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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:RO)
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A9151999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Shearon Harris Npp. with 991012 Ltr ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18017A8621999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Harris Nuclear Plant.With 990908 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18017A8361999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Shearon Harris Nuclear Power Plant.With 990811 Ltr ML18016B0151999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Shearon Harris Npp. with 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990614 Ltr ML18017A8981999-05-12012 May 1999 Technical Rept Entitled, Harris Nuclear Plant-Bacteria Detection in Water from C&D Spent Fuel Pool Cooling Lines. ML18016A9581999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990513 Ltr ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8941999-04-0505 April 1999 Revised Pages 20-25 to App 4A of non-proprietary Version of Rev 3 to HI-971760 ML18016A9101999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Shearon Harris Nuclear Power Plant.With 990413 Ltr ML18016A8661999-03-31031 March 1999 Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept. ML18017A8931999-02-28028 February 1999 Risks & Alternative Options Associated with Spent Fuel Storage at Shearon Harris Nuclear Power Plant. ML18016A8551999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Shearon Harris Npp. with 990312 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8531999-02-18018 February 1999 Non-proprietary Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFP 'C' & 'D'. ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18022B0631999-02-0404 February 1999 Rev 0 to Nuclear NDE Manual. with 28 Oversize Uncodable Drawings of Alternative Plan Scope & 4 Oversize Codable Drawings ML20202J1161999-02-0101 February 1999 SER Accepting Relief Requests Associated with Second 10-year Interval Inservice Testing Program ML18016A8041999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Shearon Harris Nuclear Power Plant.With 990211 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7801998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Shearon Harris Npp. with 990113 Ltr ML18016A7671998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Shnpp,Unit 1.With 981215 Ltr ML18016A9731998-11-28028 November 1998 Changes,Tests & Experiments, for Harris Nuclear Plant.Rept Provides Brief Description of Changes to Facility & Summary & of SE for Each Item That Was Implemented Under 10CFR50.59 Between 970608-981128.With 990527 Ltr ML18016A8351998-11-28028 November 1998 ISI Summary 8th Refueling Outage for Shearon Harris Power Plant,Unit 1. ML18016A7411998-11-25025 November 1998 Rev 1 to Shnpp Cycle 9 Colr. ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A7071998-11-0303 November 1998 Rev 0 to Harris Unit 1 Cycle 9 Colr. ML18016A7201998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Shearon Harris Nuclear Power Plant.With 981113 Ltr ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves ML18016A6201998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Harris Nuclear Power Plant.With 981012 Ltr ML18016A5971998-09-21021 September 1998 Rev 1 to Harris Unit 1 Cycle 8 Colr. ML18016A5881998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Shnpp,Unit 1.With 980914 Ltr ML18016A5071998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Shearon Harris Nuclear Plant.W/980811 Ltr ML18016A9431998-07-0707 July 1998 Rev 1 to QAP Manual. ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A9371998-06-30030 June 1998 Technical Rept on Matl Identification of Spent Fuel Piping Welds at Hnp. ML18016A4861998-06-30030 June 1998 Monthly Operating Rept for June 1998 for SHNPP.W/980715 Ltr ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18016A4521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Shearon Harris Nuclear Power Plant.W/980612 Ltr ML18016A7711998-05-26026 May 1998 Non-proprietary Rev 2 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris Spent Fuel Pools 'C' & 'D'. 1999-09-30
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UA.'l'P'(90RY REGULATORY INFORMATION DZSTRZBUTZ N SYSTEM (RIDE)ACCESSION NBR:9610040148 DOC.DATE: 96/09/27 NOTARIZED:
NO FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina AUTH.NAME AUTHOR AFFILIATION EADSFJ.Carolina Power S Light Co.DONAHUE,J.W.
Carolina Power a Light Co.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000400
SUBJECT:
LER 96-010-02:on 960628,CVI Radiation Monitors provided indication in Main Control Room.Caused by inadequate surveillance test procedures.
Surveillance test procedure OST-1008&OST-1092 have been revised.W/960927 ltr.DISTRIBUTION CODE: ZE22T COPIES RECEIVED:LTR I ENCL 3 SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:Application for permit renewal filed.C 05000400 G RECIPIENT ID CODE/NAME PD2-1 PD INTERNAL: ACRS AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DSIR/EIB EXTERNAL: L ST LOBBY WARD NOAC MURPHY,G.A NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME LE,N OD4QPD/RA FILE CXN NRR/DE/EELB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN2 FILE 01 LITCO BRYCEFJ H NOAC POOREFW.NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 D U E N NOTE TO ALL"RIDS" RECIPZENTS:
PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD)ON EXTENSION 415-2083 FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24
Carolina Power&Light Cotnpany Harris Nuclear Plant PO Box 165 New Hill NC 27562 SEP 87 1996 U.S.Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 Serial: HNP-96-159 10CFR50.73 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO.50-400 LICENSE NO.NPF-63 LICENSEE EVENT REPORT 96-010-02
Dear Sir or Madam:
In accordance with Title 10 to the Code of Federal Regulations, the enclosed revision to Licensee Event Report 96-010 is submitted.
This revision provides the safety significance discussion of the previously reported deficiencies that caused Technical Specification
3.0.3 entries
during past testing.An updated status of corrective actions is also provided.Sincerely, J.W.Donahue Director of Site Operations Harris Plant JHE/jhe Enclosure c: Mr.J.B.Brady (NRC Sr.Resident Inspector-HNP)Mr.S.D.Ebneter (NRC Regional Administrator
-RII)Mr.N.B.Le (NRC-Project Manager/NRR) 9610040i48 960927 PDR ADQCK 05000400 S PDR State Road 1134 New Hill NC l
NRC FORM 366 FLS5)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)(See reverse for required nu(nber of digits/characters for each block)APPROVED BY OMB NO.3150-0104 EXPIRES 04/30/96 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION CO(LECT)ON REOUEST: 5M HRS.REPORTED LESSONS LEARNED ARE DICORPORATED INTO THE UCENSING PROCESS ANO FED BACK TO O(DUSTRY.FORWARD COMMENTS REGARDDIG BURDEN ESTIMATE TO THE INfORMATIDN AND RECORDS MANAGEMENT BRANCH IT@F33L US.NUCLEAR REGU(ATORY COMMISSION, WASHDIGTON, OC 20555000l, ANO TO THE PAPERWORK REDUCTION PR(LIECT (3150.0(0(L Off)CE OF MANAGEMENT AND BUDGET, WASHINGTON, OC 20503.FACILITY NAME (1)Harris Nuclear Plant Unit-1 DOCKET NUMBER (3)50-400 PAGE (3)1 OF 6 TITLE (4)Surveillance testing deficiencies that caused past entries into TS 3.0.3.EVENT DATE (5)LER NUMBER (6)REPORT DATE (7)OTHER FACILITIES INVOLVED (6)MONTH OAY YEAR SEBUENTIAL REVISION NUMBER NUMBER MONTH DAY YEAR FACILITY NAME FACIUTY NAME DOCKET NUMBER 05000 DOCKET NUMBER 06 28 96 96-010-02 09 27 96 05000 OPERATING MODE{9)POWER LEVEL (10)100%50.73(a)(2)(viii) 50.73(a)(2)(x)X 50.73(a)I2)(i)50.73(al(2)(ii) 20.2203(a)(2)(v)20.2203(a)(3)(i) 20.2201 (b)20.2203(a)
{1)73.71 50,73(a)(2)(iii)20.2203(a)(3)(ii) 20.2203(a)
(2)(i)OTHER 50.73(a)(2)(iv) 50.73(a)(2)(v) 20.2203(a)
(4)50.36(c)(1)20.2203(a)
(2){ii)20.2203(a)(2)(iii)specrly rn Abstract below or in NRC Form 366A THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Chock one or more)(11)20.2203(a)
(2)liv)50.36(c)(2)LICENSEE CONTACT FOR THIS LER (12)50.73(a)(2)(vii)NAME TELEPHONE NUMBER ((ncrcrde Area Code)Johnny Eads Project Engineer-Licensing{919)362-2646 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPROS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPROS SUPPLEMENTAL REPORT EXPECTED (14)YES{It yes, complete EXPECTED SUBMISSION DATE).re;;rc (Ic@Sgc:'.jtkc cb.'Tcc,4t)b X NO EXPECTED SUBMISSION DATE (15)MONTH DAY YEAR ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single.spaced typewritten lines)(16)On June 14, 1996 with the plant operating in Mode-1 at 100%power, Operations personnel identified a deficiency in the quarterly Residual Heat Removal{RHR)System surveillance test procedures
{OST-1008 Br OST-1092).
Section 7.1 verifies that the RHR pump discharge check valves properly back seat during system operation.
Prior to performing this section of OST-1008, Operators realized that during the check valve back seat test, a system alignment is established that cross connects the operable RHR train, with the inoperable train being tested, and in this condition the operable train would be incapable of providing the minimum required low head safety injection flow to the Reactor Coolant System.While in this cross-connected test alignment, the plant is actually in Technical Specification 3.0.3, which is reportable per 10CFR50.73.
On June 28, 1996 while investigating LER 96-010 Revision 0, one additional surveillance testing deficiency was identified.
With the plant operating in Mode-1 at 100%power, Operations personnel identified a deficiency in Maintenance Surveillance Test MST-(0417,"Containment Ventilation Isolation Area Radiation Monitors Relay Actuation Test." The surveillance test as written caused both trains of Containment Vacuum Relief System to become inoperable requiring entry into Technical Specification
{TS)3.0.3.This deficiency was first identified by Operations personnel on December 11, 1995.However, the significance and reportability of this deficiency was not recognized.
These conditions were caused by inadequate surveillance test procedures resulting from personnel errors during revisions to OST-1008 and OST-1092 in October 1992 and during original procedure development of MST-(0417 in December 1987.Subsequent technical and safety reviews also failed to identify that the test procedures resulted in a Technical Specification 3.0.3 entry.Immediate corrective actions included not performing the scheduled tests as written and placing these procedures on administrative hold.Procedure revisions were then completed for OST-1008(OST-1092 and MST-(0417 to allow surveillance testing without entry into TS 3.0.3.Additional actions included reviewing this event with appropriate personnel.The reportability requirements of TS 3.0.3 entry and restrictions related to voluntary TS 3.0.3 entry were a(so reinforced with licensed operators and included in Licensed Operator training programs.In addition, sampling of additional procedures to identify any similar deficiencies was also completed.
No additional TS 3.0.3 entry problems were identified.
KRC FORM 366A I6-96)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION US.NUCLEAR REGULATORT COMMISSION FACIL)TT KAME II)OOCXET LBI NUMBER 16)PAGE Cn Shaaron Harris Nucfaar Plant~Unit 0'1 TEXT Pl kooko spooorr koqvroC ooo okrCk)Cpoor onto or HRC Fokko 366lU i)7)50400 TEAR SEOUENTIAL REV610N NUMBER NUMBER 96-010-02 2 OF 6 EVENT DESCRIPTION:
On June 14, 1996 with the plant operating in Mode-1 at 100%power, Operations personnel in the main control room identified a deficiency in the quarterly interval Residual Heat Removal (RHR, EIIS Code-BP)Pump surveillance tests (OST-1008 and OST-1092).
Section 7.1 of these tests are performed to satisfy the RHR pump In-Service-Testing Program requirements and verify that the RHR pump discharge check valves (1RH-70 and 1RH-34)properly back seat during system operation.
Prior to performing this section of OST-1008, Operators realized that during the check valve back seat test, a system alignment is established that cross connects the operable RHR train, with the inoperable train being tested.Specifically, the A-train check valve (1RH-34)back seat test is performed by using the discharge pressure of the opposite loop RHR pump.The B-train RHR pump is started and is aligned to recirculate to the Refueling Water Storage Tank (RWST), with the opposite hot leg cross-over valve (1SI-326)shut.In this alignment, the B-train of RHR is completely isolated from the A-train and is fully operable.To verify that"A" RHR Pump check valve (1RH-34)is on it's backseat, 1SI-326 is then opened and a pump discharge flow measurement is taken.A flow rate increase of less than 50 gpm indicates that 1RH-34 is properly back seated.After observing and recording pump flow, 1SI-326 is shut.(reference page 6 for flow diagram)During the time period when 1SI-326 is open, the two RHR trains are cross-connected.
In this condition, the path of least resistance would be the recirculation line to the RWST.This would create the potential for a significant reduction in low head safety injection flow to the Reactor Coolant System in the event of an accident that required Safety Injection.
Based on this, both trains of RHR are rendered inoperable and the plant is in Technical Specification 3.0.3, which is reportable per 10CFR50.73.
Investigation revealed that this back seat testing process was incorporated into OST-1008 and OST-1092 in October 1992 as a new testing methodology.
Prior to this, the recirculation flow path to the RWST was secured prior to opening the cross-over valve, thus eliminating the potential for a reduction in low head safety injection flow during testing.Since October 1992, the A-train has been tested 18 times by performing OST-1008 and OST-1092 has been performed to test the B-train 15 times.On June 28, 1996 while investigating LER 96-010 Revision 0, one additional surveillance testing deficiency was identified.
With the plant operating in Mode-1 at 100%power, Operations personnel identified a deficiency in Maintenance Surveillance Test MST-I0417,"Containment Ventilation Isolation Area Radiation Monitors Relay Actuation Test." The surveillance test as written caused both trains of Containment Vacuum Relief System (EIIS Code-BF)to become inoperable requiring entry into Technical Specification (TS)3.0.3.The deficiency within MST-I0417 has existed since it was originally developed in December 1987.MST-I0417 provides instructions for performing a Relay Actuation Logic Test for Containment Ventilation Isolation System (EIIS Code-JM)actuation on a Two-of-Four High Radiation test signal from the Containment Ventilation Isolation Signal Area Radiation Monitors.This procedure satisfies part of the Monthly Surveillance Requirements of TS 4.3.2.1 (Table 4.3-2, Items 3.c.2 and 3.c.4.a)and TS 4.3.3.1 (Table 4.3-3, Item l.a).The surveillance as originally written generates a Containment Ventilation Isolation Signal which blocks the automatic Containment Vacuum Relief function which causes both trains of Containment Vacuum Relief to become inoperable.
This MST deficiency has resulted in the Containment Vacuum Relief system being inoperable for approximately 45 minutes during each monthly performance of this surveillance test since December 1987.
Li NRC EORM 366A H.96)LICENSEE EVENT REPORT (LERj TEXT CONTINUATION US.NUCLEAR REGULATORZ COMMISSION EACILITZ NAME ll)Shearon Harris Nuciear Plant~Unit)i)1 OOCKEf 50400 LER NUMOER (6)TEAR SEOUENHAL REVISION NUMOER kUMBER 96-010-02 PAGE)3)3 OF 6 TEXT rsl mort sptstis rtqoimL ott tdittmotl rooms or Fir)C Form 3IRSU I)T)EVENT DESCRIPTION Cont'd: The four Containment Ventilation Isolation Radiation Monitors provide indication in the Main Control Room of the activity inside the Containment.
These monitors provide a high radiation alarm when radiation levels reach preset limits.The receipt of these alarms, 2 of 4 logic, initiates a Containment Ventilation Isolation, and alerts Operations personnel of abnormal radiation inside Containment.
In the event of a Containment Ventilation Isolation Signal, the Containment Vacuum Relief butterfly valve and damper of each train will receive a close signal and be prevented from opening until this signal is reset.The Containment Vacuum Relief valves are designed to prevent the differential pressure between Containment and the outside atmosphere from exceeding the design value as a result of inadvertent actuation of the Containment Spray system.The MST-I0417 deficiency was first identified by Operations personnel on December 11, 1995.However, Operations personnel at that time did not recognize the reportability of short duration entry into TS 3.0.3 caused by surveillance testing.As a result, the Condition Report generated in December 1995 was improperly classified as a procedure improvement item and not as an adverse condition.
As a result of the misclassification, the adverse condition did not receive timely corrective actions.CAUSE: These conditions were caused by inadequate surveillance test procedures.
The RHR surveillance test deficiency resulted from personnel error during revisions to OST-1008 and OST-1092 in October 1992.These revisions implemented a change in the RHR pump discharge check valve back seat testing methodology without fully assessing the impact on the RHR system.The Containment Ventilation Isolation surveillance test deficiency resulted from a failure to fully assess the impact on Containment Vacuum Relief System operability during procedure development in December 1987.In both cases, subsequent technical and safety reviews also failed to identify that the test procedures resulted in a Technical Specification 3.0.3 entry.The failure to recognize the significance and reportability of TS 3.0.3 entry on December 11, 1995 was the result of a personnel error.SAFETY SIGNIFICANCE:
The safety significance discussion for both the RHR system surveillance test deficiency and the Containment Vacuum Relief system surveillance test deficiency are provided below: RHR During performance of OST-1008 and OST-1092, the recirculation valve (1SI-331)from the RHR system back to the RWST was partially opened (9 1/2 turns per procedure step 7.1.14.b)to allow the OST required pump flow (3663 gpm100 psid)to pass.This flow is the TS minimum flow for the RHR pumps.This is also the flow required for the testing of the injection path check valves (OST-1088).
Since OST-1008 and OST-1092 (recirculation path)use the same flow requirement as OST-1088 (injection path), it is concluded that the line resistance of the recirculation path is approximately the same as the line resistance of the injection path.Since the line resistance of the recirculation path is approximately the same as the line resistance of the injection path, then the fiow through these two paths during an accident (with this test alignment) would be expected to split in half.Approximately one half of a single pump's flow would be expected to be delivered through the injection path.This delivered flow would not have met the minimum injection flow requirement for the RHR system.Also, it is expected that this one pump would exceed its maximum flow (run out)which could damage this pump.
NRC FORM 366A FL.9SI LICENSEE EVENT REPORT (LER)TEXT CONTINUATION US.NUCLEAR REGULATORT COMMISSION FACILITY NAME (II Shearon Harris Nuclear Plant-Unit Pl OOCKET 50400 LER NUMBER I6)TEAR SEOUENTML REVISION NUMBER NUMBER 96-Ol0-02 PAGE Iii 4 OF 6 TEXT Pl nrae guceir kkqvlkd, osr PCkfriaMI cod Pf lllIC Fnakk JSQ/IITI SAFETY SIGNIFICANCE Cont'd: However, with both trains of RHR available, using the same logic as above, it is concluded that one half of the flow from two pumps would be diverted through the recirculation path and one half delivered through the injection path.With both pumps available, the delivered flow would be the equivalent of one pump's flow.Therefore, with both RHR trains available, the RHR system would be able to deliver the required fiow.Additionally, an evaluation of the safety significance of this condition was made using probabilistic safety assessment (PSA).The test alignment was assumed to occur four times per year (quarterly testing)for a duration of one hour per test.It was further assumed that both RHR pumps are required to operate following a large break LOCA to provide sufficient safety injection (SI)flow to the reactor coolant system (RCS), and no credit was taken for proceduralized operator action to isolate the test flow path to the RWST for large break LOCA scenarios.
For other conditions requiring operation of the RHR pumps, it was found that adequate time was available to permit restoration of the test alignment since precautions and limitations in OST-1008 and OST-1092 required an operator to be stationed at the recirculation valve to the RWST (1SI-331)and be in direct communication with the control room.The increase in annual core damage risk was determined to be 0.0065%of the nominal annual core damage frequency, which is about 6E-5 per year.This is a very small increase in core damage frequency; therefore, it is concluded that the safety significance of this condition with regard to core damage accidents is minimal.Containment Vacuum Relief The consequences of the MST-I0417 surveillance deficiency are that both trains of the Containment Vacuum Relief system were inoperable for approximately 45 minutes during each monthly performance of MST-I0417 since December 1987.The Containment Vacuum Relief system is not relied upon to mitigate the consequences of any FSAR Chapter 15 accidents.
The Containment Vacuum Relief system is designed to assure the structural integrity of the Containment against the differential pressure associated with the inadvertent operation of the Containment Spray system.If an inadvertent operation of the Containment Spray system had occurred during the performance of MST-I0417, operators would have been required to manually reset the Containment Ventilation Isolation signal from the Control Room to allow proper operation of the Containment Vacuum Relief system.A Control Room annunciator (ALB-028-5-1) is provided to alert the operators to a high vacuum in Containment.
In response to the alarm, the Annunciator Panel Procedure (APP-ALB-028) requires the operator to verify that the vacuum relief valves are open if required.In addition, a Control Room annunciator (ALB-001-4-1) is provided to alert the operators to a containment spray pump start.Without appropriate operator intervention, the containment design limit of-2 psid could have been exceeded.\No instances of inadvertent containment spray system operation coincident with MST-I0417 performance have been identified at the Harris Plant.These conditions are reportable per 10CFR50.73(a)(2)(i) and 10CFR50.73(a)(2)(vii).
A(4-)
NRC EORM 366A)4.SS)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION US.NUCLEAR REGUIATORT COMMISSION FACIL)TT NAME (I)Shearon Harris Nuclear Plant Unit 0'1 DOCKET 50400 LER NUMBER 16)SEOUENTIAL REVISION NUMBER NUMBER 96-010-02 PAGE I3)5 OF 6'tEXT Pr moro sposo r's npr)rorL vso orrrprraool sop'os o/FYRC Farm 3664)il))PREVIOUS SIMILAR EVENTS: There have been no previous Harris Plant LERs caused by deficient procedures that resulted in an inadvertent Technical Specification 3.0.3 entry.CORRECTIVE ACTIONS COMPLETED:
1.Surveillance test procedure OST-1008 and OST-1092 have been revised to allow for required RHR system testing without cross-connecting the safety trains and entering Technical Specification 3.0.3.The revision to OST-1008 was approved on July 5, 1996 and the revision to OST-1092 was approved on June 28, 1996.2.Surveillance test procedure MST-I0417 has been revised to prevent inoperability of both trains of Containment Vacuum Relief simultaneously.
MST-I0417 was revised on July 26, 1996.Operations personnel involved with the failure to recognize the significance and reportability of this condition on December 11, 1995 have been counselled.
This counselling was completed by July 24, 1996.This event has been reviewed with appropriate operations and maintenance personnel involved in developing and reviewing procedures.
This review included insight on how this deficiency occurred and how it can be prevented in the future.This review was completed on August 1, 1996 for procedure group personnel or if unavailable by this date, the'review was provided for personnel prior to writing and reviewing procedures.
5.The reportability requirements of TS 3.0.3 entry and restrictions related to voluntary TS 3.0.3 entry were reinforced with licensed operators.
This subject was also included in Licensed Operator training programs on September 16, 1996.An additional sample of procedures has been reviewed to identify any similar procedure deficiencies.
This review was completed on September 10, 1996.No additional TS 3.0.3 entry problems were identified.
CORRECTIVE ACTIONS PLANNED: No additional corrective actions planned.EIIS Codes: Residual Heat Removal System BP Containment Vacuum Relief System BF Containment Ventilation Isolation System JM A (4.)
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