plant operation. The Nuclear Shift Supervisors did not review key plant
parameters as frequently as required by the Operations Standards. (Section 01.3)
The affects on human performance were not evaluated prior to implementing a schedule
that included work weeks of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> and 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> before a scheduled day off. (Section
01.3)
Plant operations department personnel effectively identified a potential emergency diesel
generator surveillance test pre-conditioning concern, and implemented prompt and
appropriate corrective actions to resolve the issue. (Section O2.1)
A non-licensed equipment operator error resulted in operation of an emergency diesel
generator at full load with half of the cylinder petcocks in the open position, indicating a
lack of attention to detail and inadequate independent verification of petcock position
following maintenance. An engineering evaluation to determine the potential impact of this
event on future engine operation was good. (Section 04.1)
Station operators exhibited good control of the plant during both planned evolutions and
unanticipated events. (Section 04.2)
The inspectors concluded that the licensee's use of performance monitoring was good and
provided valuable assessment data regarding both human performance and equipment
performance. (Section 08.1)
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Maintenance
The observed maintenance activities were conducted properly and indicated generally good
performance in adherence with station procedures. (Section M1.1)
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The inspectors identified several examples of minor degradation of the Hope Creek plant I
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paging system and concluded that existing programmatic controls to ensure that the
system remained in an acceptable condition were not fully effective. (Section M2.1)
Enaineerina
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A safety auxiliaries cooling system temporary modification which replaced system crosstie
valves with blank flanges was adequately justified in an associated safety evaluation, and
was properly implemented in accordance with station procedures. (Section E2.1)
All current temporary modifications were appropriately scheduled for removal during or
before the next refueling outage. (Section E2.1) l
NRC inspectors discovered additional examples of inadequate implementation of the
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PSE&G scaffolding control program, indicating weaknesses in the immediate corrective
actions taken following the initial NRC identification of this concern. (Section E2.2)
i Plant Sucoort
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j The inspectors concluded that access to abandoned Unit 2 areas was positively controlled
and administered. Hope Creek management ensured that Unit 1 vital area boundaries were
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maintained and that no radioactive waste materials were stored in unauthorized locations.
', Housekeeping in the Unit 2 spaces was poor, yet did not appear to impact the material
condition of Unit 1 support equipment. (Section R1.1)
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i The inspector concluded that the licensee was maintaining the Radiation Monitor'.ng
l System (RMS) equipment properly as indicated by performance monitoring data review. In
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addition, it was also noted that the overall availability of the RMS was very good and
, showed much improvement over operations in 1995 and early 1996. (Section R2.2)
. The security program was determined to be adequate to protect public health and safety.
- Appropriate corrective actions have been implemented to address previously identified
! weaknesses in the program. The alarm station operators were knowledgeable of their
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duties and responsibilities and security training was being performed in accordance with
l the NRC-approved training and qualification plan. Protected area detection equipment
i satisfied the NRC-approved Physical Security Plan (the Plan) commitments, security
equipment testing was being performed as required by the Plan, and maintenance of
i security equipment was being performed in a timely manner as evidenced by minimal
compensatory posting associated with security equipment repairs. Based on observations
and discussions with security officers, the inspectors determined that they possessed the
' requisite knowledge to carry out their assigned duties and that the training program wus
effective. As an addition to the inspection, the UFSAR initiative, Section 4.2.2 of the Plan
, titled, " Vehicle and Cargo Controls," was reviewed. The inspcctors determined, based on
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i discussions with security supervision, procedural reviews, and observations, that vehicles
! were being searched and controlled prior to entry into the protected area as described in
the Plan and applicable procedures. (Section S)
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TABLE OF CONTENTS
EXEC UTIVE SU M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii
TABLE O F CO NT ENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . v ,
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1. O p e r a t i o n s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
I I . M ai n t e n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
111. Engineering ................................................... 10- '
I V . Pl a n t S u p p o rt . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
V. Management Meeting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18
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Report Details
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- Summarv of Plant Status
Hcpe Creek began the inspection period at 100 percent power. Full power operations were
maintained throughout the inspection period spanning March 18,1997, through April 28,
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1997, except for a power reduction to 30 percent power on April 5 and 6 to r.apport
maintenance activities including a temporary repair to a steam leak on the high pressure
- coolant injection (HPCI) and reactor core isolation cooling (RCIC) systems' steam line drain
pots' common drain line in the steam tunnel; repair a steam leak on a moisture separator
instrument; and, repair the fast acting solenoid on the No. 2 main turbine stop valve.
- Other minor power reductions occurred during the period to support maintenance and
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testing activities. At the end of the inspection period on April 28,1997, the reactor was
at 100 percent power, had operated continuously for 172 days, and was 134 days from
the beginning of its seventh refueling outage.
The licensee announced the following organizational changes during the inspection peiiod: '
On April 7,1997, the Nuclear Engineering Department was reorganized to have four
engincering directors reporting to the Senior Vice President of Engineering. The four
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directors were: Mark Reddemann, Director of Salem Design Engineering and Fuels; Mark
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McGough, Director of Plant Engineering and Projects; Gary Overbeck, Director of Hope
Creek and Component Engineering; and, Mike Rencheck, Director of Salem System
Engineering.
On April 17,1997, the Nuclear Business Unit was reorganized as follows: Leon Eliason,
- Chief Nuclear Officer; L. Storz, Senior Vice President - Operations
- E. Simpson, Senior Vice
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President - Engineering: J. McMahon, Director, Quality Assurance; and, E. Salowitz,
Director, Business Support. Among the changes in the organization responsibilities were:
creating a new organization and director position for Salem Unit 1 Recovery; moving the
Licensing function and organization into the Nuclear Engineering organization from the
former Quality Assurance / Nuclear Safety Review (QA/NSR) & Licensing organization;
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consolidating the planning functicn into the Business Support organization; and,
- consolidating the maintenance organizations for both Salem and Hope Creek into a tingle !
support organization. Key personnel assignments within the new organization were: J.
Benjamin, Director, Salem Unit 1 Recovery; M. Trum, General Manager, NBU Maintenance;
and, D. Crouch, Manager, Maintenance & Construction Planning.
1. Operations
01 Conduct of Operations
01.1 General Comments (71707)
Using Inspection Procedure 71707, the inspectors conducted frequent reviews of
ongoing plant operations. In general, the conduct of operations was professional
and safety-conscious; specific events and noteworthy observations are detailed in
the sections below.
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01.2 Operator Response to Events
Three non-emergency event notifications were made during this report period. The ;
first event involved the high pressure coolant injection (HPCI) system being declared
inoperable on March 22,1997, due to an unexpected closure of its steam supply
line containment isolation valve during system testing. Additional information on
this event and the licensee's corrective actions are found in Section M8.1 of this
report. The second event involved a report of degraded equipment (Struthers-Dunn
219 NE Series relays) necessary for accident mitigation on April 7,1997.
Additional information on this event and the licensee's corrective actions can be
found in Section M2.3 of NRC IR 50-354/97-01 and Section M8.2 of this report.
The third event involved a licensee notification of a minor oil spill to the State of
1 New Jersey Department of Environmental Protection. The inspectors concluded
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that this last event was considered minor and no additional information is provided
in this report. The inspectois further concluded that operator response to the events !
was' good, in that the necessary immediate actions were taken; the events were l
i properly classified in accordance with the licensee's Event Classification Guide
(Emergency Plan); and, NRC reporting requirements were met.
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01.3 Extended Control Room Observations
a. Insoection Scoce (71715)
- An inspector performed an extended control room observation to evaluate the
impact of Hope Creek's low Senior Reactor Operator (SRO) shift manning levels.
The inspector focused on SRO on-shift activities.
b. Observations and Findinas
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Hope Creek implemented a new schedule for on-shift SRO's on March 14,1997.
The intent of this new schedule Was to alleviate scheduling difficulties associated
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with vacation and low SRO shift manning levels. The new schedule is based on a
10 week cycle and a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> snift. This new schedule includes a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> and a 60
hour work week once every 10 week cycle. As an example, Crew E SROs are
scheduled to work 6 night shifts starting May 10,1997, followed by 3 days off,
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and then followed by 5 night shifts before another day off. The previous schedule
required on-shift SRO's to work no more than 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to a scheduled day off.
4 The inspector noted that the new schedule includes wcrk weeks that are an
exception to the nominal work week schedule definsa in Hope Creek Technical
Specification (T.S.) 6.2.2.. T.S. 6.2.2 in part requires that operating personnel
work a nominal 40-hour week while the unit is operating. Hope Creek Technical
Specifications further define the shift schedule to be based upon a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shift
with a work week of either 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> or 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. Hope Creek senior management
is taken exception to the nominal 40 hour4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> work week described in T.S. 6.2.2 due to
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the low SRO shift manning levels. Hope Creek senior management considers the
low SRO shift manning levels to be an unforeseen problem requiring overtime above
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the nominal 40 hour4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> week. T.S. 6.2.2 in part allows the use of overtime in the
event of unforeseen problems.
The inspector was concerned that Hope Creek did not evaluate the potential affects
' on human performance prior to implementing the new schedule, especially during
the extended work weeks of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> and 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br />. The inspector reviewed time
sheets for the on-shift SHOs from October 3,1996 through March 14' 1997 and he ,
verified the working hours to be within T.S. 6.2.2 requirements.
It appeared to the inspector that Nuclear Shift Supervisors (NSS) did not meet the
Operations Standards by not reviewing key plant parameters at least once per hour.
The inspector observed Nuclear Control Operators (NCO) monitoring panels as j
described by the Operations Standards. The inspector observed other instances
where control room personnel did not meet the Operations Standards. The %nior I
Nuclear Shift Supervisor (SNSS) and NSS often leaned on the inner horseshoe
. panels while conducting turnover.in the outer horseshoe area. Food was displayed
on the NCO's desk for extended periods. Personnel not assigned to the shift,
including Operations senior management, consumed food in the control room. It
appeared 14 the inspector that the Senior Nuclear Shift Supervisor did not enforce
these Operations Standards.
The inspector interviewed six on-shift SROs. Each SRO interviewed indicated a
concern with the administrative duties required of the Nuclear Shift Supervisor. The ;
' SROs feel that they are challenged to prevent administrative activities from _ i
distracting their safe' operation of the unit. It appeared to the inspector that the
NSSs spent excessive time on the computer involved with work control processes
and especially the action request process. The Operations Manager is considering-
alternatives to alleviate some of the significant administrative duties of the Nuclear
Shift Supervisor. The Operations Manager intends to add two licensed operators to
the Operations Support Staff. Full time clerical support has ben assigned to support
the Control Room. Operators interviewed considered this a significant
improvement.
The inspector observed both the SNSS and NSS to engage in activities in the NSS
Office. The NSS Office is within the control room boundary defined by Station
Operating Practices. However, the NSS Office is not in audible range of the reactor
operator at the co,1 trois nor in audible range of the control room annunciators. If
the SRO in the control room is not in audible range, he must remain in sight of the
reactor operator at the controls in accordance with Station Operating Practices.
The inspector observed both the SNSS and NSS simultaneously engage in activities
in the NSS Office and neither individual visually monitored the control room.
The inspector observed the use of " peer check" to be frequent and adequate. " Peer
check," as mentioned in this report, refers to a human performance initiative
wherein a second individual verifies correct equipment manipulation before any
action is performed.
The inspector identified a discrepancy between the Hope Creek Updated Final
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! Safety Analysis Report (UFSAR) Section 8.3.1.1.3.10 and the Hope Creek standard
- operating procedure, Emergency Diesei Generators Operation (HC.OP-SO.KJ-
- 0001(Q) Rev. 26). The UFSAR requires specific action to be taken after an
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emergency diesel generator operates longer than four hours at less than 20 percent
' rated load. Hope Creek does not track cumulative unloaded time and the actions for
i extended operation at light load conflict with the UFSAR. The licensee initiated an
- Action Request to track this issue to resolution.
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The inspector noted headphones and cables stored in a control room panel during
the performance of a seismic monitor surveillance. The licensee promptly removed
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the headphones and cables and initiated an Action Request,
c. Conclusions
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l_ Operators safely operated the Hope Creek Station. However, the Nuclear Shift i
!_ Supervisors were challenged with a large number of administrative tasks not directly
j. associated with safe and reliable plant operation. The Nuclear Shift Supervisors did
! not review key plant parameters as frequently as required by.the Operations
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- Standards. The affects on human performance were not evaluated prior to
j implementing a schedule that included work weeks of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> and 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> before
a scheduled day off.
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{ 02 Operational Status of Facilities and Equipment
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02.1 Pre-Conditionina of Emeraency Diesel Generator Air Start Valves
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l a. Insoection Scooe (62707,61726)
[ The inspectors evaluated the Hope Creek operations department response to an
l' industry operating experience feedback issue involving pre-conditioning of
i emergency diesel generator (EDG) air start valves.
- b. Observations and Findinas
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On April 10,1997, operations department staff personnel determined that the
!- manner in which Hope Creek operators prepared the EDG's for monthly operability l
h surveillance testing was similar to the process employed by another nuclear utility i
{ . which had recently been issued a Notice of Violation for preconditioning the engine
j for successful testing. Specifically, operators typically "bar-over" the EDG's using
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l the air start system to implement a vendor recommendation to remove accumulated
moisture in the engine cylinders when the machine has not been operated within the
j. ' previous 7 days.- However, as a result of the industry experience, operations and
- engineering department management appropriately concluded that the Hope Creek
- practice constituted pre-conditioning the air start valves, effectively nullifying the
j validity of the subsequent surveillance test. As a result, the operations department
i issued a " night order" to the operating shifts to ensure that, until this concern could
4 be fully evaluated, all EDG pre-start evolutions would include barring-over the '
engines using a an alternate air supply.
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The inspectors observed that operations personnel appropriately entered this issue
into the station's corrective action program for condition evaluation, reportability
review, and corrective action development. Additionally, the inspectors witnessed
operations training department instructors in the field with equipment operators
demonstrating the use of the alternate air supply and EDG manual barring device.
The inspectors questioned whether this issue should have been identified earlier as
part of the recently completed Technical Specification Surveillance improvement
Project (TSSIP). However, it was subsequently determined that finding an issue of
this nature, i.e. potential pre-conditioning mechanisms, was outside the scope of
the TSSIP review,
c. Conclusions
Plant operations department personnel effectively identified a potential emergency
diesel generator surveillance test pre-conditioning concern, and implemented prompt
and appropriate corrective actions to resolve the issue.
04 Operator Knowledge and Performance
04.1 Observation of "C" Emeroency Diesel Generator Surveillance Test
a. Insoection Scoce (61726)
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The inspectors witnessed a periodic technical specification surveillance test of the
"C" Emergency Diesel Generator (EDG). Interviews with the personnel responsible
for implementing and supervising the activity were conducted, as was a detailed
test procedure review.
b. Observations and Findinas
On April 23,1997, the inspectors observed plant equipment operators (EO)
completing the field portions of surveillance test procedure HC.OP-ST.KJ-0003(Q)
for the "C" EDG. This test was required to implement the requirements of TS 4.8.1.1.2. Three different EOs were assigned to perform various portions of the
field activities. One of the pre-startup activities required to support EDG test
operation involved "barring-over" the engine with air to remove moisture which may
have accumulated in the cylinders. At Hope Creek, small petcocks installed on each
of the 12 EDG cylinders are installed which, if opened, permit compressed gaces in j
the cylinders to vent to the room housing the engine. By procedure EOs open then I
close these petcocks during the barring-over process to ensure moisture is
eliminated.
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Prior to engine start, the inspectors verified that the barring-over process was l
completed by reviewing the field copy of the test procedure and by questioning the
EOs. However, once control room operators started and fully loaded the "C" EDG, I
it was evident that some of the petcocks had been left in the open position because
of smoke and unusual noise emanating from one side of the engine. The field EOs
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promptly recognized that 6 of the 12 petcocks had been left open and closed them
without incident. The responsible EO, a relatively new employee, drafted an action
request in accordance with the corrective action program to document the
occurrence.
The inspectors discussed the implications of this event with cognizant station
operators and managers, including a discussion of a similar event which occurred on
this same EDG in February of 1996 (see NRC Inspection Report 50-354/96-80).
Additionally, the inspectors reviewed the fact finding summary completed by the
operations department to validate stated causal factors, safety significance, and
generic implications. The inspectors agreed with PSE&G's assertion that the event
was caused by human error (inattention to detail, inadequate skills or knowledge,
lack of experience), but further judged that this error was clearly a failure to adhere l
to the operating procedure for barring-over the EDG. Further the inspectors l
quesDned the lack of independent verification of petcock position following '
operation. The inspectort, noted that operations management conducted i
coaching / counseling sessions with the responsible individual, and reinforced I
expectations for procedural adherence before allowing him to resume shift
responsibilities. Additionally, station personnel were evaluedng the need for
independent verification and/or whether a " peer check" process was necessary to
ensure that future petcock operations would be correct.
The "C" EDG surveillance was completed satisfactorily, and a post-event
engineering analysis concluded that operating the EDG at fullload with 6 petcocks
open did not result in any consequence to the machine. However, the inspectors
judged that the failure to shut the EDG cylinder petcocks following pre-startup
evolutions constituted a violation of HC.OP-SO.KJ-0001(Q), "EDG System
Operation" (VIO 50-354/97-02-01).
c. Conclusions
A non-licensed equipment operator error resulted in operation of an emergency
diesel generator at fullload with half of the cylinder petcocks in the open position,
indicating a lack of attention to detail and inadequate independent verification of
petcock position following operation. An engineering evaluation to determine the
potential impact of this event on future engine operation was good.
04.2 Ooerations Shift Performance Observations I
The inspectors observed control room operators and equipment operators in the I
field respond to various transient events at the station, both planned and unplanned.
Specifically, the inspectors witnessed unplanned trips of the "A" control room
ventilation system and the "A" control rod drive hydraulic pump, the latter of which
led to several control rod hydraulic control unit accumulator low pressure alarms.
Additionally, pre-planned transfers of reactor protection system power supplies and
steam jet air ejectors were observed. Both of these evolutions had the potential to
induce significant plant transients if performed incorrectly, Finally, the inspectors
observed operators conduct a significant plant power reduction to support emergent
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corrective maintenance in the steam tunnel. l
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The inspectors noted that in all cases, operators appropriately employed the
procedural guidance applicable for each event or evolution. Good command and
control of the evolutions were evident. Operators logs accurately reflected each of
the events / evolutions after they were completed. Overhead alarms were promptly
acknowledged and evaluated. Technical specification action statement entries were
. made as required. Where appropriate, operators initiated action requests in
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accordance with the PSE&G corrective action program to determine root cauces and
corrective actions.
Station operators exhibited good control of the plant during both planned evolutions
and unanticipated events.
08 Miscellaneous Operations issue
08.1 Operations Performance Monitorina
The inspectors reviewed the licensee's current performance monitoring practices
and observed regular management discussions based on the performance
monitoring indications. The licensee frequently discusses the aggregate impact of
plant deficiencies and assesses the nature of the deficiencies to ensure that
corrective actions are timely and effective. The inspector noted that the
performance monitoring indicators show some improvement in reducing control
room deficiencies. However, other indicators, such as the " cumulative unplanned
LCO hours indicator," show some weakness in schedule adherence by plant
personnel and an increasing equipment failure rate. Overall, the inspector concluded
that the licensee's use of performance monitoring was good and provided valuable
assessment data regarding both human performance and equipment performance.
II. Maintenance
M1 Conduct of Maintenance !
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M 1.1 General Comments '
a. insoection Scoce (62707. 61726)
The inspectors observed all or portions of the following maintenance and ,
surveillance activities: i
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HPCl/RCIC common drain pot drain line temporary leak repair by
encapsulation
"B" reactor protection system (RPS) motor-generator set repair
"A" service water system (SWS) pump replacement and screen repair
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"E" filtration, recire, and ventilation system (FRVS) " Hiller" valve replacement
Agastat and Struthers-Dunn relay replacements
"B" steam Jet air ejector (SJAE) pressure control valve emergent repair
"A" control rod drive (CRD) pump troubleshooting
"C" emergency diesel generator (EDG) 184-day surveillance test
b. Observations and Findinas
Except for the previously noted problem noted with observed equipment operator
performance during the conduct of the "C" EDG 184-day surveillance test (see
Section 04.1), the inspector observed generally good work coordination between ,
operations, radiation protection, maintenance and engineering departments in the I
conduct of the above activities. For example, good ALARA practices were l
observed for the encapsulation of the HPCl/RCIC drain line that was leaking into the
steam tunnel. Also, good Station Operations Review Committee (SORC) reviews of ;
the proposed temporary repair method and development of specific monitoring !
conditions for the degraded pipe and its affect on nearby safety-related equipment
were observed by the inspectors.
c. Conclusions - l
The inspectors concluded that the observed maintenance activities were conducted l
properly and indicated generally good performance in adherence with station
procedures.
M2 Maintenance and Material Condition of Facilities and Equipment
M2.1 - Dearadation of the Plant Paaina (Gai-Tronics) System
During routine tours of the Hope Creek station, the inspectors noted several areas
of the plant in which it was difficult to hear station-wide plant page '
announcements. Subsequent investigation resulted in the identification of several
paging system speakers that were either not functioning or were barely audible.
Individual action requests were drafted to initiate work orders to correct each of the
deficiencies noted by the inspectors. However, after the inspectors raised the
possibility of a potential programmatic concern with respect to paging system
monitoring and maintenance, station management initiated a level 2 condition report
to evaluate the full extent of the condition and to develop any necessary corrective i
actions.
The inspectors reviewed the UFSAR section which describes the Hope Creek paging
system operation and design basis. Wnile information regarding system monitoring l
and maintenance was not specific, in general the inspectors concluded that the -
station was maintaining the system in an adequate condition. Station management l
agreed that more stringent programmatic controls for ensuring that the paging
system remained fully functional were necessary.
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The inspectors identified several examples of minor degradation of the Hope Creek
plant paging system and concluded that existing programmatic controls to ensure
that the system remained in an acceptable condition were not fully effective.
M8 Miscellaneous Maintenance issues
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M8.1 (Closed) LER 50-354/97-06: High Pressure Coolant injection isolation Due to
Personnel Error During Functional Testing. This event involved an automatic
isolation of the HPCI system steam line containment isolation valve that occurred on i
March 22,1997 during the performance of a scheduled functional test of the high !
drywell pressure instrumentation. Based on the licensee investigation into the I
cause of this event, it was determined that the technician conducting the
aforementioned test erroneously inserted test leads into a test point associated with l
the HPCI isolation logic causing the event. This test point was located just above l
the test point that the technician was supposed to use. The licensee's corrective
'
actions included: restoring the isolated HPCI system to proper lineup; reporting the
event to the NRC via both 10 CFR 50.72 and 10 CFR 50.73, as required; taking
appropriate disciplinary action with involved personnel; and, communicating the
nature of the event with all station personnel, as well as conducting specific
lessons-learned training with l&C technicians. The inspector concluded that the
licensee's actions promptly corrected this procedure adherence inadequacy. This
licensee identified and corrected violation is being treated as a Non-Cited Violation,
consistent with Section Vll.B.1 of the NRC Enforcement Poliev.
M8.2 LOcen) URI 50-354/97-01-02: The licensee informed the NRC of potential failure of
Struthers-Dunn 219 NE series relays, used in a variety of safety-related applications
at the plant. The licensee had observed an increasing trend in failures and then
identified that the failures were related to wrong or missing bearing pad materials
leading to thermal degradation and ultimate failure of the components. On April 23,
1997, the licensee provided additional information regarding observations of the
affected relays to NRC representatives for vendor inspection and event assessment
and generic communications. The licensee stated that it planned to submit an LER ,
about this concern in early May 1997. The inspector concluded that the licensee's I
efforts to date were comprehensive. The licensee confirmed the failure mechanism
and failure modes with the vendor and have taken appropriate action to ensure that
affected relays in safety-related applications are known to be functional. This
matter remains open pending review of the licensee's planned LER submittal.
M8.3 {Q. pen) LER 50-354/97-05 and URI 50-354/97-01-04: Operation in a Technical
Specification Prohibited Condition due to Failure to Perform Monthly Flowpath
Verification Surveillance Checks of the Residual Heat Removal (RHR) System
Crosstie Valves. This event documents part of the licensee evaluation of an NRC
identified concern with a modification to the RHR system providing crosstie
flowpaths for the "C" and "D" RHR pumps. This concern is identified in Section
E1.1 of NRC IR 50-354/97-01. This LER specifically addresses the fact that after
implementation of the modification to the "C" RHR subsystem in 1994, the licensee
failed to revise appropriate surveillance and operating procedures to ensure that the
associated low pressure coolant injection (LPCI) flowpath was maintained properly.
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Failure to ensure the flowpath alignment was considered by the licensee to be a
violation of technical specification surveillance requirements. The LER further
described that this condition was corrected in December 1995 when the crosstie
isolation valve was locked closed. The inspector noted that additional evaluations
of this problem were in progress at the close of the inspection period. The
inspector considered this matter to be open pending further NRC review of the
crosstie modification package.
M8.4 (Closed) LER 50-354/95-033. Sucolement 14 and VIO 50-354/95-11-02: Technical
Specification Surveillance Requirement Implementation Deficiencies. This final
supplemental report documents the last findings of the licensee's Technical
Specification Surveillance Improvement Program (TSSIP). The TSSIP identified two
additional surveillance deficiencies associated with the containment hydrogen
recombiner system and the rod block monitor. Both surveillance deficiencies were
corrected by performance of appropriate testing; however, additional modifications
were necessary to fully resolve the rod block monitor concerns. Overall, the
inspectors concluded that the licensee actions to identify and correct the
surveillance test deficiencies were broad and comprehensive. The conditions
leading to the violation cited in NRC IR 50-354/95-11 have been fully evaluated by
the licensee and corrected. The surveillance test procedures have been corrected to
ensure that the technical specification surveillance requirements were being
appropriately implemented. The inspector concluded that the licensee's corrective
actions were reasonable and complete.
Ill. Enaineerina
E2 Engineering Support of Facilities and Equipment
E2.1 Safety Auxiliaries Coolina System Temocrary Modification
a. Insoection Scope (37551)
The inspectors performed a detailed review of a temporary modification recently
installed in the safety auxiliaries cooling system (SACS). This review included an
assessment of the associated 10 CFR 50.59 safety evaluation, documents and
drawings which describe the operation of the affected system, and an in-plant
walkddown of the modified components. Additionally, the number and status of all
active temporary modifications at Hope Creek were reviewed
b. Observations and Findinas
Hope Creek personnel installed temporary modification 96-023 in the SACS system
on March 21,1997, which replaced two spent fuel pool cooling system heat
exchanger crosstie valves (1EGV-545 and 1EGV-547) with blank flanges. PSE&G
deemed this modification necessary to minimize the " sluicing" effect between the
two independent SACS loops caused by excessive valve seat ic:Aege. The
inspectors independently reviewed the safety evaluation that justified
11
implementation of this modification, and judged that it satisfied the requirements of
10 CFR 50.59 and the licensee internal " Control of Temporary Modifications"
procedure NA.NC-AP.ZZ-0013(Q).
In addition to the safety evaluation review, the inspectors verified that the affected
piping and instrumentation drawings were revised to reflect the modified system
configuration. Finally, field implementation of the modification was appropriate and
was conspicuously labeled as temporary. The temporary modification log in the
Hope Creek work control center also correctly tracked this modification. The
inspectors noted that this modification would have to be removed prior to spent fuel
pool operations in the upcoming refueling outage in order to support the planned full
core offload.
The inspectors observed that at the close of the reporting period, there were 24
active temporary modifications installed at the station,17 of which were l
implemented subsequent to the last refueling outage. The oldest temporary J
modification, involving water intrusion into the primary containment instrument gas )
system, was installed in September 1994. The inspectors noted that all of the
modifications were scheduled for removal before or during the next refueling
outage.
c. Conclusions
A safety auxiliaries cooling system temporary modification which replaced system
crosstie valves with blank flanges was adequately justified in an associate safety
evaluation, and was properly implemented in accordance with station procedures.
.
Additionally, all current temporary modifications were appropriately scheduled for
removal during or before the next refueling outage.
E2.2 Follow Up to Previousiv identified Temocrary Structure Control Problems (Open) VIO i
50-354/97-01-05 I
a. Insoection Scoce (37551. 92903)
The inspectors conducted follow up reviews of Hope Creek's scaffolding control
program to determine the effectiveness of short term corrective actions stemming
from previously identified concerns. The NRC isaued a Notice of Violation in
inspection Report 50-354/97-01 for inadequate controls associated with scaffold
implementation and tracking,
b. Observations and Findinas
PSE&G's immediate response to the violation regarding effective control of
temporary scaffolding, documented in detail in Inspection Report 50-354/97-01, in
part included a detailed walkdown of all accessible areas at the station to locate
installed scaffolding, and a " roll out" to all maintenance and engineering personnel
reinforcing the expectation that internal administrative controls for scaffolding be
effectively implemented. However, during a reactor building walkdown on April 14,
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1997, several weeks after initially identifying the problems, the inspectors
discovered additional examples of inadequate scaffold control and implementation.
Additionally, unlike the original concerns, the inspectors identified scaffolding
installed in the plant which was used for equipment protection and for structural
support for temporary lead shielding which was not tracked or inspected as required
by PSE&G's administrative control procedure, NA.NC-AP.ZZ-0023 (NAP-23).
The inspectors met with station engineering management to discuss the newly
identified issues. During this discussion PSE&G indicated that it had validated the
inspectors recent findings, and admitted that the short term actions implemented
subsequent to the initial findings were ineffective. Engineering management stated
that most of the newly identified scaffolds with inadequate controls were
constructed following initial communication of the concerns nearly one month prior.
As a result, Hope Creek management upgraded the condition report which tracked
this issue from a level 2 (determine apparent cause) to a level 1 (detailed root cause
analysis). All the newly discovered problems were promptly corrected. Further,
PSE&G as a whole planned to centralize the scaffold construction and control
function in an effort the better control the efficiency and consistency of the
program.
The inspectors considered the scaffolding construction and control problems
identified subsequent to the initial findings as additional examples of the same 1
violation cited in the NRC Inspection Report noted above; specifically, PSE&G )
personnel failed to implement adequately the requirements of NAP-23. l
c. Conclusions
NRC inspectors discovered additional examples of inadequate implementation of the
PSE&G scaffolding control program, indicating weaknesses in the immediate
corrective actions taken following the initial NRC identification of this concern.
E8 Miscellaneous Engineering issues
E8.1 Licensee Service Water System Ooerational Performance insoection:
a. Insoection Scope 40501
A region-based inspector observed portions of the licensee's Service Water System
Operational Performance Inspection (SWSOPI). The licensee's evaluation of the
safety auxiliary cooling system (SACS) was not yet complete,
b. Observations and Findinas
The inspector noted the following: (1) SWS analyses were detailed; (2) recent root
cause analyses were thorough; and, (3) previous engineering self-assessments on
SWS had identified many of the issues found during the SWSOPl.
13
Most notably, the licensee's self-assessment tearn found that: (1) corrective actions
implemented to monitor for SWS strainer problems were not effective; (2) the
implementation of corrective actions from past self-assessments were not in all
cases complete and timely; (3) performance monitoring for the SACS heat I
exchangers was weak; (4) instances of inadequate 10 CFR 50.59 safety
evaluations; and, (5) some weaknesses in configuration control for design
calculations.
c. Conclusions
The inspector concluded that the licensee's SWSOPl self assessment effort, to date
was thorough. Further NRC observation of the SACS portion of the self-assessment
is on going.
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IV. Plant Support 1
R1 Radiological Protection and Chemistry (RP&C) Controls
R1.1 Walk Down of (Abandoned) Hooe Creek Unit 2 Spaces
On April 28,1997, the inspectors conducted a comprehensive tour of abandoned
Hope Creek Unit 2 buildings to verify that these areas were not being used for
unauthorized radioactive waste storage and that vital area boundaries to Unit 1
spaces were adequately posted and controlled. Housekeeping and material
condition of Unit 1 support equipment in the Unit 2 spaces were also evaluated.
. The inspectors did not identify any areas of the Unit 2 facility that contained
radioactive waste material. There were some areas of Unit 2 that required
radiologically controlled area postings because of radiation fields induced by the
Unit 1 offgas system; these postings were deemed adequate. Further, all of the
Unit 1 vital area boundaries which interfaced with Unit 2 structures wcre adequately
posted and positively secured. Housekeeping in all of the Unit 2 areas was poor, in
stark contrast to the conditions typically observed in the occupied Unit 1 spaces.
Most of the debris in the areas was left over from initial construction, in spite of
this assessment, the inspectors judged that none of the Unit 1 support equipment
located in Unit 2 spaces (e.g. auxiliary boiler steam, telecommunications wiring and
junction boxes, etc.) would likely be affected by the adverse conditions.
Additionally, none of the noted Unit 1 support equipment was classified as safety-
related.
The inspectors noted that access to the Unit 2 spaces was effectively controlled in
that relatively few senior PSE&G individuals had keys to associated door locks.
Additionally, a current station administrative procedure provided positive controls to
ensure that all personnel entries into the Unit 2 spaces would be conducted safely.
The inspectors concluded that access to abandoned Unit 2 areas was positively
controlled and administered. Hope Creek management ensured that Unit 1 vital
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area boundaries were maintained and that no radioactive waste materials were
stored in unauthorized locations. Housekeeping in the Unit 2 spaces was poor, yet
did not appear to impt e the material condition of Unit 1 support equipment.
R2 Status of RP&C Facilitit - J Equipment
R2.1 Revised TLD Guidelines
On April 1,1997, the licensee revised the TLD guidelines at the site. The new
guidelines now rouuire allindividuals with radiological controlled area (RCA) access
to be issued a ' O. All radiation workers will be required to wear their TLD and en
electronic dosimeter while in the RCA. The inspector observed personnel in the
RCA after implementation of these new guidelines and found their performance
acceptable.
R2.2 Radiation Monitorina System (RMS) Performance Indicators
The inspector reviewed the licensee's RIVS performance indicators to ascertain that
the licensee was properly maintaining the equipment available for process
monitoring of effluents. The inspector observed that, except for the South Plant
Vent RMS, that all effluent monitors were being maintained available in excess of
95 percent available. The South Plant Vent RMS annual average was in excess of
85 percent available; however, some of this out-of-service time was necessary to
implement improvements to the system. The inspector concluded that the licensee
was maintaining the equipment properly as indicated by the performance
monitoring. In addition, the inspector noted that the overall availability of the RMS
was very good and showed much improvement over operations in 1995 and early
1996.
P5 Staff Training and Qualification in EP
P5.1 Unannounced Off-hours Callout Trainino Drill Cr...gue rieview
The inspector reviewed the subject critique, dated April 16,1997, to ascertain that
the critique assessed performance of the drill responders appropriately and provided
reasonable assurance that performance objectives were met. The inspector noted
that the critique provided an overall assessment that drill performance met
expectations. There were a few areas identified requiring corrective actions or
improvements; but, none of these items were considered significant by the
inspector. Overall, the licensee's drill conduct was good and the inspector
considered this activity as providing good traing for the responders.
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i S1 Conduct of Security and Safeguards Activities
A routine core inspection of the security program was conducted by Messrs. G. C.
Smith and E. B. King during the period of March 17-21 and April 14-17,1997.
Areas inspected included: previously identified items; protected area barriers and
detection aids; alarm stations and communications; testing, maintenance and
compensatory measures; training and qualification; organization and administration;
quality assurance; and security and safeguards activities. The security inspection
feeder report was integrated into the Salem routine resident inspection report, IR
50-272/97-07 50-311/97-07. The conclusions and overall executive summary
assessment from that inspection are included in this inspection report, however, the
supporting inspection details are documented in the referenced Salem inspection
report only.
The inspectors determined that the licensee was conducting its security and
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safeguards activities in a manner that protected public health and safety.
S2 Status of Security Facilities and Equipment
On April 16,1997, the inspectors determined by observation, that the actions taken
by the licensee to correct the concern were adequate. The inspectors determined
that the height of the Protected Area Barrier (PAB) satisfied the requirements of the
Plan and that the intrusion Detection Systems (IDSs) were functional and effective,
and were installed and maintained as described in the Plan.
The inspectors determined by discussions with the Central Alarm Station / Secondary
Alarm Station (CAS/SAS) operators on April 16,1997, that the actions taken by the
licensee to reiterate expectations concerning alarm assessment were effective. The
determination was based on the CAS/SAS operators' responses to the inspectors'
questioning. The CAS/SAS operators were knowledgeable of their alarm
assessment responsibilities and the alarm stations and communications met the
licensee's Plan commitments and NRC requirements.
Documentation on file, reviewed April 16,1997, confirmed that security equipment
was being tested and maintained as required; however, failures of search equipment
were not being documented in the test records. The licensee agreed to change its
practice to allow for tracking and trending of equipment failures found during
testing. Repair work was timely and the use of compensatory measures was found
to be appropriate and minimal.
SS Security and Safeguards Staff Training and Qualification
The inspectors determined that training had been conducted in accordance with the
Training and Qualification (T&O) Plan. Based on the Security Force Members'
(SFM) responses to the inspectors' questions and the inspectors' observations, the
training provided by the security training staff was considered effective.
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S6 Security Organization and Administration
Management support for the physica! security program was determined to be
adequate. No problems with se eganizational structure that would be detrimental
to the effective implementation of the security and safeguards programs were
observed or reported.
S7 Quality Assurance in Security and Safeguards Activities
The inspectors concluded that the self-assessment program in place to identify,
prevent and resolve potential problems was weak and an improved self-assessment
program would enhance program effectiveness.
The review concluded that the audit was comprehensive in scope and depth, that
the findings were appropriately distributed and addressed and that the audit
program was being properly administered.
S8 Misce!Ianeous Security and Safeguards issues
S81. (Closed) Insoection Followuo item 50-272. 50-311. 50-354/93-28-01 - Review the
effectiveness of assessment aids after upgrade is complete. The program to
upgrade the assessment aids has been completed and the assessment aids were
determined to be adequate to perform their intended function.
S8.2 (Closed) Violation 50-272, 50-311, 50-354/96-10-03 - Failure to control
badge /keycards and failure to display photo badges in the protected area. The
inspectors verified the corrective actions described in the licensee's recponse letter,
dated February 26,1997, to be reasonable and complete and they were found to be
properly implemented. No similar problems were identified.
S8.3 (Closed) Violation 50-272. 50-311, 50-354/EA96-344-01013 - Failure to exercise
positive access control over photo badge keycards thereby creating the opportunity
for unauthorized access to the vital areas. The inspectors verified that corrective
actions described in the licensee's response to letter, dated January 10,1997, to
be reasonable and complete and they were found to be properly implemented. No
similar problems were identified.
S8.4 1 Closed) Violation 50-272, 50-311, 50-354/EA96-344-02013 - Failure to conduct a
physical pat-down search of a contractor that had caused two portal metal
detectors to alarm on three different attempts to pass through them, although these
alarms provided reasonable cause to suspect that the contractor was attempting to
introduce firearms, explosives, incendiary devices, or other unauthorized material
into the protected area, before issuing him a photo badge keycard, and allowing him
to enter the protected area. The inspectors verified the corrective actions described
in the licensee's response letter dated January 10,1997, to be reasonable and
complete and they were found to be properly implemented. No similar problems
were identified.
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S8.5 (Closed) Violation 50-272, 50-311, 50-354/EA96-344-02023 - Failure to notify the
senior nuclear shift supervisor (SNSS) of a security threat when a contractor that
] should have received a pat-down search entered the protected area without a pat-
down search. The failure to notify the SNSS resulted in the event not being
classified per Event Classification Guide 16. The inspectors verified the corrective
, actions described in the licensee's response letter, dated January 10,1997, to be
reasonable and complete and they were found to be properly implemented. No
similar problems were identified.
S8.6 LQlosed) Violation 50-272. 50-311, 50-354/EA96-344-03014 - Failure to inactivate
the security photo badges and personnel access clearance for 12 employees
terminated in June and July 1996 within two working days of termination of
employment. The inspectors verified the corrective actions described in the
licensee's response letter, dated January 10,1997, to be reasonable and complete
and they were found to be properly implemented.
S8.7 (Closed) Violation 50-272, 50-311, 50-354/EA96-344-04014 - Failure of two
security supervisors to qualify in all required critical security tasks prior to being
assigned field operations supervisor duties. The inspectors verified the corrective
actions described in the licensee's response letter, dated January 10,1997, to be
reaconable and complete and they were found to be properly implemented. No
similar problems were identified.
S8.8 (Closed) Violation 50-272, 50-311, 50-354/EA96-344-05014 - Failure to complete
all required tests of an alarm zone prior to releasing the security force member
posted at the alarm zone. The inspectors verified the corrective actions described
int he licensee's response letter, dated January 10,1997, to be reasonable and
complete and they were found to be properly implemented. No similar problems
were identified.
S8.9 Environmental Activist Rally on April 28,1997
The environmental activist group, Environmental Response Network, in cooperation
with Greenpeace and several other environmental organizations conducted a rally
and press conference on April 28,1997, to protest the planned restart of the Salem
Generating Station. The inspectors observed the licensee's planning and
coordination with locallaw authorities to ensure that the planned demonstration
was conducted in a safe manner and would pose no threat to operat:ons at the
Hope Creek facility. Ths inspector observed good coordination with the local law
authorities, as well as good implementation of enhanced monitoring of the facility
surround;ngs for threat assessment. The demonstration was completed peacefully
with no affect on the plant.
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V Manaaement Meetinas
X1 Exit Meeting Summary
A recent discovery of a licensee operating its facility in a manner contrary to the UFSAR
description highlighted the need for a special focused review that compares plant practices,
procedures, and parameters to the UFSAR description.
I
The inspector identified a discrepancy between the Hope Creek Updated Final Safety
Analysis Report (UFSAR) Section 8.3.1.1.3.10 and the Hope Creek standard operating
procedure Emergency Diesel Generators Operation (HC.OP-SO.KJ-0001(Q) Rev. 26). The
UFSAR requires specific actico to be taken after an emergency diesel generator operates
longer than four hours at lets than 20 percent rated load. Hope Creek does not track
cumulative unloaded time and the actions for extended operation at light load conflict with
the UFSAR.
Since the UFSAR does not specifically include security program requirements, the
inspectors compared licensee activities to the NRC-approved physical security plan, which
is the applicable document. While performing the inspection discussed in this report, the
inspectors reviewed Section 4.2.2 of the Plan, titled " Vehicle and Cargo Control," the
inspectors determined, based on discussions with security supervision and reviews of
applicable procedures and records, that vehicles were bemg searched and controlled prior
to entry into the protected area as described ir. the Plan and applicable procedures.
The inspectors presented the inspection results to members of licensee management at the
conclusion of the inspection on May 9,1997. The licensee acknowledged the findings
presented.
The inspectors asked the licensee whether any materials examined during the inspection
should be considered proprietary. No proprietary information was identified.
X3 Management Meeting Summary
On April 15 and 16,1997, William L. Axelson, Deputy Regional Administrator for Region I
and James C. Linville, Chief of the Reactor Projects Branch No. 3, Region I, toured the
Hope Creek and Salem facilities and met with representatives of both organizations. There
were no significant findings during the management tour.
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INSPECTION PROCEDURES USED
IP 37550: Engineering
IP 37551: Onsite Engineering
IP 61726: Surveillance Observations
IP 62707: Maintenance Observations
IP 71707: Plant Operations
IP 71715: Extended Control Room Observations
ITEMS OPENED, CLOSED, AND DISCUSSED
_O2p.e_ned
30-3S4/97-02-01 VIO Operators failed to follow procedure for testing the
50-354/97-005 LER Failure to perform monthly technical specification
flowpath verification surveillance checks of the LPCI
system (RHR crosstie valves)
Closed
50-354/97-006 LER High pressure coolant injection isolation due to
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personnel error during functional testing
k 50-453/95-033 LER Technical specification surveillance requirement
deficiencies
50-354/95-11-02 VIO Technical specification surveillance requirement
performance deficiencies
50-354/96-10-03 VIO Failure to control and display photo-badge keycards for
the protected area
50-354/EA96-344-01013 VIO Failure to exercise positive access control over photo-
badge keycards
50-354/EA96-344-02013 VIO Failure to conduct a required physical pat-down search
of a contractor
50 954/EA96-344-02023 VIO Failure to properly notify the nuclear shift supervisor of
a security threat in a timely manner
50-354/EA96-344-03014 VIO Failure to inactivate photo-badge keycards for 12
terminated employees
50-354/EA96-344-04014 VIO Failure of two security supervisors to qualify in all
required critical tasks prior to being assigned to duty
50-354/EA96-344-05014 VIO Failure to complete all required tests of an alarm zone
prior to release of the post
Discussed
50-354/97-01-02 URI Degraded safety-related Agastat and Struthers-Dunn
relays
50-354/97-01-04 URI RHR system crosstie modification
50-354/97-01-05 VIO Failure to properly control temporary structures -
scaffold, etc., in safety-related areas.
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PARTIAL LIST OF PERSONS CONTACTED
Licensee
M. Trum Director, Nuclear Operations Support
G. Gibson Manager, Nuclear Security
J. DeFabo Supervisor, Quality Assessment
M. Ivanick Sr. Security Regulato;y Specialist
C. Weiser Security Engineer
A. Kaplinger Superintendent, Loss Prevention
J.Zudans Manager, Hope Creek Design Engineering
J. Pollock Manager, Quality Assurance
P. Roberts Manager, Hope Creek System Engineering
M. Meltzer, Superintendent, Hope Creek Chemistry
W. Mattingly Supervisor, Hope Creek Quality Assurance
T. Cellmer, Superintendent, Hope Creek Radiation Protection
S. Jones, Manager, Plant Maintenance
L. Wagner, Manager, Hope Creek Operations
M. Bezilla, General Manager, Hope Creek Operations
L. Storz, Senior Vice President - Operations
Contractor
R. Cogdall Project Manager, The Wackenhutt Corporation
,
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LIST OF ACRONYMS USED
HPCl High Pressure Coolant injection
RCIC Reactor Core Isolation Cooling
<
SRO Senior Reactor Operator
NCO Nuclear Control Operator
NSS Nuclear Shift Supervisor
SNSS Senior Nuclear Shift Supervisor
EDG Emergency Diesel Generator
TSSIP Technical Specification Surveillance Improvement Project
EO Equipment Operators
LCO Limiting Condition for Operation
SORC Station Operations Review Committee
SWS Service Water System
FRVS Filtration, Recirculation, and Ventilation System
CRD Control Rod Drive
LPCI Low Pressure Coolant injection
SACS Safety Auxiliaries Cooling System
SWSOPl Service Water System Operational Performance inspection
RCA Radiological Controlled Area
RMS Radiation Monitoring System
PDR Public Document Room
NRC Nuclear Regulatory Commission
PSE&G Public Service Electric and Gas
SFM Security Force Members
OA Quality Assurance
QA/NSR Quality Assurance / Nuclear Safety Review
PA Protected Area
T&Q Training and Qualification
IDS Intrusion Detection Systems
CAS Central Alarm System
SAS Secondary Alarm System
UFSAR Updated Final Safety Analysis Report
CCTV Closed Circuit Television
1/